ML20028E782
ML20028E782 | |
Person / Time | |
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Site: | Millstone |
Issue date: | 01/21/1983 |
From: | Stadnick S NORTHEAST NUCLEAR ENERGY CO. |
To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
Shared Package | |
ML20028E766 | List: |
References | |
LER-82-051-03L, LER-82-51-3L, NUDOCS 8301280193 | |
Download: ML20028E782 (1) | |
Similar Documents at Millstone | |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J3301994-10-0707 October 1994
[Table view]LER 94-011-00:on 940908,manual Reactor Trip Initiated Due to MSIV Failure During part-stroke Test.Solenoid Valve & Number of Pins Replaced & MSIVs Tested satisfactorily.W/941007 Ltr ML20024J3291994-10-0303 October 1994 LER 94-027-00:on 940903,determined That Channel B Linear Range Nuclear Instrument Inoperable as Result of Connector J6 Being Disconnected from Jack.Connector J6 Reinstalled.W/ 941003 Ltr ML20029E5291994-05-13013 May 1994 LER 94-007-00:on 940414,determined That Valve Stroke Time Acceptance Criterion Exceeded System Response Time.Caused by Programmatic Error During Initial Startup.Corrective Action: Stroke Time Acceptance Has Been reduced.W/940513 Ltr ML20029E1361994-05-11011 May 1994 LER 94-007-00:on 940412,CRAC & Ebfs Were Inoperable Due to Previous Charcoal Testing Performed to Industry Std Different than Ts.Corrective Actions:Ts Changed to Reflect Newest Charcoal Testing procedure.W/940511 Ltr ML20029D8491994-05-0202 May 1994 LER 94-006-00:on 940407,plant Did Not Meet Requirements of LCO 3.7.6.1 Re Two Independent Control Room Emergency Ventilation Sys.Caused by Inadequate Work Organization. Corrective Action:Revised OP 2315A.W/940502 Ltr ML20029D6221994-04-29029 April 1994 LER 94-005-00:on 940401,determined That Both Facilities of Ebfs Had Never Been Tested in Accordance W/Ts.Caused by Program Failure/Personnel Error.Corrective Action: Surveillance Was Completed satisfactorily.W/940429 Ltr ML20029D2531994-04-28028 April 1994 LER 94-008-00:on 940329,discovered That Data in OPS Form 2604P-2,was Recorded Incorrectly.Caused by Program Failure, Procedure Deficiencies & Technical Error.Corrective Action: Recalculated ESF Equipment Circuit response.W/940428 Ltr ML20046C7771993-08-0606 August 1993 LER 93-010-00:on 930707,reactor Trip Input to Turbine Trip Portion of ESFAS Declared Inoperable Due to Inadequate Surveillance Testing.Test to Verify Operability Written & performed.W/930806 Ltr ML20046C2161993-08-0303 August 1993 LER 93-017-00:on 930701,possible Inoperability of Power Operated Relief Valve Blocking Valves Caused by Original Design Basis.Changed Designs & Performed tests.W/930803 Ltr ML20046B0311993-07-23023 July 1993 LER 93-012-01:on 930524,turbine & Reactor Tripped During Mussel Cook (Thermal Backwash) Due to Lack of Heat Removal Capabilities from Main Generator Stator Water Cooling Sys. Installed Thermoconductivity filler.W/930723 Ltr ML20045H8991993-07-15015 July 1993 LER 93-009-00:on 930617,determined That Suppl Leak Collection & Release Sys May Have Been Inoperable During Certain Weather Periods in Past.Caused by Failure to Account for Chimney Effect.Suppl Will Be sent.W/930715 Ltr ML20045H4021993-07-0909 July 1993 LER 93-007-00:on 930611,plant Mgt Discovered Reduction in EDG Fuel Oil Storage Capacity Per SER & Fsar,Constituting Event Outside Design Basis of Plant.Caused by Inadequate Design Interface.Temporary Tanker utilized.W/930709 Ltr ML20045H8921993-07-0909 July 1993 LER 