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 Report dateSiteEvent description
05000313/LER-1950-313, Responds to NRC 920505 Request for Addl Info Re Offsite Power Supplies,Delineated in LER 50-313/91-010-01.Long-range Plans to Ensure That 161 Kv Offsite Power Source Will Meet GDC 17 & 5 Requirements Also ProvidedArkansas Nuclear
05000313/LER-1978-028, Forwards LER 78-028/03L-0Arkansas Nuclear
05000313/LER-1982-008, Forwards LER 82-008/03L-0Arkansas Nuclear
05000313/LER-1982-009, Forwards LER 82-009/01T-0Arkansas Nuclear
05000313/LER-1982-010, Forwards LER 82-010/03L-0Arkansas Nuclear
05000313/LER-1982-011, Forwards LER 82-011/03L-0Arkansas Nuclear
05000313/LER-1982-012, Forwards LER 82-012/03L-0Arkansas Nuclear
05000313/LER-1982-013, Forwards LER 82-013/03L-0Arkansas Nuclear
05000313/LER-1982-014, Forwards LER 82-014/03L-0Arkansas Nuclear
05000313/LER-1982-015, Forwards LER 82-015/03L-0Arkansas Nuclear
05000313/LER-1982-016, Forwards LER 82-016/03L-0Arkansas Nuclear
05000313/LER-1982-017, Forwards LER 82-017/03L-0Arkansas Nuclear
05000313/LER-1982-018, Responds to Requesting Addl Info Re Fire Barrier Penetration Seals Per LER 82-018/03L-0.All Penetrations & Conduits Properly SealedArkansas Nuclear
05000313/LER-1982-019, Forwards LER 82-019/03L-0Arkansas Nuclear
05000313/LER-1982-020, Forwards LER 82-020/03L-0Arkansas Nuclear
05000313/LER-1982-021, Forwards LER 82-021/03L-0Arkansas Nuclear
05000313/LER-1982-024, Forwards LER 82-024/03L-0Arkansas Nuclear
05000313/LER-1982-025, Forwards LER 82-025/03L-0Arkansas Nuclear
05000313/LER-1982-026, Forwards LER 82-026/03L-0Arkansas Nuclear
05000313/LER-1982-027, Forwards LER 82-027/03L-0Arkansas Nuclear
05000313/LER-1983-002, Forwards Revised LER 83-002/03X-1Arkansas Nuclear
05000313/LER-1983-003, Forwards LER 83-003/03L-0Arkansas Nuclear
05000313/LER-1983-004, Forwards LER 83-004/03L-0Arkansas Nuclear
05000313/LER-1983-005, Forwards LER 83-005/03L-0Arkansas Nuclear
05000313/LER-1983-006, Forwards LER 83-006/03L-0Arkansas Nuclear
05000313/LER-1983-007, Revised LER 83-007/03X-1:on 830308 & 21,reactor Bldg Pressure Switches PS-2403 & PS-2401 Found to Be Out of Tolerance,Opening at 18.9 Psia.Pressure Switches Reset at 18.5 Psia Per Calibr ProcedureArkansas Nuclear
05000313/LER-1983-008, Forwards LER 83-008/03L-0Arkansas Nuclear
05000313/LER-1983-009, Forwards LER 83-009/03L-0Arkansas Nuclear
05000313/LER-1983-010, Forwards LER 83-010/03L-0Arkansas Nuclear
05000313/LER-1983-023, Updated LER 83-023/03X-6:on 830916-1120,fire Protection Deficiencies Discovered.Caused by Inadequate Original Installation Specs & Acceptance Criteria.Walkdown Insp in Progress.Insp Program Being DevelopedArkansas Nuclear
05000313/LER-1986-002, Requests Extension Date of 860930 to Allow Time to Update LER 86-002-00 Re Inadequate 10CFR50.59 Design Change ReviewArkansas Nuclear
05000313/LER-1988-029, Forwards LER 88-029-00 Re Seismic Qualification of RCS Letdown.Rept Date in Relation to Date of Determination Discussed W/Nrc in 890714 & 0721 LtrsArkansas Nuclear
05000313/LER-1989-030, Forwards LER 89-030-00 Re Piping Support Discrepancies Caused by Use of Unacceptable Modeling Techniques.Ler Date, Versus Date of Determination of Potential Inoperability of Piping,Discussed in Util 890714 & 21 LtrsArkansas Nuclear
05000313/LER-1989-041, Revises Commitment Completion Date for LER 89-041-00 Re Proper Method of Calibr of Startup Feedwater Control Valves CV-2623 & 2673 to 900915.Delay Due to Time Needed to Review & Implement New Calibr Guidance CriteriaArkansas Nuclear
05000313/LER-1990-004Arkansas Nuclear
05000313/LER-1990-021, Submits Synopsis of LER 90-021-00 Re 901222 Discovery of Potential RCS Leak in Area of Pressurizer Upper Level Instrumentation Nozzle.Caused by Pure Water Stress Corrosion Cracking.Deferral of Repair Under ReviewArkansas Nuclear
05000313/LER-1995-005, Forwards Review of NRC Preliminary Accident Sequence Precursor Analysis of LER 95-005-00 as Requested in Ltr Dtd 960423.Procedures EnclArkansas Nuclear
05000313/LER-2005-001Arkansas Nuclear

