ML18039A848
| ML18039A848 | |
| Person / Time | |
|---|---|
| Site: | Browns Ferry |
| Issue date: | 08/16/1999 |
| From: | NRC (Affiliation Not Assigned) |
| To: | |
| Shared Package | |
| ML18039A847 | List: |
| References | |
| NUDOCS 9908200112 | |
| Download: ML18039A848 (12) | |
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UNITED STA ES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 SAFETY EVALUATIONBYTHE OFFICE OF NUCLEAR REACTOR REGULATION RElATED TO AMENDMENTNO. 2601 0 FACILITYOPERATING LICENSE NUMBER DPR-52 ANDAMENDMENTNO 219 TO FACILITYOPERATING LICENSE NUMBER DPR-68 TENNESSEE VALLEYAUTHORITY BROWNS FERRY NUCLEAR PLANT UNITS 2 AND 3 DOCKET NOS. 50-260 AND 50-296
1.0 INTRODUCTION
By application dated June 3, 1999, the Tennessee Valley Authority (the licensee) requested amendments to Facility Operating License Nos. DPR-52, and DPR-68 for the Browns Ferry Nuclear Plant Units 2 and 3, respectively.
The proposed amendments would reduce the Allowable Value (Av) specified for Reactor Vessel Water Level - Low, Level 3, for several instrument functions, in the Technical Specifications (TS).
The intent of the proposed TS changes is to reduce the likelihood of unnecessary reactor scrams and the associated engineered safety feature (ESF) actuations by increasing the operating range between the normal reactor vessel water level and Level 3 trip functions. The increased range willprovide additional time for operators or automatic features to respond to recoverable transients and, thus, may avert unnecessary actuations of protective features.
2.0 DISCUSSION AND EVALUATION 2.1 Descri tion of Functional Chan e
During operation, significant changes in vessel water level can occur due to pressure transients that cause shrinking or swelling of the steam within the coolant system, or due to excessive rates of addition or removal of coolant from the vessel, such as might result from a feedwater pump trip. There is a 23-inch difference in elevation between the normal reactor water level (561 inches) and the current reactor trip (scram) initiation level (Level 3, 538 inches).
Process control systems are designed such that the reactor can automaticaiiy recover from many transients such. as a trip of a feedwater system pump, which might cause a significant change in the water level. However, in some cases, with this narrow water level range, reactor scrams may result that would have been avoidable ifplant control systems or operators had slightly more time to take control.
In addition to tripping the reactor, a drop in vessel level to Level 3 initiates primary and secondary containment isolations, Standby Gas Treatment System (SGTS) operation, Control Room Emergency Ventilation-System (CREVS)
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I 44 operation and arming of the Automatic Depressurization System (ADS). These actuations are unneeded distraction factors for the operators in responding to the associated reactor trip.
The proposed change willprovide an additional 10 inches of operating range between the normal reactor vessel water level and the level used as the setpoint for initiation of the above functions. The increased range willprovide additional time for operators or plant control systems to automatically respond to recoverable transients such as feedwater system malfunctions.and, thus, may avert unnecessary reactor scrams.
This change willsimilarly reduce the likelihood of initiation of the other aforementioned system actuations, without increasing the consequences of events that rely upon these functions.
For each analyzed accident/event the effect of the change in initiation of these protective safety functions is discussed below:
2.2.1
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The licensee's amendment application presents a safety analysis to support;the proposed change.
The safety, analysis identified the role each of the affected protective action plays in the mitigation of (a) abnormal operational occurrences, (b) loss of coolant accidents (LOCA),
(c) anticipated operational occurrences (AOO), (d) anticipated transients without scram (ATWS), (e) Appendix R events (fires) and,(f) other events involving a potential-radiological release.
The subsections below discuss the results of the licensee's analysis, for each category of event.
2.2.2 Abnormal 0 erational Occurrences The licensee utilized a screening process to examine each design basis AOO to determine if a Level 3 reactor protection system (RPS) actuation is credited for mitigation of the event. The licensee found that a Loss of Feedwater event is the only AOO for which a Level 3 Low Water initiated scram occurs.
For this event, a Reactor Core Isolation Cooling initiation subsequently occurs at a lower level and adequately maintains core coverage.
Thus, no unacceptable safety consequences would occur for any AOO ifthe Level 3 setpoint is reduced.
2.2.3 Loss of Coolant Accident LOCA The licensee's analysis determined that, for a large break LOCA, a reactor scram is initiated by high drywell pressure prior to the time that vessel level decreases to Level 3. Due to this action, the licensee concluded that the change in vessel level trip would have no effect on large break LOCA consequences.
For a small break LOCA, the licensee found that the effect of the reduced water level at the time of scram initiation is to decrease the peak cladding temperature (PCT) from 1367 degrees F to 1346,degrees F. The PCT is decreased due to the earlier initiation of the ADS.
The licensee's analyses also encompassed a review of the potential effects on containment dynamic loads, safety/relief valve discharge loads, and suppression pool response for a design-basis accident (D8A) LOCA. The analysis indicates that because a scram would be
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initiated as a result of high drywell pressure, prior to Level 3, the Level 3 setpoint change would have.no effect on these responses.
2.2.4 Fire The licensee's analysis indicates that, forAppendix R (fire) events, the reactor is manually scrammed and, thus, the Level 3 setpoint has no effect on the consequences.
2.2.5 ATWS In an ATWS scena;lo, no automatic or manual scram occurs.
Thus, the change in RPS Level 3 initiation has no effect.
2.2.6 Main Steamline Break Outside Containment:
The licensee's analysis states that for the main steam line break event, a scram occurs due to the high steamline flowprotective function and, thus, the change in the low water level function willnot affect the consequences.
For smaller breaks forwhich the high steam flowfunction is not sufficiently sensitive, the break would be sensed by other leakage detection systems that are not affected by the Level 3 setpoint.
'I Ql 2.2.7 Prima Containment Isolation Includin Shutdown Coolin S stem Isolation A protective feature of the Browns Ferry facilities is isolation ui the primary containment penetrations ifvessel level drops to Level 3. This function assures that onsite and offsite dose limits established by 10 CFR Part 20 and 10 CFR Part 100 are not exceeded.
The licensee's analysis states that significant radiation'releases cannot occur until after the core is uncovered and, with the reduced Level 3 setpoint, containment isolation willstill occur well before core uncovery; thus, the small delay in primary containment isolation willhave no effect in the event of an accident during operation.
The staff notes that the DBA-LOCA radiological dose consequences analysis is not affected by the scram delay, since the release is a bounding, standard source term, which is unchanged,, and forwhich the release is assumed to begin at the time of a simultaneous break initiation and scram.
The residual heat removal system (RHRS) Primary Containment Isolation function is also required to be operable during shutdown cooling operations.
During shutdown cooling operations a Level 3 condition willinitiate closure of the shutdown cooling isolation valves.
This prevents any further loss of coolant inventory via the RHRS if RHRS leakage is the reason for the reduction in vessel level. Ifthe vessel level continues to drop to Level 1, the low pressure coolant injection function willbe initiated and willrestore water level. Because th safety, injection function is not affected, the change in the Level 3 setpoint willhave no adverse effect on a shutdown cooling event.
Another primary containment isolation function that occurs on a Low Level 3 signal is isolation of the Reactor Water Cleanup (RWCU) System.
This signal is one of several that initiate an RWCU isolation in the event of loss of reactor coolant due to an RWCU line break. The
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licensee's analysis states that the reduced Level 3 setpoint would not impact the capability of.
the RWCU isolation valves to perform their intended function. The staff agrees, noting that, in the event of an RWCU line break the RWCU system would likely be isolated earlier as the result of other RWCU system leakage detection functions.
2.2.8 Seconda Containment Isolation and Standb Gas Treatment S stem The primary, containment system is enclosed by a secondary containment system which, in the event of an accident, confines gaseous primary containment leakage.
This leakage is exhausted from the secondary containment enclosure by an SGTS, and discharged to an elevated release point. Like primary containment isolation, operation of the secondary containment system, is also initiated upon a vessel Low Level 3 condition.
Radiological dose calculations for the design basis LOCA assume that, in the event of a DBA-LOCA, primary containment isolation and secondary containment/SGTS initiation occur simultaneously with all primary containment leakage being released untreated at ground level until a negative pressure is established in the secondary containment by the SGTS. The system must be capable of establishing.a specified negative pressure in secondary containment within a specified time from initiation, and with a specified secondary containment infiltration rate. Since secondary containment/SGTS initiation willcontinue to occur at the same. time as primary containment isolation, and the design basis performance requirements are not changed, the radiological dose mitigation function of the secondary containment/SGTS would be, unaffected.
2.2.9 CREVS Actuation The CREVS is designed to provide a radiologically controlled environment to ensure the habitability of the control room for all plant conditions.
