Information Notice 2018-04, Operating Experience Regarding Failure of Operators to Trip the Plant When Experiencing Unstable Conditions

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Operating Experience Regarding Failure of Operators to Trip the Plant When Experiencing Unstable Conditions
ML17269A262
Person / Time
Issue date: 02/26/2018
From: Mcginty T, Chris Miller
Division of Construction Inspection and Operational Programs, Division of Inspection and Regional Support
To:
Govan T
References
TAC MG0173 IN 2018-04
Download: ML17269A262 (5)


UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

OFFICE OF NEW REACTORS

WASHINGTON, DC 20555-0001 February 26, 2018 NRC INFORMATION NOTICE 2018-04: OPERATING EXPERIENCE REGARDING FAILURE

OF OPERATORS TO TRIP THE PLANT WHEN

EXPERIENCING UNSTABLE CONDITIONS

ADDRESSEES

All holders of an operating license for a non-power reactor (research reactor, test reactor, or

critical assembly) under Title 10 of the Code of Federal Regulations (10 CFR) Part 50,

Domestic Licensing of Production and Utilization Facilities, except those who have

permanently ceased operations.

All holders of an operating license or construction permit for a nuclear power reactor under

10 CFR Part 50, Domestic Licensing of Production and Utilization Facilities, except those that

have permanently ceased operations and have certified that fuel has been permanently

removed from the reactor vessel.

All holders of and applicants for a combined license under 10 CFR Part 52, Licenses, Certifications, and Approvals for Nuclear Power Plants.

PURPOSE

The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform

addressees of several reactor events during which operators failed to take timely action to place

the plant in a stable condition. It is expected that recipients will review the information for

applicability to their facilities and consider actions, as appropriate, to avoid similar problems.

However, suggestions contained in this IN are not NRC requirements; therefore, no specific

action or written response is required.

DESCRIPTION OF CIRCUMSTANCES

Fermi, Unit 2

On March 19, 2015, Fermi, Unit 2 (Fermi) experienced a closed cooling water leak within

primary containment, causing operators to trip one of the two reactor recirculation pumps. The

resulting reactor conditions (45 percent recirculation flow, 61 percent reactor power) placed the

plant in the exit region of the power-to-flow map. This required the licensee to place the plant

in a more stable configuration (either by raising flow or lowering power) to avoid

thermal-hydraulic instability (THI) and the oscillating flux distributions this can cause within the

active fuel region. Control room operators entered the appropriate abnormal operating

procedures (AOPs) for the plant conditions, but failed to prioritize the inserting of rods to quickly

lower power during the trip of the recirculation pump. As the transient progressed, the expected

loss of feedwater heating caused a 12 percent power increase over approximately a 10-minute

ML17269A262 period. This drove the reactor further into the exit region of the power-to-flow map, and while

operators were initiating actions to insert control rods, two channels on the oscillation power

range monitor (OPRM) system tripped, resulting in an automatic reactor scram.

When the OPRM system was first made operable at Fermi in May 2000, three AOPs were

revised. These AOPs were "Loss of Feedwater Heating," "Recirculation Pump Trip," and "Jet

Pump Failure." These revisions incorporated the functions of the OPRM system, but removed

important control room operator actions from the procedures. In all cases, the requirement to

monitor for THI through the selection of control rods was removed, as was the statement to

place the reactor mode switch in "shutdown" if THI was observed. The bases for the procedure

changes reflected the licensees belief of the superior capability of the newly installed electronic

OPRM system to detect and suppress neutron flux instability as compared to a human operator.

The procedure changes during implementation of the OPRM system negatively impacted

licensed operator training, which in turn affected the ability to maneuver the plant when

confronted with plant conditions susceptible to THI. Post-trip review of operator actions during

this event found a lack of timely operator response during power oscillations caused by THI.

Further details are available in Fermi Licensee Event Report 05000341/2015-003, dated May 5,

2015 (Agencywide Documents Access and Management System (ADAMS) Accession

No. ML15127A176) and in NRC Integrated Inspection Report 05000341/2015003, dated

November 5, 2015 (ADAMS Accession No. ML15309A680).

Grand Gulf Nuclear Station, Unit 1

On June 17, 2016, Grand Gulf Nuclear Station, Unit 1 (Grand Gulf) was operating at

approximately 65 percent rated thermal power while performing surveillance testing on the

turbine stop valves. With the B turbine stop valve shut as part of the surveillance procedure, the D turbine stop valve unexpectedly shut. While operators attempted to reset the B turbine

stop valve, the A and C turbine control valves were challenged in their ability to provide the

required control of turbine pressure and reactor pressure, resulting in oscillations of turbine

pressure, and hence reactor pressure and reactor power. Control room operators, including

managers in oversight roles, focused on the turbine control valve movements and possible

recovery actions, and failed to appreciate the impact that the turbine control valve fluctuations

and reset efforts were having on reactivity. Reactor power oscillations of 10-20 percent were

seen over the course of the next 42 minutes, with a maximum recorded power of 87 percent

before an automatic reactor scram occurred on an OPRM trip.

Operators had recently received training on the Fermi event discussed above. The training

emphasized the need to scram the reactor in the event that THI resulted in reactor power

oscillations. However, Grand Gulf lacked a procedure for responding to malfunctions of the

reactor pressure control system, and after verifying that the power oscillations they were seeing

were not the result of THI, the operators concluded that the guidance to insert a manual scram

did not apply.