93-005-01:on 930311,discovered That Automatic RPS Actuation Occurred on 930222 & Not Immediately Reported to Nrc.Caused by Personnel Error.Memo Sent to All Licensed Operators/Personnel Re Reporting requirements.W/930709 Ltr ML20045H8571993-07-0909 July 1993 LER 93-008-00:on 930614,one Channel of Electrical Environmentally Qualified Temp Monitor for Main Steam Valve Bldg Found Indicating Improperly.Caused by Personnel Error. Manual Logging of Temp initiated.W/930709 Ltr ML20045F5891993-07-0202 July 1993 LER 93-013-00:on 930603,noted That Main Turbine Generator EHC Sys Caused an Increase in Pressurizer Pressure,Resulting in Reactor Trip,Due to Closing of Intercept & Cv.Operators Performed EOP & Sys Performed as expected.W/930702 Ltr ML20045F6881993-07-0202 July 1993 LER 93-004-02:on 930222,reactor Trips on SG Low Water Level Occurred.Caused by Automatic Trip of MFW Pump B on Low Suction Pressure Due to High FW Flow Rates.Classroom Training on Main & Afwc Received by Licensed Operators ML20045D9041993-06-23023 June 1993 LER 93-012-00:on 930524,reactor Trip Occurred Due to Turbine Trip & Malfunction Caused Feedwater Regulating Valve a to Stay Approx 56% Open.Caused by Lack of Heat Removal Capabilities.Hand Wheels secured.W/930623 Ltr ML20045D8601993-06-21021 June 1993 LER 93-006-00:on 930525,two HPSI Discharge Check Valves Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Personnel Error.Test Written & Performed to Demonstrate Valve operability.W/930621 Ltr ML20045D9031993-06-21021 June 1993 LER 92-003-01:on 920207,discovered Potential Barrier Breach Via Direct Openings Around Main Feedwater Bypass Line Penetrations.On 920130,plant Entered Mode 4 W/O Encl Bldg Integrity.Erosion/Corrosion Exam Procedure Modified ML20045D3091993-06-18018 June 1993 LER 93-005-00:on 930520,cold Over Pressure Protection Sys Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Mgt Deficiency.Overlap Task Force Will Continue to Review Procedures Associated W/Reactor trip.W/930618 Ltr ML20045A4491993-06-0404 June 1993 LER 93-009-00:on 930506,inlet & Outlet skid-mounted Isolation Valves to Radiation Monitor Found Shut.Caused by Procedure Noncompliance by I&C Personnel.Personnel Will Review & Edit Radiation procedures.W/930604 Ltr ML20045A2321993-06-0101 June 1993 LER 93-008-00:on 930505,determined That Electrical Starter for Both Charging Pumps Inoperable.Caused by Program Failure.Administrative Controls Have Been Established to Ensure Minimum TS requirements.W/930601 Ltr ML20044C9191993-05-0707 May 1993 LER 93-002-01:on 930206 & 07,Train a & Train B CR Pressurization Sys Failed 18-month Surveillance Test, Respectively.Caused by Moisture in Air Banks & Pressure Oscillations.Air Banks purged.W/930507 Ltr ML20044C9331993-04-30030 April 1993 LER 91-002-01:on 910118,engineering Evaluation Determined That Operation of Four Vital 120-volt Ac Buses,On Alternate Sources,Unsatisfactory.Caused by Failure to Update TS to Reflect Configuration.Inverter Sys replaced.W/930430 Ltr ML19346B2411992-08-20020 August 1992 LER 92-018-00:on 920722,both RHR Trains Rendered Inoperable Due to Procedure Deficiency.Both Trains of RHR Restored to Operable Condition & Surveillance Procedures for Both Trains revised.W/920820 Ltr ML20024H3241991-05-24024 May 1991 LER 91-001-01:on 910110,electro-hydraulic Control Sys Failure Occurred,Causing Reactor Trip.Caused by Turbine Trip.Both EHC Pump Discharge Filters Changed Out & Pump B Replaced W/Spare pump.W/910524 Ltr ML20029C1281991-03-18018 March 1991 LER 91-004-00:on 910216,unexpected Trip of 'B' Steam Generator Feed Pump & Subsequent Manual Reactor Trip Occurred.Cause Unknown.Monitoring Capability Added to Sgfp Circuitry & Design Change made.W/910318 Ltr ML20029B6001991-03-0707 March 1991 LER 91-004-00:on 910205,leakage Found During Local Leak Rate Testing for Four Containment Isolation Valves.Caused by Improper Valve Seating.Valve Removed from Svc & Sent to Mfg for overhaul.W/910307 Ltr ML20029B6031991-03-0404 March 1991 LER 91-002-00:on 910202,setpoint Drift Identified During Testing of Main Steam Safety Valves.Caused by Inadequate Design.Nine out-of-tolerance Valves Reset within Specified +1% Tolerance ML20029B5981991-03-0404 March 1991 LER 91-003-00:on 910203 & 16,spurious Control Bldg Isolation Signals Received from Train a Control Bldg Ventilation Inlet Radiation Monitor.Caused by Equipment Malfunction.Detector replaced.W/910304 Ltr ML20029A6501991-02-19019 February 1991 LER 91-001-00:on 910117,discovered That Source Check Surveillance Procedure to Verify Operability of Beta Scintillation Radiation Detectors Did Not Meet TS Requirements.Surveillance Procedure revised.W/910219 Ltr ML20028H4261990-12-27027 December 1990 LER 89-005-01:on 890330,intermittent Connection While Sliding Module Into Position Caused Automatic Test Insertion Circuit to Send Signals Greater than Normal Pulse Thus Allowing Three SIAS Modules to actuate.W/901227 Ltr ML20028H4391990-12-27027 December 1990 LER 90-015-01:on 900919,inadvertent Isolation of Containment Isolation Valves Occurred.On 900920,inadvertent Actuation of Sias,Containment Isolation Actuation Sys & Encl Bldg Filtration Sys occurred.W/901227 Ltr ML20028H4271990-12-27027 December 1990 LER 90-021-00:on 901127,LCO Paragraph 3.0.3 Entered.Caused by Poor Communications.Mgt Reviewed Event & Events Leading Up to Incident & Concluded That Increased Awareness W/ Respect to Sys Status Must Be pursued.W/901227 Ltr ML20028H4401990-12-24024 December 1990 LER 90-019-00:on 900606,automatic Reactor Trip from Negative Flux Rate Signal Occurred Due to Dropped Control Rod.Caused by Broken Connection in Gripper Coil Power Cable.Connector Replaced & Power Loop checked.W/901224 Ltr ML20028G9421990-09-26026 September 1990 LER 90-012-00:on 900827,automatic Reactor Trip Occurred During Bypass Switch Operations.Caused by Operator Error. Procedure Sp 2601D Revised to Incorporate Separate Section on Performing calibrs.W/900926 Ltr ML20028G9111990-09-18018 September 1990 LER 89-008-01:on 891002,determined That Plant Failed to Perform Functional Check of Control Board Annunciators During Channel Functional Tests.Caused by Personnel Error. Procedures Revised Re Annuciator testing.W/900918 Ltr ML20044B0441990-07-10010 July 1990 LER 90-007-00:on 900611,discovered That Surveillance Procedure 2609E Re Encl Bldg Filtration Sys Testing - Refueling Not Performed Prior to Entering Mode 4.Caused by Personnel Error.Missed Surveillance performed.W/900710 Ltr ML20044A1581990-06-18018 June 1990 LER 90-017-00:on 900518,loss of Both Trains of HPSI Occurred.Caused by Cognitive Failure by Licensed Operator. Personnel Counseled on Causes of Event & Importance of Recognizing When Event reportable.W/900618 Ltr ML20043H2021990-06-15015 June 1990 LER 90-005-00:on 900503,identified Potential for High Energy Line Break in Auxiliary Steam Sys That Could Degrade Plant Areas Determined as Mild Environs.Probably Caused by Incorrect Conclusions from