|
|
| Line 1: |
Line 1: |
| #REDIRECT [[05000336/LER-1996-031, Forwards LER 96-031-00 Which Documents Event That Occurred at Mnps,Unit 2 on 961003.Commitments,listed]] | | {{Adams |
| | | number = ML20137N881 |
| | | issue date = 04/03/1997 |
| | | title = :on 961003,discovered Potentially non-conservative Assumptions Used in Analysis Cold Result in Exceeding ASME Code Max Relief Valve Accumulation for Sg. Caused by Inadequate Design of Mssv.Plant Mods Initiated |
| | | author name = Joshi R |
| | | author affiliation = NORTHEAST NUCLEAR ENERGY CO. |
| | | addressee name = |
| | | addressee affiliation = |
| | | docket = 05000336 |
| | | license number = |
| | | contact person = |
| | | document report number = LER-96-031-01, LER-96-31-1, NUDOCS 9704090079 |
| | | package number = ML20137N861 |
| | | document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT |
| | | page count = 3 |
| | }} |
| | {{LER |
| | | Title = :on 961003,discovered Potentially non-conservative Assumptions Used in Analysis Cold Result in Exceeding ASME Code Max Relief Valve Accumulation for Sg. Caused by Inadequate Design of Mssv.Plant Mods Initiated |
| | | Plant = |
| | | Reporting criterion = 10 CFR 50.73(a)(2)(i), 10 CFR 50.73(a)(2)(ii)(B) |
| | | Power level = |
| | | Mode = |
| | | Docket = 05000336 |
| | | LER year = 1996 |
| | | LER number = 31 |
| | | LER revision = 1 |
| | | Event date = |
| | | Report date = |
| | | ENS = |
| | | abstract = |
| | }} |
| | |
| | =text= |
| | {{#Wiki_filter:- ~ _.. |
| | . ~ |
| | NRC FORM 366 U.s. NUCLEAR REGULATORY COMMisslON APPROYED BY OMB NO. 3160-0104 (4 95) |
| | EXPlRES 04/30/98 l |
| | LICENSEE EVENT REPORT (LER) |
| | Wo~aE' OWE'"c''"*E"a''E'ISI 5'oU$*i U "o^"IE EAc"UE 'S'sIf" IOU 7a0 EMUS'rsiE'o"2n'UN5'" |
| | I |
| | ^ |
| | A See reverse for reSuired number of Es E'A R O'N "I |
| | G Mi 0 AND TO THE PAPERWORK R& DUCTION PROJECT (3160 0104), OFFICE OF digits / Characters fOr each block) |
| | M ANAGEMENT AND BWGG. W ASHINGTON. DC 20603. |
| | MCIUTY NAME Of DOCKET NUMDER (2' PAGE (3) |
| | Millstone Nuclear Power Station Unit 2 05000336 1OF3 TITLE 14) 1 Non-conservative Assumptions identified in Analysis for Peak Secondary System Pressure i |
| | EVENT DATE (5) |
| | LER NUMBER (6) |
| | REPORT DATE (7) |
| | OTHER FACILITIES INv0LvED (8) sE U AL RE $ N MONTH DAY YEAR YEAR MONTH DAY YEAR NU R |
| | 10 03 96 96 |
| | -- 031 -- |
| | 01 04 03 97 |
| | ) |
| | l OPERATING THis REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or more) (11) |
| | MODE (9) 5 20.2201(b) 20.2203(aH2Hv) 50.73(a)(2)(i) |
| | So.73(aH2)(viii) l POWER 20.2203(aH1) 20.2203(a)(3)(i) |
| | X So.73(aH2Hii) 50.73(aH2)(x) |
| | LEVEL (10) 000 20.2203(aH2)(i) 20.2203(a)(3)(ii) 50.73(aH2Hiii) 73.71 |
| | ] |
| | 20.2203(aH2Hii) 20.2203(a)(4) |
| | So.73(aH2Hiv) |
| | OTHER 20.22o3(aH2)(iii) |
| | So.36(cH1) |
| | So.73(aH2)(v) specirY in Abstract belOw |
| | ^ |
| | I 20.2203taH2)(iv) |
| | So.36(cH2) |
| | So.73(aH2Hvii) |
| | Rf NRC Form 366A LICENSEE CONTACT FOR THIS LER (12) |
| | NAME TELEPHONE NUMBER (include Area Codel R. G. Joshi, MP2 Nuclear Licensing (860) 440-2080 i |
| | COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THis REPORT (13) |
| | ^ |
| | |
| | ==CAUSE== |
| | SYSTEM COMPONENT MANUFACTURER |
| | |
| | ==CAUSE== |
| | SYSTEM COMPONENT MANUFACTURER PRD g |
| | i s< |
| | I SUPPLEMENTAL REPORT EXPECTED (14) |
| | EXPECTED MONTH DAY YEAR l- |
| | 'YES SUBMISSION (if yes, complete EXPECTED sUBMisslON DATE). |
| | X NO DATE (15) j ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) l On October 3,1996, it was discovered that potentially non-conservative assumptions used in an analysis could result l |
| | in exceeding the ASME Code maximum relief valve accumulation for the steam generators (SG) and main steam l |
| | line piping during an analyzed design basis event. During a review of the analysis for the single main steam j |
| | isolation valve (MSIV) closure event, it was discovered that potentially non-conservative assumptions were made in the modeling of the main steam line, main steam safety valves (MSSV), and SGs. A preliminary analysis of these i |
| | conditions has been performed. The results indicate that the 110 percent of design rating of the SGs would be exceeded for the single MSIV closure and loss of load design basis events. |
| | The cause of this event was an inadequate design of the MSSV inlet piping and the failure to adequately assess the l |
| | l piping pressure losses to the MSSVs. |
| | l As a result of this event, corrective actions will be implemented to ensure that the plant response to analyzed events will not result in exceeding the design requirements of the SG. These actions will include any necessary reanalysis and plant modifications. These actions will be completed prior to plant restart from the current Outage. |
| | J 9704090079 970403 PDR ADOCK 05000336 S |
| | PDR NRC FORM 366 (4-95) |
| | |
| | NRC FORM,366A U.S. NUCLEAR REGULATORY COMMisslON (4-95) |
| | UCENSEE EVENT REPORT (LER) |
| | TEXT CONTINUATION FACILITY NAME (1) |
| | DOCKET LER NUMBER i 6) |
| | PAGE (3) |
| | SEQUENTIAL REvlsioN A |
| | NUMBER NUMBER 2OF3 Millstone Nuclear Power Station Unit 2 05000336 96 -- 031 - |
| | 01 TEXT fit more space is required, tise additional copie: of NRC Form 366A) (17) 1. |
| | |
| | ==Description of Event== |
| | On October 3,1996, it was discovered that potentially non-conservative assumptions used in an analysis could result in exceeding the ASME Code maximum relief valve accumulation for the steam generators (SG) and main steam line piping during an analyzed design basis event. At the time of discovery of this event, the unit was in Mode 5 at 0 percent power. |
| | During a review of the analysis for the single main steam isolation valve (MSIV) closure event, it was discovered that potentially non-conservative assumptions were made in the modeling of the main steam line, main steam i |
| | safety valves (MSSV), and SGs. It has been determined that the piping pressure losses between the SG and the MSSV inlets were not fully evaluated with respect to the MSSV performance and not fully addressed within plant safety analyses involving MSSV actuation. |
| | Additionally in reviewing this event, it was identified that the relieving capacity of the MSSVs was significantly reduced due to the design of the connective piping between the main steam line and the MSSVs. The 6 inch connective piping is XXS grade piping with an inside diameter of less than 5 inches. The original analysis also did not identify peak steam generator pressure at the limiting location, resulting in a pressure slightly lower than the actual peak steam generator pressure. However, this error does not significantly affect the analysis. |
| | A preliminary analysis of these conditions has been performed. The results indicate that the 110 percent of design rating of the SGs would be exceeded for the single MSIV closure and loss of load design basis events. |
| | |
| | ==II. Cause of Event== |
| | The cause of this event was an inadequate design of the MSSV inlet piping and the failure to adequately assess the piping pressure losses to the MSSVs. The MSSVs were not capable of relieving their rated capacity at an acceptable pressure due to the smaller diameter installed connective piping. Additionally, subsequent analysis failed to account for the effects of the inadequate design in the analysis of peak pressures for the design basis events. |
| | I The original design basis for Unit 2 did not require analysis for the single MSIV closure event. Analysis of this event was included at a later time and was originally performed by Westinghouse Electric Corporation. The identified potential non-conservative assumptions are believed to have existed in the original analysis also. The current analysis was performed by Siemens Power Corporation. |
| | 111. Analysis of Event The Single MSIV Closure Event is the limiting event for secondary side pressure. The closure of a single MSIV during operation will decrease the heat removal by the secondary system. Upon cessation of steam flow to the turbine, the pressure in the affected steam generator willincrease above the opening setpoint of the MSSVs. |
| | l The peak analyzed SG dome pressure for this event is 1096 psia. |
| | Due to the non-conservative assumptions identified in the analysis, the peak secondary side pressure would be greater than previously calculated. Based on the preliminary analysis, the peak secondary side pressure would exceed the design pressure rating of the SGs and main steam line piping. This would also be true for the Loss of Load Event. Therefore, this event is considered to be safety significant. |
| | The effect of this condition on a small break loss of coolant accident (LOCA) was evaluated since the SG pressure is controlled by the MSSVs during the initial phases of the LOCA. The effect of the inlet losses on SG |
| | { |
| | l NRC FORM 360A (4-95) |
| | :- NRC FORM 366A U.S. NUCLEAR REGULATORY Commission (4 95) |
| | UCENSEE EVENT REPORT (LER) |
| | TEXT CONTINUATION FACILITY NAME (1) |
| | DOCKET LER NUMBER (6) |
| | PAGE (3) |
| | SEQUENTIAL REvlslON YEAR NUMBER NUMBER 3OF3 Millstone Nuclear Power Station Unit 2 05000336 96 - 031 - |
| | 01 TEXT (if more space is required, use additional copies of NRC Form 366A) (17) pressure is not significant if all the MSSV banks have not opened. Since the net loss of capacity caused by the intet losses is less then the capacity of 1 MSSV, the maximum increase in SG pressure would equal the maximum difference in MSSV opening setpoint, or 10 psi. This magnitude change in SG pressure was evaluated I |
| | by Siemens Power Corporation to be insignificant to peak fuel cladding temperature. |
| | This event is reportable in accordance with 10 CFR 50.73(a)(2)(ii)(B), any event or condition that resulted in the condition of the nuclear power plant, including the principal safety barriers, being seriously degraded, or that resulted in the nuclear power plant being in a condition that was outside the design basis of the plant. This event i |
| | was reported in accordance with 10 CFR 50.72(b)(1)(ii) on October 3,1996. |
| | |
| | ==IV. Corrective Action== |
| | As a result of this event, corrective actions will be implemented to ensure that the plant response to analyzed j |
| | events will not result in exceeding the design requirements of the SG. These actions will include any necessary i |
| | reanalysis and plant modifications. These actions will be completed prior to plant restart from the current outage. |
| | V. |
| | |
| | ==Additional Information== |
| | None |
| | |
| | ==Similar Events== |
| | LER 91-010: On October 18,1991, a reportability determination was made concerning a reanalysis of the main steam line break event inside the containment. The reanalysis confirmed that the assumptions made for the existing (1979) main steam line break (MSLB) analysis were non-conservative with respect to power level, break size, and single active failure. Using more restrictive assumptions, design limits for containment pressure and I |
| | temperature could be exceeded. A multi-disciplinary task force was established to investigate containment response to postulated MSLBs. Plant modifications required to ensure an acceptable containment pressure response for a main steam line break inside the containment were installed and tested. |
| | Manufacturer Data None Ells Codes SG - Steam Generator RV-Main Steam Safety Valve SB - Main Steam System ISV-Main Steam Isolation Valve WRC FORPA 366A (4 95) |
| | }} |
| | |
| | {{LER-Nav}} |
:on 961003,discovered Potentially non-conservative Assumptions Used in Analysis Cold Result in Exceeding ASME Code Max Relief Valve Accumulation for Sg. Caused by Inadequate Design of Mssv.Plant Mods Initiated| ML20137N881 |
| Person / Time |
|---|
| Site: |
Millstone  |
|---|
| Issue date: |
04/03/1997 |
|---|
| From: |
Joshi R NORTHEAST NUCLEAR ENERGY CO. |
|---|
| To: |
|
|---|
| Shared Package |
|---|
| ML20137N861 |
List: |
|---|
| References |
|---|
| LER-96-031-01, LER-96-31-1, NUDOCS 9704090079 |
| Download: ML20137N881 (3) |
|
text
- ~ _..
. ~
NRC FORM 366 U.s. NUCLEAR REGULATORY COMMisslON APPROYED BY OMB NO. 3160-0104 (4 95)
EXPlRES 04/30/98 l
LICENSEE EVENT REPORT (LER)
Wo~aE' OWE'"c"*E"aE'ISI 5'oU$*i U "o^"IE EAc"UE 'S'sIf" IOU 7a0 EMUS'rsiE'o"2n'UN5'"
I
^
A See reverse for reSuired number of Es E'A R O'N "I
G Mi 0 AND TO THE PAPERWORK R& DUCTION PROJECT (3160 0104), OFFICE OF digits / Characters fOr each block)
M ANAGEMENT AND BWGG. W ASHINGTON. DC 20603.
MCIUTY NAME Of DOCKET NUMDER (2' PAGE (3)
Millstone Nuclear Power Station Unit 2 05000336 1OF3 TITLE 14) 1 Non-conservative Assumptions identified in Analysis for Peak Secondary System Pressure i
EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACILITIES INv0LvED (8) sE U AL RE $ N MONTH DAY YEAR YEAR MONTH DAY YEAR NU R
10 03 96 96
-- 031 --
01 04 03 97
)
l OPERATING THis REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or more) (11)
MODE (9) 5 20.2201(b) 20.2203(aH2Hv) 50.73(a)(2)(i)
So.73(aH2)(viii) l POWER 20.2203(aH1) 20.2203(a)(3)(i)
X So.73(aH2Hii) 50.73(aH2)(x)
LEVEL (10) 000 20.2203(aH2)(i) 20.2203(a)(3)(ii) 50.73(aH2Hiii) 73.71
]
20.2203(aH2Hii) 20.2203(a)(4)
So.73(aH2Hiv)
OTHER 20.22o3(aH2)(iii)
So.36(cH1)
So.73(aH2)(v) specirY in Abstract belOw
^
I 20.2203taH2)(iv)
So.36(cH2)
So.73(aH2Hvii)
Rf NRC Form 366A LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (include Area Codel R. G. Joshi, MP2 Nuclear Licensing (860) 440-2080 i
COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THis REPORT (13)
^
CAUSE
SYSTEM COMPONENT MANUFACTURER
CAUSE
SYSTEM COMPONENT MANUFACTURER PRD g
i s<
I SUPPLEMENTAL REPORT EXPECTED (14)
EXPECTED MONTH DAY YEAR l-
'YES SUBMISSION (if yes, complete EXPECTED sUBMisslON DATE).
X NO DATE (15) j ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) l On October 3,1996, it was discovered that potentially non-conservative assumptions used in an analysis could result l
in exceeding the ASME Code maximum relief valve accumulation for the steam generators (SG) and main steam l
line piping during an analyzed design basis event. During a review of the analysis for the single main steam j
isolation valve (MSIV) closure event, it was discovered that potentially non-conservative assumptions were made in the modeling of the main steam line, main steam safety valves (MSSV), and SGs. A preliminary analysis of these i
conditions has been performed. The results indicate that the 110 percent of design rating of the SGs would be exceeded for the single MSIV closure and loss of load design basis events.
The cause of this event was an inadequate design of the MSSV inlet piping and the failure to adequately assess the l
l piping pressure losses to the MSSVs.
l As a result of this event, corrective actions will be implemented to ensure that the plant response to analyzed events will not result in exceeding the design requirements of the SG. These actions will include any necessary reanalysis and plant modifications. These actions will be completed prior to plant restart from the current Outage.
J 9704090079 970403 PDR ADOCK 05000336 S
PDR NRC FORM 366 (4-95)
NRC FORM,366A U.S. NUCLEAR REGULATORY COMMisslON (4-95)
UCENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET LER NUMBER i 6)
PAGE (3)
SEQUENTIAL REvlsioN A
NUMBER NUMBER 2OF3 Millstone Nuclear Power Station Unit 2 05000336 96 -- 031 -
01 TEXT fit more space is required, tise additional copie: of NRC Form 366A) (17) 1.
Description of Event
On October 3,1996, it was discovered that potentially non-conservative assumptions used in an analysis could result in exceeding the ASME Code maximum relief valve accumulation for the steam generators (SG) and main steam line piping during an analyzed design basis event. At the time of discovery of this event, the unit was in Mode 5 at 0 percent power.
During a review of the analysis for the single main steam isolation valve (MSIV) closure event, it was discovered that potentially non-conservative assumptions were made in the modeling of the main steam line, main steam i
safety valves (MSSV), and SGs. It has been determined that the piping pressure losses between the SG and the MSSV inlets were not fully evaluated with respect to the MSSV performance and not fully addressed within plant safety analyses involving MSSV actuation.
Additionally in reviewing this event, it was identified that the relieving capacity of the MSSVs was significantly reduced due to the design of the connective piping between the main steam line and the MSSVs. The 6 inch connective piping is XXS grade piping with an inside diameter of less than 5 inches. The original analysis also did not identify peak steam generator pressure at the limiting location, resulting in a pressure slightly lower than the actual peak steam generator pressure. However, this error does not significantly affect the analysis.
A preliminary analysis of these conditions has been performed. The results indicate that the 110 percent of design rating of the SGs would be exceeded for the single MSIV closure and loss of load design basis events.
II. Cause of Event
The cause of this event was an inadequate design of the MSSV inlet piping and the failure to adequately assess the piping pressure losses to the MSSVs. The MSSVs were not capable of relieving their rated capacity at an acceptable pressure due to the smaller diameter installed connective piping. Additionally, subsequent analysis failed to account for the effects of the inadequate design in the analysis of peak pressures for the design basis events.
I The original design basis for Unit 2 did not require analysis for the single MSIV closure event. Analysis of this event was included at a later time and was originally performed by Westinghouse Electric Corporation. The identified potential non-conservative assumptions are believed to have existed in the original analysis also. The current analysis was performed by Siemens Power Corporation.
111. Analysis of Event The Single MSIV Closure Event is the limiting event for secondary side pressure. The closure of a single MSIV during operation will decrease the heat removal by the secondary system. Upon cessation of steam flow to the turbine, the pressure in the affected steam generator willincrease above the opening setpoint of the MSSVs.
l The peak analyzed SG dome pressure for this event is 1096 psia.
Due to the non-conservative assumptions identified in the analysis, the peak secondary side pressure would be greater than previously calculated. Based on the preliminary analysis, the peak secondary side pressure would exceed the design pressure rating of the SGs and main steam line piping. This would also be true for the Loss of Load Event. Therefore, this event is considered to be safety significant.
The effect of this condition on a small break loss of coolant accident (LOCA) was evaluated since the SG pressure is controlled by the MSSVs during the initial phases of the LOCA. The effect of the inlet losses on SG
{
l NRC FORM 360A (4-95)
- - NRC FORM 366A U.S. NUCLEAR REGULATORY Commission (4 95)
UCENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET LER NUMBER (6)
PAGE (3)
SEQUENTIAL REvlslON YEAR NUMBER NUMBER 3OF3 Millstone Nuclear Power Station Unit 2 05000336 96 - 031 -
01 TEXT (if more space is required, use additional copies of NRC Form 366A) (17) pressure is not significant if all the MSSV banks have not opened. Since the net loss of capacity caused by the intet losses is less then the capacity of 1 MSSV, the maximum increase in SG pressure would equal the maximum difference in MSSV opening setpoint, or 10 psi. This magnitude change in SG pressure was evaluated I
by Siemens Power Corporation to be insignificant to peak fuel cladding temperature.
This event is reportable in accordance with 10 CFR 50.73(a)(2)(ii)(B), any event or condition that resulted in the condition of the nuclear power plant, including the principal safety barriers, being seriously degraded, or that resulted in the nuclear power plant being in a condition that was outside the design basis of the plant. This event i
was reported in accordance with 10 CFR 50.72(b)(1)(ii) on October 3,1996.
IV. Corrective Action
As a result of this event, corrective actions will be implemented to ensure that the plant response to analyzed j
events will not result in exceeding the design requirements of the SG. These actions will include any necessary i
reanalysis and plant modifications. These actions will be completed prior to plant restart from the current outage.
V.
Additional Information
None
Similar Events
LER 91-010: On October 18,1991, a reportability determination was made concerning a reanalysis of the main steam line break event inside the containment. The reanalysis confirmed that the assumptions made for the existing (1979) main steam line break (MSLB) analysis were non-conservative with respect to power level, break size, and single active failure. Using more restrictive assumptions, design limits for containment pressure and I
temperature could be exceeded. A multi-disciplinary task force was established to investigate containment response to postulated MSLBs. Plant modifications required to ensure an acceptable containment pressure response for a main steam line break inside the containment were installed and tested.
Manufacturer Data None Ells Codes SG - Steam Generator RV-Main Steam Safety Valve SB - Main Steam System ISV-Main Steam Isolation Valve WRC FORPA 366A (4 95)
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000336/LER-1996-001, :on 960625,discovered Reactor Coolant Sys Heatup Rate Exceeded Tech Spec.Caused by Design & Procedural Weaknesses Re Plant Heatup Controls.Revised Plant Operating Procedures & Heatup/Cooldown Computer Program |
- on 960625,discovered Reactor Coolant Sys Heatup Rate Exceeded Tech Spec.Caused by Design & Procedural Weaknesses Re Plant Heatup Controls.Revised Plant Operating Procedures & Heatup/Cooldown Computer Program
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-001-02, :on 960120,supplementary Leak Collection & Release Sys Declared Inoperable Due to Equipment Failure of Door Latch.Door Repaired & Plant Returned to 100% Power |
- on 960120,supplementary Leak Collection & Release Sys Declared Inoperable Due to Equipment Failure of Door Latch.Door Repaired & Plant Returned to 100% Power
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000336/LER-1996-002, :on 960108,determined That Ice Plug in Common Line Resulted in Inability to Backwash Svc Water Strainers. Caused by Mod to Backwash Line Piping.Ice Plug Removed, Restoring Ability to Backwash |
- on 960108,determined That Ice Plug in Common Line Resulted in Inability to Backwash Svc Water Strainers. Caused by Mod to Backwash Line Piping.Ice Plug Removed, Restoring Ability to Backwash
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000423/LER-1996-002-02, :on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Identified. Caused by Inadequate Procedure.Procedures Revised |
- on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Identified. Caused by Inadequate Procedure.Procedures Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) | | 05000423/LER-1996-002, :on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Occurred Due to Procedure Inadequacy.Changes Will Be Made to Technical Requirements Manual |
- on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Occurred Due to Procedure Inadequacy.Changes Will Be Made to Technical Requirements Manual
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000245/LER-1996-003, :on 960111,discovered Existing Anchorage of EDG Day Tank Not Seismically Adequate.Caused by Original Design Deficiency.Anchorage of EDG Tank Will Be Graded to Meet Design Basis of Seismic Load Requirements |
- on 960111,discovered Existing Anchorage of EDG Day Tank Not Seismically Adequate.Caused by Original Design Deficiency.Anchorage of EDG Tank Will Be Graded to Meet Design Basis of Seismic Load Requirements
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(e)(2)(i) 10 CFR 50.73(e)(2)(viii) | | 05000336/LER-1996-003-01, :on 960205,failed to Recognize Requirement to Enter TS LCO 3.0.3 Following Discovery of Ice Blockage. Caused by Inadequate Problem Identification Methods.Design Basis Summary Documents Have Been Prepared Re TS Safety Sys |
- on 960205,failed to Recognize Requirement to Enter TS LCO 3.0.3 Following Discovery of Ice Blockage. Caused by Inadequate Problem Identification Methods.Design Basis Summary Documents Have Been Prepared Re TS Safety Sys
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000245/LER-1996-003-02, Forwards LER 96-003-02 Which Documents an Event That Occurred at Mnps,Unit 1 on 960111,per 10CFR50.73(a)(2)(i) & 10CFR50.73(a)(2)(ii).Commitments Made in Ltr,Submitted | Forwards LER 96-003-02 Which Documents an Event That Occurred at Mnps,Unit 1 on 960111,per 10CFR50.73(a)(2)(i) & 10CFR50.73(a)(2)(ii).Commitments Made in Ltr,Submitted | 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-003-01, :on 960312,temporary I-Beams Located Overhead of Recirculation Spray Sys HXs Discovered.Caused by Inadequate Work Control.Work Control Procedures Revised |
- on 960312,temporary I-Beams Located Overhead of Recirculation Spray Sys HXs Discovered.Caused by Inadequate Work Control.Work Control Procedures Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-004-01, :on 960319,determined That Auxiliary Feedwater Isolation Valves Were in Noncompliance W/Ts.Caused by Misinterpretation of Ts.Revised Operating Procedure to Preclude cross-connected Sys Alignment |
- on 960319,determined That Auxiliary Feedwater Isolation Valves Were in Noncompliance W/Ts.Caused by Misinterpretation of Ts.Revised Operating Procedure to Preclude cross-connected Sys Alignment
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | | 05000336/LER-1996-004, :on 960131,svc Water Strainer Backwash Sys Susceptibility to Freezing Following Loss of Intake Structure non-vital Heating Occurred.Caused by Inadequate Original Design.Design Change Implemented |
- on 960131,svc Water Strainer Backwash Sys Susceptibility to Freezing Following Loss of Intake Structure non-vital Heating Occurred.Caused by Inadequate Original Design.Design Change Implemented
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000423/LER-1996-004-02, :on 960316,auxiliary Feedwater Isolation Valves Noncompliance W/Ts Occurred.Caused by Misinterpretation of Ts.Event Reviewed W/Station Personnel to Caution Others on TS Surveillance Requirements |
- on 960316,auxiliary Feedwater Isolation Valves Noncompliance W/Ts Occurred.Caused by Misinterpretation of Ts.Event Reviewed W/Station Personnel to Caution Others on TS Surveillance Requirements
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1996-005-01, :on 960212,discovered PEO Improperly Utilized to Replace Automatic Backwash Function of Svc Water Strainer Backwash Sys.Caused by Failure to Enter TS Action Statement. Revise Procedures for IST SWS Pump Operability |
- on 960212,discovered PEO Improperly Utilized to Replace Automatic Backwash Function of Svc Water Strainer Backwash Sys.Caused by Failure to Enter TS Action Statement. Revise Procedures for IST SWS Pump Operability
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-005-02, :on 960321,service Water Booster Pump Auto Start Discovered Disable.Caused by Inadequate Review.C/A: Bypass Jumper Removed & Mod Initiated |
- on 960321,service Water Booster Pump Auto Start Discovered Disable.Caused by Inadequate Review.C/A: Bypass Jumper Removed & Mod Initiated
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) 10 CFR 50.73(s)(2) | | 05000423/LER-1996-005-03, :on 960321,design Noncompliance Noted for High Temp Automatic Start Feature of SWS Booster Pumps.Caused by Weakness in Design Control Process.Operating Procedures Revised |
- on 960321,design Noncompliance Noted for High Temp Automatic Start Feature of SWS Booster Pumps.Caused by Weakness in Design Control Process.Operating Procedures Revised
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) | | 05000336/LER-1996-006-01, :on 960207,service Water Pump Motor Flood Protection Not Provided.Caused by Inadequate Administrative Controls.Administrative Controls Established |
- on 960207,service Water Pump Motor Flood Protection Not Provided.Caused by Inadequate Administrative Controls.Administrative Controls Established
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000423/LER-1996-006-02, :on 960330,plant Shutdown Required by TS for AFW Containment Isolation Valves Declared Inoperable.Caused by Opened Valves Outside Containment.Unit Was Shutdown in Orderly Manner |
- on 960330,plant Shutdown Required by TS for AFW Containment Isolation Valves Declared Inoperable.Caused by Opened Valves Outside Containment.Unit Was Shutdown in Orderly Manner
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | | 05000423/LER-1996-007, :on 960403,containment Recirculation Spray, Quench Spray & Safety Injection Sys Were Outside Design Basis Due to Design Errors.Design Reviews of Rss,Qss,Si & Other Sys Will Be Performed |
- on 960403,containment Recirculation Spray, Quench Spray & Safety Injection Sys Were Outside Design Basis Due to Design Errors.Design Reviews of Rss,Qss,Si & Other Sys Will Be Performed
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1996-007, :on 960220,discovered RCS C/D Rate Exceeded TS Limit.Caused by Use of Wrong Temp Sensor.Plant Operating Procedures,Heatup/C/D Monitoring Computer Program & Operator Training Involving These Events Revised |
- on 960220,discovered RCS C/D Rate Exceeded TS Limit.Caused by Use of Wrong Temp Sensor.Plant Operating Procedures,Heatup/C/D Monitoring Computer Program & Operator Training Involving These Events Revised
| | | 05000423/LER-1996-007-01, :on 960403,CRS & Qs Sys Found Outside Design Basis Due to Design Errors.Restored Sys to Appropriate Design Basis Requirements Prior to Declaring Sys Inoperable |
- on 960403,CRS & Qs Sys Found Outside Design Basis Due to Design Errors.Restored Sys to Appropriate Design Basis Requirements Prior to Declaring Sys Inoperable
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000423/LER-1996-007-02, Forwards LER 96-007-02 Which Supplements Rept Submitted on 960502,per 10CFR50.73(a)(2)(ii)(B),10CFR50.73(a)(2)(v)(B&D), 10CFR50.73(a)(2)(vii)(B&D).Commitments in Response to Event, Encl | Forwards LER 96-007-02 Which Supplements Rept Submitted on 960502,per 10CFR50.73(a)(2)(ii)(B),10CFR50.73(a)(2)(v)(B&D), 10CFR50.73(a)(2)(vii)(B&D).Commitments in Response to Event, Encl | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) | | 05000336/LER-1996-008, :on 960222,concluded That Condition of Wire Mesh Screen Encl Over Two Containment Recirculation Suction Pipes Outside Design Basis.Caused by Const/Installation Error.Screen Encl Being Replaced |
- on 960222,concluded That Condition of Wire Mesh Screen Encl Over Two Containment Recirculation Suction Pipes Outside Design Basis.Caused by Const/Installation Error.Screen Encl Being Replaced
| | | 05000423/LER-1996-008-01, :on 960412,reactor Protection Sys Lead/Lag Time Constants Found non-conservative.Caused by Failure of Vendor to Identify Conservative Calibr Requirements.Tss Changed to Correctly Identify Direction of Conservatism |
- on 960412,reactor Protection Sys Lead/Lag Time Constants Found non-conservative.Caused by Failure of Vendor to Identify Conservative Calibr Requirements.Tss Changed to Correctly Identify Direction of Conservatism
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000423/LER-1996-009, :on 960423,inoperable Shutdown Margin Monitors from Low Count Rate Occurred Due to Inadequate Design Control.Reduced SMM Setpoint |
- on 960423,inoperable Shutdown Margin Monitors from Low Count Rate Occurred Due to Inadequate Design Control.Reduced SMM Setpoint
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000245/LER-1996-009-01, :on 960109,isolation Condenser Makeup Water Temperature Below Design Basis Limit,Determined.Caused by Inadequate Design Specification.Preliminary Assessment of non-ductile Failure of Isolation Condenser Sys Performed |
- on 960109,isolation Condenser Makeup Water Temperature Below Design Basis Limit,Determined.Caused by Inadequate Design Specification.Preliminary Assessment of non-ductile Failure of Isolation Condenser Sys Performed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000336/LER-1996-009-01, :on 960216,post LOCA Contianment Pressure Prevented Timely Extraction of PASS Air Sample & H Sample. Caused by Inadequate Assessment of Revised Post LOCA Response Analysis.Implemented Design Change |
- on 960216,post LOCA Contianment Pressure Prevented Timely Extraction of PASS Air Sample & H Sample. Caused by Inadequate Assessment of Revised Post LOCA Response Analysis.Implemented Design Change
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000423/LER-1996-009-02, Submits Table of Commitments Re LER 96-009-02 Per 10CFR50.73(a)(2)(ii) | Submits Table of Commitments Re LER 96-009-02 Per 10CFR50.73(a)(2)(ii) | 10 CFR 50.73(a)(2)(i) | | 05000336/LER-1996-010, :on 960222,identified That Containment Hydrogen Monitor Flow Could Not Be Established W/Containment at Atmospheric Pressure Due to Improper Setting of Sys Pressure Regulators.Sys Calib Procedure Will Be Revised |
- on 960222,identified That Containment Hydrogen Monitor Flow Could Not Be Established W/Containment at Atmospheric Pressure Due to Improper Setting of Sys Pressure Regulators.Sys Calib Procedure Will Be Revised
| | | 05000423/LER-1996-010-02, :on 960425,determined That Potential Failure Mode of Rod Control Sys Acopian Power Supplies Could Create Unanalyzed Condition.Caused by Inadequate Design Review. Reset Feature Will Be Deleted |
- on 960425,determined That Potential Failure Mode of Rod Control Sys Acopian Power Supplies Could Create Unanalyzed Condition.Caused by Inadequate Design Review. Reset Feature Will Be Deleted
| 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000336/LER-1996-011-01, :on 960222,required Time to Enter Mode 5 Exceeded.Caused by Effective Action Not Being Initiated to Revise SDC & Cooldown Rate Monitoring Procedures.Operating & Surveillance Procedures Will Be Revised |
- on 960222,required Time to Enter Mode 5 Exceeded.Caused by Effective Action Not Being Initiated to Revise SDC & Cooldown Rate Monitoring Procedures.Operating & Surveillance Procedures Will Be Revised
| | | 05000423/LER-1996-011-02, :on 960512,determined That Both Trains of CR Envelope Pressurization Sys Inoperable Due to Imbalance in air-conditioning Sys.Cr air-conditioning Sys Rebalanced.W/ |
- on 960512,determined That Both Trains of CR Envelope Pressurization Sys Inoperable Due to Imbalance in air-conditioning Sys.Cr air-conditioning Sys Rebalanced.W/
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-012, :on 960515,containment Leakage in Excess of TS Limits Noted,Due to Valve Leakage.Containment Spray Line Penetration 100 Flushed to Remove Any Boron Deposits.W/ |
- on 960515,containment Leakage in Excess of TS Limits Noted,Due to Valve Leakage.Containment Spray Line Penetration 100 Flushed to Remove Any Boron Deposits.W/
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i) | | 05000336/LER-1996-012-01, :on 960228,SIS Drain Stop Valves Failed to Meet Functional Requirements of Ts.Caused by Personnel Error & Inadequate Retest Requirements.C/A:Valve 2-SI-618 Modified & Safety Related Solenoid Valves Inspected |
- on 960228,SIS Drain Stop Valves Failed to Meet Functional Requirements of Ts.Caused by Personnel Error & Inadequate Retest Requirements.C/A:Valve 2-SI-618 Modified & Safety Related Solenoid Valves Inspected
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000423/LER-1996-012-02, :on 960515,containment Leakage Exceeded Tech Spec Limit.Caused by Boric Acid Residue.Performed Flush of Line to Remove Boron Deposits |
- on 960515,containment Leakage Exceeded Tech Spec Limit.Caused by Boric Acid Residue.Performed Flush of Line to Remove Boron Deposits
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000423/LER-1996-013, :on 960612,design Deficiency in Rhrs.Caused by Inconsideration That Failure Mode of RHS Flow Control Valves Could Create High RHS Heat Exchanger CCP Discharge Temps. Actuators for Heat Exchanger Valves,Modified |
- on 960612,design Deficiency in Rhrs.Caused by Inconsideration That Failure Mode of RHS Flow Control Valves Could Create High RHS Heat Exchanger CCP Discharge Temps. Actuators for Heat Exchanger Valves,Modified
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000336/LER-1996-013-01, :on 960314,assessed Wide Range Logarithmic Neutron Flux Monitors Nuclear Instrumentation Channels A,B,C & D as Inoperable Due to Potential Susceptability to Common Mode Failure.Replaced Failed Power Supply |
- on 960314,assessed Wide Range Logarithmic Neutron Flux Monitors Nuclear Instrumentation Channels A,B,C & D as Inoperable Due to Potential Susceptability to Common Mode Failure.Replaced Failed Power Supply
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-013-02, :on 960515,determined Design Deficiency in Residual Heat Removal System (Rhs).Caused by Original Plant Design.Corrective Actions Will Be Described in Supplement |
- on 960515,determined Design Deficiency in Residual Heat Removal System (Rhs).Caused by Original Plant Design.Corrective Actions Will Be Described in Supplement
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000336/LER-1996-014-01, :on 960311,weekly TS Surveillances Missed. Caused by Personnel Error W/Respect to Scheduling.C/A: Implemented Requirements of Surveillance Procedure Sp 2614A-3 |
