05000317/LER-1981-057-03, /03L-0:on 810721,during Normal Startup Operations, Pressurizer Level Deviated Slightly from Program Level Several Times.Caused by RCS Temp Swings.No Corrective Action Necessary

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/03L-0:on 810721,during Normal Startup Operations, Pressurizer Level Deviated Slightly from Program Level Several Times.Caused by RCS Temp Swings.No Corrective Action Necessary
ML20010C640
Person / Time
Site: Calvert Cliffs 
Issue date: 08/11/1981
From: Junge M
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20010C639 List:
References
LER-81-057-03L, LER-81-57-3L, NUDOCS 8108200260
Download: ML20010C640 (1)


LER-1981-057, /03L-0:on 810721,during Normal Startup Operations, Pressurizer Level Deviated Slightly from Program Level Several Times.Caused by RCS Temp Swings.No Corrective Action Necessary
Event date:
Report date:
3171981057R03 - NRC Website

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8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 RE PORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 i Between 2020 on July 21, and 0540 on July 22 durinq normal startup I

lo lai i operations, pressurizer level deviated slightly from the program level I

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