Analysis in 1973.W/900615 Ltr ML20043G1031990-06-12012 June 1990 LER 90-016-00:on 900513,steam Generator B lo-lo Signal Generated Reactor Trip Signal,Causing Automatic Start of motor-driven Auxiliary Feedwater Pumps a & B.Caused by Inadequate Guidance.Procedure revised.W/900612 Ltr ML20043G3921990-06-11011 June 1990 LER 90-014-00:on 900519,manual Reactor Trip Initiated as Result of Anticipated Turbine Trip Due to Condenser Vacuum. Caused by Design Deficiency in That Traveling Screen Capacity Inadequate.Traveling Screen modified.W/900611 Ltr ML20043F7021990-06-11011 June 1990 LER 90-015-00:on 900512,feedwater Isolation Occurred While Opening Msivs.Caused by MSIV 2 Opening Faster than Other Msivs,Resulting in Swell in Steam Generator 2.Steam Generator Level Restored to normal.W/900611 Ltr ML20043F8261990-06-0707 June 1990 LER 90-006-00:on 900508,reactor Manually Tripped When Decreasing Levels Noted in Steam Generator 1 & Feedwater Regulating Valve Indicated Full Open.Caused by Valve Stem Separating from Plug.Feedwater Flow restored.W/900607 Ltr ML20043D4711990-05-30030 May 1990 LER 85-002-01:on 850302 & 25,unplanned Actuation of Containment Purge Valve Isolation Occurred.Caused by Personnel Error.Caution Signs Placed on Radiation Monitors & Reset Button on Monitor Made inaccessible.W/900530 Ltr ML20043A7841990-05-16016 May 1990 LER 90-013-00:on 900416,manual Reactor Trip Initiated Due to Imminent Loss of Condenser Vaccum.Caused by Inadequate Administrative Guidance When Debris Collected on Trash Rack. Severe Weather Procedure revised.W/900516 Ltr ML20042G7201990-05-0707 May 1990 LER 90-012-00:on 900406,review of Steam Generator Blowdown Monitor High Radiation Alarm Setpoint Revealed That Setpoint Was Nonconservative.Caused by Administrative Deficiency. Correct Setpoint installed.W/900507 Ltr ML20042E6751990-04-20020 April 1990 LER 90-002-00:on 900322,Tech Spec Action Statement 3.3.3.10 Not Entered for Out of Svc Stack Gas & Particulate Radiation Monitor.No Particulate Radiation Increases Detected.Caused by Personnel error.W/900420 Ltr ML20042E1621990-04-0909 April 1990 LER 90-009-00:on 900309,automatic Turbine Trip W/Subsequent Reactor Trip Occurred Due to High Stator Cooling Water Temp. Caused by Failure of Mechanical Linkage on Fisher & Portor Controller.Controller Replaced w/spare.W/900409 Ltr ML17223A7901990-04-0202 April 1990 LER 89-009-01:on 891025,radiation Monitor RM 8262 Inlet Valve (2-AC-82) Found Closed.Caused by Personnel Error. Isolation Valve Opened,Sample Flow Restored & Radiation Monitor Restored to Operable status.W/900402 Ltr 1994-05-02 Category:RO) MONTHYEARML20024J3301994-10-0707 October 1994
[Table view]LER 94-011-00:on 940908,manual Reactor Trip Initiated Due to MSIV Failure During part-stroke Test.Solenoid Valve & Number of Pins Replaced & MSIVs Tested satisfactorily.W/941007 Ltr ML20024J3291994-10-0303 October 1994 LER 94-027-00:on 940903,determined That Channel B Linear Range Nuclear Instrument Inoperable as Result of Connector J6 Being Disconnected from Jack.Connector J6 Reinstalled.W/ 941003 Ltr ML20029E5291994-05-13013 May 1994 LER 94-007-00:on 940414,determined That Valve Stroke Time Acceptance Criterion Exceeded System Response Time.Caused by Programmatic Error During Initial Startup.Corrective Action: Stroke Time Acceptance Has Been reduced.W/940513 Ltr ML20029E1361994-05-11011 May 1994 LER 94-007-00:on 940412,CRAC & Ebfs Were Inoperable Due to Previous Charcoal Testing Performed to