ML20236P661

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Summary of 980708 Briefing 98-06 to Inform Senior Managers from Ocm,Edo,Aeod & NRR & Regional Ofcs of Selected Events That Occurred Since Last Brief on 980701.List of Attendees & Briefing Slides Encl
ML20236P661
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 07/10/1998
From: Stolz J
NRC (Affiliation Not Assigned)
To: Roe J
NRC (Affiliation Not Assigned)
References
OREM-98-6, NUDOCS 9807170088
Download: ML20236P661 (12)


Text

1 o

July 10,1998 L;Z)M

' MEMORANDUM TO: Jack W. Roe, Acting Director Division of Reactor Program Management FROM: Jo n . to hi Events Assessment and Generic Communications Branch Division of Reactor Program Management j

SUBJECT:

OPERATING REACTORS EVENTS BRIEFING JULY 8,1998 - BRIEFING 98-06

On July 8,1998, we conducted an Operating Reactors Events Briefing (98-06) to inform senior -

managers from the Offices of the Commission, EDO, AEOD, NRR and regional offices of selected events that occurred since our last briefing on July 1,1998. Attachment i lists the attendees.' Attachment 2 presents the significant elements of the discussed event.

The statements contained in the attached briefing slides represent the best information currently available to the NRC. Future followup could produce new information that may alter the NRC's current view of the event discussed.

Attachments:

L 1. List of attendees

'2. Briefing slides cc w/atts:

See next page C'ONTACT: Beverly Sweeney, NRR (301) 415-1166 >

DISTRIBUTION (w/atts)

^ Central Files . PUBLIC LKilgore, SECY PECB R/F BSweeney WBurton l

l DOCUMENT NAME: G:\KAG\ORTRANS To receive a copy of this document, Indicate in the box: "C" = Copy without attachment / enclosure "E" =

Copy with attachment / enclosure "N" = No copy - %

OFFICE - PECB' lE PECB1 l PEC;(//L.] C/PE Q - lN f

J ppOF NAME BSweeney ,f WBurton Vf RDhnnlg JStotA  ; 3 1 07/ Q /98 @) 07/ /$ /98 l DATE 07/}O /98 07/ 9 /98 OFFIC(AL RECORD COPY ,

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. I 98-06 l

OPERATING REACTORS EVENTS BRIEFING 98-06 i

LOCATION: 0-12B4, WHITE FLINT WEDNESDAY, JULY 8,1998,11:00 A.M.

l DAVIS-BESSE LOSS OF OFFSITE POWER  ;

l PRESENTED BY:

EVENTS ASSESSMENT, GENERIC COMMUNICATIONS AND SPECIAL INSPECTION BRANCH DIVISION OF REACTOR PROGRAM MANAGEMENT, NRR Attachment 2 L

98-06 DAVIS-BESSE NUCLEAR PLANT i LOSS OF OFFSITE POWER DURING TORNADO JUNE 24,1998 PROBLEM O LOSS OF OFFSITE POWER (LOOP),

TURBINE / REACTOR TRIP, DAMAGE TO TURBINE l BUILDING, AND DAMAGE TO TOWERS ON ONE OF l THREE 345-KV LINES.

CAUSE i

O TORNADO l SAFETY SIGNIFICANCE O RISK SIGNIFICANCE DETERMINED TO BE RELATIVELY LOW (PRELIMINARY CCDP OF 2.8E-6).

t 1

CONTACT: B. BURTON, NRR/DRPM/PECB AIT: NO

REFERENCE:

10 CFR 50.72 #34435; SIGEVENT: TBD i PNO-3-98-035, 035A i

DAVIS-BESSE 98-06 O LOW RISK SIGNIFICANCE. LOW SBO CONTRIBUTION TO CDF (2% OF TOTAL CDF OF 1.3E-6/YR).

PLANT CONDITION O INITIALLY IN MODE 1 AT 99% REACTOR POWER. I REMAINED IN HOT STANDBY THROUGHOUT l EVENT.

J ,

DISCUSSION O SEQUENCE OF EVENTS: l l JUNE 24,1998 I i

~2040 - LIGHTNING STRIKES OBSERVED IN SWITCHYARD. LICENSEE STARTED BOTH EMERGENCY DIESEL GENERATORS (EDGs).

i f

1 i DAVIS-BESSE 98-06 2043 - TURBINE / REACTOR TRIP DUE TO LOOP.

PLANT WENT ON NATURAL CIRCULATION  !

DUE TO LOSS OF REACTOR COOLANT PUMPS. AUXILIARY FEEDWATER SUPPLIED STEAM GENERATORS. l l

2118 - ALERT DECLARED.

JUNE 26,1998 0200 - LICEN'SEE DOWNGRADED TO AN UNUSUAL EVENT BASED ON RESTORATION OF ONE OFFSITE POWER '

SOURCE.

1358 - LICENSEE EXITED UNUSUAL EVENT BASED ON RESTORATION OF SECOND OFFSITE POWER SOURCE.

r DAVIS-BESSE 98-06 i

EVALUATION I

O THREE 345-KV LINES SUPPLY OFFSITE POWER. l TWO LINES (OHIO EDISON AND LEMOYNE)

SUFFERED NO DAMAGE FROM STORM. THIRD LINE (BAYSHORE) HAD DAMAGE TO 11 TOWERS.

