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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML20012D9651990-03-22022 March 1990 RO 50-20/1990-1:on 900312,incorrect Calculation of Estimated Critical Position (ECP) Attained During Reactor Startup. Caused by Failure to Check Second Portion of ECP Calculation Performed by Individual in Training ML19345B9941980-11-26026 November 1980 RO 50-020/79-4A:supplemental Info Re Apparent Fuel Element Cladding Failure Originally Reported on 790702.Caused by Mfg Deficiency.Element Continously Monitored ML19312E6141980-05-27027 May 1980 Forwards Revised Page 2 of RO 50-20/80-2 Dtd 800523.Revision Corrects Second Paragraph of Section 7 Re Frequency of Blade Thickness Measurements & Clarifies Description of Electromagnetic Coupling of Blade ML19323G4221980-05-23023 May 1980 RO 50-20/80-02:on 800519,intermittent Binding of Shim Blade Number 1 Not in Accordance W/Tech Specs.Caused by Foreign Matl Impeding Motion.Electromagnet Containing Foreign Matl Replaced & Other Blades Checked ML19323D5081980-04-25025 April 1980 RO 50-20/80-1:on 800322,initial Rept Was Made Re Failure of Outer Door of Truck Airlock to Maintain Leak Rate of Bldg Containment Limits.Caused by Seal Leak in Outer Door. Door Will Not Be Routinely Opened Until Gasket Is Replaced ML19250C0681979-10-19019 October 1979 RO 50-20/79-5:on 791010,compiled 10-day Startup W/Only One Operable Nuclear Safety Channel Level Scram.Caused by Broken Resistor on Amplifier Circuit Board.Circuit Board Repaired 1990-03-22
[Table view] Category:LER)
MONTHYEARML20012D9651990-03-22022 March 1990 RO 50-20/1990-1:on 900312,incorrect Calculation of Estimated Critical Position (ECP) Attained During Reactor Startup. Caused by Failure to Check Second Portion of ECP Calculation Performed by Individual in Training ML19345B9941980-11-26026 November 1980 RO 50-020/79-4A:supplemental Info Re Apparent Fuel Element Cladding Failure Originally Reported on 790702.Caused by Mfg Deficiency.Element Continously Monitored ML19312E6141980-05-27027 May 1980 Forwards Revised Page 2 of RO 50-20/80-2 Dtd 800523.Revision Corrects Second Paragraph of Section 7 Re Frequency of Blade Thickness Measurements & Clarifies Description of Electromagnetic Coupling of Blade ML19323G4221980-05-23023 May 1980 RO 50-20/80-02:on 800519,intermittent Binding of Shim Blade Number 1 Not in Accordance W/Tech Specs.Caused by Foreign Matl Impeding Motion.Electromagnet Containing Foreign Matl Replaced & Other Blades Checked ML19323D5081980-04-25025 April 1980 RO 50-20/80-1:on 800322,initial Rept Was Made Re Failure of Outer Door of Truck Airlock to Maintain Leak Rate of Bldg Containment Limits.Caused by Seal Leak in Outer Door. Door Will Not Be Routinely Opened Until Gasket Is Replaced ML19250C0681979-10-19019 October 1979 RO 50-20/79-5:on 791010,compiled 10-day Startup W/Only One Operable Nuclear Safety Channel Level Scram.Caused by Broken Resistor on Amplifier Circuit Board.Circuit Board Repaired 1990-03-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20209C9331999-07-0808 July 1999 Vols 1 & 2 to SAR for Ma Institute of Technology Nuclear Reactor Lab ML20196K0331999-06-30030 June 1999 Quality Mgt Program for Generation of MITR-II Medical Therapy Facility Beams for Human Therapy, Reflecting Change to Provision 14 ML20205A6551999-03-19019 March 1999 Ro:On 990310,main Ventilation Damper Failed to Close on Receipt of High Radiation Test Signal.Cause Indeterminate. Relays Associated with Main Exhaust Damper/Fans & Main Intake Damper