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{{#Wiki_filter:<os/~</~REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)DISTRIBUTION FOR INCOMING MATERIAL 50-315 t J REC: KEPPLER J G ORG: SHALLER D V DOCDATE: 03/17/78 NRC IN 4 MI PWR DATE RCVD: 03/22/78 DOCTYPE: LETTER NOTARIZED:
{{#Wiki_filter:< os /~</~
NO COPIES RECEIVED  
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS) t DISTRIBUTION FOR INCOMING MATERIAL                       50-315 J REC:   KEPPLER J G               ORG:   SHALLER D V               DOCDATE: 03/17/78 NRC                               IN 4 MI PWR                 DATE RCVD: 03/22/78 DOCTYPE: LETTER     NOTARIZED: NO                                   COPIES RECEIVED


==SUBJECT:==
==SUBJECT:==
LTR 1 ENCL 1 LICENSEE EVENT REPT<RO 50-315/78-017/03L-0)
LTR 1     ENCL 1 LICENSEE EVENT REPT <RO 50-315/78-017/03L-0) ON 02/15/78 CONCERNING WATER SPRAYED INTO THE INVERTOR FOR THE CD DIESEL GENERATOR SPEED GOVENOR RESULTED IN FAILURE QF THE INVERTER POWER SUPPLY... W/ATT LER 78-018/03L-0.
ON 02/15/78 CONCERNING WATER SPRAYED INTO THE INVERTOR FOR THE CD DIESEL GENERATOR SPEED GOVENOR RESULTED IN FAILURE QF THE INVERTER POWER SUPPLY...W/ATT LER 78-018/03L-0.
PLANT NAME: COOK UNIT     1                             REVIEWER INITIAL: X JM DISTRIBUTOR   INITIAL:
PLANT NAME: COOK-UNIT 1 REVIEWER INITIAL: X JM DISTRIBUTOR INITIAL: DISTRIBUTION OF THIS MATERIAL IS AS FOLLOWS INCIDENT REPORTS (DISTRIBUTION CQDE A002)FOR ACTION: INTERNAL: EXTERNAL: BR CHIEF b ENCER++W/4 ENCL EG FILE44W NCL SCHROEDER/I PPOL I TO++W/ENCL NGVAI<f CHECK+4EWlENCL KNI GHT+~W/ENCL IHAIWAUER+4W/
DISTRIBUTION OF THIS MATERIAL IS AS FOLLOWS INCIDENT REPORTS (DISTRIBUTION CQDE A002)
ENCL EI SENHUT++W/ENCL SHAG~~~~W/
FOR ACTION:     BR CHIEF b       ENCER++W/4 ENCL INTERNAL:          EG FILE44W                   NRC PDR++W/ENCL NCL             MIPC4+Wf3 .ENCL SCHROEDER/I PPOL I TO++W/ENCL    HGUSTON++W/ENCL NGVAI<fCHECK+4EWlENCL           GR IMES4 +W/ENCL KNIGHT+~W/ENCL                  BUTLER++W/ENCL IHAIWAUER+4W/ENCL                TEDESCO~~W/ENCL EI SENHUT++W/ENCL                BAER++W/ENCL SHAG~~~~W/ ENCL                  VOLLMER/BUNCH++W/ENCL KREGERl J. COLL I NS++W/ENCL  ROSA++W/ENCL K SEYFRIT/ IE++WfENCL EXTERNAL:        LPDR'S ST. JOSEPH'I ++W/ENCL TIC4~+WfENCL NS I C+~W/ENCL ACRS     CAT B4+Wf 16 ENCL COPIES NOT SUBMITTED PER REGULATORY GUIDE 10.1 DISTRIBUTION:     LTR 45       ENCL 45                     CONTROL NBR:    78083007 SIZE: lP+iP+iP THE END
ENCL KREGERl J.COLL I NS++W/ENCL K SEYFRIT/IE++Wf ENCL LPDR'S ST.JOSEPH'I++W/ENCL TIC4~+Wf ENCL NS I C+~W/ENCL ACRS CAT B4+Wf 16 ENCL NRC PDR++W/ENCL MIPC4+Wf 3.ENCL HGUSTON++W/ENCL GR IMES4+W/ENCL BUTLER++W/ENCL TEDESCO~~W/ENCL BAER++W/ENCL VOLLMER/BUNCH++W/ENCL ROSA++W/ENCL COPIES NOT SUBMITTED PER REGULATORY GUIDE 10.1 DISTRIBUTION:
 
LTR 45 ENCL 45 SIZE: lP+iP+iP CONTROL NBR: 78083007 THE END  
C o II
,I I C o II f%4.~'7 P g~~erleen Itteotrla lower QSCd dO'ONALD C.COOK NUCLEAR PLANT P.O.Box 458, Bridgman, Michigan 49106 F a.E Cytf March 17, 1978 Mr., J.G.Keppler, Regional Director.Office of In specti on and Enforcement United States Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Operating License DPR-58 Docket No.50-315  
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      ~erleen Itteotrla lower           dO'ONALD QSCd C. COOK   NUCLEAR PLANT P.O. Box 458, Bridgman, Michigan 49106 March 17, 1978 Mr., J. G. Keppler, Regional Director       .
Office of In specti on and Enforcement United States Nuclear Regulatory Commission Region   III 799 Roosevelt Road Glen Ellyn, IL 60137 Operating License DPR-58 Docket No. 50-315
 