IN SWITCHYARD, DAMAGE TO NUMEROUS INSULATORS AND HIGH VOLTAGE CONNECTORS.

PART OF TURBINE BUILDING ROOF WAS BLOWN OFF.

l ALL NORMAL AND EMERGENCY TELE-COMMUNICATIONS WERE LOST. CORPORATE I MICROWAVE SYSTEM AVAILABLE.

O EDG #1 FAILED TO START FROM CONTROL ROOM.

STARTED LOCALLY. CAUSE WAS DEFECTIVE

CONTACTS.

i- ,

. DAVIS-BESSE 98-06 9 EDG #1 DECLARED INOPERABLE DUE TO ELEVATED ROOM TEMPERATURES ABOVE 120 DEGREE LIMIT. CAUSE WAS FAILED DAMPER HYDRAULIC ACTUATOR, CAUSING DAMPER TO Fall OPEN. DAMPER WAS MANUALLY CLOSED AND FANS PROVIDED TO COOL ROOM. EDG #1 REMAINED FUNCTIONAL THROUGHOUT EVENT.

l 9 HIGH TEMPERATURE IN EDG #2 ROOM ALSO (ITS DAMPER ACTUATOR ALSO FAILED) BUT 4 REMAINED BELOW 120 DEGREE LIMIT.

G ONE MS SAFETY VALVE LIFTED BELOW SETPOINT AND DID NOT FULLY RESEAT.

HEADER PRESSURE REDUCED TO SHUT VALVE.

G ATMOSPHERIC VENT VALVE #2 FAILED TO CLOSE AUTOMATICALLY DUE TO FAILURE OF 1/P CONVERTER. VALVE FAILED AT 10% - 14%

OPEN POSITION WITH 0% DEMAND. VALVE WAS OPERATED MANUALLY.

DAVIS-BESSE 98-06 e WHEN RETURNING TO OFFSITE POWER, CIRCUlT BREAKER ABDC1 FAILED TO CLOSE WHEN PARALLELING EDG #1 TO OFFSITE POWER. CAUSE WAS INADEQUATE MECHANICAL CLEARANCE BETWEEN THE TRIPPING TRIGGER CAM AND TRIP PLUNGER PIN.

O WHEN RETURNING TO OFFSITE POWER FROM EDG #2, RECEIVED EDG BREAKER TRIP ON REVERSE POWER. POSTULATED THAT FAILURE OF R3 RELAY CAUSED FAILURE OF BYPASS FOR REVERSE POWER TRIP FUNCTION ON LOOP.

CORRECTIVE ACTIONS O BAYSHORE TOWERS BEING REPAIRED

(~2 WEEKS).

l l

DAVIS-BESSE 98-06 G TEMPORARY ROOF INSTALLED ON TURBINE BUILDING.

O EDG #1 SWITCH CONTACT BLOCK REPLACED.

O DAMPER HYDROMOTORS REPAIRED. ROOT CAUSE EVALUATION TO BE PERFORMED.

G 1/P CONVERTER REPLACED FOR ATMOSPHERIC VENT VALVE #2. ROOT CAUSE EVALUATION TO BE PERFORMED.

O BREAKER ABDC1 REPLACED WITH SPARE. ROOT CAUSE TO BE DETERMINED.

.O R3 RELAY HAS BEEN REPLACED AND SUCCESSFULLY TESTED.

I PLANT REMAINED IN HOT STANDBY IN ANTICIPATION OF RETURNING TO POWER.

AGENCY RESPONSE O REGION: INCIDENT RESPONSE CENTER ACTIVATED HOUR MONITORING.

(

DAVIS-BESSE 98-06 9 13-MEMBER SPECIAL INSPECTION TEAM DISPATCHED.

DETERMINED LICENSEE RESPONSE AND CORRECTIVE ACTIONS WERE SATISFACTORY.

FINDINGS WILL BE DOCUMENTED IN INSPECTION REPORT 50-349/98012.

G RESTART PANEL FORMED ALL RESTART ISSUES RESOLVED ON JUNE 29, 1998.

MC 0350 PROCESS USED TO DETERMINE RESTART CAPABILITY.

i O HQ: 6/24/98 l

2201 - ENTERED STANDBY RESPONSE MODE.

ACTIVATED HQ OPERATIONS CENTER (OC) DUE TO UNCERTAINTIES CONCERNING THE EVENT.

  • 4 DAVIS-BESSE 98-06 6/25/98 0211 - DOWNGRADED RESPONSE FROM i STANDBY TO MONITORING PHASE OF l NORMAL RESPONSE MODE.

6/26/98 1330 - TERMINATED MONITORING PHASE AND RETURNED TO FULL NORMAL OPERATIONS.

I

Davis-Besse FROM TO TO 8"iefi"9 98'#>

.- UNIT NO. I START-UP START - UP

( MAIN TRANSF.

NO. I TRANSF.

NO.Ol TRANSF.

NO.02

\

l l 'J'(EAST) BUS j

I 34560 [34563 1 1 I T I

l ._,j34561 34564

1 l 34562 l \

l " K'( WEST ) BUS  !

TO BAYSHORE TO LEMOYNE TO OHIO j SUBSTATlON SUBSTATION EDISON CO.

i DAVIS 8 ESSE NUCLEAR POWER STATlDN I- 345 KV SilTCHYARD ONE LINE DIAGRAN FIGURE 8.2-2 REVISION O JULY 1982 l

L _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .