Similar Documents at Salem |
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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0261998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 1.With 990115 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr ML18106A9831998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 2.With 981214 Ltr ML18106A9801998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 1.With 981214 Ltr ML18106A9641998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 2. with 981112 Ltr ML18106A9631998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 1. with 981112 Ltr ML18106A9151998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 2.With 981012 Ltr ML18106A9131998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 1.With 981012 Ltr ML18106A8751998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Generating Station,Unit 2.With 980915 Ltr ML18106A8741998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Unit 1.With 980915 Ltr ML18106A8161998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 1. W/980817 Ltr ML18106A8151998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 2. W/980817 Ltr ML18106A7151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 2. W/980715 Ltr ML18106A7141998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 1. W/980715 Ltr ML18106A6541998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 1. W/980615 Ltr ML18106A6531998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 2. W/980615 Ltr ML18106A6121998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Generating Station,Unit 1.W/980515 Ltr ML18106A6111998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Unit 2. W/980515 Ltr ML18106A5561998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem,Unit 1. W/980415 Ltr ML18106A4591998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem Unit 2. W/980415 Ltr ML18106A3771998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 1.W/980316 Ltr ML18106A3761998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 2.W/980316 Ltr ML18106A3281998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 2. W/980217 Ltr ML18106A3271998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 1. W/980217 Ltr ML18106A2721997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem,Unit 2. W/980115 Ltr ML18106A2711997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem Generating Station,Unit 1.W/980115 Ltr ML18106A2081997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 1. W/971212 Ltr ML18106A2071997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 2. W/971212 Ltr ML18102B6811997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 2.W/ 971117 Ltr ML18102B6801997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 1.W/ 971117 Ltr ML18102B6271997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Salem,Unit 2. W/971015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit June 14, 1995 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Attn.: Document Control Desk MONTfilY OPERATING REPORT SALEMNO. 1 DOCKET NO: 50-272 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating reports for the month of May are being sent to you.
~John C. Summers General Manager -
Salem Operations RH:vls Enclosures C Mr. Thomas T. Martin Regional Administrator USNRC, Region I 631 Park Avenue King of Prussia, PA 19046 8-l-7.R4 9506200068 950531 PDR ADDCK 05000272 R PDR The power is in your hands.
95-2168 RE . 6/94
.VERAGE DAILY UNIT POWER L~L Docket No.: 50-272 Unit Name: Salem #1 Date: 06/10/95 Completed by: Robert Phillips Telephone: 339-2735 Month MAY 1995 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 1048 17 0 2 1046 18 0 3 1045 19 0 4 1074 20. 0 5 528 21 0 6 445 22 0 7 505 23 0 8 404 24 0 9 472 25 0 10 453 26 0 11 463 27 0 12 470 28 0 13 468 29 0 14 526 30 0 15 620 31 0 16 914 P. 8.1-7 Rl L
OPERATING DATA REPORT Docket No: 50-272 Date: 06/10/95 Completed by: Robert Phillips Telephone: 339-2735 Operating Status
- 1. Unit Name Salem No. 1 Notes
- 2. Reporting Period May 1995
- 3. Licensed Thermal Power (MWt) 3411
- 4. Nameplate Rating {Gross MWe) 1170
- 5. Design Electrical Rating (Net MWe) 1115
- 6. Maximum Dependable Capacity(Gross MWe) 1149
- 7. Maximum Dependable Capacity (Net MWe) 1106
- 8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason NA
- 9. Power Level to Which Restricted, if any (Net MWe) N/A
- 10. Reasons for Restrictions, if any NA This Month Year to Date Cumulative
- 12. Hours in Reporting Period 744 3623 157080
- 12. No. of Hrs. Rx. was Critical 387.3 2660.9 104380.45
- 13. Reactor Reserve Shutdown Hrs. 0 0 0
- 14. Hours Generator On-Line 386.03 2632.09 100388.27
- 15. Unit Reserve Shutdown Hours 0 0 0
- 16. Gross Thermal Energy Generated (MWH) 829060.8 5781911. 6 315833814.4
- 17. Gross Elec. Energy Generated (MWH) 267840 2689850 105301000
- 18. Net Elec~ Energy Gen. (MWH) 247176 2554430 100236594
- 19. Unit Service Factor 51. 9 72.6 63.9
- 20. Unit Availability Factor 51. 9 72.6 63.9
- 21. Unit Capacity Factor (using MDC Net) 30.0 63.7 57.7
- 22. Unit Capacity Factor (using DER Net) 29.8 63.2 57.2
- 23. Unit Forced Outage Rate 48.l 27.4 21. 5
- 24. Shutdowns scheduled over next 6 months (type, date and duration of each)
A 60 day refueling outage scheduled to start 9-9-95.
- 25. If shutdown at end of Report Period, Estimated Date of Startup:
Start up is presently scheduled for July 5, 1995.
