05000260/LER-1999-010, :on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily1999-10-15015 October 1999
- on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily
05000260/LER-1999-009, :on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug1999-10-14014 October 1999
- on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug
05000260/LER-1999-008, :on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions1999-10-0808 October 1999
- on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions
05000296/LER-1999-005-02, :on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With1999-09-30030 September 1999
- on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With
05000296/LER-1999-004-02, :on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position1999-07-26026 July 1999
- on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position
05000260/LER-1999-007, :on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With1999-07-20020 July 1999
- on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With
05000260/LER-1999-006, :on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With1999-07-19019 July 1999
- on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With
05000260/LER-1999-005, :on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With1999-07-12012 July 1999
- on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With
05000260/LER-1999-004-01, :on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset1999-06-28028 June 1999
- on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset
05000260/LER-1999-002-02, :on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With1999-06-14014 June 1999
- on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With
05000260/LER-1999-001-05, :on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With1999-06-14014 June 1999
- on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With
05000260/LER-1999-003-02, :on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram1999-06-14014 June 1999
- on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram
05000296/LER-1999-003-01, :on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened1999-05-0606 May 1999
- on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened
05000260/LER-1999-001-03, :on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable1999-04-0707 April 1999
- on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable
05000296/LER-1999-002, :on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With1999-02-19019 February 1999
- on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With
05000259/LER-1999-001-01, :on 990115,inoperable CR Emergency Ventilation Sys During Post Maint Testing Was Noted.Caused by Failure of Procedure Writers & Reviewers.Returned a Crev to Operable State & Revised B Crev Train Procedures.With1999-02-12012 February 1999
- on 990115,inoperable CR Emergency Ventilation Sys During Post Maint Testing Was Noted.Caused by Failure of Procedure Writers & Reviewers.Returned a Crev to Operable State & Revised B Crev Train Procedures.With
05000296/LER-1999-001-02, :on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With1999-02-12012 February 1999
- on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With
05000260/LER-1998-004-03, :on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With1998-12-31031 December 1998
- on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With
05000296/LER-1998-007, :on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor1998-12-15015 December 1998
- on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor
05000296/LER-1998-006, :on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With1998-12-0707 December 1998
- on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With
05000296/LER-1998-005, :on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With1998-11-12012 November 1998
- on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With
05000296/LER-1998-004-01, :on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With1998-11-0404 November 1998
- on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With
05000260/LER-1998-003-03, :on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve1998-10-28028 October 1998
- on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve
05000260/LER-1998-002-04, :on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls1998-09-15015 September 1998
- on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls
05000259/LER-1998-003-01, :on 980616,determined That Required TS Min Nitrogen Storage Onsite for CAD Is Not Sufficient to Meet Design Basis.Caused by Error in Preparation & Approval of Original Ts.Cad Tank Levels Being Maintained to Meet TS1998-07-16016 July 1998
- on 980616,determined That Required TS Min Nitrogen Storage Onsite for CAD Is Not Sufficient to Meet Design Basis.Caused by Error in Preparation & Approval of Original Ts.Cad Tank Levels Being Maintained to Meet TS
05000259/LER-1998-001, :on 980414,determined That Requirements of ANSI N510-1975 Were Not Being Met W/Respect to DOP Aerosol Mixing & Uniformity.Caused by Lack of Understanding of DOP Testing. Will Revise Test Instructions to Incorporate DOP Testing1998-07-16016 July 1998
- on 980414,determined That Requirements of ANSI N510-1975 Were Not Being Met W/Respect to DOP Aerosol Mixing & Uniformity.Caused by Lack of Understanding of DOP Testing. Will Revise Test Instructions to Incorporate DOP Testing
05000259/LER-1998-002-01, :on 980521,determined That Flow Switch Calibr Test Did Not Ensure Calibr of Both Instrument Channels as Required by Tss.Caused by Technical Inaccuracies in Surveillance Instruction.Surveillance Instructions Revised1998-06-19019 June 1998
