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Issue date | Title | |
---|---|---|
Information Notice 1993-89, Potential Problems with BWR Level Instrumentation Backfill Modifications | 26 November 1993 | Potential Problems with BWR Level Instrumentation Backfill Modifications |
Information Notice 1994-36, Undetected Accumulation of Gas in Reactor Coolant System | 24 May 1994 | Undetected Accumulation of Gas in Reactor Coolant System |
Information Notice 1994-52, Inadvertent Containment Spray and Reactor Vessel Draindown at Millstone Unit 1 | 15 July 1994 | Inadvertent Containment Spray and Reactor Vessel Draindown at Millstone Unit 1 |
Information Notice 1996-05, Partial Bypass of Shutdown Cooling Flow from Reactor Vessel | 18 January 1996 | Partial Bypass of Shutdown Cooling Flow from Reactor Vessel |
Information Notice 1996-37, Inaccurate Reactor Water Level Indication and Inadvertent Draindown During Shutdown | 18 June 1996 | Inaccurate Reactor Water Level Indication and Inadvertent Draindown During Shutdown |
Information Notice 1996-42, Unexpected Opening of Multiple Safety Relief Valves | 5 August 1996 | Unexpected Opening of Multiple Safety Relief Valves |
Information Notice 1996-56, Problems Associated with Testing, Tuning, or Resetting of Digital Control Systems While at Power | 22 October 1996 | Problems Associated with Testing, Tuning, or Resetting of Digital Control Systems While at Power |
Information Notice 1996-65, Undetected Accumulation of Gas in Reactor Coolant System and Inaccurate Reactor Water Level Indication During Shutdown | 11 December 1996 | Undetected Accumulation of Gas in Reactor Coolant System and Inaccurate Reactor Water Level Indication During Shutdown |
Information Notice 1997-83, Recent Events Involving Reactor Coolant System Inventory Control During Shutdown | 5 December 1997 | Recent Events Involving Reactor Coolant System Inventory Control During Shutdown |
Information Notice 1999-14, Unanticipated Reactor Water Draindown at Quad Cities Unit 2, Arkansas Nuclear One Unit 2, & FitzPatrick | 5 May 1999 | Unanticipated Reactor Water Draindown at Quad Cities Unit 2, Arkansas Nuclear One Unit 2, & FitzPatrick |
L-94-013, Evaluation of Util Response to Suppl 1 to NRC Bulletin 90-01, for Plant | 30 November 1994 | Evaluation of Util Response to Suppl 1 to NRC Bulletin 90-01, for Plant |
ML021230299 | 25 March 2002 | Transmittal of Written Summary of Recent Reactor Water Level Indication Issues at Pilgrim Nuclear Power Station |
ML030300440 | 23 January 2003 | Request for Amendment to TS Emergency Core Cooling System Requirements During Shutdown Conditions |
ML030970705 | 22 April 2003 | License Amendment 200 Emergency Core Cooling System Requirements During Shutdown Conditions |
ML031130309 | 22 April 2003 | Tech Spec Pages for Amendment 200 Emergency Core Cooling System Requirements During Shutdown Conditions |
ML031150585 | 29 January 1985 | Withdrawn NRC Generic Letter 1985-004: Operator Licensing Examinations |
ML041670615 | 8 June 2004 | LER 99-008-01 for Pilgrim Regarding Automatic Scram at 100 Percent Power Due to Turbine Trip |
ML061370622 | 11 May 2006 | LER 06-01-000, Pilgrim Re Manual Scram Due to High Offgas Recombiner Temperature Resulting from Inadequate Preventive Recombiner Preheater Pressure Control Valve Controller |
ML061870469 | 30 June 2006 | Technical Specifications Amendment Request to Revise the Surveillance Requirements for the High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) Systems |
ML070610451 | 11 December 2006 | Draft - RO & SRO Written Exam (Folder 2) |
ML070820363 | 20 February 2007 | Final - RO & SRO Written Examination with Answer Key (401-5 Format) (Folder 3) |
ML080670419 | 7 March 2008 | CDBI Findings |
ML091400064 | 14 May 2009 | G20090292/LTR-09-0210/EDATS: SECY-2009-0248 - Mary E. Lampert, Rebecca J. Chin Pilgrim NPS RFO 2009: 2.206 Petition Requesting That NRC Require All Work Packages Inspected Prior to Pilgrim'S Re-start - Urgent Action Requested Due to Timing |
ML100770451 | 31 March 2010 | NEDO-33532, Rev 0, Pilgrim Nuclear Power Station Safety Valve Setpoint Increase. |
ML110420306 | 31 January 2011 | GE Hitachi Nuclear Energy Report, NEDC-33532, Revision 2, Pilgrim Nuclear Power Station Safety Valve Setpoint Increase, Enclosure 4 to 2.11.007 |
ML110620474 | 7 January 2011 | Draft Written Exam (Draft 2) |
ML111010406 | 24 January 2011 | Final Written Examination with Answer Key (401-5 Format) |
ML11326A153 | 9 November 2011 | FSAR Update Revision 28, Technical Specifications Bases Changes, 10 CFR 50.59(d) Report, and Commitment Changes |
ML13042A302 | 9 February 2013 | PNO-I-13-001 - Pilgrim Station: Unusual Event Declared Due to Loss of Offsite Power During Winter Storm Nemo |
ML13323A518 | 14 November 2013 | Technical Specifications Proposed Change No. 306 Eliminate Certain ESF Requirements During Movement of Irradiated Fuel |
ML14003A046 | 12 December 2013 | FSAR Update Revision 29, Technical Specifications Bases Changes, 10 CFR 50.59(d) Report, and Regulatory Commitment Changes |
ML15147A412 | 27 May 2015 | IR 05000293/2015007; 02/02/2015 - 03/20/2015; Pilgrim Nuclear Power Station (Pnps); Special Inspection to Review the January 27, 2015 Partial Loss of Offsite Power (LOOP) and Reactor Scram Event; Inspection Procedure 93812, Special Inspecti |
ML15202A415 | 17 July 2015 | Station'S Notification of Full Compliance with Order EA-12-049, Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events, Submittal of Final Integrated Plan, Response.. |
ML16055A461 | 18 February 2016 | Emergency Plan Implementing Procedure Revisions, Including Revision 6 to EP-AD-601 and Revision 8 to EP-IP-261 |
ML16083A448 | 30 November 2015 | Redacted - Updated Final Safety Analysis Report (UFSAR) Part 1 - November 2015 |
ML16083A453 | 30 November 2015 | Redacted - Updated Final Safety Analysis Report (UFSAR) Part 2 - November 2015 |
ML16083A461 | 30 November 2015 | Redacted - Updated Final Safety Analysis Report (UFSAR) Part 3 - November 2015 |
ML16211A067 | 22 July 2016 | Errata Change for Final Safety Analysis Report Revision 30 |
ML17202G680 | 17 July 2017 | Attachment 1 of Letter Number 2.17.053, EP-AD-601, Emergency Action Level Technical Bases Document, Revision 8 and Associated 10 CFR 50.54(q) Review |
ML18158A130 | 7 June 2018 | Evaluation - Memorandum Regarding Licensee Event Report Safety Significance Review in Response to Findings Associated with Inspection Procedure 95003; Evaluation of NRC Assessment and Inspection Processes at Pilgrim Nuclear Power Station |
ML18194A587 | 11 July 2018 | Attachment 1 to 2.18.045, EP-AD-301, Emergency Action Level Technical Bases Document, Revision 9 and Associated 10 CFR50.54(q) Review |
ML19211A159 | 30 October 1979 | Tech Specs for post-accident Monitoring Instrumentation, Containment Sys & Special Test Exceptions |
ML20002C063 | 5 January 1981 | Responds to NUREG-0737.Provides Info Re Shift Technical Advisor,Guidance for Evaluation & Development of Procedures for Transients & Accidents,Procedures for Feedback of Operating Experience & Training for Mitigating Core Damage |
ML20002E381 | 22 January 1981 | Forwards Addl Info in Response to NUREG-0737 Requirements Re Containment Isolation Dependability,Eccs Outage Rept & Auto Switchover of Reactor Core Isolation Cooling |
ML20005D742 | 6 December 1989 | LER 89-033-00:on 891106,automatic Actuation of Group 1 Portion of Primary Containment Isolation Control Sys (PCIS) Occurred.Caused by High Reactor Vessel Water Level.Manual Valve Closed & PCIS Logic Circuitry reset.W/891206 Ltr |
ML20005G098 | 8 January 1990 | LER 89-038-00:on 891208,unplanned Automatic Reactor Protection Sys Scram Signal & Reactor Scram Occurred.Caused by False Low Reactor Vessel Water Level Signal.Local Level Indicators Satisfactorily calibr.W/900108 Ltr |
ML20006A263 | 15 January 1990 | Forwards Summary of Compliance W/Reg Guide 1.97,Rev 3 Re Emergency Response Capability.Util Endorses BWR Owners Group Position That Fully Qualified Class 1E post-accident Neutron Monitoring Sys Inappropriate |
ML20011D165 | 31 December 1989 | Final Assessment Rept. |
ML20012D449 | 15 March 1990 | Proposed Tech Specs Re Limiting Condition for Operation & Surveillance Requirements for Core & Containment Cooling Sys & Core Spray & LPCI Sys |
ML20012F575 | 6 April 1990 | LER 90-003-00:on 900311,automatic Actuation of Main Steam Sys Group 1 Portion of Primary Containment Isolation Control Sys Occurred.Caused by False High Reactor Vessel Water Level Signal.Procedure Developed Re backfill.W/900406 Ltr |