ML20133L969

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Monthly Operating Rept for Sept 1985
ML20133L969
Person / Time
Site: Salem PSEG icon.png
Issue date: 09/30/1985
From: Ronafalvy J, White P, Zupko J
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
NUDOCS 8510240396
Download: ML20133L969 (11)


Text

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  • AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-272 Unit Name Salem # 1 Date October 10,1985 Completed by Pell White Telephone 609-935-6000 Extension 4455 Month September 1985 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 1105 17 1083 2 1061 18 1071 3 1064 19 1078 4 1067 20 1072 5 1059 21 1057 6 1060 22 1067 7 1056 23 1080 8 1058 24 1089 9 1045 25 1090 10 1062 26 1083 11 1050 27 822 12 1061 28 688 13 1066 29 957 14 1089 30 1094 15 1094 31 16 1074 P. 8.1-7 R1 8510240396 850930 PDR ADOCK 0500ggj2 Ig>/1 1

OPERATING DATA REPORT Docket No.50-272 Date October 10, 1985 Telephone 935-6000 Completed by Pell White Extension 4455 Operating Status

1. Unit Name Salem No. 1 Notes
2. Reporting Period September 1985
3. Licensed Thermal Power (MWt) 3338
4. Nameplate Rating (Gross MWe) 1170
5. Design Electrical Rating (Net MWe) 1090
6. Maximum Dependable Capacity (Gross MWe)1124
7. Maximum Dependable Capacity (Net MWe) 1079
8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason N/A
9. Power Level to Which Bestricted, if any (Net MWe) N/A
10. Reasons for Restrictions, if any N/A This Month Year to Date Cumulative
11. Hours in Reporting Period 720 6551 72360
12. No. of Hrs. Reactor was Critical 720 6533.6 42357.1
13. Reactor Reserve Shutdown Hrs. 0 0 3088.4
14. Hours Generator On-Line 720 6530.7 40689.3
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (FOGI) 2351246 21698013 124466010
17. Gross Elec. Energy Generated (FDGI) 785040 7357750 41273800
18. Net Elec. Energy Generated (MWH) 753627 7070558 39168540
19. Unit Service Factor 100 99.7 56.2
20. Unit Availability Factor 100 99.7 56.2
21. Unit Capacity Factor (using MDC Net) 97.0 100 50.2
22. Unit Capacity Factor (using DER Net) 96.0 99.0 49.7
23. Unit Forced Outage Rate 0 .3 29.5
24. Shutdowns scheduled over next 6 months (type, date and duration of each)

Refueling, March 15, 1986, approximately 60 days

25. If shutdown at end of Report Period, Estimated Date of Startup:

N/A

26. Units in Test Status (Prior to Commercial Operation) :

Forecast Achieved Initial Criticality 9/30/76 12/11/76 Initial Electricity 11/1/76 12/25/76 Commercial Operation 12/20/76 6/30/77 8-1-7.R2 Page of L

7 UNIT SHUTDOWN AND POWER REDUCTIONS Docket No.50-272 '

REPORT MONTH September 1985 Unit N;me Salen No.1 Date October 10,1985 Completed by Pell White Telephone 609-935-6000

  • Extension 4455 Method of Duration Shutting- License Cause and Corrective No. Date Type' Hours Reason Down Event System Component Action to 1 2 Rea cto r Report Code 4 Code 5 Prevent Recurrence Travelling Screen /

Trash Rack /

85-584 0927 F 6.5 A 5 -

HC FILTER Canal Screen Travelling Screen /

Trash Rack /

85-586 0927 F 17.9 A 5 - HC FILTER Canal Screen Travelling Screen /

Trash Rack /

85-588 0928 F 13.9 A 5 - HC FILTER Canal Screen 1 2 Reason 3 Method 4 Exhibit G 5 Exhibit 1 F: Forced A-Equipment Failure-explain 1-Manual Instructions Salem as S: Scheduled B-Maintenance or Test 2-Manual Scram. for Prepara- Source C-Refueling 3-Automatic Scram. tion of Data D-Regulatory Restriction 4-Continuation of Entry Sheets E-Operator Training & Licensing Exam Previous Outage for Licensee F-Administrative 5-Load Reduction Event Report G-Operational Error-explain 9-Other (LER) File H-Other-explain (NUREG 0161)

r MAJOR PLANT MODIFICATIONS DOCKET NO.: 50-272 REPORT MONTH SEPTEMBER 1985 UNIT NAME: Salem 1 DATE: October 10, 1985 COMPLETED BY: J. Rcnatalvy TELEPHONE: 609/339-4455

  • DCR NO. PRINCIPLE SYSTEM SUBJECT 1 EC-19 68 Lighting Replace light fixtures on various areas of the plant.

