| | | Reporting criterion |
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| 05000245/LER-1987-001-01, :on 870113,insp on All Model 4160 Vac Load Ctrs Revealed Cracking Along Horizontal Noryl Insulators. Caused by GE Mfg Defect.Plant Replaced Cracked Insulation W/Bayblend Insulation to Preclude Recurrence |
- on 870113,insp on All Model 4160 Vac Load Ctrs Revealed Cracking Along Horizontal Noryl Insulators. Caused by GE Mfg Defect.Plant Replaced Cracked Insulation W/Bayblend Insulation to Preclude Recurrence
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000336/LER-1987-001, :on 861222,intermittent Fire Alarms Received from Heat Detectors Above Reactor Coolant Pump 5.Caused by Heat Detector Failure.Faulty Detector Will Be Replaced.W/ |
- on 861222,intermittent Fire Alarms Received from Heat Detectors Above Reactor Coolant Pump 5.Caused by Heat Detector Failure.Faulty Detector Will Be Replaced.W/
| |
| 05000423/LER-1987-001-02, :on 870113,plant Received Automatic Reactor Trip as Result of Automatic Turbine Trip.Caused by Inadequate Communications Between Operations Personnel. Operational Procedures Updated |
- on 870113,plant Received Automatic Reactor Trip as Result of Automatic Turbine Trip.Caused by Inadequate Communications Between Operations Personnel. Operational Procedures Updated
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000336/LER-1987-002, :on 870102,reactor Tripped on Low Steam Generator Level.Caused by Failure of Steam Generator 2 Feedwater Regulating Valve.Valve Repaired |
- on 870102,reactor Tripped on Low Steam Generator Level.Caused by Failure of Steam Generator 2 Feedwater Regulating Valve.Valve Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) |
| 05000423/LER-1987-002-01, :on 870114,reactor Trip Occurred When Reactor Operator Accidently Reset Source Range High Flux Reactor Trip Block.Caused by Operator Error Compounded by Sensitive Switch.Extenders Removed & Caution Tags Added |
- on 870114,reactor Trip Occurred When Reactor Operator Accidently Reset Source Range High Flux Reactor Trip Block.Caused by Operator Error Compounded by Sensitive Switch.Extenders Removed & Caution Tags Added
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000336/LER-1987-003-01, :on 870129,reanalysis of Steam Generator Tube Exam Data Identified Tube Containing Repairable Defect. Caused by Incorrect Recording of Original Test.Tube Retested & Analyzed |
- on 870129,reanalysis of Steam Generator Tube Exam Data Identified Tube Containing Repairable Defect. Caused by Incorrect Recording of Original Test.Tube Retested & Analyzed
| 10 CFR 50.73(a)(2)(1) |
| 05000423/LER-1987-003, :on 870114 & 0205,Train B Emergency Diesel Generator Did Not Start within Required 10 During Surveillance Testing.Caused by Inadequate Purge of Air from Fuel Injectors & Low Oil Temp.Maint Performed |
- on 870114 & 0205,Train B Emergency Diesel Generator Did Not Start within Required 10 During Surveillance Testing.Caused by Inadequate Purge of Air from Fuel Injectors & Low Oil Temp.Maint Performed
| |
| 05000336/LER-1987-003, :on 870129,reanalysis of Steam Generator Tube Exam Data Identified That One Tube Which Contained Repairable Defect,Not Been Repaired,As Required by Tech Spec 4.4.5.1.4.b.Defective Tubes Plugged |
- on 870129,reanalysis of Steam Generator Tube Exam Data Identified That One Tube Which Contained Repairable Defect,Not Been Repaired,As Required by Tech Spec 4.4.5.1.4.b.Defective Tubes Plugged
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000336/LER-1987-004-01, :on 870202 & 08,automatic Actuation by Emergency Safeguards Actuation Sys Resulted in Containment Purge Valve Isolation.Caused by Broken Mylar Window on Beta Scintillation Detector |
- on 870202 & 08,automatic Actuation by Emergency Safeguards Actuation Sys Resulted in Containment Purge Valve Isolation.Caused by Broken Mylar Window on Beta Scintillation Detector
| |
| 05000423/LER-1987-004, :on 870127 Motor Driven Auxiliary Feedwater Pump Train a Tripped.Cause Not Determined.Train B Tripped on 870129 During Surveillance Testing.Caused by Low Suction Pressure Trips.Trip Function Removed |
- on 870127 Motor Driven Auxiliary Feedwater Pump Train a Tripped.Cause Not Determined.Train B Tripped on 870129 During Surveillance Testing.Caused by Low Suction Pressure Trips.Trip Function Removed
