| | | Reporting criterion |
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| 05000220/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | |
| 05000220/LER-1981-001-03, /03L:on 810107,emergency Diesel Generator Output Breaker Tripped on Excessive Current.Caused by Failure of Generator Voltage Regulator Due to Protective Fuse Blow | /03L:on 810107,emergency Diesel Generator Output Breaker Tripped on Excessive Current.Caused by Failure of Generator Voltage Regulator Due to Protective Fuse Blow | |
| 05000220/LER-1981-002, Has Been Cancelled | Has Been Cancelled | |
| 05000220/LER-1981-003, Has Been Cancelled | Has Been Cancelled | |
| 05000220/LER-1981-004, Forwards LER 81-004/01T-0 | Forwards LER 81-004/01T-0 | |
| 05000220/LER-1981-004-01, /01T-0:on 810209,main Steam Radiation Monitor 111 Signal Fluctuated,Causing Multiple Half Scrams.Caused by Loose detector-to-cable Connector.Connector Tightened | /01T-0:on 810209,main Steam Radiation Monitor 111 Signal Fluctuated,Causing Multiple Half Scrams.Caused by Loose detector-to-cable Connector.Connector Tightened | |
| 05000220/LER-1981-005, Forwards LER 81-005/04L-0 | Forwards LER 81-005/04L-0 | |
| 05000220/LER-1981-005-04, /04L-0:on 810202,plant Discharge Temp Vs Plant Inlet Temp Tech Spec Was Exceeded for 52-h During Circulating Water Reverse Flow Operation.Cause Not Stated. Checklist to Be Revised to Prevent Future Occurrence | /04L-0:on 810202,plant Discharge Temp Vs Plant Inlet Temp Tech Spec Was Exceeded for 52-h During Circulating Water Reverse Flow Operation.Cause Not Stated. Checklist to Be Revised to Prevent Future Occurrence | |
| 05000220/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | |
| 05000220/LER-1981-006-03, /03L-0:on 810207,during Fire Sys Preventive Maint Test,Electric Fire Pump Failed to Start.Caused by Broken Prop Spring in 4160V Motor Breaker.Spring Replaced & Pump Returned to Svc | /03L-0:on 810207,during Fire Sys Preventive Maint Test,Electric Fire Pump Failed to Start.Caused by Broken Prop Spring in 4160V Motor Breaker.Spring Replaced & Pump Returned to Svc | |
| 05000220/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | |
| 05000220/LER-1981-007-03, /03L-0:on 810202,during Weekly Surveillance,Diesel Fire Pump Oil Leak Was Identified.Caused by Leak in Coupling to Tubing Weld Joint.Joint Removed,Rebrazed & Returned to Svc | /03L-0:on 810202,during Weekly Surveillance,Diesel Fire Pump Oil Leak Was Identified.Caused by Leak in Coupling to Tubing Weld Joint.Joint Removed,Rebrazed & Returned to Svc | |
| 05000220/LER-1981-008, Forwards LER 81-008/01X-1 | Forwards LER 81-008/01X-1 | |
| 05000220/LER-1981-008-01, /01X-1:on 810316,ultrasonic Testing Revealed Indication on Southeast Reactor Feedwater Nozzle Inside Bore.Caused by Inadequate Investigation.Dye Penetrant & Surface Exam Revealed Indication Nonreportable | /01X-1:on 810316,ultrasonic Testing Revealed Indication on Southeast Reactor Feedwater Nozzle Inside Bore.Caused by Inadequate Investigation.Dye Penetrant & Surface Exam Revealed Indication Nonreportable | |
| 05000220/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | |
| 05000220/LER-1981-012-03, /03L-0:on 810420,during Refueling outage,1-inch Drywell Sampling Isolation Valve 201.7-02 Did Not Meet Tech Spec Min Leak Rate Requirement for One Isolation Valve. Caused by Dust Accumulation on Mating Surfaces | /03L-0:on 810420,during Refueling outage,1-inch Drywell Sampling Isolation Valve 201.7-02 Did Not Meet Tech Spec Min Leak Rate Requirement for One Isolation Valve. Caused by Dust Accumulation on Mating Surfaces | |
| 05000220/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | |
| 05000220/LER-1981-013-03, /03L-0:on 810428,during Outage Frequency Isolation Valve Pneumatic Leak Rate testing,2-inch Rx Head Spray Isolation Valve 34-01 Did Not Meet Tech Specs Min Leak Rate Requirement for One Isolation Valve | /03L-0:on 810428,during Outage Frequency Isolation Valve Pneumatic Leak Rate testing,2-inch Rx Head Spray Isolation Valve 34-01 Did Not Meet Tech Specs Min Leak Rate Requirement for One Isolation Valve | |
| 05000220/LER-1981-014-03, /03L-0:on 810429,during Diesel Fire Pump Test, Diesel Auto Started at Lower than Required Setpoint in Fire Sys Header.Caused by Mercoid O-250 Psig Pressure Switch Failure Due to Natural End of Life.Switch Replaced | /03L-0:on 810429,during Diesel Fire Pump Test, Diesel Auto Started at Lower than Required Setpoint in Fire Sys Header.Caused by Mercoid O-250 Psig Pressure Switch Failure Due to Natural End of Life.Switch Replaced | |
| 05000220/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | |
| 05000220/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | |
| 05000220/LER-1981-015-03, /03L-0:on 810508,during Routine Testing of Reactor Bldg Ventilation Monitors,Sys Failed to Actuate,Although Sys Responded Normally to Simulated Signal.Cause Unknown. Radiation Monitors Recalibr to Alarm Using Gamma Source | /03L-0:on 810508,during Routine Testing of Reactor Bldg Ventilation Monitors,Sys Failed to Actuate,Although Sys Responded Normally to Simulated Signal.Cause Unknown. Radiation Monitors Recalibr to Alarm Using Gamma Source | |
| 05000220/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | |
| 05000220/LER-1981-016-03, /03L-0:on 810515,while Performing Outage Frequency Isolation Valve Local Leak Rate Testing, Streamseal Isolation Valves 201-31 & 201-32 Did Not Meet Tech Spec Min Leak Rate Requirement.Streamseal Replaced | /03L-0:on 810515,while Performing Outage Frequency Isolation Valve Local Leak Rate Testing, Streamseal Isolation Valves 201-31 & 201-32 Did Not Meet Tech Spec Min Leak Rate Requirement.Streamseal Replaced | |
| 05000220/LER-1981-017-03, /03L-0:on 810521,during Routine Testing & Calibr, Core Spray Sparger Delta Pressure Alarms RV30A & RV30B Were Found to Be Out of Tolerance.Caused by Instrument Drift. Devices Recalibr to Alarm within Tolerance | /03L-0:on 810521,during Routine Testing & Calibr, Core Spray Sparger Delta Pressure Alarms RV30A & RV30B Were Found to Be Out of Tolerance.Caused by Instrument Drift. Devices Recalibr to Alarm within Tolerance | |
| 05000220/LER-1981-017, Forwards LER 81-017/03L-0 | Forwards LER 81-017/03L-0 | |
| 05000220/LER-1981-018, Forwards LER 81-018/03L-0 | Forwards LER 81-018/03L-0 | |
| 05000220/LER-1981-018-03, /03L-0:on 810526,during Refueling Outage Local Leak Rate testing,4-inch Crane Check Valve Failed to Meet Tech Spec Min Leak Rate Requirement.Caused by Dirt Between Teflon on Clapper & Valve Body.Parts Cleaned | /03L-0:on 810526,during Refueling Outage Local Leak Rate testing,4-inch Crane Check Valve Failed to Meet Tech Spec Min Leak Rate Requirement.Caused by Dirt Between Teflon on Clapper & Valve Body.Parts Cleaned | |
| 05000220/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | |
| 05000220/LER-1981-019-03, /03L-0:on 810607,while Performing Local Leak Rate testing,1-inch Fisher Isolation Valve 39-11 of Emergency Condenser Steam Line Drain Sys Failed to Seat.Caused by Worn Seating & Packing Matls.Valve Repacked | /03L-0:on 810607,while Performing Local Leak Rate testing,1-inch Fisher Isolation Valve 39-11 of Emergency Condenser Steam Line Drain Sys Failed to Seat.Caused by Worn Seating & Packing Matls.Valve Repacked | |
| 05000220/LER-1981-020-03, /03L-0:on 810605,during Refueling Outage,Check Valves X-81R & X-71E Failed When Tested.Caused by Improper Seating of Valves During Test Procedure.Valves Replaced & Tested Successfully | /03L-0:on 810605,during Refueling Outage,Check Valves X-81R & X-71E Failed When Tested.Caused by Improper Seating of Valves During Test Procedure.Valves Replaced & Tested Successfully | |
| 05000220/LER-1981-021-03, /03L-0:on 810609,temporary Changes to Operating Procedure N1-OP-33A & to Station Jumper Log 975 Found Not to Have Been Performed within 7-day Limit.Cause Not Given. Reviews Completed | /03L-0:on 810609,temporary Changes to Operating Procedure N1-OP-33A & to Station Jumper Log 975 Found Not to Have Been Performed within 7-day Limit.Cause Not Given. Reviews Completed | |
| 05000220/LER-1981-021, Forwards LER 81-021/03L-0 | Forwards LER 81-021/03L-0 | |
| 05000220/LER-1981-022-03, /03L-0:on 810603,during Refueling Outage,While Performing Local Leak Rate Testing,Reactor Bldg to Torus Vacuum Breaker Valve 68-09 Failed to Meet Tech Spec Requirements.Caused by Worn Seating & Packing Matls | /03L-0:on 810603,during Refueling Outage,While Performing Local Leak Rate Testing,Reactor Bldg to Torus Vacuum Breaker Valve 68-09 Failed to Meet Tech Spec Requirements.Caused by Worn Seating & Packing Matls | |
| 05000220/LER-1981-023-03, /03L-0:on 810603,while Performing Local Leak Rate Testing,During Refueling Outage,Torus Vacuum Breaker Valve 68-08 Failed to Meet Tech Spec Requirements.Caused by Worn Seating & Packing Matl.Rubber Goods Replaced | /03L-0:on 810603,while Performing Local Leak Rate Testing,During Refueling Outage,Torus Vacuum Breaker Valve 68-08 Failed to Meet Tech Spec Requirements.Caused by Worn Seating & Packing Matl.Rubber Goods Replaced | |
| 05000220/LER-1981-023, Forwards LERs 81-022/03L-0,81-020/03L-0 & 81-023/03L.W/o LER 81-023/03L-0 | Forwards LERs 81-022/03L-0,81-020/03L-0 & 81-023/03L.W/o LER 81-023/03L-0 | |
| 05000220/LER-1981-024-03, /03L-0:on 810615,containment Oxygen Sampling Isolation Valve 201.2-23 Failed to Meet Acceptance Criteria of N1-1SP-25.6 During Local Leak Rate Testing.Caused by Dirt Under Seat.Valve Bonnet Removed & Body & Seat Cleaned | /03L-0:on 810615,containment Oxygen Sampling Isolation Valve 201.2-23 Failed to Meet Acceptance Criteria of N1-1SP-25.6 During Local Leak Rate Testing.Caused by Dirt Under Seat.Valve Bonnet Removed & Body & Seat Cleaned | |
