05000313/LER-2009-002

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LER-2009-002, 1 OF 4
Arkansas Nuclear One
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation
3132009002R00 - NRC Website

9. OPERATING MODE

1

10. POWER LEVEL

90 11, LW comer . MOB LEM

FACILITY NAME

David B. Bice, Acting Manager, Licensing TELEPHONE NUMBER (Include Area Code) 479-858-4710

CAUSE SYSTEM

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COMPONENT

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i4. atfilliumorrk. mr ~me 15. EXPECTED_ um' n YES (If yes, complete 15. EXPECTED SUBMISSION DATE) 17 NO ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) On February 7, 2009, at approximately 1046 CST, the reactor was manually tripped from 90 percent power in response to a report of a fire at the main generator hydrogen addition station. Prior to the occurrence of the fire, Operations personnel were preparing to add hydrogen to the main generator.

The Inside Auxiliary Operator (IA0) who was to perform the task conducted a pre-job brief with the Shift Technical Advisor, who was also a qualified Shift Manager. The IA0 then proceeded to the hydrogen addition station to perform the task. The procedure requires that the hydrogen station to generator inlet isolation valve, which is a normally open valve, be verified open. The IA0 first attempted to open the valve with no success, then unsuccessfully attempted to close the valve.

Assuming the valve was stuck on its closed seat; the operator obtained a pipe wrench and proceeded to rotate the valve handle in the open direction. Suddenly, the bonnet, hand wheel, and valve internals assembly ejected from the valve body, releasing hydrogen under pressure to the atmosphere. The operator immediately exited the area and the hydrogen quickly ignited. Operations personnel expeditiously initiated action to isolate the hydrogen leak. As a conservative action, the reactor was manually tripped at 1046 CST. The cause of this event was personnel error. The involved individual will receive remedial training and go through a requalification process.

A. Plant Status At the time of this event, Arkansas Nuclear One, Unit 1 (ANO-1) was at approximately 90 percent power following restart from a forced outage. Preparations for a nuclear instrumentation calibration were in progress.

B. Event Description

On February 7, 2009, at approximately 1046 CST, the reactor was manually tripped from 90 percent power in response to a report of a fire at the main generator hydrogen addition station.

Prior to the occurrence of the fire, Operations personnel were preparing to add hydrogen to the main generator. The Inside Auxiliary Operator (IA0) who was to perform the task conducted a pre-job brief with the Shift Technical Advisor, who was also a qualified Shift Manager. Topics discussed during the brief were the procedure, basic steps and associated limits.

The IAO, with procedure in hand, then proceeded to the hydrogen addition station on elevation 354' of the Turbine Building, to perform the task. In the process of aligning hydrogen to the generator, the procedure requires that the hydrogen station to generator inlet isolation valve (H2-109), which is a normally open valve, be verified open. The IA0 first attempted to open the valve using both hands with no success. The IA0 then unsuccessfully attempted to close the valve using both hands. Assuming the valve was stuck on its closed seat, the IA0 obtained a pipe wrench and proceeded to rotate the valve handle in the open direction approximately six turns. Because the valve was actually on its open seat, this action resulted in the valve bonnet unscrewing from the valve body. Suddenly, the bonnet, hand wheel, and valve internals assembly ejected from the valve body, releasing hydrogen under pressure to the atmosphere.

The IA0 immediately exited the area and the hydrogen quickly ignited. Upon being notified of the hydrogen leak and associated fire, Operations personnel quickly initiated action to isolate the hydrogen leak from the Hydrogen Bulk Storage Facility. As a conservative action, the reactor was manually tripped at 1046 CST. The fire was reported extinguished at 1055; however, at 1057, the Control Room was notified that a re-flash had occurred in the cable tray located above the hydrogen addition station. Upon receiving this report, a Notification of Unusual Event (NUE) was declared at 1059 based on a fire within the protected area that was not extinguished within 10 minutes. The fire was quickly extinguished and a re-flash watch was posted. The NUE was terminated at 1238 CST.

C. Root Cause The root cause of this event was determined to be personnel error. The IA0 mistakenly assumed that H2-1 09 was stuck on its closed seat and proceeded to attempt to open the valve using aTorque Amplifying Device (TAD) without first requesting prior supervisor approval to use such a device, as required by procedure. In addition, the IA0 did not apply acquired skills and abilities to the task.

D. Corrective Actions

Immediate corrective actions taken with respect to this event included:

  • The IA0 was removed from shift.
  • Stand Down meetings were conducted with Operations Department personnel regarding this event.

In addition, remediation training and requalification will be provided for the IA0 involved with this event.

E. Safety Significance

Operations personnel responded quickly and appropriately to the hydrogen fire by expeditiously isolating the hydrogen supply and extinguishing the fire. In addition, a conservative decision to manually trip the reactor was made. All systems performed as designed during and after the plant trip. Main steam safety valves lifted as expected following the plant trip from 90 percent power and subsequently reseated, as designed.

Considering the expeditious and appropriate actions taken by the operators to minimize the consequences of this event, the actual safety significance is considered to be minimal.

F. Basis for Reportability The NUE and manual reactor trip were reported to the NRC Operations Center at 1118 CST on February 7, 2009. An update notification reporting the termination of the NUE was made at 1238 CST on February 7, 2009.

A manual reactor trip from power is reportable pursuant to 10CFR50.73(a)(2)(iv)(A).

G. Additional Information

There have been no previous similar events in which a fire resulted in a reactor trip reported as LERs at ANO.