8-l-7.R2
UNIT SHUTDOWN AND POWER REDUCTIONS REPORT MONTH MAY 1995 DOCKET NO.: 50-272 UN IT NAME: _sa~l..._e~m~#.._1~--:
DATE: -'6=--....:.1-=-0-_,9""'5-~
COMPLETED BY: Robert Phillips TELEPHONE: 609-339-2735 METHOD OF SHUTTING LICENSE DURATION DOWN EVENT SYSTEM COMPONENT CAUSE AND CORRECTIVE ACTION NO. DATE TYPE 1 (HOURS) REASON 2 REACTOR REPORT # CODE 4 CODE 6 TO PREVENT RECURRENCE 2577 5-4-95 F 132.9 A 5 .. __ ................ CH PUMP XX NUCLEAR STEAM GENERATOR FEEDPUMP 2614 5-15-95 F 19.9 A 5 ...................... SH CKTBRK SWITCHGEAR ROOM* VENTILATION 2616 5-16-95 F 4.6 A 4 SH CKTBRK SWITCHGEAR ROOM VENTILATION 2671 5-17-95 . F 357.97 D 1 ----------- SH CKTBRK TECH. SPEC. 3.0.3 1 2 3 4 5 F: F.orced Reason Method: Exhibit G - Instructions Exhibit 1 - Same S: Scheduled A-Equipment Failure (explain) 1-Manual for Preparation of Data Source B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report CLER) File D-Requlatory Restriction 4-Continuation of CNUREG-0161)
E-Operator Training & License Examination Previous Outage F-Administrative 5-Load Reduction G-Operational Error (Explain) 9-0ther H-Other (Explain)
IOCFR50.59 EVALUATIONS DOCKET NO: 50-272 MONTH: MAY I995 UNIT NAME: SALEM I DATE: 06/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5I62 The following items were evaluated in accordance with the provisions of the Code of Federal Regulations IOCFR50.59. The Station Operations Review Committee has reviewed and concurs with these evaluations.
I. Design Change Packages (DCP)
IEC-3387, Pkgs I- 3 "EDG IA, B & C Air Receiver Low Pressure Alarms" Rev. 0 -
The purpose ofthis design change is to install two pressure switches each, along with all associated tubing, valves, and wiring for the starting air receivers for Diesel Generators IA, IB & IC. These pressure switches are to provide new low pressure alarms for each of the starting air receivers. These will provide early warning to the operating personnel so that they can take adequate action to mitigate starting air receiver degraded conditions and maintain the receiver pressure adequate for three diesel starts. The Diesel Air Start System and its components, including instruments, are not the subject of any technical specifications or technical specification basis.
There is no reduction in the margin of safety as defined in the basis for any technical specification. (SORC 95-042)
IEC-3252, Pkg. 1 "Reracking of Spent Fuel Pool for Increased Storage Capacity" Rev. 3 - This DCP removes nine existing Exxon racks and replaces them with nine maximum density Holtec racks. This revision to the DCP is being made to: I) delete references to the Offset Tool; 2) clarify the rack handling procedure, and 3) address minor errors observed during Part A closure. This revision involves neither the addition, deletion or modification of any equipment designed to monitor or control plant systems or components. There is no reduction in the margin of safety as defined in the basis for any technical specification. (SORC 95-053)
10CFR50.59 EVALUATIONS DOCKET NO: 50-272 MONTH: MAY 1995 UNIT NAME: SALEM 1 DATE: 06/i0/95 C01\.1PLETED BY: R. HELLER TELEPHONE: 609-339-5162 (Cont'd)
- 2. Temporary Modifications (T-Mod)95-035 "Temporary Blank for 1VHE838" Rev. 1 - 1VHE57, 12 Switchgear Ventilation Supply Fan and Motor are to be removed for maintenance. To support this activity, the filter plenum, 1VHE838 must be isolated. There is no isolation point on the upstream side of the fan. There is only one on the downstream side. Therefore, the upstream side is to be blanked off The temporary blank is to be constructed from safety related steel, with a thickness equivalent to or greater than that required of the plenum. The blank will take the place of the current nozzle, there is no loading on the existing nozzle area; immediately downstream is a rubber expansion joint.
Therefore, no seismic loading contribution exists. The .
modification involves neither the addition, deletion or modification of any equipment designed to monitor or control plant systems or components. There is no reduction in the margin of safety as defined in the basis for any technical specification. (SORC 95-051)95-036 "Temporary Blank for 1VHE838" Rev. 1 - 1VHE58, 13 Switchgear Ventilation Supply Fan and Motor are to be removed for maintenance to replace a bad motor. To support this activity, the filter plenum, 1VHE838 must be isolated.
There is no isolation point on the upstream side of the fan.