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability |
| 05000336/LER-1987-004, :on 870202 & 0208,automatic Actuations of Emergency Safeguards Actuation Sys Resulted in Containment Purge Valve Isolations.Caused by Broken Window on Beta Scintillation Detector.Detector Replaced |
- on 870202 & 0208,automatic Actuations of Emergency Safeguards Actuation Sys Resulted in Containment Purge Valve Isolations.Caused by Broken Window on Beta Scintillation Detector.Detector Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000423/LER-1987-005, :on 870201,control Room Envelope Pressurization Surveillance Failed Due to Mispositioned Throttle Valve. Caused by Personnel Error.Procedure Implemented to Establish Correct Valve Position |
- on 870201,control Room Envelope Pressurization Surveillance Failed Due to Mispositioned Throttle Valve. Caused by Personnel Error.Procedure Implemented to Establish Correct Valve Position
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) |
| 05000336/LER-1987-005, :on 870306,charging Pump B Found Leaking Water from Pump Head Area.Caused by Cracked Block.Pump Block Replaced W/Spare |
- on 870306,charging Pump B Found Leaking Water from Pump Head Area.Caused by Cracked Block.Pump Block Replaced W/Spare
| |
| 05000245/LER-1987-005-01, :on 870221,while Returning Condensate Demineralizer to Svc,Automatic Actuation of Standby Gas Treatment Occurred.Caused by Air Becoming Entrained in Feedwater Sys.Procedures Revised |
- on 870221,while Returning Condensate Demineralizer to Svc,Automatic Actuation of Standby Gas Treatment Occurred.Caused by Air Becoming Entrained in Feedwater Sys.Procedures Revised
| |
| 05000336/LER-1987-006-01, :on 870403,during Mode 1,inconsistency Noted Between FSAR Table for Svc Water Flow Thru Reactor Bldg Closed Cooling Water HX & Calculated Design Flow.Cause Unknown.Fsar Revised |
- on 870403,during Mode 1,inconsistency Noted Between FSAR Table for Svc Water Flow Thru Reactor Bldg Closed Cooling Water HX & Calculated Design Flow.Cause Unknown.Fsar Revised
| 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded |
| 05000423/LER-1987-006, :on 870201,shift Supervisor Discovered That Surveillance of Area Temp Monitoring in TN-02 Area Not Performed within Alloted Time Frame.Caused by Personnel Error.Personnel Reminded of Duties |
- on 870201,shift Supervisor Discovered That Surveillance of Area Temp Monitoring in TN-02 Area Not Performed within Alloted Time Frame.Caused by Personnel Error.Personnel Reminded of Duties
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) |
| 05000245/LER-1987-007, :on 870322,reactor Scram & Group I Isolation Occurred.Caused by Operator Error.Operating Procedures Clarified & Operator Training Increased |
- on 870322,reactor Scram & Group I Isolation Occurred.Caused by Operator Error.Operating Procedures Clarified & Operator Training Increased
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000336/LER-1987-007, :on 870416,reactor Tripped Automatically Due to Turbine Trip Caused by Generator Exciter Field Breaker Opening.Caused by Generator Volts/Hertz Relay Actuation. Emergency Operating Procedure 2525 & 2526 Done |
- on 870416,reactor Tripped Automatically Due to Turbine Trip Caused by Generator Exciter Field Breaker Opening.Caused by Generator Volts/Hertz Relay Actuation. Emergency Operating Procedure 2525 & 2526 Done
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) |
| 05000423/LER-1987-007, :on 870211,plant Tech Spec Surveillance Requirement for Containment Drain Sump Inventory & Discharge Monitoring at Least Once Every 12 H Missed.Caused by Operator Error.New Policy Initiated |
- on 870211,plant Tech Spec Surveillance Requirement for Containment Drain Sump Inventory & Discharge Monitoring at Least Once Every 12 H Missed.Caused by Operator Error.New Policy Initiated
| 10 CFR 50.73(a)(2)(1) |
| 05000336/LER-1987-007-01, :on 870416,automatic Trip from 100% Power Operation Occurred.Caused by Actuation of Generator Volts/ Hertz Relay 59X1.Reason for Actuation of Relay Unknown. Relay Removed from Svc |
- on 870416,automatic Trip from 100% Power Operation Occurred.Caused by Actuation of Generator Volts/ Hertz Relay 59X1.Reason for Actuation of Relay Unknown. Relay Removed from Svc
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) |
