IR 05000454/2008005

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February 10, 2009

Mr. Charles Senior Vice President, Exelon Generation Company, LLC President and Chief Nuclear Officer (CNO), Exelon Nuclear 4300 Winfield Road Warrenville IL 60555

SUBJECT: BYRON STATION, UNITS 1 AND 2 INTEGRATED INSPECTION REPORT 05000454/2008-005 05000455/2008-005

Dear Mr. Pardee:

On December 31, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Byron Station, Units 1 and 2. The enclosed inspection report documents the inspection findings which were discussed on January 15, 2009, with Mr. D. Hoots and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, two NRC-identified findings of very low safety significance were identified. The findings involved violations of NRC requirements. However, because of their very low safety significance, and because the issues were entered into your corrective action program, the NRC is treating the issues as Non-Cited Violations in accordance with Section VI.A.1 of the NRC Enforcement Policy. Furthermore, four licensee identified violations are listed in Section 4OA7 of this report. If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Byron Station. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/ Richard A. Skokowski, Chief Branch 3 Division of Reactor Projects Docket Nos. 50-454; 50-455 License Nos. NPF-37; NPF-66

Enclosure:

Inspection Report No. 05000454/2008-005 and 05000455/2008-005

w/Attachment:

Supplemental Information cc w/encl: Site Vice President - Byron Station Plant Manager - Byron Station Manager Regulatory Assurance - Byron Station Senior Vice President - Midwest Operations Senior Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Director - Licensing and Regulatory Affairs Manager Licensing - Braidwood, Byron, and LaSalle Associate General Counsel Document Control Desk - Licensing Assistant Attorney General Illinois Emergency Management Agency J. Klinger, State Liaison Officer, Illinois Emergency Management Agency P. Schmidt, State Liaison Officer, State of Wisconsin Chairman, Illinois Commerce Commission B. Quigley, Byron Station

SUMMARY OF FINDINGS


1

REPORT DETAILS


.3 Summary of Plant Status -------------------------.3

REACTOR SAFETY

....----------------------.3

1R01 Adverse Weather Protection

.....................................................3

1R04 Equipment Alignment

................................................................4

1R05 Fire Protection

...........................................................................4

1R06 Flooding

....----------------------.6

1R07 Annual Heat Sink Performance

.................................................6

1R11 Licensed Operator Requalification Program

.............................7

1R12 Maintenance Effectiveness

.......................................................8

1R13 Maintenance Risk Assessments and Emergent Work Control

..9

1R15 Operability Evaluations

...........................................................10

1R18 Plant Modifications

..................................................................11

1R19 Post-Maintenance Testing

......................................................12

1R20 Outage Activities

.....................................................................13

1R22 Surveillance Testing

................................................................15

1EP6 Drill Evaluation

........................................................................18 2. Radiation SAFETY......---------------------..19 2OS1 Access Control to Radiologically Significant Areas (71121.01).................19 2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)...22

4OA1 Performance Indicator Verification

...............................................23

4OA2 Identification and Resolution of Problems

....................................28

4OA5 Other Activities -------------------------30 4OA6

Management Meetings---------------------..32 4OA7 Licensee-Identified Violations....................................................................33

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

D. Hoots, Site Vice President
W. Grundmann, Regulatory Assurance Manager
Z. Cox, Chemist
G. Contrady, Programs Manager
H. Do, Corporate ISI Engineer
S. Greenlee, Engineering Director
D. Thompson, Radiation Protection Manager

Nuclear Regulatory Commission

R. Skokowski, Branch Chief

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened

05000454/2008005-01
05000455/2008005-01 NCV Failure to Remove or Evaluate Loose Debris Inside of Containment Prior to Applicable Mode
05000454/2008005-02
05000455/2008005-02 NCV Failure to Evaluate Radiological Hazards for Airborne Radioactivity

Closed

05000454/2008005-01
05000455/FIN-2008005-01 NCV Failure to Remove or Evaluate Loose Debris Inside of Containment Prior to Applicable Mode
05000454/2008005-02
05000455/FIN-2008005-02 NCV Failure to Evaluate Radiological Hazards for Airborne Radioactivity
05000454;
455/2008-003-06 URI Unit 1 and Unit 2 Auxiliary Feedwater Tunnel Hatch Margin to Safety
2

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection.

Inclusion on this list does not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that selected sections of portions of the documents were evaluated as part of the overall inspection effort.
Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report.