Were Replaced ML20206P5321999-01-0606 January 1999 Ro:On 981229,only One Nuclear Safety Period Scram Channel Was Operable,For Period of Five Minutes.Caused by Placement of Nuclear Safety Sys Channel 1 Input Signal Cable on Wrong Bnc Connector.Placed Channel on Correct Bns Connector ML20199H2371998-12-31031 December 1998 Revised SER for Fission Converter Facility ML20196B7541998-06-30030 June 1998 Mit Research Reactor Nuclear Reactor Lab Ma Inst of Technology,Annual Rept to Us NRC for Period 970701-980630. with ML20217E8071998-03-23023 March 1998 Ro:On 980127,containment Integrity No Longer Existed & Key Switch Was Still 'On' for One of Test & Calibr Procedures. Caused by Retrieving Tool Box from Truck Air Lock.Discussed Occurrence W/Personnel & Will Consider TS Rev Re Key Switch ML20217G2181997-10-0303 October 1997 SER for Fission Converter Facility ML20198P8071997-06-30030 June 1997 Annual Operating Rept for Jul 1996 - June 1997 ML20137L5901997-04-0303 April 1997 Safety Evaluation Supporting Amend 30 to License R-37 ML20129B3201996-06-30030 June 1996 Annual Rept to Us NRC for Period 950701-960630 ML20092K8281995-09-22022 September 1995 Corrective Action for RO 50-20/1995-4,re Abnormal Situations Which Occurred on 950711 ML20091K3091995-08-18018 August 1995 Ro:On 950809,malfunction of Shim Blade Drive Mechanism Occurred.Determined That Mechanism Experienced Intermittent Slippage When Blade Being Withdrawn.Blade Drive Mechanism Assembly Procedure PM 7.1.1.1 Will Be Reviewed ML20086T7571995-07-28028 July 1995 RO 50-20/1995-4:on 950720,operated W/One Shim Blade Fully Inserted.Caused by Failure of Licensed Operators to Follow Written Procedure for Investigating Mismatch.Failed Proximity Switches Replaced ML20092K2301995-06-30030 June 1995 Mit Research Reactor Annual Rept to NRC for Period Jul 1994 - June 1995 ML20082B8551995-03-30030 March 1995 RO 50-20/1995-2:on 950320,operation of Reactor in natural- Circulation Mode W/O Required Two Operable Nuclear Safety Level Channels Set to Scram at or Less than 100 Kw,Mitr TS 3.7 ML20078S2241995-02-17017 February 1995 Reportable Occurrence 50-020/95-01:on 950206,voltage & Specific Gravity Measurements of Cell of Emergency Battery Bank Recorded at Less than Specified Weekly SR in TS 4.3.5. C/A Will Modify SR to Monthly ML20072T3041994-06-30030 June 1994 Annual Rept for Mit Research Reactor for 930701-940630 ML20058Q2371993-12-17017 December 1993 RO 50-20/1993-1:on 931207,operation W/Fewer than Required Number of 100 Kw Nuclear Safety Sys Level Channels Identified.Caused by Faulty four-segment Relay in low-range Amplifier of Channel 5.Amplifier Replaced ML20056G8011993-06-30030 June 1993 Mit Research Reactor Nuclear Reactor Lab Mit,Annual Rept to NRC for Period 920701-930630 ML20128P4371993-02-16016 February 1993 Safety Evaluation Supporting Amend 27 to License R-37 ML20073H1451992-12-0909 December 1992 Study of MITR-II Core Tank Aging for Relicensing Consideration ML20114D9261992-06-30030 June 1992 Mit Research Reactor Nuclear Reactor Lab Mit,Annual Rept to NRC for 910701-920630 ML20094K0721992-03-12012 March 1992 RO 50-020/1992-2:on 911030,three Fission Chambers Missing During Annual Inventory of SNM Matl.Search for Missing Chambers Completed on 920311 W/O Locating Chambers.Snm Inventory for 1991 Has Been Amended ML20090D6661992-03-0202 March 1992 RO 50-20/92-1 on:920218,malfunction Occurred in Reactor Analog Controller Due to Improper Performance of Increase in Reactor Power.Caused by Operator Error.Analog Automatic Control Sys