Industry Std Different than Ts.Corrective Actions:Ts Changed to Reflect Newest Charcoal Testing procedure.W/940511 Ltr ML20029D8491994-05-0202 May 1994 LER 94-006-00:on 940407,plant Did Not Meet Requirements of LCO 3.7.6.1 Re Two Independent Control Room Emergency Ventilation Sys.Caused by Inadequate Work Organization. Corrective Action:Revised OP 2315A.W/940502 Ltr ML20029D6221994-04-29029 April 1994 LER 94-005-00:on 940401,determined That Both Facilities of Ebfs Had Never Been Tested in Accordance W/Ts.Caused by Program Failure/Personnel Error.Corrective Action: Surveillance Was Completed satisfactorily.W/940429 Ltr ML20029D2531994-04-28028 April 1994 LER 94-008-00:on 940329,discovered That Data in OPS Form 2604P-2,was Recorded Incorrectly.Caused by Program Failure, Procedure Deficiencies & Technical Error.Corrective Action: Recalculated ESF Equipment Circuit response.W/940428 Ltr ML20046C7771993-08-0606 August 1993 LER 93-010-00:on 930707,reactor Trip Input to Turbine Trip Portion of ESFAS Declared Inoperable Due to Inadequate Surveillance Testing.Test to Verify Operability Written & performed.W/930806 Ltr ML20046C2161993-08-0303 August 1993 LER 93-017-00:on 930701,possible Inoperability of Power Operated Relief Valve Blocking Valves Caused by Original Design Basis.Changed Designs & Performed tests.W/930803 Ltr ML20046B0311993-07-23023 July 1993 LER 93-012-01:on 930524,turbine & Reactor Tripped During Mussel Cook (Thermal Backwash) Due to Lack of Heat Removal Capabilities from Main Generator Stator Water Cooling Sys. Installed Thermoconductivity filler.W/930723 Ltr ML20045H8991993-07-15015 July 1993 LER 93-009-00:on 930617,determined That Suppl Leak Collection & Release Sys May Have Been Inoperable During Certain Weather Periods in Past.Caused by Failure to Account for Chimney Effect.Suppl Will Be sent.W/930715 Ltr ML20045H4021993-07-0909 July 1993 LER 93-007-00:on 930611,plant Mgt Discovered Reduction in EDG Fuel Oil Storage Capacity Per SER & Fsar,Constituting Event Outside Design Basis of Plant.Caused by Inadequate Design Interface.Temporary Tanker utilized.W/930709 Ltr ML20045H8921993-07-0909 July 1993 LER 93-005-01:on 930311,discovered That Automatic RPS Actuation Occurred on 930222 & Not Immediately Reported to Nrc.Caused by Personnel Error.Memo Sent to All Licensed Operators/Personnel Re Reporting requirements.W/930709 Ltr ML20045H8571993-07-0909 July 1993 LER 93-008-00:on 930614,one Channel of Electrical Environmentally Qualified Temp Monitor for Main Steam Valve Bldg Found Indicating Improperly.Caused by Personnel Error. Manual Logging of Temp initiated.W/930709 Ltr ML20045F5891993-07-0202 July 1993 LER 93-013-00:on 930603,noted That Main Turbine Generator EHC Sys Caused an Increase in Pressurizer Pressure,Resulting in Reactor Trip,Due to Closing of Intercept & Cv.Operators Performed EOP & Sys Performed as expected.W/930702 Ltr ML20045F6881993-07-0202 July 1993 LER 93-004-02:on 930222,reactor Trips on SG Low Water Level Occurred.Caused by Automatic Trip of MFW Pump B on Low Suction Pressure Due to High FW Flow Rates.Classroom Training on Main & Afwc Received by Licensed Operators ML20045D9041993-06-23023 June 1993 LER 93-012-00:on 930524,reactor Trip Occurred Due to Turbine Trip & Malfunction Caused Feedwater Regulating Valve a to Stay Approx 56% Open.Caused by Lack of Heat Removal Capabilities.Hand Wheels secured.W/930623 Ltr ML20045D8601993-06-21021 June 1993 LER 93-006-00:on 930525,two HPSI Discharge