- on 960311,weekly TS Surveillances Missed. Caused by Personnel Error W/Respect to Scheduling.C/A: Implemented Requirements of Surveillance Procedure Sp 2614A-3
| 10 CFR 50.73(a)(2)(i) | | 05000423/LER-1996-014-02, :on 960516,surveillances for Emergency Diesel Generator Performed During Operation,Versus Shutdown.Caused by Misinterpretation of Shutdown Stipulation.Surveillances Performed During Shutdown |
- on 960516,surveillances for Emergency Diesel Generator Performed During Operation,Versus Shutdown.Caused by Misinterpretation of Shutdown Stipulation.Surveillances Performed During Shutdown
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-015-05, Forwards LER 96-015-05,documenting Event That Occurred at Plant,Unit 3 on 960610,per 10CFR50.73(a)(2)(ii)(B). Commitments Made within Ltr Submitted | Forwards LER 96-015-05,documenting Event That Occurred at Plant,Unit 3 on 960610,per 10CFR50.73(a)(2)(ii)(B). Commitments Made within Ltr Submitted | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) | | 05000423/LER-1996-015-04, Forwards LER 96-015-04,documenting Condition Determined at Unit 3 on 960610.Util Commitments in Response to Event Contained within Attachment 1 to Ltr | Forwards LER 96-015-04,documenting Condition Determined at Unit 3 on 960610.Util Commitments in Response to Event Contained within Attachment 1 to Ltr | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000336/LER-1996-015-01, :on 960312,failed to Perform Action Requirement for TS LCO 3.3.1.1.Caused by Failure to Recognize Applicability of TS During Abnormal Equipment Configuration. Revised Procedures |
- on 960312,failed to Perform Action Requirement for TS LCO 3.3.1.1.Caused by Failure to Recognize Applicability of TS During Abnormal Equipment Configuration. Revised Procedures
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-015-02, Forwards LER 96-015-02 Re Inadequate Electrical Separation Between Redundant Protection Trains Associated W/Reactor Trip Switches & Reactor Trip Breaker Indicating Lights | Forwards LER 96-015-02 Re Inadequate Electrical Separation Between Redundant Protection Trains Associated W/Reactor Trip Switches & Reactor Trip Breaker Indicating Lights | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000423/LER-1996-016-02, :on 960619,switchgear Cabinet in Noncompliance W/Seismic Design Basis & Subsequently Inadvertent Esfa Signal Occurred.Personnel Did Not Latch Known Seismic Latches as Required.Engaged Latches |
- on 960619,switchgear Cabinet in Noncompliance W/Seismic Design Basis & Subsequently Inadvertent Esfa Signal Occurred.Personnel Did Not Latch Known Seismic Latches as Required.Engaged Latches
| | | 05000336/LER-1996-016-01, :on 960312,common Power Supply Cable to 4 Condenser Pit Level Switches Found Improperly Connected. Caused by Inadequate Work Control.Cable Properly Connected & Trip Circuits Tested |
- on 960312,common Power Supply Cable to 4 Condenser Pit Level Switches Found Improperly Connected. Caused by Inadequate Work Control.Cable Properly Connected & Trip Circuits Tested
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000336/LER-1996-017, :on 960320,discovered That Hydrogen Monitoring Sys Does Not Meet Single Failure Criterion by Reg Guide 1.97.Caused by Failure to Adequately Consider Sys Design Basis Requirements.Design Change Modified |
- on 960320,discovered That Hydrogen Monitoring Sys Does Not Meet Single Failure Criterion by Reg Guide 1.97.Caused by Failure to Adequately Consider Sys Design Basis Requirements.Design Change Modified
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-017-02, :on 960621,determined Design Deficiency Existed in Tornado Protection Ventilation Dampers,Could Have Affected EDGs Following Tornado.Caused by Inadequate Original Plant Const Design.Procedure Revised |
- on 960621,determined Design Deficiency Existed in Tornado Protection Ventilation Dampers,Could Have Affected EDGs Following Tornado.Caused by Inadequate Original Plant Const Design.Procedure Revised
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000336/LER-1996-018-01, Forwards LER 96-018-01,documenting Condition That Was Discovered at Unit 2 on 960319.LER Suppl Provides Update on Analyses & Investigation of Condition.Attachment 1 Is Clarification of Original Commitment Associated W/Ler | Forwards LER 96-018-01,documenting Condition That Was Discovered at Unit 2 on 960319.LER Suppl Provides Update on Analyses & Investigation of Condition.Attachment 1 Is Clarification of Original Commitment Associated W/Ler | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000336/LER-1996-018, :on 960316,gaps Discovered in Encls Door Seals for Motor Control Ctrs B51 & B61.Caused by Weakness in Existing Program to Inspect & Verify Integrity of Environ Protective Barriers.Doors for MCC B51 & MCC B61 Replaced |
- on 960316,gaps Discovered in Encls Door Seals for Motor Control Ctrs B51 & B61.Caused by Weakness in Existing Program to Inspect & Verify Integrity of Environ Protective Barriers.Doors for MCC B51 & MCC B61 Replaced
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-019-02, :on 960627,RCS PORV Block Valves Were Determined to Be Unable to Perform Intended Safety Functions.Caused by Structural Design Deficiency.C/A Will Be Provided in Supplement to Rept |
- on 960627,RCS PORV Block Valves Were Determined to Be Unable to Perform Intended Safety Functions.Caused by Structural Design Deficiency.C/A Will Be Provided in Supplement to Rept
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) |
|