05000255/LER-1981-031-03, /03L-0:on 810725,LPSI Pump Suction Valves from Sirw Tank & PCS Were Misaligned.Caused by Cl 3.2 Incorrect Identification of Valve Positions.Administrative Controls for Cl Revisions Will Be Changed to Require Proofreading

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/03L-0:on 810725,LPSI Pump Suction Valves from Sirw Tank & PCS Were Misaligned.Caused by Cl 3.2 Incorrect Identification of Valve Positions.Administrative Controls for Cl Revisions Will Be Changed to Require Proofreading
ML20010E130
Person / Time
Site: Palisades 
Issue date: 08/25/1981
From:
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20010E125 List:
References
LER-81-031-03L, NUDOCS 8109030127
Download: ML20010E130 (1)


LER-1981-031, /03L-0:on 810725,LPSI Pump Suction Valves from Sirw Tank & PCS Were Misaligned.Caused by Cl 3.2 Incorrect Identification of Valve Positions.Administrative Controls for Cl Revisions Will Be Changed to Require Proofreading
Event date:
Report date:
2551981031R03 - NRC Website

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