| 05000220/LER-1981-024, Forwards LER 81-024/03L-0 | Forwards LER 81-024/03L-0 | |
| 05000220/LER-1981-025, Has Been Canceled | Has Been Canceled | |
| 05000220/LER-1981-026-03, /03L-0:on 810624,while Performing Surveillance Test Procedure of Torus/Drywell Vacuum Relief Valves, Switches Which Monitor Distance Between Clapper & Seat Found Out of Spec.Cause Not Stated.Switches Recalibr | /03L-0:on 810624,while Performing Surveillance Test Procedure of Torus/Drywell Vacuum Relief Valves, Switches Which Monitor Distance Between Clapper & Seat Found Out of Spec.Cause Not Stated.Switches Recalibr | |
| 05000220/LER-1981-026, Forwards LER 81-026/03L-0 | Forwards LER 81-026/03L-0 | |
| 05000220/LER-1981-027, Forwards LER 81-027/03L-0 | Forwards LER 81-027/03L-0 | |
| 05000220/LER-1981-027-03, /03L-0:on 810623,leak Rate Test on Reactor Feedwater Isolation Valves 31-03 & 31-04 Showed Unacceptable Leakage.Caused by Limitorque Operator Failing to Put Out Enough Torque to Make Valve Seat Properly.Setting Increased | /03L-0:on 810623,leak Rate Test on Reactor Feedwater Isolation Valves 31-03 & 31-04 Showed Unacceptable Leakage.Caused by Limitorque Operator Failing to Put Out Enough Torque to Make Valve Seat Properly.Setting Increased | |
| 05000220/LER-1981-028, Forwards LER 81-028/03L-0 | Forwards LER 81-028/03L-0 | |
| 05000220/LER-1981-028-03, /03L-0:on 810624,during Refueling Outage,While Performing Surveillance Test ISP-02-13.1B,turbine Oil Switch Was Found at 175 Psi.Cause Not Specified.Switch Recalibr to Provide for Correct Pressure Settings | /03L-0:on 810624,during Refueling Outage,While Performing Surveillance Test ISP-02-13.1B,turbine Oil Switch Was Found at 175 Psi.Cause Not Specified.Switch Recalibr to Provide for Correct Pressure Settings | |
| 05000220/LER-1981-029-03, /03L-0:on 810623,during Carbon Dioxide Hazards Puff Test,Hazards 1,2,5,9 & 12 Were Found Inoperable.Caused by Loose Wires on 1 & 12 & Sticky Relays on 2,5 & 9.Loose Wires Tightened & Sticky Relays Lubricated | /03L-0:on 810623,during Carbon Dioxide Hazards Puff Test,Hazards 1,2,5,9 & 12 Were Found Inoperable.Caused by Loose Wires on 1 & 12 & Sticky Relays on 2,5 & 9.Loose Wires Tightened & Sticky Relays Lubricated | |
| 05000220/LER-1981-029, Forwards LER 81-029/03L-0 | Forwards LER 81-029/03L-0 | |
| 05000220/LER-1981-030-03, /03L-0:on 810630,all Emergency Condenser Vent Monitors Exceeded Upscale Trip Setpoint During Calibr. Caused by Difference in Response Between Test Signal & Actual Signal.Procedure Revised | /03L-0:on 810630,all Emergency Condenser Vent Monitors Exceeded Upscale Trip Setpoint During Calibr. Caused by Difference in Response Between Test Signal & Actual Signal.Procedure Revised | |
| 05000220/LER-1981-030, Forwards LER 81-030/03L-0 | Forwards LER 81-030/03L-0 | |
| 05000220/LER-1981-031-03, /03L-0:on 810704,during Startup W/Reactor at Low Pressure,Emergency Condenser Loop 11 Was Removed from Svc Because of Water Hammer.Caused by Inadequate Draining of Emergency Condenser Sys.Loop Cooled Down & Isolated | /03L-0:on 810704,during Startup W/Reactor at Low Pressure,Emergency Condenser Loop 11 Was Removed from Svc Because of Water Hammer.Caused by Inadequate Draining of Emergency Condenser Sys.Loop Cooled Down & Isolated | |