Section 1R01: Adverse Weather Protection

WO 1020141 01; 89-13 Heat Exchanger Inspection for 2B Diesel Driven AF Pump Closed Cycle Cooler, October 16, 2008 Issue
846625; Procedure Enhancement, November 18, 2008 BOP
SX-T2; SX Tower Operations Guidelines, Revision 12

Section 1R04: Equipment Alignment (Quarterly) 2BOSR 7.8.1-1; Unit 2 Essential Service Water System Valve Position Monthly Surveillance, Revision 16

BOP
DG-1; Diesel Generator Alignment to Standby Condition, Revision 11
BOP
VD-5; DG Room Ventilation System Operation, Revision 6
BwOP
VD-5; DG Room Ventilation System operation, Revision 12
BwOS
VD-1a; Diesel Ventilation Systems; Revision 4 10
CFR 50.59 Screening, BOP Vd-5 DG Room Ventilation System Operation; January 06, 1986
Corrective Action Documents as a Result of NRC Inspection
IR 852537; Compensatory Actions Not Procedurally Directed, December 4, 2008

Section 1R05: Fire Protection (Quarterly) Corrective Action Documents as a Result of

NRC Inspection
IR 842026; Fire Zone Walkdown Issues, November 07, 2008
IR 850920; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
IR 850922; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
IR 850925; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
IR 850926; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
IR 850929; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
IR 850931; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
IR 850932; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
IR 842026; Fire Zone Walkdown Issues, November 07, 2008
IR 847572; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008

Section 1R05: Fire Protection (Annual)

BAP 1100-10; Response Procedure for Fire, Revision 7
BAP 1100-10T1; 401' Fire Brigade Equipment Inventory, Revision 7
Byron Emergency Self-Contained Breathing Apparatus Storage Locations Monthly Inventory, September 2008
OP-AA-201-003; Fire Drill Performance, Revision 7
3OP-AA-201-005; Fire Brigade Qualification, Revision 6
OP-AA-201-008; Pre-Fire Plans, Revision 1
RP-BY-1000; Maintenance Care and Inspection of the ISI Viking Self-Contained Breathing Apparatus (SCBA), Revision 9 Self-Contained Breathing Apparatus Monthly Inspection, September 2008
Byron Station Fire Drill Critique Form, August 24, 2008
Summary Report for Each Shift Reflecting Fire Brigade and HazMat Qualification Status, October 12, 2008
IR 823253; Safe-Guards Information Slows Fire Response, September 27, 2008

Section 1R07: Heat Sink Performance

WO 1036955; Perform As-Found/As-Left Inspections of 2C RCFC Issue
830146; Replace RCFC Channel Heads with stainless Steel in B2R15, October 13, 2008
IR 830370; Restricted Tubes in 2C RCFC, Need to Plug, October 13, 2008
IR 829315; 2C RCFC Channel Head Degradation, Divider Plates, October 10, 2008

Section 1R08: Inservice Inspection Activities

IR 829647; Penetration 41 Not Examined During B2R13; October 11, 2008
IR 831084; Foreign Objects Found In 2C SG Secondary Side - B2R14; October 15, 2008
IR 829610; Acceptance Criteria Used On SX Pipe Was Not Appropriate; October 11, 2008
IR 843635, Steam Generator Tube Sheet Inspection Results - B2R14, November 11, 2008
IR 832181; Foreign Objects Found In 2A SG Secondary - B2R14; dated October 17, 2008
IR 830452; B2R14 - Weld Defects Revealed During Radiography Of Repair;
October 14, 2008
IT00717275-02; Buildup of Deposits in Steam Generators, NRC
IN 2007-37
ER-AP-335-1012; Bare Metal Visual Examination of PWR Vessel Penetration and Nozzle Safe-Ends; Revision 3
ER-AP-335-040; Evaluation of Eddy Current Data for Steam Generator Tubing; Revision 4
EXE-ISI-11; Liquid Penetrant Examination, Revision 4
EXE-UT-350; Procedure for Acquiring Material Thickness and Weld Contours; Revision 2
EXE-PDI-UT-2; Ultrasonic Examination of Austenitic Piping Welds in Accordance with
PDI-UT-2; Revision 5
EXAE-ISI-8;
VT-1 Direct; Revision 1
ER-AP-335-039; Multi-Frequency Eddy Current Data Acquisition of Steam Generator Tubing;
Revision 5
ER-MW-335-1009; Site Specific Performance; Revision 4
ER-AP-331; Boric Acid Corrosion Control (BACC) Program; Revision 3
ER-AP-331-1001; Boric Acid Corrosion control (BACC) Inspection Locations, Implementation and Inspection Guidelines; Revision 3
ER-AP-331-1002; Boric Acid Corrosion control Program Identification, Screening, and Evaluation; Revision 4
ER-AP-331-1004; Boric Acid Corrosion Control (BACC) Training and Qualification, Revision 2
ER-AP-420-002; Byron/Braidwood Unit 2:
Steam Generator Eddy Current Activities; Revision 8