Investigated & Temporarily Repaired ML20082K5911991-08-22022 August 1991 RO 50-20/1991-1:on 910813,fission Product Gas Levels Rose from Normal Operating Levels to Max of 15% of Mpc.Caused by Small Blister on One of Element MIT-17 Fuel Plates. Corrective Action Consisted of Removing MIT-17 from Core ML20082L8451991-06-30030 June 1991 Mit Research Reactor Annual Rept to NRC for Jul 1990 to June 1991 ML20058N5741990-08-10010 August 1990 QA Program for MITR-II Spent Fuel Shipment ML20059G4331990-06-30030 June 1990 Mit Research Reactor Annual Rept to NRC for Jul 1989 - June 1990 ML20012D9651990-03-22022 March 1990 RO 50-20/1990-1:on 900312,incorrect Calculation of Estimated Critical Position (ECP) Attained During Reactor Startup. Caused by Failure to Check Second Portion of ECP Calculation Performed by Individual in Training ML20012C2771990-03-0909 March 1990 SER for BWR Coolant Chemistry Loop to Be Installed & Operated in Mitr ML20248C7111989-08-0404 August 1989 RO 50-20/1989-2:on 890726,console Operator Received Abnormal Bldg Alarm.Leak Test Revealed Crack on Sys Ref Line Which Senses Atmospheric Pressure Outside Containment.All Polyethylene Tubing in Sys Replaced ML20247H7041989-06-30030 June 1989 Mit Research Reactor Annual Rept for Jul 1988 - June 1989 ML20246P3071989-03-17017 March 1989 RO 50-20/1989-1:on 890308,operation W/Fewer than Required Number of Nuclear Safety Channel Level Scrams Due to Lack of High Voltage Power Supply (Hvps) to Channel 5.Reactor Shut Down & Hvps Energized to Supply Channel 5 ML20195K1161988-10-24024 October 1988 Suppl to PWR Loop Ser:Use of Large Circulating Pump ML20154J6221988-08-29029 August 1988 Revised Mit Research Reactor Annual Rept to NRC for Jul 1987 - June 1988 ML20153F5591988-06-30030 June 1988 Mit Research Reactor Annual Rept to NRC for Jul 1987 - June 1988 ML20154M6501988-05-26026 May 1988 RO 50-20/1988-1:on 880511,incipient Fuel Clad Defect Detected.Caused by Small Blister on One Element MIT-12 Fuel Plate.Element MIT-12 Removed from Core ML20151R7341988-04-19019 April 1988 Sser for PWR Coolant Chemistry Loop (Pccl) MITNRL-020 ML20236S4931987-11-19019 November 1987 RO 50-20/1987-2:on 871110,improper Performance of Reactor Reshim Resulted in Excessive Power Rise.Caused by Operator Error.Operator Suspended from All Licensed Duties Pending Further Review of Circumstances & Disciplinary Measures ML20237K6121987-06-30030 June 1987 Mit Research Reactor Annual Rept to NRC for Jul 1986 - June 1987 ML20151R7271987-02-13013 February 1987 SER for PWR Coolant Chemistry Loop (Pccl) MITNRL-020 ML20213G0601986-11-0606 November 1986 RO 50-20/1986-3:on 861027,shim Blade 6 Could Not Operate at full-out Position Due to Mechanical Interference.Caused by Misalignment of Blade Proximity Switch Tube.Switch Tube Reinstalled Properly ML20214V9001986-10-17017 October 1986 Revised RO 50-20/1986-2:on 861008,elevated Levels of Fission Gases Discovered in Primary Containment.Cause Undetermined. Refueling Initiated & Element MIT-19 Removed.All in-core Elements Sipped.No Abnormalities Found ML20214H9541986-10-17017 October 1986 RO 50-020/86-02:on 861008,elevated Levels of Fission Gases in Primary Containment Observed.Cause Unknown.Element MIT-19 Removed from Core & All in-core Elements Sipped ML20148B3011986-06-30030 June 1986 Mit Research Reactor Annual Rept to NRC for Period Jul 1985 - June 1986 ML20154S4591986-02-28028 February 1986 RO 50-20/1986-1:on 860219,fission Product Gas Levels Rose from Normal Operating Levels.Caused by Blister on Surface of Outer Fuel Plate of Element MIT-11.Element MIT-11 Removed from Core ML20214R3811986-01-31031 January 1986 Rept of Educational & Research Activities for Academic/ FY84-85 W/Selected Data from Previous Yrs ML20137G3661985-07-23023 July 1985 RO 50-20/1985-2:on 850715,defect in Fuel Element Cladding Observed.Caused by High Rate of Outgassing from Fuel Element MIT-32.Defective Element Removed ML20133H4081985-06-30030 June 1985 Mit Research Reactor Annual Rept to Us NRC for Jul 1984 - June 1985 1999-07-08