ISC-1005 Waste Disposal (Gas) Change the type of device on

  1. 11 and #12 Waste Gas Compressors that monitors separator pressure (1PD1839 for 11 and IPD1842 for 12).

1SC-1429 Fuel llandling (BPRA Replace comb push rods, clevis Tool) and clevis pins, retainers, etc. in accordance with instructions supplied with Westinghouse modification kit.

Design Change Request

(_

MAJOR PLANT MODIFICATIONS DOCKET i,J.: 50-272 REPORT MONTH SEPTEMBER 1985 UNIT NAME: Salem 1 DATE: October 10, 1985 COMPLETED BY: J. Ronafalvy TELEPHONE: 609/339-4455

  • DCR NO. SAFETY EVALUATION 10 CFR 50.59 lEC-1968 This design change replaces obsolete lighting fixtures in the Turbine Building. It will not adversely affect any safety related equipment and will not chang, the basis for the Technical Specification. No unreviewed safety or environmental questions are involved.

ISC-1005 The replacement pressure switches meet the original design requirements except for accuracy. They, however, only monitor separator pressure and perform no safety related function. No unreviewed safety or environmental questions are invovled.

1SC-1429 This modification includes replacement of the original comb rods on the 3PRA handling tool with those of heavier gauge parts. It does not reduce the margin of safety as defined in the basis of any Technical Specification. This design change does not increase the probability of occurrence or the consequences of any accident previously evaluated in the FSAR. No unreviewed safety or environmental questions are invovled.

  • DCR - Design Change Request w.

.. S i

l PSE&G SALEM GENERATING STATION SAFETY RELATED WORK ORDER LOG ..

SALEM UNIT 1 l

WO NO DEPT UNIT EQUIPMENT 1DENTIFICATION 0099006391 SMD 1 IPS1 FAILURE DESCRIPTION: BODY TO BONNET LEAK THRU MUD HOLE.

CORRECTIVE ACTION: REPUMPED WITH FURMANITE: STILL LEAKS VERY SMALL AMT. STEAM 0099006405 SMD 1 1PS3 FAILURE DESCRIPTION: BODY TO BONNET LEAK.

CORRECTIVE ACTION: RE-PUMP WITH FURMANITE, STILL LEAKS VERY LITTLE STEAM 0099162016 SMD 1 1PS28 FAILURE DESCRIPTION: VALVE HAS PACKING LEAK.

CORRLCTIVE ACTION: FURMANITED VALVE IAW T-169 WO TO BE WRITTEN TO PERFORM PERMANENT REPAIR NEXT OUTAGE l

f l

( SALEM UNIT 1 WO NO DEPT UNIT EQUIPMENT IDENTIFICATION 0099177994 SMD 1 13 SERVICE WATER PUMP FAILURE DESCRIPTION: TiiE PUMP HAS EXCESSIVE PAKCING LEAKAGE CORRECTIVE ACTION: REPACKED PUMP 8507260691 SMD 1 13 CHARGING PUMP FAILURE DESCRIPTION: PUMP IIAS A SEAL LEAK. SEAL TANK OVERFLOWING.

PUMP IS NOT OUT OF SERVICE.

CORRECTIVE ACTION: NEW PLUNGER, PACKING AND GASKETS AND INSPECTED 8508260814 SMD 1 12 CONT. SPRAY PUMP FAILURE DESCRIPTION: THERE IS A SMALL LEAK AT THE DISCHARGE FLANGE.

CORRECTIVE ACTION: REPLACED DISCHARGED FLANGE GASKET 0509030588 SIC 1 LOOP 12 DP'S INDICATION FAILURE DESCRIPTION: LOOP 12 DP IS NOW READING 790 IN. THE OTHER THREE LOOPS ARE AT 660 IN.