Following the event, the licensee implemented a standing order that gave clear guidance on

how to address issues that cause oscillations and has since created an off-normal event

procedure for reactor pressure control system malfunctions.

Further details on this event can be found in Grand Gulf Licensee Event Report

05000416/2016-004-00, dated August 12, 2016 (ADAMS Accession No. ML16225A724) and in NRC Integrated Inspection Report 05000416/2016003, dated November 10, 2016 (ADAMS

Accession No. ML16315A372).

Joseph M. Farley Nuclear Plant, Unit 1

On October 1, 2016, with the Joseph M. Farley Nuclear Plant, Unit 1 (Farley) operating at

99 percent power, operators in the control room received indications that the 1A steam

generator main steam isolation valve (MSIV) had drifted off its backseat and was in an

intermediate position, including a main control board annunciator for low air pressure for the

valve. In accordance with the annunciator response procedure, operators attempted to

recharge the accumulator by moving the switch for the valve to open, but the indications

remained.

The next step of the procedure directed a manual reactor trip in order to reduce the challenge to

the plant that would result from the MSIV failing shut. Instead, operators attempted to isolate

the leaking test solenoid valve that was causing the loss of air pressure and restore the MSIV to

the full open position. Prior to performing the test valve isolation, and 37 minutes after

operators first received an alarm in the control room, the MSIV failed shut on loss of air

pressure. This resulted in an automatic reactor trip and a safety injection on low steam line

pressure (rate compensated) in the 1B and 1C steam lines, as expected for this event. Contrary

to procedural requirements, licensed senior reactor operators decided to maintain the reactor

online while attempting to isolate the leak. Had operators followed the procedure and manually

tripped the reactor, they could possibly have prevented the safety injection.

To address the issue, the licensee conducted simulator training for all crews emphasizing

procedure use and adherence standards, and took further steps to address gaps in operator

performance.

Additional information appears in Farley Licensee Event Report 05000348/2016-002-00, dated

November 30, 2016 (ADAMS Accession No. ML16335A450) and NRC Integrated Inspection

Report 05000348/2016004 and 05000364/2016004, dated January 17, 2017 (ADAMS

Accession No. ML17027A147).

DISCUSSION

Since the average nuclear power plant now spends over 90 percent of its time online, operators

have less experience dealing with transients, startup, and shutdown operations than in the past.

This places increased emphasis on the importance of complete and accurate procedures to

guide operators through unfamiliar situations. Regulations in 10 CFR 50 Appendix B, Criterion

V, Instructions, Procedures, and Drawings, as well as individual plant technical specifications, require licensees to maintain and adhere to quality procedures for activities affecting safety.

Regulatory Guide 1.33, Quality Assurance Program Requirements (Operation), provides a

comprehensive list of systems, situations, and processes that might require quality procedures, as specified by the individual plant licensing basis. However, emergency operating procedures

are symptom-driven and are not intended to cover every possible contingency. Regulatory

requirements for licensee training programs are structured to ensure that operators have a

thorough understanding of integrated plant operations and system interactions so that they can

respond appropriately to events not anticipated by procedures to place the plant in a safe

condition. The events discussed in this IN involved operators misinterpreting procedures, failing to adhere

to procedure requirements, or failing to recognize incomplete or faulty procedures. In each

case, the failure to maintain a conservative bias in the decision-making process left the reactor

in an unstable condition for extended periods of time before automatic protective features

actuated, increasing the probability that a more significant event could occur. Industry operating

experience has shown the importance of diverse simulator scenarios that accurately represent

plant response while incorporating complex system interactions. By stressing procedure

adherence and challenging critical thinking skills, these scenarios can improve operator

understanding of event consequences and the actions necessary to mitigate those

consequences.

CONTACT

This information notice requires no specific action or written response. Please direct any

questions about this matter to the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation (NRR) project manager.

/RA/ (Paul G. Krohn for) /RA/

Timothy J. McGinty, Director Christopher G. Miller, Director

Division of Construction Inspection Division of Inspection and Regional Support

and Operational Programs Office of Nuclear Reactor Regulation

Office of New Reactors

Technical Contacts: Rebecca Sigmon, NRR

301-415-0895 E-mail: Rebecca.Sigmon@nrc.gov

Note: NRC generic communications may be found on the NRC public Web site, https://www.nrc.gov, under NRC Library. NRC INFORMATION NOTICE 2018-04, OPERATING EXPERIENCE REGARDING FAILURE

OF OPERATORS TO TRIP THE PLANT WHEN EXPERIENCING UNSTABLE CONDITIONS,

DATE: February 26, 2018 ADAMS Accession Number: ML17269A262 *via email TAC No. MG0173 OFFICE TECH EDITOR* NRR/DIRS/IOEB/TR NRR/DIRS/IOLB/BC NRR/DIRS/IOEB/TR NRR/DIRS/IEOB/BC

NAME JDougherty* RSigmon* NSalgado for AIssa RElliott

CCowdry

DATE 09/27/2017 10/25/2017 11/17/2017 11/29/2017 12/05/2017 OFFICE NRR/DIRS/IRGB/ NRR/DIRS/IRGB/LA NRR/DIRS/IRGB/BC NRO/DCIP/D NRR/DIRS/D

PM

NAME TGovan ELee HChernoff TMcGinty (PKrohn for) CMiller

DATE 12/05/2017 12/06/2017 02/06/2018 02/14/2018 02/26/2018 OFFICIAL RECORD COPY