ML18219C210

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LER 1978-016-03L. Re Removal of Emergency Diesel Generator from Service for Maintenance
ML18219C210
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 03/14/1978
From: Shaller D
Indiana Michigan Power Co
To: James Keppler
NRC/RGN-III
References
LER 1978-016-03L
Download: ML18219C210 (9)


Text

REGULATORY I NFORI"IAT ION DISTRIBUTION, SYSTEN (R IDS)DISTRIBUTION FOR INCONING NATERIAL 50-315 REC: NRC QRG: SHALLER D V DOCDATE: 03/14/78 NRC IN 8c NI PWR DATE RCVD: 03/20/78 DOCTYPE: LETTER NOTARIZED:

NO COPIES RECEIVED

SUBJECT:

LTR 1 ENCL 1 LICENSEE EVENT REPT (RO 50-315/78-016l03L-0)

ON 02/15/78 CONCERNING 1AB ENERGENCY DIESEL GENERATOR WAS REI"IOVED FROM SERVICE FOR MAINTENANCE AND THE BREAKER ALIGNMENT VERIFICATION AS REQUIRED BY TECH SPEC 4.8.1.1.1A WAS NOT PERFORNED WITHIN ONE HOUR.PLANT MANE: COOK-UNIT 1+~~~~~~~~~HI

~~~~~~~DISTR I BUT ION INCIDENT REPORTS (DISTRIBUTION CODE A002)REVIEWER INITIAL: X JN DISTRIBUTOR INITIAL: g, A OF THIS NATERIAL IS AS FOLLOWS+++~~~~~~~~~~~~~~~

FOR ACTION: INTERNAL: EXTERNAL: EI4CER++W/4 ENCL REG FILE4+W NCL SCHRQEDER/

IPPQL I TO+4 M/ENCL NQVAK/CHECK++W/ENCL KNIGHT44W/

ENCL HANAUER++W/ENCL EI SENHUT~+W/ENCL SHAO++W/ENCL KREGER/J.COLL INS4+I Jf ENCL K SEYFRIT/IE++W/ENCL LPDR S ST.JOSEPH'I++l JlENCL TIC++W/ENCL NSIC+4l J/ENCL ACRS CAT B+4 W/1 6 ENCL NRC PDR++Wf ENCL NIPC++4f/3 ENCL HOUSTQN4+W/ENCL GRINES++W/ENCL BUTLER++W/ENCL TEDESCO++W/ENCL BAER44 Wf ENCL VOLLMER/BUNCH++W/ENCL ROSA'Wf ENCL I COPIES NOT SUBMITTED PER REGUIATORY GUIDE 10.1 DISTRIBUTION:

LTR 45 ENCL 45 SIZE: iP+iP CONTROL NBR: 780810 5 THE END 0 I 1 II i yO M mertoan OI HA 8 NICHIGAIlI POIEER CONPAIIIY IE>gQig)P P()~li~f'I'frn DONALD C.COOK NUCLEAR PLANT'8 P.O.Bov 458, Bridgman, Michigan 49106 March 14, 1978 Hr.J.G.Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Comnission Region III 799 Roosevelt, Road Glen Ellyn, IL 60137

Dear Hr.Keppler:

u,s'"mc p 79pg COAIAIEG GEO'~~ESS Qa l~C'perating License DPR-58 Docket No.50-315 Pursuant to the requirements of Appendix A Technical Specifications the following report is submitted:

RO 78-016/03L-O.

Sincerely, D.V.Shaller Plant Manager/bab cc: J.E.Dolan R.W.Jurgensen G.E.Lien R.Kilburn R.J.Vollen BPI K.R.Baker RO: I I I R.C.Callen HPSC P.W.Steketee, Esq.R.Walsh, Esq.G.Charnoff, Esq.G.Olson J.M.Hennigan PNSRC J.F.Stietzel Dir., IE (30 copies)Dir., HIPC (3 copies)780810015]gooa./~%/ji R NRC FRORhl 366 I7.77)LlCENSEE EVENT REPORT~01 8 CONTROL BLOCK:{PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

I 6 N I 0 C C 1QE 0 0 0 0 0 0 0 0 0 0 0 QE4 1 1 1 1 OR~OR 9 LICENSEE CODE 14 15 LICENSE NUhIBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T~01 7 8 SOU CE L~JQG 0 Q 60 61 DOCKET NUMBER 68 69 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 UNIT WAS OPERATING NORMALLY IN M D 1.T EVENT DATE QB 74 75 REPORT DATE 80 OB~03 FROM SERVICE AT 0130 HOURS ON 2 15 78 FOR MAIf]TENANCE.

H R TION AS RE UIRED BY APPENDIX A TECH.SPEC.4...W~OG HOUR.THE CORRECT BREAKER ALIGNMENT WAS VERIFIED AT 10 5 H UR~OG REMAINED AT STEADY~07 CALLED UPO.T~OB 7 8 80 7 8 SYSTE'M CAUSE CAUSE COMP.VALVE.CODE CODE SUBCODE COMPOiVENTCODE SUBCODE SUBCODE~ZZ Q>>~AQ>>~AQ>>Z Z Z Z Z Z Qi~ZQEE~Z Q's 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LER)RO EVENT YEAR REPORT NO.CODE TYPE NO.Q17 RERRRE~78~~01 6~~~03~L-~P 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDX PRIME CohIP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS~22 SUBMITTED FORM'SUB.SUPPLIER MAiNUFACTURER

~HS~ZQ L~JQ20 LZJO~023~Q24 MQ26 Q26 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 027 o THE EVENT WAS CAUSED BY THE UNIT SUPERVISOR FAILING TO RE UIRE HAVING THE BREAKER ALIGNMENT VERIFIED.THE SHIFT OPERATING ENGINEER REINSTRUCTED THE UNIT P THE REQUIREMENTS FOR REMOVING VITAL EQUIPMENT FROM SERVICE WITH RESPECT TO PERFORM-3 ING SURVEILLANCE AS DIRECTED BY THE TECH.SPECS.AND OPERATING DEPARTMENT INSTRUCTIONS 4 7 8 9 FACILITY~30 hIETHOO OF STATUS%POWER OTHER STATUS~DISCOVERY 6 Oss~io o OE>>A~AQ>>P ANT STAT 7 8 9 10 12 13 44 45 ACTIVITY CONTENT RELEASED OF REI.EASE AhIOUNT OF ACTIVITY~36 Z Q33~ZQ34 NA 7 8 9 10 11 44 45 PERSONNEL EXPOSURES NUi4IBER TYPE DESCRIPTION Q3B~77~00 0 0 Z Oss NA 7 8 9 11 12 13 PERSONNEL INJURIES 7 8 9 11 12 LOSS OF OR OAhIAGE TO FACILITY Q43 TYPE DESCRIPTION

~IB 7 8 9 10 PUBLICITY ISSUED DESCRIPTION

~~O44 7 8 9 10 NAME OF PREPARER R.S.Keith DISCOVERY DESCRIPTION Q32 Y 80 80 80 80 NRC USE ONLY 80 ER 0 68 69 PHDNE.61 6 465 5901 ENG INEER Bo LOCATION OF RELEASE Q 80 h~.RECEIVEO OOCUVFN~CO>CIRCE BESIDE U.S.NRC DIS TRIBUT ION SERVICES BRANCH CoP//W>ee~~L, i~Nolcw I NIGHIG 8 PDIYE4 coN IN DONALD C.COOK NUCLEAR PLANT P.O.Box 456, Bridgman, Michigan 49106 March 14, 1978 Mr.J.G.Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Comnission Region III 799 Roosevelt Road Glen Ellyn, IL 60137

Dear Mr.Keppler:

Operating License DPR-58 Docket No.50-315 Pursuant to the requirements of Appendix A Technical Specifications the following report is submitted:

RO 78-016/03L-O.

Sincerely, D.V.Shaller Plant Manager/bab cc: J.E.Dolan R.W.Jurgensen G.E.Lien R.Kilburn R.J.Vollen BPI K.R.Baker RO: III R.C.Callen MPSC P.W.Steketee, Esq.R.Walsh, Esq.G.Charnoff, Esq.G.Olson J.M.Hennigan PNSRC J.F.Stietzel Dir., IE (30 copies)Dir., MIPC (3 copies)i~~~l,)S78 II'I~~I t Ili U.S.NUCLEAR REGULATORY COMMISSION NRC FORM 366{7-77)+~~~-~0 7 8 CON'T~0 7 8 LICENSEE EVENT REPORT O1{PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 6 1Qs 0 0 0 0 0 0 0.0 0 0 0 Qs4 1 1 1 1 Q4~Qs 14 15 25 26 I.ICENSE'TYPE 30 57 CAT 58 CONTROL BLOCK: I M I D C C LICENSEE CODE 0 SOURCE L~JQ 0 60 61 DOCKET NUMBER 68 69 EVENT DESCRIPTION AND PROBABI.E CONSEQUENCES QIO UNIT WAS OPERATING NORMALLY IN ODE 1.EVENT DATE 74 75 REPORT DATE 80~03 FROM SERVICE AT 01 30 HOURS ON 2 1 5 78 FOR MAIl TENANCE.THE~04 TION AS RE UIRED BY APPENDIX A TECH.SPEC~os HOUR.THE CORRECT BREAKER ALIGNMENT WAS VERIFIED AT 1 5 UR~06 REMAINED AT STE D~0 7 CALLED UP~OB 80 7 8 9 g SYSTEM CAUSE CAUSE COMP.VALVE.CODE CODE SUBCODE COMPONENT CODE SVBCODE SUBCODE~ZZ Q>>A Q>>~AQ>>Z Z Z Z Z Z Qs~ZQs~ZQs 7 8 9 10 11 12 l3 18 19 20 SEaUENTIAL OCCURRENCE REPORT REVISION LERIRP EVENT YEAR REPORT NO.CODE TYPE NO.Q17 REpoRT~78 Q~01 6 Qx~03 QL[J QQ 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDP PRIME COMP.COMPONENT TAKEN ACTION ON PLANT~METHOD HOURS Q22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER

~HO>>~ZO>>~ZO20&O21 MQss LzLIQ4[zJQss O26 33 34 35 36 37 40 41 42 43 44 47 , CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 027 o THE EVENT WAS CAUSED BY THE UNIT SUPERVISOR FAILING TO RE UIRE HAVING THE BREAKER ALIGNMENT VERIFIED.THE SHIFT OPERATING ENGINEER REINSTRUCTED THE UNIT S P THE REQUIREMENTS FOR REMOVING VITAL EQUIPMENT FROM SERVICE WITH RESPECT TO PERFORM 1 3 ING SURVEILLANCE AS DIRECTED BY THE TECH.SPECS.AND OPERATING DEPARTMENT INSTRUCTIONS 4 7 8 9 FACILITY M30 METHOD OF STATUS%POWER OTHER STATUS 0 DISCOVERY 6 Q>>~l0 0 Qss NA'AQ>i PLA T 8 9 10 12 13 44 45 46 ACTIVITY CONTENT RELEASED OF REI.EASE AMOUNT OF ACTIVITY~Z Q33 Z Q34 NA 7 8 9 10 44 45 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q3g~00 0$ZQss NA 7 8 9 11 12 13 PERSONNEL INJURIES DISCOVERY DESCRIPTION 032 T R 80 80 80 ENGINEER 80 LOCATION OF RELEASE Q 7 8 7 8 o 9 11 12 LOSS OF OR DAMAGE TO FACILITY Q43 TYPE DESCRIPTION Ir JQs 9 10 PUB L I CITY ISSUED DESCRIPTION

~4.~Q44 7 8 9 10 NAMF PF PREPARER R" S~Ke'I th NRC USE ONLY 80 68 69 PHoNE'16 465-5901 80 80 o 0 L 0 I 4,.IW I