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f f f NUCLEAR REACTOR LABORATORY l MASSACHUSETTS INSTITUTE OF TECHNOLOGY '$[M oM.HARUNG 138 Albany Street Cambridge, Mass. 02139 L CLARK. JR.
o'ractor (617)253-42 11 Director of Reactor operahons April 25, 1980 Mr. Boyce H. Grier, Director U.S. Nuclear Regulatory Commission l Region #1 631 Park Avenue King of Prussia, Pennsylvania 19406 Attention: Mr. E. Greenman, Reactor Inspector Re: Reportable Occurrence 50-20/80-1, License R-37: Inability of the Outer Door of the Truck Lock to Maintain Containment Integrity Gentlemen:
1 Massachusetts Institute of Technology hereby submits this 10 day report of an occurrence at the MIT Research Reactor in accordance with Paragraphs 7.13.2d, 1.15.1, and 3.7.1 of the Technical Specifications.
An initial report was made by telephone to Region #1 (Mr. T. Stetka) on April 22; 1980.
The format and content of this report is based on Regulatory Guide 1.16.
- 1. Report No. 50-20/1980-1
- 2. a) Report Date: April 25, 1980 b) Date of Occurrence: April 19, 1980 - (Test data taken.)
April 22, 1980 - (Computer analysis of test data complete.)
- 3. Facility: M. I. T. Research Reactor 138 Albany Street Cambridge, Massachusetts 02139
- 4. Identification of Occurrence: Failure of the outer door of the truck airlock to maintain the leakage ra::e of the building containment at less than one percent of the contained air volume per day per psig pres-sure as specified by Technical Specification 3.5.2.
- 5. Conditions Prior to Occurrence: A normal reactor shutdown had been conducted at 0700 April 18, 1980 in order to perform a measurement of the containment building leak rate. This measurement is performed I annually as required by Technical Specification 4.2.l(a).
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Reportable Occurrence Report April 25, 1980 Page 2
- 6. Description of Occurrence: Preparations for the containment building leakage rate measurement began at 1000 April 18, 1980 in accord with approved test and calibration procedures. The test is conducted in two separate phases so that each isolation device of any building pene- )
tration that is equipped with a double closure may be tested separately.
This is done in order to demonstrate that containment integrity is ,
maintained even when one isolation device of a double-closure facility !
is open. This permits the use of airlocks for entry to and from the i building while the reactor is at power.
l Data from the second phase of the test, which was initiated at 0130 {
April 19, 1980, indicated that an excessive leak rate of approximately l 1.7 times permissible existed. Investigation showed that the high {
1eakage was occurring at the gasket of the outer door of the truck lock. i Accordingly, the inner truck lock door, which had been successfully {
tested during the first phase of the test and which had been opened to allow testing of the outer door during the second phase, was closed. '
The second phase of the test was restarted and successfully completed.