In the event of a Level 3 signal, the CREVS is automatically initiated to pressurize the control room with filtered air to minimize the radiological doses to control room personnel.
The LOCA provides the most severe potential radiological release to the primary and secondary containment and, thus, serves as the bounding DBA in determining the control room dose, which must not exceed the criteria of General Design Criterion-19. For LOCA events, the CREVS willactuate on high drywell pressure prior to reaching the Level 3 water level trip. Therefore, a reduced'Level 3 Avwould have no effect on the LOCA event analysis.
2;2.10 Automatic De ressurization S stem The proposed TS change lowers ADS confirmatory signal Level 3 Av from 544 inches to 528 inches to maintain consistency with the other Level 3 trip functions. This Level 3 signal is a confirmatory low water level signal forADS initiation, which serves to prevent unnecessary ADS initiation resulting from spurious Level 1 (398 inches) water level actuations or as a result of a break in the Level 1 instrument line. The intended function of this confirmatory signal will still be successfully accomplished even ifthe Level 3 signal is reduced since the Level 3 signal willoccur well prior to Level 1. Therefore, reducing the Level 3 Av willnot affect the ability of ADS to perform its intended function.
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~I 3.0 STATE CONSULTATIGN In accordance with'the U.S. Nuclear Regulatory Commission's regulations, the Alabama State officialwas notified of the, proposed issuance of the amendments.
The State official had no comments.
4.0 ENVIRONMENTALCONSIDERATION The amendments change a requirement with respect to installation or use of a.facility component located'within the restricted area as defined in.10 CFR Part 20 and changes.a surveillance requirement.
The NRC staff has determined that the amendments involve no significant increase in the amounts, and no'significant change in the types of any effluents that may be released offsite,, and that there is no significant increase in individual or cumulative occupational radiation exposure.
The Commission has previously issued a proposed'finding that the amendments involve no significant hazards consideration, and there has been no public comment on such finding (64 FR 38037). Accordingly, the amendments meet the eligibilitycriteria for categorical exclusion set'forth in.10 CFR 51.22(c)(9).
Pursuant to 10 CFR 51.22(b), no environmental impact statement or environmental assessment need be prepared in connection with the issuance of the amendments.
5.0 CONCLUSION
The Commission-has concluded, based on the considerations discussed above, that: (1).there is reasonable assurance that the health and safety of the public willnot be endangered by operation in the proposed manner, (2) such activities willbe conducted in compliance with the Commission's regulations, and (3) the issuance of the amendments will not.be inimical to the common defense and security or to the health and safety of the public.
Principal Contributor.
W.O. Long August 16, 1999
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Mr. J. A..Scalice Tennessee Valley Authority BROWNS FERRY NUCLEAR PLANT CC:
Senior Vice'President Nuclear Operations Tennessee Valley Authority 6A Lookout Place 1101 Market Street Chattanooga, TN 37402-2801 Mr. Jack A. Bailey, Vice President Engineering &Technical Services Tennessee Valley Authority 6A Lookout. Place 1101 Market Street Chattanooga, TN 37402-2801 Mr. Mark J. Burzynski, Managar Nuclear Licensing Tennessee Valley Authority 4X Blue Ridge 1101 Market Street Chattanooga, TN 37402-2801 Mr. Timothy E. Abney, Manager Licensing and'Industry Affairs
'Browns Ferry Nuclear Plant Tennessee Valley Authority P;O. Box 2000 Decatur, AL35609 Mr. Karl W. Singer, Site Vice President Browns Ferry Nuclear Plant Tennessee Valley.Authority P.O. Box 2000 Decatur, AL 35609 Senior Resident Inspector U.S. Nuclear. Regulatory Commission Browns Ferry Nuclear Plant I0833 Shaw Road.
Athens,.AL 35611 General Counsel Tennessee Valley Authority ET 10H 400 West'Summit Hill Drive Knoxville, TN 37902 Mr. Kirk E. Whatley Office of Radiation Control Alabama Dept. of Public Health, 2001 Monroe Street, Suite 700 Montgomery, AL36104 Mr. N; C. Kazanas, General Manager Nuclear Assurance Tennessee Valley Authority 5M Lookout Place 1101 Market Street Chattanooga, T.N 37402-2801 Chairman Limestone County Commission 310 West Washington Street Athens, AL 35611 Mr. Robert:G. Jones, Plant Manager Browns Ferry Nuclear'Plant Tennessee Valley Authority P.O. Box 2000 Decatur, AL 35609
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