Section 1R11: Licensed Operator Requalification Program

Six Reactor Operator Biennial Written Examinations for
CY 2008; no dates Thirty Senior Reactor Operator Examination Questions for
CY 2008 Exams; no dates Twelve Dynamic Simulator Scenarios; no dates
448 Job Performance Measures; no dates Licensed Operator Written Examination and Operating Test Results,
CY 2008; no date

Section 1R12: Maintenance Effectiveness

IR 417274; Hydramotor Indication Shows Open but Damper Blades are Closed, March 11, 2002
IR 460411; VA Supply/Exhaust Fan Vibration Alarm Setpoint Basis Concern
IR 717005;
VA-Tolerance for Equipment Degradation, January 1, 2008
IR 726481; High Vibrations on 0C VA Fan (Supply Fan), January 24, 2008
IR 727128; VA Issues, January 26, 2008
IR 735812; VA Concerns, February 13, 2001
IR 748406; Need (A)(1) Determination: VA Unacceptable Performance Trend, March 12, 2008
IR 850742; Control Damper Problems for 1A DG Ventilation, December 01, 2008
IR 869580; MM Expanded Scope Replace Linear Converter, January 23, 2007
IR 999934; Replace Linear Converter, November 07, 2008
WO 99270872; 1A DG Vent Outside Damp Not Fully Closed, September 13, 2008 VA Degradation/Status Presentations to the Plant Health Committee, December 10, 2007, February 4, 2008, and May 5, 2008

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Unit 1 Risk Configurations; Week of October 13, 2008, Revision 3 Unit 2 Risk Configurations; Week of November 17, 2008
Protected Equipment Log for 2B DG Outage, October 11, 2008
Protected Equipment Log for Line 0622/Bus 12 Outage, October 12, 2008
Protected Equipment Log for Unit 0 Component Cooling Water Heat Exchanger, October 11, 2008 Protected Equipment Log for Unit 2 CC Heat Exchanger, November 16, 2008 Protected Equipment Log for 2RA RH Pump Suction OOS, November 17, 2008
B2R14 Shutdown Risk Evaluation; October 15, 2008
B2R14 Outage Status, October 16, 2008
Byron Operations Log; October 15, 2008, to October 16, 2008
OU-AP-104; Shutdown Safety Management Program Byron/Braidwood Annex, Revision 11
IR 832167; NOS Identified OPS Lacks Sensitivity to OLR/SDR, October 17, 2008
Unit 0/1/2 Standing Order; Operator Ownership During IMD Surveillances, October 17, 2008
IR 829481; NOS ID Shutdown Risk Vulnerability, October 10, 2008

Section 1R15: Operability Evaluations

IR 810117; Unit 1 LM Indicates Potential Source of Noise as Near 1RC8002D, August 22, 2008
IR 810867; Expansion Tank Overflow When Started and Running, August 26, 2008
IR 814019; Low JW Level in the 1B AF Pump, September 04, 2008
IR 846398; Need Work Order Created to Replace Grease, November 18, 2008
IR 846420; 2SI8811A; Motor Found Degraded Per Inspection Criteria, November 18, 2008
EC 366163; Operations Evaluation 07-005, Unventable Gas Voids in Containment Recirculation Sump Piping, November 20, 2008
EC 371879; Operations Evaluation 08-007, Gas Void at 2CS009A, November 20, 2008
EC 371965; Operations Evaluation 08-008, 2B AF Pump Jacket Water Overflow, Revision 000
EC 373393; Operations Evaluation 08-010, 1B DG Cylinder and Head Indications, December 18, 2008 Fluid Analysis Report; Unit 2 AF Cooler, September 24, 2008
5Operational and Technical Decision Making 2008 - 2009; Suspect 1RC8002D Valve guide(s) Not Properly Retained in Valve Body Adverse Condition Monitoring and Contingency Plan; Unit 1 Loose Parts Monitoring System (LPMS) Noise, August 26, 2008
CAE-02-31 Westinghouse Letter; LSIV Loose Parts 50.59 Screen
EVAL-02-062, Revision 1, March 21, 2002
WO 1072112 02; MOV PM, Actuator Inspection, Diagnostic testing, November 18, 2008