On October 13, 2005, during a scheduled refueling outage, with fuel offload in progress, super particulate iodine noble gas (SPING) effluent monitor, SPING-1, was removed from service for required surveillance testing. Operations personnel failed to recognize that Technical Specifications (TS) require SPING-1 to be operable when the reactor building purge isolation valves are open and fuel movement is in progress in the reactor building. Sampling was performed and SPING-1 was returned to service. On October 14, 2005, prior to removing SPING-1 from service again for sampling, operations personnel recognized that this configuration was not allowed with fuel movement in progress in the reactor building and realized that the removal of SPING-1 from service the previous day resulted in operation prohibited by TS. This event can be attributed to inadequate guidance regarding the TS requirement to maintain SPING-1 operability during fuel movement in the reactor building.

Procedures will be revised to ensure SPING-1 is not removed from service during fuel handling operations in the reactor building unless TS requirements are satisfied.

05000313/LER-2008-001Arkansas Nuclear

At 0855 CST, on December 12, 2008, and again at 1212 CST, on December 20, 2008, Arkansas Nuclear One, Unit-1, initiated a manual plant trip from power in accordance with plant procedures in response to receipt of asymmetric rod alarms and recognition of abnormal control rod group 7 movements. The Control Rod Drive Control System (CRDCS) was in automatic at the time of each occurrence. Post trip responses were normal with all plant systems functioning as expected and with no safety system actuations. Testing and analysis determined that the probable root cause was degradation of two of the Automatic Bus Transfer (ABT) relays as the result of inadequate preventive maintenance. The two subject ABT relays were replaced as well as the programmer for the Group 7 Control Rods which was identified as single point failure vulnerable. In addition to the immediate actions to replace the above components, actions have been initiated to evaluate and upgrade the preventive maintenance associated with the CRDCS. Additional online monitoring requirements were implemented to obtain diagnostic information and enhanced inspection requirements were implemented for the CRD programmers. Both occurrences were reported to the NRC Operations center pursuant to 10CFR50.72 reporting requirements.

  • . � A �
05000313/LER-2009-001Arkansas Nuclear

Di 20.2201(b) 0 ❑ 20.2203(a)(3)(i) p 20.2201(d) 0 20.2203(a)(3)(ii) D 20.2203(a)(1) 0 20.2203(a)(4)

  • 20.2203(a)(2)(i) 0 50.36(c)(1)(i)(A) L 20.2203(a)(2)(ii) 0 50.36(c)(1)(ii)(A)
  • 20.2203(a)(2)(iii) 0 ❑ 50.36(c)(2) E 20.2203(a)(2)(iv) 0 50.46(a)(3)(ii) ( 20.2203(a)(2)(v) 0 50.73(a)(2)(i)(A)
  • 20.2203(a)(2)(vi) 0 50.73(a)(2)(i)(B)
  • 50.73(a)(2)(i)(C) 111 50.73(a)(2)(ii)(A)
  • 50.73(a)(2)(ii)(B) 111 50.73(a)(2)(iii) U 50.73(a)(2)(iv)(A)
  • 50.73(a)(2)(v)(A) 111 50.73(a)(2)(v)(B) U 50.73(a)(2)(v)(C) 111 50.73(a)(2)(v)(D) 11. L1CF CINITACT Pen TH78 LER
05000313/LER-2009-002Arkansas Nuclear
05000313/LER-2009-00317 December 2009Arkansas Nuclear
  • 20.2203(a)(2)(vi) 0
  • 50.73(a)(2)(i)(B) 0
  • 50.73(a)(2)(v)(D)
05000313/LER-2010-001Arkansas Nuclear

On March 18-19, 2010, during setpoint testing of the main steam safety valves (MSSVs), four valves (PSV-2686, PSV-2691, PSV-2697, and PSV-2698) were discovered out-of-tolerance (00T) with respect to the technical specification (TS) +/-3% surveillance requirement (SR) 3.7.1.1. PSV-2686 was 3.75% OOT, PSV-2691 was 3.86% OOT, PSV-2697 was -3.02% 00T, and PSV-2698 was -3.18% 00T. There were two apparent causes for these conditions. The PSV-2686 and PSV-2691 OOT condition was due to seat bonding, which is characterized by the formation of an oxide adhesion layer between metal parts. The PSV-2697 and PSV-2698 OOT condition was due to transient- induced drift, characterized by a valve lifting below the desired setpoint, which occurs when the spring is exercised due to valve actuations. The MSSVs were reset to within +/-1% tolerance.

Current planned follow-up actions include retesting the affected valves after six months of operation and to continue exercising newly refurbished and installed valves within four months of installation as required by the model work order.

05000313/LER-2010-002Arkansas Nuclear

On March 27, 2010, with Arkansas Nuclear One - Unit 1 (ANO-1) in Mode 6 for a refueling shutdown, visual examinations discovered indications of through wall leakage on an ANO-1 Reactor Coolant System (RCS) pressurizer level instrument tap nozzle.

Leakage was indicated by a small amount of dry boron on the lower portion of the nozzle bore with rust stains on the Alloy 600 nozzle and in the vicinity surrounding the nozzle outlet. Subsequent inspections and evaluation revealed minor corrosion of the nozzle bore and concluded that the failure mechanism for the degradation was Primary Water Stress Corrosion Cracking (PWSCC) of Alloy 600 material. A planned mitigation repair method for the affected nozzle was implemented to resolve this condition. Also, in accordance with Arkansas Nuclear One's Inservice Inspection program, the remaining 8 pressurizer nozzles were visually inspected and exhibited no indications of leakage or degradation. During the refueling outage, all 9 pressurizer instrument nozzles were replaced with materials that are resistant to PWSCC. The pressurizer nozzles with dissimilar metal butt welds (surge, spray, and safety valve nozzles) had previously been mitigated by a full structural weld overlay.

05000313/LER-2010-0039 June 2010Arkansas Nuclear
  • 20.2203(a)(2)(vi) D
  • 50.73(a)(2)(i)(B) D
  • 50.73(a)(2)(v)(D)
05000313/LER-2010-00422 June 2010Arkansas Nuclear
  • 20.2203(a)(2)(vi) 0
  • 50.73(a)(2)(i)(B) 0
  • 50.73(a)(2)(v)(D)
05000313/LER-2011-00111 April 2011Arkansas NuclearDuring the period beginning January 22, 2008 until January 4, 2011, Arkansas Nuclear One Unit 1 (ANO-1) periodically implemented compensatory measures during maintenance or failure of Emergency Switchgear Chillers (VCH-4A, VCH-4B), Battery Room Unit Coolers (VUC-14A, VUC-14C), or Switchgear Room Unit Coolers (VUC-2B, VUC-2D). During some of these instances, compliance with Technical Specification (TS) 3.8.4, "DC Sources - Operating" and TS 3.8.9, "Distribution Systems - Operating" was not met. ANO-1 1 did not enter or remain in the appropriate TS for an inoperable system, subsystem, train or component when all the necessary attendant non-technical specification support equipment that are required for the system, subsystem, train, component or device to perform its specified safety function are also capable of performing their support function. VCH-4A or B individually have not been shown to be capable of supporting 100% of the room cooling requirements of both trains of vital switchgear when one of the chillers is out of service without implementing additional compensatory actions. Therefore, reliance on the opposite train chiller alone is not sufficient to maintain all cooling requirements of the affected train's vital switchgear. A misapplication of industry guidance resulted in the use of non-safety related unit coolers and additional compensatory measures as an acceptable alternative. Currently, TS LCO compliance is maintained when the switchgear room cooling is removed from service.
05000313/LER-2012-00112 April 2012Arkansas NuclearOn February 15, 2012, Arkansas Nuclear One Unit-1 (ANO-1) received the NRC 4th quarter Integrated Inspection Report identifying a noncited violation of Unit 1 Technical Specification (TS) 3.8.4, "DC Sources-Operating," TS 3.8.7, "Inverters-Operating," and TS 3.8.9, "Distribution Systems-Operating," due to the licensee's failure to complete the associated required actions prior to the specified completion times while the associated emergency switchgear room chillers were out of service for planned maintenance. Specifically, on December 7, 2011, VCH-4A Switchgear Room Chiller was removed from service to perform maintenance for 27.3 hours, and on December 19, 2011, VCH-4B Switchgear Room Chiller was removed from service to perform maintenance for 15.5 hours. During both maintenance periods, ANO-1 did not enter the subject specifications above, but entered the following: (1) TS 3.7.7 Condition "A" for one loop of Service Water System (SWS) being inoperable with an associated completion time of 72 hours, (2) TS 3.8.1 Condition "B" for one Emergency Diesel Generator inoperable with a 7 day completion time, and (3) TS 3.0.6, to support the emergency switchgear room chiller being out of service for planned maintenance. The SWS specification was applied as allowed by the ANO-1 TS Bases, considering that the switchgear room chillers were supplied by the SWS, which is the ultimate cooling medium for rooms which contain the electrical equipment. In light of the aforementioned non-cited violation, ANO-1 currently complies with all applicable switchgear TS actions (the most limiting being 8 hours) when either switchgear room chiller is out of service.
05000313/LER-2012-002Arkansas Nuclear

On 2/15/2012 at 0300 (CST), Arkansas Nuclear One - Unit 1 Control Room Operators discovered that the CV-2673 Feedwater Train "B" Start-Up Valve Hand/Auto (H/A) station and the CV-2672 Feedwater Train "B" Low Load Valve H/A station on Control Room panel CO3 had no light indications for the "auto" or "hand" mode. Appropriate Technical Specifications (TS) were entered at the time of discovery, with TS 3.7.3 Condition E (two feedwater control valves in the same flow path inoperable) requiring flowpath isolation within 8 hours; otherwise TS 3.7.3 Condition F requires the unit to be in Mode 3 within 6 hours and Mode 4 within 12 hours. TS 3.7.3 Condition E completion time expired at 1100 on 02/15/2012, at which time the Operations staff began preparations for shutdown. After corrective maintenance, both subject H/A stations were returned to auto, and applicable TS were exited at 1323 on 02/15/2012.

Plant computer points indicated that both H/A stations had previously transferred from auto to hand with no operator action at 1924 on 2/14/2012, resulting in the subject valves being inoperable for a total of 18 hours, a condition prohibited by TS. Subsequent investigation revealed that a degraded carbon resistor on an Integrated Control System (ICS) 24 vDC auxiliary relay module resulted in a blown fuse in an ICS transfer relay module, causing both of the subject H/A stations to transfer from auto to hand.

The apparent cause was determined to be a latent design change error from 1990 that resulted in the 24 vDC auxiliary relay module being utilized in a 48 vDC service application.

05000313/LER-2013-00122 August 2013Arkansas Nuclear

On March 31, 2013, at approximately 0750 CDT, during lifting and removal of the Arkansas Nuclear One Unit 1 (ANO-1) original Main Generator Stator (Stator), the temporary lift assembly collapsed due to failure of one of the structural columns, resulting in the Stator falling onto the turbine deck (386' elevation) and rolling down into the ANO-1 train bay (354' elevation) adjacent to Arkansas Nuclear One Unit 2 (ANO-2).

The event resulted in one fatality, multiple injuries, structural damage to the ANO-1 and ANO-2 turbine buildings, and damage to non-vital systems and electrical equipment. At the time of the event, ANO-1 was in MODE 6 and ANO-2 was in MODE 1 at approximately 100 percent power. The event resulted in a loss of offsite power for ANO-1, with both Emergency Diesel Generators (EDGs) starting to supply safety loads.

ANO-1 decay heat removal was lost for approximately four minutes. ANO-2 automatically tripped off-line after the vibration from the dropped Stator resulted in the actuation of relays in the ANO-2 switchgear located adjacent to the train bay, subsequently tripping a reactor coolant pump motor breaker. After the reactor trip, emergency feedwater was manually initiated by ANO-2 Control Room Operators. As debris fell into the train bay, an 8-inch firewater pipe was ruptured and the Alternate AC Diesel Generator electrical tie to ANO-1 was severed. At 0923 CDT that same day, water intrusion from the ruptured firewater piping into a 4160 volt breaker resulted in an ANO-2 Startup Transformer lockout, de-energizing a safety bus. An EDG automatically started as designed and supplied the affected safety bus. An ANO-2 Notification of Unusual Event was declared at 1033 CDT due to fire or explosion from an electrical fault in the 4160 volt switchgear with indications of bus damage. After damage assessment and repairs, ANO-2 returned to power operation on April 28, 2013. ANO-1 returned to power operation on August 7, 2013.