| 05000336/LER-1987-008-02, :on 870611,scheduling Error Discovered W/ Battery Surveillance 2736B-1,due on 870406.Surveillance Performed on 870506.Maint Dept Surveillance Scheduling Procedure Changed |
- on 870611,scheduling Error Discovered W/ Battery Surveillance 2736B-1,due on 870406.Surveillance Performed on 870506.Maint Dept Surveillance Scheduling Procedure Changed
| 10 CFR 50.73(a)(2)(1) |
| 05000423/LER-1987-008, :on 870307,reactor Trip Occurred Due to lo-lo Steam Generator Level in Steam Generator D.Caused by Failure of Solenoid Valve.Solenoid Valve Replaced & Tested for Operability |
- on 870307,reactor Trip Occurred Due to lo-lo Steam Generator Level in Steam Generator D.Caused by Failure of Solenoid Valve.Solenoid Valve Replaced & Tested for Operability
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000245/LER-1987-008-01, :on 870310,reactor Bldg Ventilation Exhaust Radiation Monitor Channel 2 Recorder Observed Upscale While Indicating Trip Unit Observed Downscale.Caused by Wire Shorting to Ground.Recorder Recalibr |
- on 870310,reactor Bldg Ventilation Exhaust Radiation Monitor Channel 2 Recorder Observed Upscale While Indicating Trip Unit Observed Downscale.Caused by Wire Shorting to Ground.Recorder Recalibr
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000336/LER-1987-010-01, :on 870730,inadequacies Identified in Fire Protection Coating on Raceway Support Structures in Main Cable Vault & Hallway Leading to Charging Pumps.Hourly Fire Watch Started & Automatic Sprinkler Installed |
- on 870730,inadequacies Identified in Fire Protection Coating on Raceway Support Structures in Main Cable Vault & Hallway Leading to Charging Pumps.Hourly Fire Watch Started & Automatic Sprinkler Installed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 05000423/LER-1987-011, :on 870319,voltage Relays Monitoring Train a & B Found W/Trip Setpoints Below Plant Tech Specs Allowable Setpoint.Caused by Setpoint Drift & Initial Setting Position.New Setpoints Allow for Drift |
- on 870319,voltage Relays Monitoring Train a & B Found W/Trip Setpoints Below Plant Tech Specs Allowable Setpoint.Caused by Setpoint Drift & Initial Setting Position.New Setpoints Allow for Drift
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) |
| 05000336/LER-1987-011, :on 870723,automatic Reactor Trip Occurred. Caused by Low Level in Steam Generator 1.Spray Valve 2-RC-100F Repaired & Pdic 5270 Replaced |
- on 870723,automatic Reactor Trip Occurred. Caused by Low Level in Steam Generator 1.Spray Valve 2-RC-100F Repaired & Pdic 5270 Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000245/LER-1987-012, :on 870519,overhead Fireproofing Blanket Matl Over Emergency Diesel Generator (EDG) Found to Be Inadequate to Provide 3 H Fire Resistance Rating.Cause Unknown.Fire Watch Established & Firecoating Installed |
- on 870519,overhead Fireproofing Blanket Matl Over Emergency Diesel Generator (EDG) Found to Be Inadequate to Provide 3 H Fire Resistance Rating.Cause Unknown.Fire Watch Established & Firecoating Installed
| |
| 05000423/LER-1987-012, :on 870320,Tech Spec Surveillance on Snubber Visual Insp Missed.Caused by Engineering Oversight & Outdated Snubber List.List Updated & All Snubbers Inspected |
- on 870320,Tech Spec Surveillance on Snubber Visual Insp Missed.Caused by Engineering Oversight & Outdated Snubber List.List Updated & All Snubbers Inspected
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) |
| 05000336/LER-1987-012-01, :on 871116,reactor Tripped on Low Steam Generator Level.Caused by Failure of Feedwater Regulating Valve to Respond to Closing Signals from Control Board in Automatic or Manual Modes |
- on 871116,reactor Tripped on Low Steam Generator Level.Caused by Failure of Feedwater Regulating Valve to Respond to Closing Signals from Control Board in Automatic or Manual Modes
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000336/LER-1987-013-02, :on 871219,fire Watch Patrol Failed to Conduct Hourly Insp Per Tech Specs.Caused by Watchstander Failure to Releive Position in Timely Manner.Fire Watch Contractor Replaced |
- on 871219,fire Watch Patrol Failed to Conduct Hourly Insp Per Tech Specs.Caused by Watchstander Failure to Releive Position in Timely Manner.Fire Watch Contractor Replaced
| 10 CFR 50.73(a)(2)(1) |
| 05000245/LER-1987-013-01, :on 870527,standby Gas Treatment Sys Automatically Initiated & Reactor Bldg Ventilation Sys Isolated.Caused by Underwater Vacuum Canisters Floating to Surface of Fuel Pool.Procedures Revised |
- on 870527,standby Gas Treatment Sys Automatically Initiated & Reactor Bldg Ventilation Sys Isolated.Caused by Underwater Vacuum Canisters Floating to Surface of Fuel Pool.Procedures Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000423/LER-1987-013, :on 870321,discovered 120-volt Ac Nonvital Circuit Entering Containment Did Not Have Secondary Penetration Conductor Overcurrent Protection.Caused by Personnel Error.Protection Installed & Tested |
- on 870321,discovered 120-volt Ac Nonvital Circuit Entering Containment Did Not Have Secondary Penetration Conductor Overcurrent Protection.Caused by Personnel Error.Protection Installed & Tested
| 10 CFR 50.73(a)(2)(1) |
| 05000336/LER-1987-014, :on 871231,12 of 16 Valves Tested Failed Initial Main Steam Safety Valve Simmer Test.Caused by Setpoint Drift.Setpoints Adjusted.Six Valves Sent to Outside Contractor for Refurbishment |
- on 871231,12 of 16 Valves Tested Failed Initial Main Steam Safety Valve Simmer Test.Caused by Setpoint Drift.Setpoints Adjusted.Six Valves Sent to Outside Contractor for Refurbishment
| |
| 05000423/LER-1987-014, :on 870322,while in Cold Shutdown Mode 5,during Surveillance Testing,Train Emergency Diesel Generator B Failed to Start within 10 S.Caused by Buildup of Dirt/Rust in Main Air Start Valves.Valves Replaced |
- on 870322,while in Cold Shutdown Mode 5,during Surveillance Testing,Train Emergency Diesel Generator B Failed to Start within 10 S.Caused by Buildup of Dirt/Rust in Main Air Start Valves.Valves Replaced
| |
| 05000336/LER-1987-015, :on 861114,util Informed That GE Model 12 Cfd Relays Installed Above 30-ft Elevation Not Seismically Qualified for Class 1E Svc.Caused by Design Error.Relay Replaced |
- on 861114,util Informed That GE Model 12 Cfd Relays Installed Above 30-ft Elevation Not Seismically Qualified for Class 1E Svc.Caused by Design Error.Relay Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(vi) |
| 05000245/LER-1987-015, :on 870606,during Refueling Outage,Addl Isolation Valves Did Not Meet Local Leak Rate Test (LLRT) Requirement,Per Tech Spec 4.7.f.2.c.LLRT Requirement Satisfactorily Retested Subsequent to Repair |
- on 870606,during Refueling Outage,Addl Isolation Valves Did Not Meet Local Leak Rate Test (LLRT) Requirement,Per Tech Spec 4.7.f.2.c.LLRT Requirement Satisfactorily Retested Subsequent to Repair
| 10 CFR 50.73(a)(2) |
| 05000423/LER-1987-015, :on 870324,main Steam Isolation Trip Valves Did Not Meet 5 Closure Time Requirement.Caused by Procedure Deficiency.Valves Will Be Placed in Closed Position During Mode 4 Operation |
- on 870324,main Steam Isolation Trip Valves Did Not Meet 5 Closure Time Requirement.Caused by Procedure Deficiency.Valves Will Be Placed in Closed Position During Mode 4 Operation
| 10 CFR 50.73(a)(2)(1) |
| 05000245/LER-1987-015-01, :on 870606,during Local Leak Rate Testing, Discovered That B Main Steam Isolation Valves Could Not Meet Required Leak Rate Test.Causes Listed.All Failed Valves Repaired & Retested Satisfactorily |
- on 870606,during Local Leak Rate Testing, Discovered That B Main Steam Isolation Valves Could Not Meet Required Leak Rate Test.Causes Listed.All Failed Valves Repaired & Retested Satisfactorily
| |
| 05000423/LER-1987-016, :on 870325,Train a Safety Injection Signal Received.Caused by Personnel Error Due to Defective Procedure.Applicable Procedure Changed to Properly Configure Protection Sys for Test |
- on 870325,Train a Safety Injection Signal Received.Caused by Personnel Error Due to Defective Procedure.Applicable Procedure Changed to Properly Configure Protection Sys for Test
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000245/LER-1987-017, :on 870610,reactor Pressure Sys Activated by Scram Valve Air Header Low Pressure Scram Circuit.Caused by Loss of Pressure Due to Use of Air for Power Tools & Other Equipment.Jumper Bypass Placed on Circuit |
- on 870610,reactor Pressure Sys Activated by Scram Valve Air Header Low Pressure Scram Circuit.Caused by Loss of Pressure Due to Use of Air for Power Tools & Other Equipment.Jumper Bypass Placed on Circuit
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000423/LER-1987-017, :on 870329,while Performing Response Time Testing Per Tech Spec 4.3.2.2,several Components Failed to Meet Emergency Safeguards Features Actuation Sys Response Times.Caused by Inadequate Procedures |