Section 1R18: Plant Modifications

IR 842362; 2CV181 "2A RCP Standpipe PW Supply Valve" Failed to Close, November 08, 2008
IR 843783; Unexpected Alarm, November 12, 2008
IR 846404; Revised Bars for
TCP 373002 are Incorrect, November 18, 2008
EC 373002; Installation of Temporary Line to Connect the Drain Lines of RCP Standpipes 2A

and 2D, Revision 0

EC 371360; Install Vent Valve on 2SI05CA-8, Revision 2
EC 373224; Provide Temporary Fans for 1A DG Room, Revision 0
WO 01149077; Install Vent Valve on 2SI05CA-8, October 18, 2008
WO 01149077 13; SEP PMT:
VT-2 of 2SI130, October 15, 2008
WO 01149077 14; OP PMT: Verify No Seat leakage on 2SI130, October 15, 2008
WO 01149077 15; SEP PMT: Record Vibe Data 2SI130 at Full Flow Conditions, October 15, 2008

Section 1R19: Post Maintenance Testing

1BOSR 3.2.8-610B; Unit 1 ESFAS Instrumentation Slave Relay Surveillance and Automatic Actuation Test (Train B Automatic Safety Injection - K610), Revision 2 2BOSR 7.5.5-2; Unit 2 Train B Auxiliary Feedwater Valve Emergency Actuation Signal Verification Test, Revision 4
WO 999110; 1AP12E-A Relay #1-RCF2 for 1VP01CB Operations PMT Partial 1BOSR 3.2.8-
610B, November 25, 2008 2BOSR 3.2.8-632A; ESFAS Instrumentation Slave Relay Surveillance (Train A Auxiliary Feedwater Actuation - Relays k632, K639, Revision 2
WO 1165207 01;
MM-Repair of 2SI8818C During B2R14
WO 1165207 04; EP - Perform Visual Examination of Disassembled Check Valve
WO 1165207 06; Operations PMT - 2SI8818C SLT Per 2BOSR 4.14.1-1
WO 1165207 07; Operations PMT - 2SI8818C CO Per 2BOSR 5.5.8RH.2-2
WO 1020023 01; 2RH25
VT-2 Exam, October 15, 2008 ASME Section XI Repair/Replacement Plan; 2SI8818C (Loop 3 Cold Leg Accumulation Injection Check Valve, September 29, 2008
BOP
CV-19; Switching Charging Pumps, Revision 14
1BOSR 5.5.1-1; Unit 1 RCS Seal Injection Flow Verification Monthly Surveillance, Revision 4 2BVSR 5.c.2-1; Unit 2 Charging/Safety Injection System Flow Balance, Revision 4

Section 1R20: Refueling and Outage Activities Ultrasonic Thickness Calibration Data Sheet; Report Number 2008-707