There is only one on the downstream side. Therefore, the upstream side is to be blanked off The temporary blank is to be constructed from safety related steel, with a thickness equivalent to or greater than that required of the plenum. The blank will take the place of the current nozzle, there is no loading on the existing nozzle area; immediately downstream is a rubber expansion joint.
c.
10CFR50.59 EVALUATIONS DOCKET NO: 50-272 MONTH: MAY 1995 UNIT NAME: SALEM I DATE: 06/10/95 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162 Therefore, no seismic loading contribution exists. The modification involves neither the addition, deletion nor modification of any equipment designed to monitor or control plant systems or components. There is no reduction in the margin of safety as defined in the basis for any technical specification. (SORC 95-051)
- 3. Safety Ev~luations (S/E)
WO 950513085 "Freeze Seal of 13 Charging Pump Relief Valve Tailpipe" Rev.
0 - The purpose of this proposal is to install a freeze seal on the downstream piping of the Reciprocating Charging Pump discharge relief valve ICVl41. The freeze seal is needed to allow .the replacement of the relief valve. The freeze seal will prevent fluid from leaking out of the Volume Control Tank (VCT) while the valve is being replaced. In addition, the freeze seal will block any fluid should relief valves ICVl24 and I CV253 lift or leak by their seats. However, their relief path will not be affected by the freeze seal. The Chemical and Volume Control System (CVCS) will continue to be operated in accordance with normal operating procedures. At no time during the maintenance evolution, will the requirement that at least one boration injection flow path be available be challenged: The flow path from either Boric Acid Tank or Refueling Water Storage Tank to the Reactor Coolant System (RCS) will not be affected by the proposed activities. The margin of safety as defined in the bases for the technical specifications will not be reduced. (SORC 95-052)
- r 10CFR50.59 EVALUATIONS DOCKET NO: 50-272 110NTH:~Y1995 UNIT NAME: SALEM 1 I DATE: 06/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 (Cont'd)
- 4. Deficiency Reports (DR) Us~-As-Is DRDSI.8-0010/ "DR 950501234 "V5H Fuel Grid Mxing Vanes" Rev. 0 - This safety evaluation is being written to provide a use-as-is disposition to DR 950501234 which documents the non-conforming condition which presently exists in the V5H fuel loaded at Salem Units 1and2. During the manufacturing of the 17 x 17 fuel assembly grid straps, the mid-grid mixing vanes were under bent. Westinghouse has since determined that the mean production vane angle for the as loaded Salem VHS fuel assemblies could be as much as 2.2° less than the mean angle in place during design basis DNB testing. Since the vanes are under bent, there is no risk of mechanical contact with a fuel rod. Westinghouse has concluded that the under bent vanes do not adversely affect the mechanical or structural integrity of the fuel assemblies. Westinghouse has determined that a conservative evaluation of the under bent mixing vanes results in a 1.9% DNBR penalty. Since sufficient DNBR margin still exists, no safety limits have been violated and the conclusions of the UFSAR Chapter 15 accident analyses remain valid. The change in vane grid angle does not result in changing any fuel related limits or design failure points. Although generic DNBR margin is affected by this change, the limits as defined by any technical specification basis are not affected. Hence the margin of safety is preserved. (SORC 95-042)
1 I
REFUELING INFORMATION DOCKET NO: 50-272 MONTH: MAY 1995 UNIT NAME: SALEM 1
- DATE: 06/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 MONTH : MAY 1995 Refueling information has changed from last month: YES~NO X Scheduled date for next refueling: September 9. 1995 Scheduled date for restart following refueling: November 7. 1995-
- a. Will Technical Specification changes or other license amendments be required?
YES X NO~
NOT DETERMINED TO DATE
- b. Has the reload fuel design been reviewed by the Station Operating Review Committee?
YES NO X Ifno, when is it scheduled? September 1995 Scheduled date(s) for submitting proposed licensing action: NIA Important licensing considerations associated with refueling:
Number of Fuel Assemblies:
- a. Incore 193
- b. In Spent Fuel Storage 732 Present licensed spent fuel storage capacity: 1632 Future spent fuel storage capacity: 1632 Date of last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity: September 2008 8-l-7.R4
SALEM GENERATING STATION MONTHLY OPERATING
SUMMARY
- UNIT 1 MAY 1995 SALEM UNIT NO. 1 The Unit began the period operating at 94% power and continued at that level until 5/4, when load was reduced to 50% to support replacement of both Steam Generator Feedwater Pump (SGFP) governors. A power increase was initiated on 5/14, following completion of SGFP
. post maintenance testing. On 5/15, the power increase was stopped at 60% due to concerns over operability of equipment serviced by #12 & 13 switchgear supply fans. The #13 fan motor had failed on 5/14, and #12 had been out of service due to a failed motor bearing. The appropriate justification for continued operation with only one fan could not be obtained and a conservative decision was made to shutdown. The Unit was removed from service on 5/17, and remained shutdown throughout the rest of the period.