04-01-2005 | ( I&C) personnel were performing two surveillance test activities -- Surveillance Procedure ( SP) 47-316A (Channel 1 (Red) Instrument Channel Test) and SP 05A-34C-1 ( Feedwater Flow Transmitter Channel 1 (Red) Calibration). At approximately 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br />, these surveillances caused the reactor thermal power 1-minute, 15-minute, and 8-hour average indications to become inaccurate. The Control Room operators entered procedure A-CP-46 (Abnormal Plant Process Computer System) to determine appropriate actions. The Alternate Reactor Thermal Output (ARTO) system was being used to monitor reactor power. At approximately 1330 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.06065e-4 months <br />, the 1-minute thermal power readings returned to approximately 1772 megawatts thermal (MWth), 100 percent power. Procedure A-CP-46 was exited at approximately 1345 hours0.0156 days <br />0.374 hours <br />0.00222 weeks <br />5.117725e-4 months <br />, and use of ARTO was stopped. At the time the 8-hour Reactor Thermal Output (RTO) average was viewed as not valid. During shift turnover there was no direction given concerning the expected affect on the 8-hour average. At 1952 hours0.0226 days <br />0.542 hours <br />0.00323 weeks <br />7.42736e-4 months <br />, the shift performed an 11 gallon dilution to compensate for normal core burn up.
At both 2047 hours0.0237 days <br />0.569 hours <br />0.00338 weeks <br />7.788835e-4 months <br /> and at 2057 hours0.0238 days <br />0.571 hours <br />0.0034 weeks <br />7.826885e-4 months <br />, the RTO 15-minute average PPCS alarm came in at 1773 MWth. This computer annunciator cleared within minutes. As the effects of the earlier l&C surveillances were being dropped from the 8-hour average calculation, indicated 8-hour average power started to increase, resulting in a high power alarm at 2131 hrs. Indicated 8-hour average reactor power peaked at 1772.07 MWth. A 3.4 gallon boration was performed at 2141 hours0.0248 days <br />0.595 hours <br />0.00354 weeks <br />8.146505e-4 months <br />, and power reduced to less than 1772 MWth at 2216 hours0.0256 days <br />0.616 hours <br />0.00366 weeks <br />8.43188e-4 months <br />. Management provided insufficient expectations for remaining less than the limit for RTO; therefore Operations routinely operated close to the 8-hour average limit, often exceeding the 15 minute average RTO with no adverse consequences. Corrective actions have been initiated to revise procedures, to change the alarm setpoint for the 8-hour average RTO, and add the 15-minute average RTO to the alarm response procedure. This event is not identified as a Safety System Functional Failure.
NRC FORM 366A� U.S. NUCLEAR REGULATORY COMMISSION (1-2001) FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) 2005 -- 001 -- 011 |
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Event Description
On January 31, 2005, the Kewaunee Nuclear Power Plant (KNPP) was in operation at 100 percent rated thermal power of 1772 megawatts thermal (MWth). On day shift (0600 hrs to 1800 hrs), Instrument and Control (I&C) personnel were performing two surveillance test activities. These tests were being performed in accordance with Surveillance Procedure (SP) 47-316A (Channel [CHA] 1 (Red) Instrument Channel Test) and SP 05A-34C-1 (Feedwater Flow Transmitter [FT] Channel 1 (Red) Calibration). At approximately 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br />, these surveillance activities caused the indications for reactor thermal power 1-minute, 15-minute, and 8-hour averages to become inaccurate.
The Control Room operators entered abnormal operating procedure A-CP-46 (Abnormal Plant Process Computer System) to determine appropriate actions. The Alternate Reactor Thermal Output (ARTO) system was used to monitor reactor power. At approximately 1330 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.06065e-4 months <br />, the 1-minute thermal power readings returned to approximately 1772 MWth. Procedure A-CP-46 was exited at approximately 1345 hours0.0156 days <br />0.374 hours <br />0.00222 weeks <br />5.117725e-4 months <br />, and the use of ARTO was stopped. At the time, the 8-hour Reactor Thermal Output (RTO) average was viewed as not valid. The 1-minute and 15-minute RTO values had returned to normal'readings. Corrective Action Program document CAP 25257 was initiated by the Plant Process Computer System (PPCS) Group at 1453 hours0.0168 days <br />0.404 hours <br />0.0024 weeks <br />5.528665e-4 months <br />, to document the discrepancy in expected and actual reaction of the PPCS [CPU] to l&C surveillance activities.
The day shift operating crew initiated CAP 25258 to document the RTO being questionable as a result of performing procedure SP 05A-34C-1.
Turnover from day shift to night shift occurred at 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br />. Control Room Supervisor turnover items included review of questionable values resulting from MC surveillance activities, the 8-hour average RTO indicating artificially low, and initiation of CAP 25258 that documented problems that occurred during SP 05A- 34C-1 & questionable PPCS data. Reactor Operator turnover included discussion of previous dilutions and the thermal power PPCS trends, including the present 15-minute RTO being greater than 1772 MWth. Shift Manager turnover did not discuss actions to ensure the 8-hour average RTO remained below the license limit (for example keeping the 15-minute average RTO less than 1772 MWth). The night shift was aware that the 8 hour average RTO was reading low due to l&C activities on day shift. However, there was no direction given concerning the expected affect on the 8-hour average power indication, when the PPCS calculated 8-hour average value was validated. During the pre-shift brief, the night shift operations crew did not question the 8 hour average RTO indication. Also, the operating crew did not verify the 8-hour average RTO indication to monitor (PPCS or ARTO).
At 1952 hours0.0226 days <br />0.542 hours <br />0.00323 weeks <br />7.42736e-4 months <br />, the operating shift performed an 11 gallon dilution to compensate for normal core bum up. At both 2047 hours0.0237 days <br />0.569 hours <br />0.00338 weeks <br />7.788835e-4 months <br /> and 2057 hours0.0238 days <br />0.571 hours <br />0.0034 weeks <br />7.826885e-4 months <br />, the RTO 15-minute average PPCS alarm [JA] came in at 1773 MWth. These computer annunciators [ANN] each cleared within minutes. Shift management was not notified of either of these alarms, as they were expected due to the recent dilution, and there is no specific requirement to announce each computer alarm. As the effects of the l&C surveillance tests on day shift were being dropped from the 8-hour average calculation, the indicated 8-hour average power started to increase rapidly, resulting in the Trouble Light Annunciator (TLA)-11 "Reactor Thermal Power High" alarm (1772 MWth) at 2131 hrs.
Indicated 8-hour average reactor power peaked at 1772.07 MWth. Alarm Response Procedure (ARP) 47033 31 for TLA-11 was entered, a 3.4 gallon boration was performed at 2141 hours0.0248 days <br />0.595 hours <br />0.00354 weeks <br />8.146505e-4 months <br />, and 8-hour average power reduced to less than 1772 MWth at 2216 hours0.0256 days <br />0.616 hours <br />0.00366 weeks <br />8.43188e-4 months <br />.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) Event Analysis and Safety Significance This event is being reported under 10CFR50.73(a)(2)(i)(B), operation which was prohibited by the Technical Specifications.
The KNPP facility operating license states in Section 2.C.(1) — "The NMC is authorized to operate the facility at steady-state reactor core power levels not in excess of 1772 megawatts (thermal)." NRC guidance relative to "Licensed Power Level" is contained in a letter from Mr. E. L. Jordan (Assistant Director for Technical Programs, Division of Reactor Operations Inspection, Office of Inspection and Enforcement), dated August 22, 1980. This guidance specifies the following:
The average power level over any 8-hour shift should not exceed the full steady-state licensed power level (and similarly worded terms).
The exact 8-hour periods are up to the plant. It is permissible to briefly exceed the full steady-state licensed power level by as much as 2 percent for as long as 15 minutes.
In no case should 102 percent power be exceeded.
Lesser power excursions for longer periods should be allowed (i.e. 1 percent excess for 30 minutes, 0.5 percent excess for 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, etc). The 8-hour average power limit will prevent excessive multiple excursions.
The 8-hour average reactor thermal power maximum value was 1772.07 MWth for this event. This exceeded the 1772 MWth limit by only 0.07 MWth. The thermal power limitations given above relative to the 15-minute, 30-minute, and 1-hour time periods were not exceeded. The maximum 15-minute reactor thermal power value during this event was 1773 MWth.
Technical Specification 2.1, "Safety-Limits — Reactor Core", requires that the combination of rated power level, coolant pressure, and coolant temperature shall not exceed the limits specified in the Core Operating Limits Report (COLR). The Reactor Core Safety Limits Curve was not exceeded. This event is therefore determined to have a very low safety significance. This event is identified as not being a Safety System Functional Failure.
Cause
Root Cause — Management provided insufficient expectations for remaining less than the limit for RTO; therefore Operations routinely operated close to the 8-hour average limit, often exceeding the 15 minute average RTO with no adverse consequences.
Also, ARP 47033-31 for TLA-11 does not provide guidance on how the site expects the operations crew to reduce power to less than 1772 MWth when the alarm is received. Further, the ARP for TLA-11 does not identify that when the alarm is received, the site has exceeded the License Limit for rated thermal power.
Contributing Factors — When the operating shift performed a dilution at 1952 hours0.0226 days <br />0.542 hours <br />0.00323 weeks <br />7.42736e-4 months <br /> to compensate for normal core bum-up, the mismatch between indicated power and actual power was not considered when the decision to dilute the FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) 'normal' amount of 11 gallons was made. The operating shift did not verify that a dilution of 11 gallons was appropriate with indicated power less than actual power. A lesser amount of dilution was not considered.
Procedure SP-05A-034C-1 contains an incorrect step that allows an input to the RTO calculation to not be removed from scan.
Procedure A-CP-46 contains incorrect guidance as to when the crew should stop using ARTO and use the normal calculated value for RTO.
Corrective Action Interim Corrective Actions — 1. The Plant Manager issued a memo dated February 7, 2005, to the Operations Department Management, Shift Managers, and Control Room Supervisors stating his expectations concerning operation of the plant within the license requirements.
2. The Control Room Operations Crew involved in this event was removed from Control Room duties. The crew successfully completed several simulator scenarios which emphasized overpower events and distractions in the Control Room environment. Each individual was evaluated by Management prior to returning to duties in the Control Room.
Corrective Actions to Prevent Recurrence — 1. Per Work Order 05-002811:
- Add the reactor thermal power 15-minute average PPCS computer point as an input to Trouble Light Annunciator TLA-11 "Reactor Thermal Power High" alarm.
- Reduce the TLA-11 alarm setpoint for the 8-hour average thermal power to 1771.7 MWth.
2. Revise General Nuclear Procedure (GNP) 03.17.10 (Reactivity Management) to discuss the responsibility of the operating crews to maintain the steady state power less than 1772 MWth, as described in the KNPP operating license.
3. Revise ARP 47033-31. (TLA-11) to add the 15-minute thermal power alarm setpoint of 1772 MWth, change the 8-hour thermal power alarm setpoint to 1771.7 MWth, and to provide additional action to use the Valve Position Limiter (VPL) to lower turbine power.
4. Revise procedure A-CP-46 to clarify guidance to monitor reactor power, add steps to ensure 1772 MWth is not exceeded when the PPCS is out-of-service, and to clarify conditions to return to using the PPCS RTO program monitoring.
5. Revise procedure N-CP-46 (Plant Process Computer System) to add the 15-minute average RTO computer point to Attachment B TLA Computer Points.
6. Revise procedure N-0-03 (Plant Operation Greater Than 35% Power) to reference the 1771.7 MWth setpoint, and to add a note to ensure the nominal maximum reactor power 8-hour average is maintained below 1771 MWth.
7. Incorporate operating philosophy changes (as described in the above procedure revisions) into the Auxiliary Operator, Initial License Training, Licensed Operator Requalification, and Shift Manager Qualification Programs.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) Kewaunee Nuclear Power Plant 05000305 YEAR Other Corrective Actions — 1. Perform a review of other alarm setpoints that are set at Technical Specification (TS) values, and potentially would not allow sufficient time for Operations to take action before a TS required value is exceeded.
2. Revise procedures SP-05A-034C-1, 2, 3, & 4. In each SP, Step 6.2.5 identifies which channels are the controlling channels and then states to 'N/A' Steps 6.2.6 through 6.2.9. Step 6.2.6 removes the selected channel from PPCS scan, and this step should not be marked as 'N/A'.
3. Revise procedure N-CVC-35A (Boron Concentration Control) to add 'thermal power' to two verification steps prior to boration or dilution activities.
Previous Similar Events
KNPP LER 92-18; Licensed Power Exceeded Due To Inaccurate Feedwater Flow Indication On September 22, 1992, the plant was retuming to 100 percent power after a unit trip. After applying the ultrasonic flow meters (UFMs) correction factor to in-line venturi feedwater (FW) flow measurements and escalating to 100 percent power, it was noted that the electric output was 1 to 2 megawatts higher than before the unit trip. An evaluation determined indicated FW flow, measured by the UFMs, was 0.41 percent low and reactor power was approximately 0.2 percent greater than licensed thermal power. Immediate actions were taken to decrease power to within licensed limits. The change in UFM output was caused by corrosion product build up between the UFM transducers and the FW pipe in conjunction with age related degradation of the transducers.
The FW UFMs were calibrated, using the full flow bypass line venturi, to accurately measure FW flow.
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Box 249Entergy Buchanan. NY 10511-0249 Tel 914 734 6700 Fred Dacimo Site Vice President Administration July 5, 2005 Indian Point Unit No. 3 Docket Nos. 50-286 N L-05-078 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2005-002-00, "Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure." Dear Sir: The attached Licensee Event Report (LER) 2005-002-00 is the follow-up written report submitted in accordance with 10 CFR 50.73. This event is of the type defined in 10 CFR 50.73(a)(2)(iv)(A) for an event recorded in the Entergy corrective action process as Condition Report CR-IP3-2005-02478. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Sincerely, 4F-/t R. Dacimo Vice President Indian Point Energy Center Docket No. 50-286 NL-05-078 Page 2 of 2 Attachment: LER-2005-002-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 3 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 3660 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request 50 hours.RReported lessons teamed are incorporated into the licensing process and fed back to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 29555-0001, or by InternetLICENSEE EVENT REPORT (LER) e-mail to Infocoilectsenrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-l0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person Is not required to respond to, the Information collection. 1. FACIUTY NAME 2. DOCKET NUMBER 3. PAGE INDIAN POINT 3 05000-286 10OF06 4. TITLE Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000287/LER-2005-002 | Unit 3 trip with ES actuation due to CRD Modification Deficiencies | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000336/LER-2005-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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