IR 826879; Calibrate/Repair 2FI-0928A, October 05, 2008
IR 834405; Need B2R15 W/O to Retrieve Rag and Wire From Upender Pit B2R14 Work Orders Added to Date, October 15, 2008
6List of Work Orders Removed from B2R14 via SCARF Process as of 7:00 am on October 16, 2008
1BGP 100-2; Plant Startup, Revision 37 1BGP 100-2A1; Reactor Startup, Revision 26 1BGP 100-2TI; Plant Startup Flowchart, Revision 10
1BGP 100-2T3; Reactor Startup Flowchart, Revision 5
1BGP 100-4; Power Descension, Revision 36
1BGP 100-4T1; Power Descension Flowchart, Revision 11
1BGP 100-5; Plant Shutdown and Cooldown, Revision 53 1BGP 100-5TI; Plant Shutdown and Cooldown Flowchart, Revision 26 BOP
RH-6; Operation of the RH System in Shutdown Cooling, Revision 36
BOP
RH-8; Filling the Refueling Cavity for Refueling, Revision 18
BOP
RH-9; Pump Down of the Refueling Cavity to the RWST, Revision 24
ALM Corporation Material Handling Platform Lift Manual
BAP 1450-1; Access to Containment, Revision 37 2BOSR Z.5.B.1-1; Containment Loose Debris Inspection, Revision 0
Issue
834555; B2R14 Reactor Cavity Hoist Cable Ties, October 22, 2008
LS-AA-125; Corrective Action Program Procedure, Revision 12
IR 833539; White Plastic Cable Tie Not Immediately Retrievable, October 20, 2008
IR 834002; Foreign Material in 2B ECCS Recirculation Sump, October 21,2008
IR 834087; Loose Debris Walkdown Items Requiring Disposition, October 21, 2008
IR 835427; B2R14 LL - Weakness in Control of Material Left in Containment, October 23, 2008
EC 372856; Evaluation of Foreign Material in Unit 2 Containment Building, November 12, 2008
Corrective Action Documents as a Result of NRC Inspection
IR 833612; Inactive Boric Acid Leak on 2SI8822C, October 20, 2008
IR 833613; Inactive Boric Acid Leak on 2SI8810C, October 20, 2008
IR 833881; Inactive Boric Acid Leak, System Not Verified At This Time, October 21, 2008
IR 834410; B2R14 NRC Mode 3 Containment Walkdown Identified Items, October 22, 2008
IR 856813; Operator Missing a Cover During Mode 4 Walkdown, December 16, 2008
IR 856819; 2LL091E Trickle Charge Light Is Out, December 16, 2008
IR 834410; B2R14 NRC Mode 3 Containment Walkdown Identified Items, October 22, 2008

Section 1R22: Surveillance Testing 1BOSR 6.1.1-11; Primary Containment Type C Local Leakage Rate Tests and

IST Tests of Pressurizer Relief System "Partial for 1RY8028", Revision 7 2BOSR 7.5.4-2; Unit 2 Diesel Driven Auxiliary Feedwater Pump Monthly Surveillance, Revision 16
2BOSR 7.5.5-2; Unit 2 Train B Auxiliary Feedwater Valve Verification Test, Revision 4
2BOSR 8.1.2-1; Unit 2 A Diesel Generator Operability Surveillance, Revision 21
2BVSR 5.c.2-1; Unit 2 Charging/Safety Injection System Flow Balance, Revision 4
WO 1024422 01; 2B Diesel Generator SI Signal Override Test, October 14, 2008
WO 1028733 01; Reactor Coolant System CheckValve Leakage Surveillance, October 21, 2008
WO 1157684 01; 1CV01PB Group A IST Requirement for CV Pump, November 06, 2008
Byron Inservice Testing Bases Document; Valve EPN 2SI8818A-D, Loop A-D Cold Leg Accumulator Injection Check Valve Byron Inservice Testing Bases Document; Valve EPN 2SI8948A, Accumulator Outlet to RC Loop Second Check Valve
7BOP
DG-11; Diesel Generator Startup, Revision 20 BOP
DG-12; Diesel Generator Shutdown, Revision 19
Corrective Action Documents as a Result of NRC Inspection
IR 841953; IST Basis Documents for 1/2SI8818A-D Need Updating, November 06, 2008
IR 841953; IST Basis Documents for 1/2SI8818A-D Need Updating, November 07, 2008

Section 2OS1: Access Control to Radiologically Significant Areas

RP-AA-460; Controls for High Radiation and Locked High Radiation Areas; Revision 17
RP-AA-460-001; Controls for Very High Radiation Areas; Revision 1
RP-AA-460; Access to Reactor Incore Sump Area; Revision 2
RP-
BY-500-1003; Radiological Controls for Handling Items and Hanging Activated Parts in the Spent Fuel Pool Radiation Work Permit and Associated ALARA Reviews;
RWP 10008926; B2R14 Seal Table - Rack Disconnect/Maintenance/Eddy Current/Restoration Radiation Work Permit and Associated ALARA Reviews;
RWP 10009830; P-68 Penetrant Test and Vent Line Inspection
IR 795311; RWP Violations (PC Requirements); dated July 10, 2008
IR 761294; Level 1 Personal Contamination Event; dated 9, 2008
IR 756342; Worker Entered A/D Platform without Electronic Dosimeter; dated March 29, 2008
IR 754696; Worker Locked Out of RCA - Rad Worker Behavior; dated March 26, 2008
IR 756136; PCE: B1R15 Personal Contamination Event; dated March 28, 2008
IR 673712; RP Not Effectively Using Corrective Action Program; dated September 20, 2007
IR 755986; Alpha Survey Documentation Gaps; dated March 27, 2008
IR 756296;
RP-AA-460-1001; Not Completed in Timely Manner; dated March 28, 2008
IR 812338; Ni-63 Source Leak Tests Exceed 6-Month Surveillance Frequency; dated August 22, 2008