The two phases of the test demonstrated that all containment building closures except the outer door of the truck airlock were capable of maintaining containment integrity.
- 7. Description of Apparent Cause of Occurrence: This occurrence was due to leaks in the seal of the outer door of the truck airlock. The de-tected leaks are located on the side of the door nearest the restricted area fence.
- 8. Analysis of the Occurrence: The outer truck lock door's gasket is' physi-cally attached to the seating surface of a rigid metal frame that is en-bedded in the concrete structure that forms the truck lock. The truck lock's outer opening is sealed by six hydraulic rams that force the door against the gasket. There are three rams on each side of the 12.5 foot high door. Inasmuch as they are located at the bottom, middle, and top of each side, they do not apply a uniform force to the entire door. The force is strongest over the area directly under a ram and weakest at the points intermediate between any two rams.
The current gasket for the outer truck lock door was installed approxi-mately one year ago on April 30, 1979. The gasket is normally made of soft rubber. Being ductile, the rubber readily deforms under the non-uniform loading of the rams and seats the truck lock door. However, on this occasion, a harder grade of rubber had been used with the idea that it would not wear down as rapidly as did the softer material. Subsequent to the gasket replacement, the new gasket was tested as a part of the 1979 pressure test. It did not pass on the initial test trial, was re-worked, and was successfully tested.
i Reportable Occurrence Report April 25, 1980 Page 3 Since the gasket did not pass the April 19, 1980 pressure test, it is not clear that the outer truck lock door could be considered as a satis-factory seal at all times between the May 1979 and the April 19, 1980 test. The truck airlock is not routinely required for the conduct of reactor operations and is normally only used when the reactor is secured and conditions are such that containment integrity is not required. It is believed that the outer door of the truck airlock was only relied upon to provide containment integrity three times in the past year.
Each occasion lasted approximately fifteen minutes and all occurred dur-ing the period January - February 1980. No events occurred during any of these periods that would have necessitated the sealing and the isola-tion of the containment building. There were no occasions during the past year when excessive pressure existed within the building.
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- 9. Corrective Action: The immediate corrective actions consisted of: l l
(a) Placement of a " CAUTION" tag on the power supply to the truck air-lock. The tag states that the inner door of the truck airlock should not be opened unless containment integrity is not required. j (The power supply itself is, and has been, in an area that is always locked while the reactor is in operation. The console opera-tor is in possession of the only key.)
(b) Circulation to all licensed, maintenance, and electronic personnel of a memo stating the conditions under which the inner door of the truck airlock can be opened. Signed copies of this memo have been returned to the Superintendent by all individuals who might use the truck lock.
(c) Inspection of the metal door surfaces for evidence of wear. None was found.
Permanent corrective action will consist of: l (a) Replacement of the existing gasket with one of the proper hardness.
(b) Repetition of the air leakage test on the outer door of the truck lock upon installation of the new gasket.
Subsequent actions will depend on the results of the leakage test. If the new gasket fails or is marginal, consideration will be given to either reanalyzing the outer truck lock door or to developing a reliable procedure to properly seat the gasket. Restrictions on the use of the.
inner door would, of course, remain in effect while either of these op-tions was pursued. If the new gasket passes the leakage test, the test will then be repeated in several months. A decision will be made at
- that time as to whether or not the frequency of the leakage test of the 1
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Reportable Occurrence Report April 25, 1980 Page 4 truck lock should be permanently increased or continued on an annual basis. Inasmuch as the outer door always passed the leakage test when it was equipped with a gasket of the proper hardness, it is expected that the annual test will be sufficient.
- 10. Failure Data: No previous failure data for this gasket is recorded Prior to 1979 at the facility.
Sincerely, O
John Bernard Director of Reactor Operations (Acting)
JB:DKE cc: MITRSC USNRC-0MIPC I
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