- on 870329,while Performing Response Time Testing Per Tech Spec 4.3.2.2,several Components Failed to Meet Emergency Safeguards Features Actuation Sys Response Times.Caused by Inadequate Procedures
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
| 05000423/LER-1987-018, :on 870402,train a Control Bldg Inlet Radiation Monitor Not in Service as Required by Tech Spec.Caused by Personnel Error.Channel Check Surveillance Procedures on safety-related Radiation Monitors Revised |
- on 870402,train a Control Bldg Inlet Radiation Monitor Not in Service as Required by Tech Spec.Caused by Personnel Error.Channel Check Surveillance Procedures on safety-related Radiation Monitors Revised
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) |
| 05000423/LER-1987-019, :on 870411,temp of Turbine Driven Auxiliary Feedwater Pump Area ES-07 Exceeded 110 F Limit Set by Tech Specs 3.714b & 6.9.2.Cause Not Stated.Equipment Not Affected According to Maint & Inservice Insp |
- on 870411,temp of Turbine Driven Auxiliary Feedwater Pump Area ES-07 Exceeded 110 F Limit Set by Tech Specs 3.714b & 6.9.2.Cause Not Stated.Equipment Not Affected According to Maint & Inservice Insp
| |
| 05000245/LER-1987-019-01, :on 870612,misorientation of Fuel Assembly Discovered.Caused by Failure to Load in Proper Orientation. Appropriate Core Verification Procedure Changes Being Implemented |
- on 870612,misorientation of Fuel Assembly Discovered.Caused by Failure to Load in Proper Orientation. Appropriate Core Verification Procedure Changes Being Implemented
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000245/LER-1987-020, :on 870626,indication on Recirculation Sys Pipe Inside Drywell Discovered.On 870701,flaw Declared Unacceptable,Per Asme,Section Xi.Caused by Igscc.Weld Will Be Repaired Using Weld Overlay Technique |
- on 870626,indication on Recirculation Sys Pipe Inside Drywell Discovered.On 870701,flaw Declared Unacceptable,Per Asme,Section Xi.Caused by Igscc.Weld Will Be Repaired Using Weld Overlay Technique
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |
| 05000423/LER-1987-020, :on 870412,reactor Trip Occurred Due to Lo Lo Steam Level in Steam Generator D.Caused by Equipment Failure.Air Supply Line Repaired & Retested Satisfactorily |
- on 870412,reactor Trip Occurred Due to Lo Lo Steam Level in Steam Generator D.Caused by Equipment Failure.Air Supply Line Repaired & Retested Satisfactorily
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000245/LER-1987-021-01, :on 870630,during Performance of Surveillance Testing,Five Main Steam Safety/Relief Valves Lifted at Pressures in Excess of Desired Setpoint.Cause Not Stated. Valves Rebuilt & Set to Desired Setpoints |
- on 870630,during Performance of Surveillance Testing,Five Main Steam Safety/Relief Valves Lifted at Pressures in Excess of Desired Setpoint.Cause Not Stated. Valves Rebuilt & Set to Desired Setpoints
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000423/LER-1987-021, :on 870412,reactor Trip Occurred Due to lo-lo Steam Generator Level Following Feedwater Isolation Signal. Caused by Operator Error.Revised Procedures Issued.All Licensed Operators Counseled |
- on 870412,reactor Trip Occurred Due to lo-lo Steam Generator Level Following Feedwater Isolation Signal. Caused by Operator Error.Revised Procedures Issued.All Licensed Operators Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000423/LER-1987-022, :on 870415,results of Steam Generator Condensate Pot Temp Monitoring Indicated Error in Steam Generator Level.Caused by Design Configuration of Generator Ref Legs.Improved Design Will Be Installed |
- on 870415,results of Steam Generator Condensate Pot Temp Monitoring Indicated Error in Steam Generator Level.Caused by Design Configuration of Generator Ref Legs.Improved Design Will Be Installed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 05000245/LER-1987-022-01, :on 870702,unacceptable Inclusions Discovered in Base Metal of Isolation Condenser Bl Return Line Piping. Caused by Mfg Defect.Piping Replaced W/Matl More Resistant to IGSCC |
- on 870702,unacceptable Inclusions Discovered in Base Metal of Isolation Condenser Bl Return Line Piping. Caused by Mfg Defect.Piping Replaced W/Matl More Resistant to IGSCC
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition |