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 Report dateSiteEvent description
05000424/LER-1990-006, Responds to NRC 940509 Demand for Info Re Actions of Four Individuals Associate W/Plant in Finalizing 900629 Cover Ltr for Rev to LER 90-006Vogtle
05000424/LER-1990-011Vogtle
05000424/LER-1990-012Vogtle
05000424/LER-1990-013Vogtle
05000424/LER-1991-004, Submits Addl Info Re Amended 2.206 Petition Filed by M Hobby & a Mosbaugh Re Failure to Comply W/Tech Spec 3.0.4 on Entry Into Mode 6 on 900301,described in LER 91-004-00Vogtle
05000424/LER-1993-004Vogtle
05000424/LER-1993-009Vogtle
05000424/LER-1997-002, Forwards LER 97-002-02,per 10CFR50.73.Encl Is Second Rev to LER Originally Submitted on 970220 & First Revised on 970730.Revs Are Marked W/Rev Bars in Left Hand BorderVogtle
05000424/LER-1997-004, Corrected Copy of Forwarding LER 97-004-00,re Condition Discovered to Exist on 970322Vogtle
05000424/LER-1998-001, Forwards LER 98-001-01 Re Concrete Degradation Found in DG Exhaust Barriers.Changes Made Under Rev Marked W/Rev Bars on Left,Outside of LER BorderVogtle
05000424/LER-1998-006, Forwards LER 98-006-03 Re Motor Control Ctr Breaker Buckets Not Being Seismically Qualified.Rev Is Submitted to Document Results of Seismic Testing That Demonstrated That No Condition Outside Design Basis of TS Requirements ExiVogtle
05000424/LER-1998-007, Forwards LER 98-007-00,re Inadequate Surveillances Due to Improperly Performed Response Time Testing,On 981215,IAW 10CFR50.73Vogtle
05000424/LER-1998-009, Forwards LER 98-009-00 Re Event in Which Improper Testing Method Resulted in Inadequate Surveillances on 981229Vogtle
05000424/LER-2002-002Vogtle

On April 5, 2002, personnel were performing thermal overload bypass testing. A thermal overload bypass jumper was found disconnected in motor control center (MCC) cubicle 1BBE-07. The affiliated load for this circuit is the Reactor Coolant System Hot Leg Sample Valve, 1HV-3548, which is also a containment isolation valve (CIV). The jumper was promptly re-connected.

Without the jumper in place, an overcurrent condition may have tripped the valve's (1HV-3548) thermal overload, rendering it incapable of performing its containment isolation function of closing.

Technical Requirements Manual, Section 13.8.2, requires that a motor-operated valve with an inoperable thermal overload bypass jumper be declared inoperable and the appropriate Technical Specification (TS) condition be entered. Because 1HV-3548 is a CIV, TS 3.6.3, "Containment Isolation Valves," is applicable. Since steps had not been taken to comply with action statement requirements, the unit operated in a condition prohibited by the TS.

The cause of this event was the failure to properly install and verify the bypass jumper installation during the previous refueling outage. Personnel involved with this event will be counseled regarding the need for diligence when installing and verifying safety-related wiring. In addition, this event will be added to operating experience training for electricians.

05000424/LER-2002-003Vogtle

On April 20, 2002, power ascension was in progress following a refueling outage. At 0500 EDT, a control room alarm was received due to the water level decreasing in steam generator (SG) #4. The reactor operator (RO) increased the speed of the A main feedwater pump (MFP). Almost simultaneously, the balance-of-plant operator recognized that the A MFP mini-flow valve was open and an operator in the turbine building was directed to shut it. Water levels in all four SGs began to rise rapidly, and operators lowered the MFP speed and throttled the main feedwater regulating valves. However, at 0509 EDT, SG #4 reached its high level setpoint which led to a turbine trip, a main feedwater isolation, and an auxiliary feedwater system actuation. The shift superintendent ordered a manual reactor trip, which occurred at 0510 EDT.

The causes of this event are: the failure to increase MFP speed in normal increments to correspond with increased water demand as reactor power was rising, and an inadequate response to the SG water levels when it was recognized that levels had dropped too low. The operating crew involved has been counseled on the expectations of managing evolutions and performed just-in-time training prior to assuming the next shift.

05000424/LER-2004-001Vogtle

On March 27, 2004, at 2110 EST, control room operators tied the generator to the grid. At 2150 EST, an operator observed steam flow/feed flow mismatch alarms and noticed that the speed of the inservice main feed pump, MFP B, was increasing. The feed pump speed control was switched from automatic to manual, but to no effect. Operators then changed speed control systems. This also had no effect on the increasing speed, and steam generator (SG) water levels began to fluctuate. Operators manually tripped the reactor at 2205 EST. The operators then tripped MFP B and the auxiliary feedwater system (AFW) actuated. The unit was stabilized in Mode 3 (Hot Standby) at 2209 EST.

The cause of this event was a control valve hydraulic operating cylinder sticking in the open position so that the speed of the feed pump turbine could not be controlled. The valve stuck open due to misalignment of the hydraulic cylinder shaft with bushings in the cylinder cover. The bushings were properly aligned, the feed pump returned to service, and the reactor returned to normal power operations.

05000424/LER-2006-0019 June 2006Vogtle

On April 15, 2006, while at 100% power, the Unit 1 Control Room crew was challenged by an erratic response of the Loop 3 Main Feed Regulating Valve (MFRV), 1FV0530, while operating in automatic.

The crew was able to stabilize the valve in manual mode, however, over the next 24 hours the control of the valve continued to degrade. On April 16, 2006, it was decided that Unit 1 would be taken to Mode 3 for investigation of the control issue with 1FV0530. On April 17, 2006, at 0026 EDT, Unit 1 was manually tripped at 33% power when Steam Generator number 3 water level was observed to be slowly increasing with 1FV0530 unable to control level in either automatic or manual.

A review found that 1FV0530 operated erratically due to a failed I/P transducer, which resulted in the inability to reduce feedwater flow requiring a manual reactor trip. Based on the results of the observations and failure analysis performed on the I/P transducer, two failures were identified. One failure was the supply air input connector and the resultant electrical to pneumatic conversion process for a valve internal to the controller, and the second failure was the electronic circuit board. The failed transducer and the remaining Unit 1 MFRV I/P transducers were replaced with different make and model I/P transducers prior to the unit restart.

NNW.r -.Wpm JO. VErg.

U.S. NUCLEAR REGULATORY COMMISSION

05000424/LER-2006-00222 September 2006Vogtle

The week of June 6, 2005, a Vogtle Equipment Qualification Program self-assessment was performed that identified a potential problem with the Rosemount model 1153 Series B and 1154 transmitters if the neck seal is broken. This seal protects the transmitter electronics from moisture intrusion to ensure the safe operation of the transmitter during accident conditions. This self-assessment resulted in the development of an inspection plan to determine if this condition existed at Vogtle. The inspection plan was initiated in June 2005 and completed in August 2006. The following three Technical Specification (TS) instruments were determined to have been inoperable as a result of a broken neck seal: 1FT-5152, Steam Generator (SG) 1 Auxiliary Feedwater Flow, 2PT-0455, Pressurizer Channel 1 Pressure, and 1PT-0456, Pressurizer Channel 2 Pressure.

Per the vendor manual, the connection between the electronic housing and the sensor module is hermetically sealed with a baked-on environmentally qualified neck seal. The cause of the event was a result of inadequate installation and calibration procedure guidance in that a caution statement from the vendor manual not to break the neck seal between the sensor module and the electronics housing was not included. All three transmitters were replaced, and appropriate maintenance procedures have been updated to reflect the vendor manual caution to not rotate the head.

A.,,, rAllial IA& illitilllidn �NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (1-2001) Vogtle Electric Generating Plant - Unit 1 05000-424 2006 --� 002 --� 00 20F5

05000424/LER-2008-00120 June 2008Vogtle

On April 21, 2008 at 0951 EDT, Unit 1 entered Mode 3, from Mode 4, with the pressurizer heaters in Group A inoperable. Unit 1 entered Mode 3 in a condition prohibited by Technical Specification (TS) 3.0.4. The condition was identified during a pressurizer heater capacity test on April 21, 2008 at 1818 EDT, when a Maintenance electrician observed open breakers on the Group A and C heater panels. The Unit 1 Control Room was immediately notified, and Operations entered a Required Action statement for TS 3.4.9, based on inoperability of pressurizer heater Group A while in Mode 3. The heater breakers were subsequently closed within the 72-hour Required Action statement.

The primary cause of this event was inadequate work instructions to perform the necessary pressurizer heater work. The functional testing requirement to complete heater resistance measurements was not properly planned in the work order to ensure that the equipment was properly tested before being placed in service. In addition, human performance tools were not used by the individuals involved in the manipulation of the breakers when it was determined the instructions were not adequate. The supplemental electrician associated with the pressurizer heater breaker mispositioning event was unaware of the plant procedure used to document breaker manipulation.

05000424/LER-2008-002Vogtle

On December 10, 2008 at approximately 13:10 hrs Eastern Standard Time (EST), Southern Nuclear Operating Company (SNC) Nuclear Fleet Security contacted Vogtle Electric Generating Plant (VEGP) site Security, regarding the failure of a supplemental worker to self-disclose a custodial arrest that had occurred on April 23, 2004. The supplemental worker had been granted Unescorted Access to VEGP on four separate occasions. The supplemental worker was first badged at VEGP from April 5, 2004 to April 30, 2004, during which time the custodial arrest occurred. The supplemental worker was again granted Unescorted Access from February 22, 2005 to April 2, 2005, from September 15, 2005 to October 6, 2005, and from September 12, 2006 to October 9, 2006.

An investigation by SNC Nuclear Fleet Security was performed and it was determined that the supplemental worker failed to disclose the custodial arrest, while under the Unescorted Access (UA) program in April 2004, and during the subsequent requests for Unescorted Access Authorization (UAA).

The supplemental worker has been denied UA at all SNC facilities and flagged in the Personnel Access Data System (PADS).

_

05000424/LER-2009-002Vogtle

On December 7, 2009, at approximately 18:01 hours Eastern Standard Time (EST) with Unit 1 operating at 100 percent rated thermal power, an automatic turbine trip occurred due to low main condenser vacuum. In response to the turbine trip, the Reactor Protection System (RPS) actuated and automatically opened the reactor trip breakers. All control rods fully inserted into the core and all safety systems responded per design. Both Motor Driven Auxiliary Feedwater pumps and the Turbine Driven Auxiliary Feedwater pump started in accordance with plant design due to lo-lo steam generator water level in two steam generators. The unit was stabilized in Mode 3.

The cause of the low condenser vacuum was determined to be inadvertent operation of a control room handswitch that resulted in a de-energization of a non-lE 480 volt switchgear. The loss of power to the non-lE 480 volt switchgear resulted in the defeat of an interlock on the loop seal drain valve for the standby Steam Jet Air Ejector (SJAE) which allowed the valve to open. Once the water in the loop seal had drained to the main condenser, a path between the condenser and the atmosphere was established and the main condenser vacuum started to decline. Approximately nine minutes elapsed from the time the handswitch was inadvertently opened until the low main condenser vacuum turbine trip setpoint was reached which resulted in the automatic turbine trip and subsequent automatic reactor trip.

_

05000424/LER-2009-003Vogtle

On December 09, 2009 at approximately 23:10 hours Eastern Standard Time (EST), during power ascension from an unplanned shutdown, with the unit operating at approximately 24 percent rated thermal power, the reactor was manually tripped. As preparations were being made to synchronize the main generator to the grid, high vibrations were experienced on the high pressure turbine. Due to the high vibrations on the turbine, the turbine was manually tripped. As the turbine was coasting down vibration levels continued to increase. Therefore condenser vacuum was broken to slow the turbine to minimize any potential damage. Prior to breaking condenser vacuum and in anticipation of the trip of the operating main feedwater pump due to low condenser vacuum, the control room operators manually tripped the reactor.

Once condenser vacuum had decreased below the main feedwater pump trip setpoint, the main feedwater pump tripped and the motor driven auxiliary feedwater (AFW) pumps automatically started. All control rods fully inserted and all safety systems responded in accordance with plant design. The plant was stabilized in Mode 3.

_

05000424/LER-2011-00224 October 2011Vogtle

On August 31, 2011 with Unit 1 operating in Mode 1 at 100 percent rated thermal power at approximately 0906 hours Eastern Daylight Time, the Unit 1 reactor automatically tripped. In preparation for maintenance on the controls for the main feedwater regulating valve (MFRV) on steam generator (S/G) 2, the valve was placed on an air gag. The air gag maintains the MFRV in position and allows minor changes in steam generator water level to be controlled by the bypass feedwater regulating valve (BFRV). However, shortly after the air gag was installed, feedwater flow to S/G 2 increased beyond the capability of the BFRV to control. The increase in feedwater flow to S/G 2 resulted in water level on S/G 2 exceeding the Hi-Hi nominal trip setpoint (NTS). This caused a main feedwater isolation, turbine trip and subsequent reactor trip in accordance with plant design.

The cause of the event was due to increased air pressure being supplied to the MFRV when the valve was placed on the air gag. The first corrective action was revising the procedure to ensure calibrated test gauges are used to determine the pressure setting of the regulator for the air gag and for an operator to be present while the MFRV is controlled by the air gag. The second corrective action is to replace the contact type potentiometer used in the MFRV control circuit which has been proven unreliable.

05000424/LER-2011-003Vogtle

On September 22, 2011 at approximately 0155 hours Eastern Daylight Time (EDT) as a System Operator entered the control room, he noted that the differential pressure across the door was not what he was accustomed to. The Unit Operator was notified and it was determined that the Control Room Normal HVAC (Heating, Ventilation, and Air Conditioning) Outside Air Damper, AHV-12153 was closed. With AHV-12153 closed, all air flow through the control room radioactive gas monitors is stopped, rendering them inoperable. After verifying that there was not a valid reason for the damper to be closed, AHV-12153 was opened restoring air flow through the control room radioactive gas monitors. A subsequent review of the plant computer shows that the damper closed on September 19, 2011 at approximately 2029 hours EDT. Because the Technical Specifications (TS) require the control room emergency filtration system (CREFS) to be placed in the emergency mode if the control room air intake radioactive gas monitors are inoperable for more than one hour, and this was not done, the units operated in a condition prohibited by the TS.

An investigation into the cause for the damper to close was inconclusive. However, to preclude this event from happening in the future, a design change will be implemented to provide a control room annunciation to alert the operators of the condition.

05000424/LER-2012-00111 April 2012Vogtle

On February 15, 2012, with the unit at 100 percent power, it was determined that opening the boundary valve between the safety related and seismically qualified Refueling Water Storage Tank (RWST) and the non safety related and non seismically qualified Spent Fuel Pool Purification (SFPP) system in Modes 1-4, renders the RWST inoperable. Plant procedures had been revised In 2009 to allow opening this boundary valve in Modes 1-4 under administrative controls. The 10 CFR 50.59 safety evaluation that had been performed to support the procedure change had concluded that the administrative controls would allow the RWST to remain operable. However, in consideration of the new interpretation provided in NRC Information Notice 2012-01, it was judged that the RWST would be considered to be inoperable regardless of the administrative controls established when the RWST was aligned to non-seismic piping in Modes 1 - 4. Since the boundary valve had been opened in Mode 1 under administrative controls and the one hour completion time of Technical Specification 3.5.4 Condition D was not entered, under this recent interpretation, this represented a condition prohibited by Technical Specifications and is reportable pursuant to 10 CFR 50.73(a)(2)(I)(B). This event had no significant safety consequence since a seismic event had not occurred while the SFPP system was in service on the RWST.

NRC FORM 386 (10.2010)

05000424/LER-2012-003VogtleOn August 17, 2012, 1A ESF Chiller condenser vacuum was noted to be 12 inches of mercury, with a vacuum of 15 inches of mercury specified as the low limit on operating logs. The Shift Supervisor mistakenly believed condenser pressure was one of the parameters in which engineering had evaluated and was continuing to monitor. This misinformation was carried forward through subsequent shifts via logs. During the next five days, 1A ESF Chiller condenser vacuum decreased to 4 inches of mercury and stabilized for an additional four days prior to Initiation of a condition report (CR) on August 26, 2012. Subsequent investigation and consultation with the vendor determined the 1A ESF Chiller was inoperable and the technical specification LCO was entered at 1437 on August 26, 2012. As a result of the delay in recognition of the status of the subject chiller, appropriate entries into LCOs 3.7.14 and 3.0.3 were not taken. Neither the safety of the plant nor the public health and safety were affected in a significant way by these events_
05000424/LER-2012-0043 December 2012VogtleOn October 5, 2012 with Unit 1 in Mode 5 and the residual heat removal (RHR) system in service for reactor coolant system temperature control, activities were in progress in preparation for Mode 4 entry. One of the activities involved restoration of the steam generator level RPS/ESFAS instrumentation from a bypassed condition to normal alignment. During the restoration a steam generator lo-lo level actuation was received and the motor-driven auxiliary feed water (AFW) pumps started and two turbine-driven AFW discharge valves stroked full open. The AFW system had previously been removed from service per the controlling unit operating procedure; however, following safety system testing during the outage the AFW system was not properly aligned to prevent inadvertent actuations. Neither the safety of the plant nor public health and safety were affected by this event.
05000424/LER-2012-0053 December 2012VogtleVogtle Unit 1 experienced a mismatch in secondary steam flow during power ascension from 2% to 10% reactor power (Mode 2 to Mode 1). The control room operators confirmed the mismatch by observing divergence in reactor coolant system loop differential temperatures, secondary steam pressures, and secondary steam flows between loops one and four and loops two and three. At this time, the reactor was manually shutdown. Subsequent investigation determined the outboard main steam isolation valve on main steamlines two and three were indicating open in the Main Control Room when, in fact, the valves were closed. Neither the safety of the plant nor public health and safety were affected by this event.
05000424/LER-2013-00116 January 2014Vogtle

On November 27, 2013, an internal wiring discrepancy was discovered on Class 1 E battery charger 1AD1CB (EJ) following the trip of the battery charger AC input breaker.

The wiring discrepancy prevented the battery charger from performing all required functions of LCO 3.8.4, DC Sources - Operating. One of two redundant battery chargers and one battery per train must be operable to meet the requirements of LCO 3.8.4. Subsequent review of battery charger maintenance activities determined that on September 30, 2013 the remaining redundant operable battery charger was removed from service for maintenance activities for approximately 14.5 hours.

LCO 3.8.4, DC Sources - Operating requires restoration of the inoperable DC source within 2 hours or entry into Mode 3 within the next 6 hours, and entry into Mode 5 within the following 30 hours. Although the degraded charger was able to maintain battery terminal voltage within limits under minimal loading condition, the DC source was inoperable for a time greater than allowed by Technical Specification.

The safety significance of this event is very low. Unit 2 was not affected and there were no adverse effects to the health and safety of the public.

NRC FORM 365(104010) NRC RM 365I1 004010) FO LICENSEE EVENT REPORT (LEI) U.S. NUCLEAR REGULATORY COMMISSION

05000424/LER-2014-001Vogtle

On February 20, 2014 with VEGP Units 1 and 2 operating at 100 percent thermal power, VEGP identified that both units had operated outside the Pressure / Temperature Limit Report (PTLR) curve required by Technical Specification LCO 3.4.3 RCS Pressure and Temperature Limits following the seven previous refueling outages on each unit. From October 2003 through May 2013, seven refueling outages have been conducted on each unit in which the Reactor Pressure Vessel (RPV) was placed under vacuum to perform fill and vent operations. LCO 3.4.3 requires that Reactor Coolant System (RCS) pressure, temperature, and heatup and cooldown rates be maintained with the limits specified in the Pressure Temperature Limit Report (PTLR) and is applicable at all times. Although minimum RCS temperature and heatup rates were maintained within limits, RCS pressure was lowered below 0 pounds per square inch gauge (psig), the lowest RCS pressure value identified on the curve.

The cause of not entering LCO 3.4.3 was the condition was procedurally allowed and aligned with Operations training. These events are of very low safety significance and resulted in no adverse effects on the health or safety of the public.

05000424/LER-2014-002Vogtle

On 4/12/14 at 20:08, Unit 1 Reactor was manually tripped from 28 percent power. The manual trip occurred during power ascension following the 1R18 refueling outage. Control room operators received a Loop 1 Train B main steam isolation valve (MSIV) trouble annunciator followed by the MSIV not fully open annunciator. Control room operators recognized steam generator 1 level and loop 1 steam flow lowering and manually tripped the reactor.

Unit 1 was stabilized in Mode 3. Plant systems responded as expected with decay heat removal via Auxiliary Feedwater and steam discharge to the Main Condenser. Unit 2 was unaffected and there were no adverse effects on plant safety or on the health and safety of the public. This incident is of very low safety significance.

05000424/LER-2014-003Vogtle

At 11:16 on May 30, 2014 Operations declared 1A CREFS inoperable upon notification that 1A Control Room Emergency Filtration System (CREFS) charcoal adsorber sample taken on April 15, 2014 had a 99.66 percent retention value. This failed to meet the Technical Specification 5.5.11 Ventilation Filter Testing Program (VFTP) retention criteria of 99.8 percent. This report is made pursuant to 10 CFR 50.73 (a)(2)(i)(B) as a condition prohibited by Technical Specifications.

The charcoal was replaced and on June 6, 2014 Unit 1A CREFS was returned to service. During the event, Unit 1 was operating at 100 percent rated thermal power at steady-state conditions and Unit 2 was unaffected. Therefore, there were no adverse effects on plant safety or on the health and safety of the public. This incident is of very low safety significance.

05000424/LER-2014-00425 September 2014Vogtle

On July 27, 2014 at approximately 1409 Eastern Daylight Time, Vogtle Unit 1 was operating in Mode 1 at 100 percent power. While surveillance testing was being performed on the Main Feed Pump A (MFP A) a control oil leak developed in the lockout solenoid valve. The reduced control oil pressure resulted in a reduction of feed pump speed. Control Room Operators observed lowering feedwater flow to the Steam Generators and manually actuated the Reactor Protection System (RPS) system which resulted in a turbine-generator trip. All rods fully inserted into the core, the Main Feedwater Isolation system and the Auxiliary Feedwater system automatically actuated as expected. The unit was stabilized in Mode 3 and decay heat was discharged to the condenser. The cause of the event was a failure of the trip lockout solenoid valve which led to reduced pressure on the trip relay for MFP-A which reduced the speed of the pump and consequently the total feed flow to the Steam Generators.

The safety significance of the event is very low. Unit 2 was not affected and there were no adverse effects on the health and safety of the public.

APPROVED BY OMB: NO. 3150-0104 EXPIRES: 01/31/2017 Estimated burden per response to corn* Mth this mandatory collection request 80 hours.

Reported lessons teamed are incorporated into the Ficensitv process and fed back to industry.

Send comments regardng burden estimate to the FOIA. Rimy and Information Collections Branch (T-5 F53). U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NE013-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not dsplay a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

05000424/LER-2017-00229 June 2017Vogtle

On March 17, 2017, at approximately 1517 EDT, during refueling operations on Unit 1, power was being restored to the Open Phase system for the 1-B Reserve Auxiliary Transformer (RAT). During restoration, a valid undervoltage actuation signal was sent to the 1-B Emergency Diesel Generator (EDG). The EDG automatically started and tied to the safety bus.

This undervoltage condition was caused by a wiring error in the Open Phase system to the 1-B RAT.

Unit 1 was in Mode 6 at the time and remained so throughout the event. There was no change in the decay heat removal for the plant.

Because this event resulted in the automatic actuation of a system listed in 10 CFR 50.73(a)(2)(iv)(B), this event is reportable under 10 CFR 50.73(a)(2)(iv)(A). This event had no adverse effect on the health and safety of the public, and is of very low safety significance.

Unit 2 was unaffected.

05000425/LER-1990-008Vogtle
05000425/LER-1993-005Vogtle
05000425/LER-1998-004, Forwards LER 98-004-01 Re Defeat of Turbine Trip Function That Lead to Improper Mode Entry.Revised LER Corrects Statement Re Generation of Turbine Trip Signal Upon Operating Reactor Trip BreakersVogtle
05000425/LER-1998-005, Forwards LER 98-005-01,extending Completion Date for Corrective Action 6 Which Is Necessary to Involve Offsite Engineering Organizations in Performance of Broadness Review.Corrective Actions 2 & 5 Have Been UpdatedVogtle
05000425/LER-2005-00219 September 2005Vogtle

Reactor Coolant System Loop 2 Overtemperature Delta-T (OTDT) instrument channel 2T-421 was restored to service on February 26, 2005, following maintenance to correct overtemperature setpoint (OTSP) drift by replacing a summing amplifier. After the channel was returned to service, the OTSP signal continued to drift until March 3, 2005, when 2T-421 was again removed from service and a different summing amplifier replaced, correcting the drift anomaly. On July 21, 2005, an engineering evaluation of the instrument channel drift evolution concluded that this channel's OTSP signal had drifted outside of the Technical Specifications (TS) allowable values for the input signals for a period of time longer than allowed by the action requirements. Therefore, the unit had operated in a condition prohibited by the TS.

The causes of this event include the failure to perform adequate troubleshooting and post-maintenance testing on February 26, 2005. I&C technicians and their supervision were advised of the proper course of action expected for this type of event, and procedures were revised to clarify the expectations for functional testing following corrective maintenance.

05000425/LER-2006-0016 April 2006Vogtle

On February 1, 2006, control room operators received indication of an increase in radioactivity in the containment atmosphere. On February 3, 2006, a robotic camera observed leakage inside the bioshield wall in the area of reactor coolant system (RCS) loop 1. Unit 2 was placed in Mode 3 (Hot Standby) at 1806 EST, on February 3, 2006, to allow further investigation of specific leakage locations. At 2124 EST, this investigation found RCS pressure boundary leakage at two welded connections on a 'A" bypass line around the Residual Heat Removal (RHR) loop suction valve, 2HV 8701B, and shutdown to Mode 5 (Cold Shutdown) was initiated. On February 5, 2006, at 0035 EST, Unit 2 entered Mode 5 to comply with Technical Specification 3.4.13.a. due to the RCS pressure boundary leakage.

Although the cause of the weld failures is undetermined at this time, the root cause investigation is still underway. Issues being addressed include high vibration of the bypass line, support design, excessive weld stress, and weld quality. The theory presented by the root cause team is the cause of the cracks was from high cycle fatigue. Corrective actions included replacement of the Loop 1 bypass line, inspection of supports and snubbers for both Unit 2 bypass lines, inspection of welds on the Loop 4 bypass line, and installation of monitoring instrumentation. Following additional monitoring, the cause determination will be completed, follow-up corrective actions implemented and a revised LER will be submitted by July 11, 2006.

05000425/LER-2010-00212 October 2010Vogtle

On August 23, 2010 an Operations Superintendent was reviewing past performances of the reactor trip breaker surveillance test in preparation for an upcoming surveillance test on a reactor trip breaker.

During this review it was determined that on January 28, 2010 the 2B Solid State Protection System (SSPS) Mode Selector switch was placed in Test to perform a surveillance test on the 2B reactor trip breaker. Placing the 2B SSPS Mode Selector switch in Test defeats the Engineered Safety Features (ESF) automatic actuation signal to the 2B train components. At the time 2B SSPS Mode Selector was placed in test, the 2A high head safety injection (HHSI) pump was tagged out of service for planned maintenance. In this configuration, both trains of HHSI were rendered inoperable and outside the Conditions stated in Technical Specification 3.5.2, since neither train would have automatically started on an ESF actuation signal. Although not recognized at the time of the event, this condition required entry into Technical Specification LCO 3.0.3.

The cause of this event was due to an inadequate Loss of Safety Function (LOSF) determination, as described in Technical Specification 5.5.15, being performed and the work planning process not adequately identifying potential Technical Specification implications for the scheduled work.

hNRC FORM 366 (9-2007) PRINTED ON RECYCLED PAPER 5

05000425/LER-2013-00122 April 2013Vogtle

On February 26, 2013, at approximately 2302 Eastern Daylight Time (EDT) time, with Unit 2 operating in Mode 1 at 94 percent rated thermal power and End of Life (EOL) Coastdown in progress, Unit 2 operators initiated a manual reactor trip due to Reactor Coolant Pump (RCP) #4 number one seal leakoff flow exceeding the operating limits. The Reactor Trip System, the Engineered Safety Feature Actuation System, and other responding equipment performed as expected. The plant was stabilized in Mode 3. The cause of the event was the addition of air into the Chemical Volume Control System (CVCS) charging system as a result of less than adequate filling and venting of the Reactor Coolant System filter.

The safety significance of this event is low. Unit 1 was unaffected and there were no adverse effects on the health and safety of the public.

05000425/LER-2014-00130 May 2014Vogtle

On April 8, 2014 at approximately 04:30 Eastern Standard Time, Vogtle Unit 2 was operating at Mode 1 at 100 percent power when Unit 2 received a Steam Generator 3 narrow range low-low level automatic Reactor Protection System actuation as a result of the Loop 3 Main Feedwater Regulating Valve failing closed. The RPS actuation resulted in a trip of the turbine-generator. All rods fully inserted into the core, the Main Feedwater Isolation system and the Auxiliary Feedwater system automatically actuated as expected. The plant was stabilized in Mode 3 and the decay heat was discharged to the condenser. The cause of the event was a failure of the Steam Generator 3 Main Feed Regulator Valve control system.

The safety significance of the event is very low. Unit 1 was not affected and there were no adverse effects on the health and safety of the public.

05000425/LER-2014-003Vogtle

On October 12, 2014 at approximately 0944 EST, while performing Unit 2 reactor startup, control rods were being inserted to stabilize Rx power for Low Power Physics Testing. With the rod bank selector switch in Manual, operators observed control bank A inserting instead of the expected D bank inserting. Operators took action to trip the reactor and stabilize the plant. The cause of this event was incorrect setup of the Rod Bank Overlap unit.

was not affected and there were no adverse effects on the health and safety to the public. Therefore, the safety significance of this event is very low.

05000425/LER-2015-00113 May 2015Vogtle

On March 14, 2015 at approximately 04:29 AM Eastern Daylight Time (EDT), Vogtle Unit 2 was operating in Mode 1 at 100 percent power when the Loop 3 outboard Main Steam Isolation Valve (MSIV) spuriously closed. The sudden closure of the steam isolation valve caused a rapid pressure reduction in the remaining three Steam Generators (SGs) due to increased steam flow resulting in a Reactor Protection System (RPS) actuation due to rate compensated Low Main Steam Line Pressure Safety Injection and Steam Line Isolation. All control rods fully inserted and all equipment actuated as designed.

The unit was stabilized in Mode 3 with decay heat being removed through the atmospheric relief valves (ARVs) to the environment. The Loop 3 MSIV closure was due to failure of the hydraulic dump solenoid valve which resulted in a loss of hydraulic pressure to the MSIV.

This event had no adverse effect on the health and safety of the public, and is of very low safety significance. This event is reportable per 10 CFR 50.73(a)(2)(iv)(A) due to actuation of a system listed in 10CFR 50.739a)(2)(iv)(B). Unit 1 was unaffected.

NRC FORM 360 (02-2014)

05000425/LER-2015-00213 May 2015Vogtle

On March 14, 2015 at 1207 Eastern Daylight Time (EDT), Unit 2 was operating in Mode 3 following an unplanned reactor trip and safety injection, a valid Auxiliary Feedwater (AFW) actuation signal was received on B-train Auxiliary Feedwater system during post-trip recovery and unit stabilization. Both Train A and Train B motor driven AFW pumps were in service at the time. Upon receipt of the AFW actuation signal the B-train discharge valves stroked to the full open position. Operators immediately restored AFW discharge valves to their previous positions without any adverse impacts on the unit.

The plant remained in Mode 3 and decay heat continued to be removed via the Atmospheric Relief Valves.

Unit 1 was unaffected. This event had no adverse effect on the health and safety of the public, and is of very low safety significance. This event is reportable per 10 CFR 50.73(a)(2)(iv)(A) due to actuation of a system listed in 10CFR 50.739a)(2)(iv)(B).

05000425/LER-2017-001Vogtle

Between January 16 and February 13, 2017, a power supply that supports operation of one of two ventilation supply fans for the 2A Emergency Diesel Generator (EDG) failed. Vogtle Electric Generating Plant (VEGP) Technical Specifications (TS), 3.8.3 Condition F requires restoration of the fan within 14 days or the EDG must be declared inoperable. This condition was not identified by operators because there is no failure indication. Therefore, the power supply was not repaired within the required time. The EDG should have been declared inoperable and TS 3.8.1. Condition B entered.

Subsequently the completion time for TS 3.8.1 Condition B expired and the unit should have been shut down. This action was not taken and Unit 2 operated in a condition prohibited by TS.

Between February 13 and February 22, 2017, the second power supply failed on this EDG resulting in the second ventilation supply fan being inoperable. Since no failure indication is available, this condition was not identified by the operators. The TS 3.8.3 action for two power supplies inoperable is to immediately declare the EDG inoperable.

Subsequently, the completion time expired and the unit operated in a condition prohibited by TS. During a monthly surveillance run on March 8, both power supplies were discovered failed. Both power supplies were replaced on March 9, 2017 and the EDG was declared operable.

05000425/LER-2017-002Vogtle

On September 26, 2017, at approximately 0543 EDT, while performing 2B Emergency Diesel Generator (EDG) and Emergency Safety Function Actuation System (ESFAS) testing, a valid undervoltage actuation signal was sent to the Unit 2 B-Train Emergency Diesel Generator. The 2B AC emergency bus (2BA03) was load shed, the 2B EDG automatically started, and tied to 2BA03 The 2BA03 bus was loaded by the automatic load sequencer. The actuation was identified by the Control Room operators and the 2B EDG was locally monitored while in service.

An air leak on the shutdown logic board caused a non-emergency trip to actuate when the non-emergency trips were unblocked.

The reactor was in Mode 6 at the time of the event and not challenged throughout the event.

Decay heat removal and spent fuel pool cooling were not challenged throughout the event.

Because this event resulted in the automatic actuation of a system listed in 10 CFR 50.73(a)(2)(iv)(B), this event is reportable under 10 CFR 50.73(a)(2)(iv)(A). This event had no adverse effect on the health and safety of the public, and is of very low safety significance.

Unit 1 was unaffected.