Section 1EP6: Drill Evaluation

IR 844467; OSC Minimum Staffing Not Met for Crew D in Drill, November 13, 2008 Byron 2008 Drive-In Drill; Scenario Information Nuclear Accident Reporting System (NARS) Form; Utility Message No. 2, November 12, 2008
Issue
844467; OSC Minimum Staffing Not Met for During Drill, November 12, 2008

Section 4OA1: Performance Indicator Verification

LS-AA-2090; Monthly Data Elements for NRC Reactor Coolant System (RCS) Specific Activity; dated July 3, 2007 through September 2, 2008
LS-AA-2100; Monthly Data Elements for NRC Reactor Coolant System Leakage, Revision 5
LS-AA-2150; Monthly Data Elements for RETS/ODCM Radiological Effluent Occurrences; dated July 10, 2007 through September 10, 2008
MSPI Derivation Report; Unit 1 and Unit 2 High Pressure Injection System Unavailability and Unreliability Index, February 2008 Operations Log; February 01, 2008 - February 29, 2008
MSPI Derivation Report; Unit 1 and Unit 2 Cooling Water System Unavailability and Unreliability Index, March 2008
IR 854124; Inconsequential Error identified in March 2008 MSPI Data for SX, December 09, 2008
8Operations Log; March 01, 2008 - March 31, 2008 MSPI Derivation Report; Unit 1 and Unit 2 Residual Heat Removal System Unavailability and Unreliability Index, July 2008 Operations Log; July 01, 2008 - July 31, 2008 MSPI Derivation Report; Unit 1 and Heat Removal System Unavailability and Unreliability Index, October 2007
Operations Log; October 01, 2007 - October 31, 2007
MSPI Derivation Report; Unit 1 and Unit 2 Heat Removal System Unavailability and Unreliability Index, April 2008 Operations Log; March 01, 2008 - March 31, 2008 Operations Log; October 01, 2007 - October 31, 2007
MSPI Derivation Report; Unit 1 and Unit 2 Emergency AC Power System Unavailability and Unreliability Index, June 2008
Operations Log, June 01, 2008 - June 30, 2008

Section 4OA2: Identification and Resolution of Problems

IR 642107; IST Program Implementation, June 19, 2007
IR 678543; Possible Pre-Conditioning Issue - IST Testing, October 1, 2007
IR 686518; Byron Review of Braidwood Potential Pre-Conditioning Issue, October 18, 2007
ER-AA-302-1006; Generic Letter 96-05 Program Motor-Operated Valve Maintenance and Testing Guidelines, Revision 7

Section 4OA5: Other Activities 1BOSR 8.1.14-1; Unit 1A Diesel Generator 24 Hour Endurance Run, Revision 10 1BOSR 8.1.14-2; Unit 1B Diesel Generator 24 Hour Endurance Run, Revision 8 2BOSR 8.1.14-1; Unit 2A Diesel Generator 24 Hour Endurance Run, Revision 10 2BOSR 8.1.14-2; Unit 2B Diesel Generator 24 Hour Endurance Run, Revision 10

Calculation 19-T-5; Diesel Generator Loading During LOOP/LOCA, Revision 6

LIST OF ACRONYMS

US [[]]
ED [[]]
AFW Auxiliary Feedwater System

ALARA As Low As Reasonably Achievable

CAP Corrective Action Program

CFR Code of Federal Regulations

JPM Job Performance Measure
IMC Inspection Manual Chapter

IP Inspection Procedure IR Inspection Report

IR Issue Report

IST Inservice Testing
LORT Licensed Operator Requalification Training

MSPI Mitigating Systems Performance Index NCV Non-Cited Violation

NEI Nuclear Energy Institute

NRC U.S. Nuclear Regulatory Commission
OOS Out of Service

ODCM Offsite Dose Calculation Manual OSP Outage Safety Plan

PI Performance Indicator
RC [[]]

FC Reactor Containment Fan Cooler

RCS Reactor Coolant System
RETS Radiological Effluent Technical Specifications

RWP Radiation Work Permit SDP Significance Determination Process

TI Temporary Instructions

TS Technical Specification
UFSAR Updated Final Safety Analysis Report
URI Unresolved Item WO Work Order