- on 980521,determined That Flow Switch Calibr Test Did Not Ensure Calibr of Both Instrument Channels as Required by Tss.Caused by Technical Inaccuracies in Surveillance Instruction.Surveillance Instructions Revised
05000259/LER-1998-001-03, :on 980414,standby Gas Treatment Sys HEPA Filter Testing Was Not in Compliance W/Ansi Std Requirements.Caused by Lack of Understanding of DOP Testing. Filter Testing Training Will Be Provided1998-05-13013 May 1998
- on 980414,standby Gas Treatment Sys HEPA Filter Testing Was Not in Compliance W/Ansi Std Requirements.Caused by Lack of Understanding of DOP Testing. Filter Testing Training Will Be Provided
05000296/LER-1998-003, :on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-111998-05-0404 May 1998
- on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11
05000296/LER-1998-002, :on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions1998-04-0909 April 1998
- on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions
05000260/LER-1998-001-02, :on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source1998-04-0707 April 1998
- on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source
05000296/LER-1998-001, :on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized1998-04-0101 April 1998
- on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized
05000260/LER-1997-008-02, :on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges1997-12-0303 December 1997
- on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges
05000260/LER-1997-007-02, :on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced1997-11-25025 November 1997
- on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced
05000260/LER-1997-006-02, :on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated1997-11-18018 November 1997
- on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated
05000260/LER-1997-005-03, :on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped1997-11-10010 November 1997
- on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped
05000259/LER-1997-004-04, :on 971010,discovered That RHR Swp LCO Is non- Conservative.Caused by Error in Preparation & Approval of Original TS 3.5.C.Will Submit TS Change to NRC to Remove non-conservatism from TS 3.5.C1997-11-0707 November 1997
- on 971010,discovered That RHR Swp LCO Is non- Conservative.Caused by Error in Preparation & Approval of Original TS 3.5.C.Will Submit TS Change to NRC to Remove non-conservatism from TS 3.5.C
05000260/LER-1997-004-03, :on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule1997-10-0909 October 1997
- on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule
05000296/LER-1997-005-02, :on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed1997-10-0303 October 1997
- on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed
05000259/LER-1997-003-04, :on 970812,potential for Containment Pressure to Exceed Design During Purging or Inerting If LOCA Occurred Due to Unanalyzed Suppression Pool Bypass Path Was Noted. Caused by Design Error.Revised Sys Operating Instructions1997-09-0909 September 1997
- on 970812,potential for Containment Pressure to Exceed Design During Purging or Inerting If LOCA Occurred Due to Unanalyzed Suppression Pool Bypass Path Was Noted. Caused by Design Error.Revised Sys Operating Instructions
05000260/LER-1997-003-03, :on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated1997-08-0707 August 1997
- on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated
05000260/LER-1997-002-04, :on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs1997-07-25025 July 1997
- on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs
05000260/LER-1997-001-05, :on 970424,reactor Scram Occurred During Surveillance Testing.Caused by Personnel Error.Affected Sys Were Restored to pre-event Conditions,Administered Personnel Corrective Actions & Briefed Maintenance1997-05-23023 May 1997
- on 970424,reactor Scram Occurred During Surveillance Testing.Caused by Personnel Error.Affected Sys Were Restored to pre-event Conditions,Administered Personnel Corrective Actions & Briefed Maintenance
05000296/LER-1997-004-02, :on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration1997-05-14014 May 1997
- on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration
05000296/LER-1997-002-03, :on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness1997-05-0808 May 1997
- on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness
05000296/LER-1996-004, :on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored1997-04-29029 April 1997
- on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored
05000259/LER-1997-002-02, :on 970314,inadequate CREVS Surveillance Instruction Was Identified During GL 96-01 Review.Caused by Deficient Procedure.Rev to O-SI-4.2.G-2 Was Made & SI Section Was Successfully Completed1997-04-11011 April 1997
- on 970314,inadequate CREVS Surveillance Instruction Was Identified During GL 96-01 Review.Caused by Deficient Procedure.Rev to O-SI-4.2.G-2 Was Made & SI Section Was Successfully Completed
05000296/LER-1997-003-01, :on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot Replaced1997-04-0909 April 1997
- on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot Replaced
05000260/LER-1996-004-01, :on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified1997-04-0909 April 1997
- on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified
05000260/LER-1996-008, :on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges Replaced1997-04-0909 April 1997
- on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges Replaced