Check Valves Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Personnel Error.Test Written & Performed to Demonstrate Valve operability.W/930621 Ltr ML20045D9031993-06-21021 June 1993 LER 92-003-01:on 920207,discovered Potential Barrier Breach Via Direct Openings Around Main Feedwater Bypass Line Penetrations.On 920130,plant Entered Mode 4 W/O Encl Bldg Integrity.Erosion/Corrosion Exam Procedure Modified ML20045D3091993-06-18018 June 1993 LER 93-005-00:on 930520,cold Over Pressure Protection Sys Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Mgt Deficiency.Overlap Task Force Will Continue to Review Procedures Associated W/Reactor trip.W/930618 Ltr ML20045A4491993-06-0404 June 1993 LER 93-009-00:on 930506,inlet & Outlet skid-mounted Isolation Valves to Radiation Monitor Found Shut.Caused by Procedure Noncompliance by I&C Personnel.Personnel Will Review & Edit Radiation procedures.W/930604 Ltr ML20045A2321993-06-0101 June 1993 LER 93-008-00:on 930505,determined That Electrical Starter for Both Charging Pumps Inoperable.Caused by Program Failure.Administrative Controls Have Been Established to Ensure Minimum TS requirements.W/930601 Ltr ML20044C9191993-05-0707 May 1993 LER 93-002-01:on 930206 & 07,Train a & Train B CR Pressurization Sys Failed 18-month Surveillance Test, Respectively.Caused by Moisture in Air Banks & Pressure Oscillations.Air Banks purged.W/930507 Ltr ML20044C9331993-04-30030 April 1993 LER 91-002-01:on 910118,engineering Evaluation Determined That Operation of Four Vital 120-volt Ac Buses,On Alternate Sources,Unsatisfactory.Caused by Failure to Update TS to Reflect Configuration.Inverter Sys replaced.W/930430 Ltr ML19346B2411992-08-20020 August 1992 LER 92-018-00:on 920722,both RHR Trains Rendered Inoperable Due to Procedure Deficiency.Both Trains of RHR Restored to Operable Condition & Surveillance Procedures for Both Trains revised.W/920820 Ltr ML20024H3241991-05-24024 May 1991 LER 91-001-01:on 910110,electro-hydraulic Control Sys Failure Occurred,Causing Reactor Trip.Caused by Turbine Trip.Both EHC Pump Discharge Filters Changed Out & Pump B Replaced W/Spare pump.W/910524 Ltr ML20029C1281991-03-18018 March 1991 LER 91-004-00:on 910216,unexpected Trip of 'B' Steam Generator Feed Pump & Subsequent Manual Reactor Trip Occurred.Cause Unknown.Monitoring Capability Added to Sgfp Circuitry & Design Change made.W/910318 Ltr ML20029B6001991-03-0707 March 1991 LER 91-004-00:on 910205,leakage Found During Local Leak Rate Testing for Four Containment Isolation Valves.Caused by Improper Valve Seating.Valve Removed from Svc & Sent to Mfg for overhaul.W/910307 Ltr ML20029B6031991-03-0404 March 1991 LER 91-002-00:on 910202,setpoint Drift Identified During Testing of Main Steam Safety Valves.Caused by Inadequate Design.Nine out-of-tolerance Valves Reset within Specified +1% Tolerance ML20029B5981991-03-0404 March 1991 LER 91-003-00:on 910203 & 16,spurious Control Bldg Isolation Signals Received from Train a Control Bldg Ventilation Inlet Radiation Monitor.Caused by Equipment Malfunction.Detector replaced.W/910304 Ltr ML20029A6501991-02-19019 February 1991 LER 91-001-00:on 910117,discovered That Source Check Surveillance Procedure to Verify Operability of Beta Scintillation Radiation Detectors Did Not Meet TS Requirements.Surveillance Procedure revised.W/910219 Ltr ML20028H4261990-12-27027 December 1990 LER 89-005-01:on 890330,intermittent Connection While Sliding Module Into Position Caused Automatic Test