CORRECTIVE ACTION: REPLACED FAIRCHILD INDICATOR BECAUSE OF JUMPING EkRATIC READINGS l

3 SALEM UNIT 1 WO NO DEPT UNIT EQUIPMENT IDENTIFICATION 8509170495 SFS 1 1PS28 FAILURE DESCRIPTION: PLEASE HAVE FURMANITE REINJECT 1PS28.

CORRECTIVE ACTION: VALVE PACKING GLAND DID NOT NEED TO BE REINJECTED, BUT WE INSTALLED A BODY TO BONNET CLAMP PEk A DR 8509190283 SMD 1 IPS3 FAILURE DESCRIPTION: HAVE FURMANITE REPAIR BODY TO BONNET LEAK

! ON VALVE IPS3.

CORRECTIVE ACTION: VALVE INJECTED WITH FURMANITE AS PER DR; LEAK STOPPED l 8509220093 SFS 1 llSW127 FAILURE DESCRIPTION: VALVE IS LEAKING SEVERLY OUT OF FLANGE, AROUND BOLT.

CORRECTIVE ACTION: REPAIRED SPOOL PIECES AS PER DR 8509260095 SMD 1 IPS28 FAILURE DESCRIPTION: THE FURMINATE FITTING IS LEAKING STEAM.

I PLEASE REPAIR.

l l CORRECTIVE ACTION: VALVE REINJECTED WITH FURMINATE AS PER DR; LEAK ,

STOPPED l

l

(

SALEM GENERATING STATION MONTiiLY OPERATING

SUMMARY

- UNIT NO. 1 SEPTEMBER 1985 SALEM NO. 1 The Unit began the period operating at full power. On 09/27/85 at 1127 hours0.013 days <br />0.313 hours <br />0.00186 weeks <br />4.288235e-4 months <br /> power was reduced to 43% due to grasses and debris from the river partially clogging the Circ. Water screens. Upon completion of cleaning the screens, Condensate Pump repairs (oil leaks) and strainer cleaning the Unit was returned to 100% power on 11/29/85 at 1324 hours0.0153 days <br />0.368 hours <br />0.00219 weeks <br />5.03782e-4 months <br /> where it remained for the rest of the period.

r REFUELING INFOBMATION Docket No. 50-272 Unit Name Salem #1 Date October 10, 1985 Completed by J. Ronafalvy Telephone 609-935-6000 Extension 4455 Month September 1985

1. Refueling information has changed from last month:

YES NO X

2. Scheduled date of next refueling: February 22, 1986
3. Scheduled date for restart following refueling: May 4, 1986
4. A. Will Technical Specification changes or other license amendments be required?

YES NO NOT DETERMINED TO DATE B. Has the reload fuel design been reveiwed by the Station Operating Review Committee? YES NO X If no, when is it scheduled? January 1986

5. Scheduled date (s) for submitting proposed licensing action:

January 1986, if required

6. Important licensing considerations associated with refueling:

NONE

7. Number of Fuel Assemblies:

A. Incore 193 B. In Spent Fuel Storage 296

8. Present licensed spent fuel storage capacity: 1170 Future spent fuel storage capacity: 1170
9. Date of last refueling that can be discharged to spent fuel pool assuming the present licensed capacity: September 2001 8-1-7.R4

i .

O PSIEG Pubhc Serum Ehxtrie and Gas Company P O. Box E Hancocks Br idy, New Jersey 08038 Salem Generating Station October 10, 1985 Director, Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, DC 20555

Dear Sir:

MONTHLY OPERATING REPORT SALEM NO. 1 DOCKET NO. 50-272 In compliance with Section 6.9, Reporting Requirements for the Salem Technical Specifications, 10 copies of the following monthly operating reports for the month of September 1985 are being sent to you.

Average Daily Unit Power Level Operating Data Report Unit Shutdowns and Power Reductions Major Plant Modification Safety Related Work Orders Operating Summary Refueling Information Sincerely yours,p 1A fc kt) 'l ~

J. M. Zupko, Jr.

General Manager - Salem Operations JR:sbh cc: Dr. Thomas E. Murley Regional Administrator USNRC Region I 631 Park Avenue King of Prussia, PA 19406 Director, Office of Management Information and Program Control U.S. Nuclear Regulatory Commission Washington, DC 20555 ,

Enclosures 8-1-7.R4 I

The Energy People +.-m"-

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