Insertion Circuit to Send Signals Greater than Normal Pulse Thus Allowing Three SIAS Modules to actuate.W/901227 Ltr ML20028H4391990-12-27027 December 1990 LER 90-015-01:on 900919,inadvertent Isolation of Containment Isolation Valves Occurred.On 900920,inadvertent Actuation of Sias,Containment Isolation Actuation Sys & Encl Bldg Filtration Sys occurred.W/901227 Ltr ML20028H4271990-12-27027 December 1990 LER 90-021-00:on 901127,LCO Paragraph 3.0.3 Entered.Caused by Poor Communications.Mgt Reviewed Event & Events Leading Up to Incident & Concluded That Increased Awareness W/ Respect to Sys Status Must Be pursued.W/901227 Ltr ML20028H4401990-12-24024 December 1990 LER 90-019-00:on 900606,automatic Reactor Trip from Negative Flux Rate Signal Occurred Due to Dropped Control Rod.Caused by Broken Connection in Gripper Coil Power Cable.Connector Replaced & Power Loop checked.W/901224 Ltr ML20028G9421990-09-26026 September 1990 LER 90-012-00:on 900827,automatic Reactor Trip Occurred During Bypass Switch Operations.Caused by Operator Error. Procedure Sp 2601D Revised to Incorporate Separate Section on Performing calibrs.W/900926 Ltr ML20028G9111990-09-18018 September 1990 LER 89-008-01:on 891002,determined That Plant Failed to Perform Functional Check of Control Board Annunciators During Channel Functional Tests.Caused by Personnel Error. Procedures Revised Re Annuciator testing.W/900918 Ltr ML20044B0441990-07-10010 July 1990 LER 90-007-00:on 900611,discovered That Surveillance Procedure 2609E Re Encl Bldg Filtration Sys Testing - Refueling Not Performed Prior to Entering Mode 4.Caused by Personnel Error.Missed Surveillance performed.W/900710 Ltr ML20044A1581990-06-18018 June 1990 LER 90-017-00:on 900518,loss of Both Trains of HPSI Occurred.Caused by Cognitive Failure by Licensed Operator. Personnel Counseled on Causes of Event & Importance of Recognizing When Event reportable.W/900618 Ltr ML20043H2021990-06-15015 June 1990 LER 90-005-00:on 900503,identified Potential for High Energy Line Break in Auxiliary Steam Sys That Could Degrade Plant Areas Determined as Mild Environs.Probably Caused by Incorrect Conclusions from Analysis in 1973.W/900615 Ltr ML20043G1031990-06-12012 June 1990 LER 90-016-00:on 900513,steam Generator B lo-lo Signal Generated Reactor Trip Signal,Causing Automatic Start of motor-driven Auxiliary Feedwater Pumps a & B.Caused by Inadequate Guidance.Procedure revised.W/900612 Ltr ML20043G3921990-06-11011 June 1990 LER 90-014-00:on 900519,manual Reactor Trip Initiated as Result of Anticipated Turbine Trip Due to Condenser Vacuum. Caused by Design Deficiency in That Traveling Screen Capacity Inadequate.Traveling Screen modified.W/900611 Ltr ML20043F7021990-06-11011 June 1990 LER 90-015-00:on 900512,feedwater Isolation Occurred While Opening Msivs.Caused by MSIV 2 Opening Faster than Other Msivs,Resulting in Swell in Steam Generator 2.Steam Generator Level Restored to normal.W/900611 Ltr ML20043F8261990-06-0707 June 1990 LER 90-006-00:on 900508,reactor Manually Tripped When Decreasing Levels Noted in Steam Generator 1 & Feedwater Regulating Valve Indicated Full Open.Caused by Valve Stem Separating from Plug.Feedwater Flow restored.W/900607 Ltr ML20043D4711990-05-30030 May 1990 LER 85-002-01:on 850302 & 25,unplanned Actuation of Containment Purge Valve Isolation Occurred.Caused by Personnel Error.Caution Signs Placed on Radiation Monitors & Reset Button on Monitor Made inaccessible.W/900530 Ltr ML20043A7841990-05-16016 May 1990 LER 90-013-00:on 900416,manual Reactor Trip Initiated Due to Imminent Loss of Condenser Vaccum.Caused by Inadequate Administrative Guidance When Debris Collected on Trash Rack. Severe Weather Procedure revised.W/900516 Ltr ML20042G7201990-05-0707 May 1990 LER 90-012-00:on 900406,review of Steam Generator Blowdown Monitor High Radiation Alarm Setpoint Revealed That Setpoint Was Nonconservative.Caused by Administrative Deficiency. Correct Setpoint installed.W/900507 Ltr ML20042E6751990-04-20020 April 1990 LER 90-002-00:on 900322,Tech Spec Action Statement 3.3.3.10 Not Entered for Out of Svc Stack Gas & Particulate Radiation Monitor.No Particulate Radiation Increases Detected.Caused by Personnel error.W/900420 Ltr ML20042E1621990-04-0909 April 1990 LER 90-009-00:on 900309,automatic Turbine Trip W/Subsequent Reactor Trip Occurred Due to High Stator Cooling Water Temp. Caused by Failure of Mechanical Linkage on Fisher & Portor Controller.Controller Replaced w/spare.W/900409 Ltr ML17223A7901990-04-0202 April 1990 LER 89-009-01:on 891025,radiation Monitor RM 8262 Inlet Valve (2-AC-82) Found Closed.Caused by Personnel Error. Isolation Valve Opened,Sample Flow Restored & Radiation Monitor Restored to Operable status.W/900402 Ltr 1994-05-02 Category:TEXT-SAFETY REPORT MONTHYEARML20217P5391999-10-25025 October 1999
[Table view]Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20211A6631999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level,Operating Data Rept & Unit Shutdowns & Power Reductions B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17807, Monthly Operating Rept for May 1999 for Mnps,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 1.With ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206J8351999-05-0707 May 1999 Rev 20,Change 7 to QAP-1.0, Northeast Utls QA Program (Nuqap) Tr ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 B17782, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With ML20205R3531999-04-30030 April 1999 Addendum 4 to Annual Rept, B17775, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With ML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20206E2971999-04-30030 April 1999 Rev 1 to Millstone Nuclear Power Station,Unit 2 COLR - Cycle 13 B17777, Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with ML20205Q5891999-04-0909 April 1999 Rev 20,change 6 to QAP-1.0,Northeast Utils QA Program TR ML20205R8751999-04-0909 April 1999 Provides Commission with Staff Assessment of Issues Related to Restart of Millstone Unit 2 & Staff Recommendations Re Restart Authorization for Millstone Unit 2 ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 B17747, Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With 1999-09-30 |
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U. 5. C:UCLE AQ CEcuL ATC;iY COMMtSSION senC f On64 356 LICENSEE EVENT REPO lT CONTROL BLOCK: l l l l l
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EVENT DESCRIPTION AND PROSABLE CONSEQUENCES h o 2 l While at 100% power, the plant computer nm1 functioned and was declared incoerable. I I
g i peration O continued per TSAS 3.2.1 and 3.1.3.3.d for a 3 hour3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> oeriod.
- Power was re-I g i duced and core power distribution was monitored with excore detectors per TSAS g l 4.2.1.2. Similar events82-017, 81-009,80-008, 79-020,79-005, 78-027,78-021, I I
g l_78-012, and 77-041.
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