==Dear Mr. Keppler:==


==Dear Mr.Keppler:==
Pursuant to the requirements of Appendix A..Technical Specifications the following reports are submitted:
Pursuant to the requirements of Appendix A..Technical Specifications the following reports are submitted:
RO 78-017/03L-0 RO 78-018/03L-O Since rely, D.V.Shaller Plant Manager/pk cc: J.E.Dolan R.W.Jurgensen G.E.Lien R.Kilburn R.J.Vollen BPI K.R.Baker RO:III R.C.Callen MPSC P.W.Steketee, Esq.R.Walsh, Esq.G.Charnoff, Esq.G.Olson J.M.Hennigan PNSRC J.F.Stietzel Dir', IE (30 copies)Dir., MIPC (3 copies)pf  
RO 78-017/03L-0 RO 78-018/03L-O Since rely, D. V. Shaller Plant Manager
~r f P t n't n U.S.NUCLEAR REGULATORY COMMISSION SE PRINT OR TYPE ALL REQUIRED INFORMATION) 0 OQo4 1 1 1 1 Q4~Qs 25 26 LICENSE TYPE 30 57 CAT 58 QB 0 3 1 7 QB EVENT DATE 74 75 REPORT DATE 80 NRC FORM 386 (7.77)o J e LICENSEE EVENT REPORT oeCONTROL BLOCK: (PLEA I 6~o1 M I D C C 1 Q2 0 0 0 0 0 0 0 0 0'7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER CON'T[oot)"o,~LOs0 G 0 0 0 3 1 5 Oo 60 61 DOCK ET NUMB E R 68 69 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10~o~Iiater s ra ed into the inver ter for the CD D'~O3 in failure of the inverter power supply.The inverter was switched to the alternate power source and the engine was tested.The Diesel was inoperable for 36 minutest~OS This is the first occurrence of this type.~OB~O7~OB 80 7 8 SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE~EE Q>>EQu~GQio G E N E R A Q4~FQ>>~ZQ 9 10 11 12 13 18'9 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERIRO EVENT YEAR REPORT NO.CODE TYPE NO.Q>>o Poor~78+~01 7 Qx~03+L Q QO 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDX PRIME COMP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS 022 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER I A IQ>s~2Q>e~ZQoo~ZQ>>0 0 0 0 N Qoo~NQoo~AQos S 2 33 34 35 36 37 40 41 42 43 44 cAUsE DEscRIPTIQN AND coRREGTIYE AGTIQNs 027 o This condition was the result of a water su 1 ho c eanin e~OS 7 8 47 The Supervisor responsible for this.cleanin has been instructed not to use ressur ized water.cleaning equipment in the vicinity of any electrical panels~~3 METHOD OF DISCOVERY~aQ31 N/A 45 46 N A 45 NAME QF PREPARER David G.Mizner 4 7 8 9 FACILITY STATUS%POWER OTHER STATUS 0~l5~EQ28~IO 0 Qoo N/A 7 8 9 10 12 44 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY Q 6~Z Q33~ZQ34 N A 7 8 9 10 11 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION 039~l7~00 0 Q>>ZQs NA 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41
                /pk cc:   J. E. Dolan R. W. Jurgensen G. E. Lien R. Kilburn R. J. Vollen BPI K. R. Baker RO:III R. C. Callen MPSC P. W. Steketee, Esq.
~00 0 Qoo NA 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY 43 TYPE DESCRIPTION 6 Z Q42 N A 8 9 10 PUBLICITY ISSUED DESCRIPTION Q o~Z 044 N/A 8 9 10 DISCOVERY DESCRIPTION Q32 80 LOCATION OF RELEASE Q 80 80 80 80 80 NRC USE ONI Y o r 80'0 68 69 PHQNE 616-465-5901  
R. Walsh, Esq.
~J 4 C U.S.NUCLEAR REGULATORY COMMISSION NRC FORM 366 (7.77)s LICENSEE EVENT REPORT CONTROL BLOCK: Ql(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION1 1 6~oi M 10 C C 1 Qo 0 0 0 0 0 0 0 0 0 0 OQo 4 1 1 1 I Qs~Qs 7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T KDi soos~L'..Qs 0 5 0 0 03 1 5 Qo 2 QB 0 3 1 7 7 8 QB 7 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10~O2 Durin normal o erations, Ft/I0-212, the motor o crated auxiliar feed um dischar e valve for (51 S/6,'ailed to shut from the Control Room.This constituted degradation
G. Charnoff, Esq.
~o4 of an operable flow path required by Technical Specification 3.7.1.2.The failure~os did not present a substantial safety hazard since the'valve failed in the safest (ful~06 o en osition and redundant auxiliar feed s stems were o erable.This is the.first~o 7 event of this nature at the lant.~OB 7 8 9 80~OS 7 8 SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE~CH Q>>8 Q>>~C Q13 V A L V 0 P Qls~AQls~Z Qls 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LER/RO EVENT YEAR REPORT NO.CODE TYPE NO.Q>>os osr~78+~01 8+w~03+L Q+0 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDR PRIME COMP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER
G. Olson J. M. Hennigan PNSRC J. F. Stietzel Dir',   IE (30 copies)
~EQls~ZQo~ZQoo~ZQ>>0 0 0 0 N Qos~NQos~AQos..L 3 0 0 Qos 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o FMO-212 failed to o crate due to a loose screw at an electrical connection.
Dir.,   MIPC   (3 copies) pf
in.the..valve's motor o erator control circuit.This connection was robabl not ti htened during initial installation, although previous operations with FMO-212 were success-3 ful.The 1 pose screw'as ti htened and subse uent retest was sati sfactory.No other N A 44 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY Q43 TYPE DESCRIPTION zQ-vA 7 8 9 10 PUBLICITY ISSUED DESCRIPTION
 
~S LILtQ44 O 7 8 9 10 Michael S.Brown NAME OF PREPARER NRC USF.ONLY 68 69 616-465-5901 PHONE: connections were found to be loose and no further actions are 1 armed.7 8 9 FACILITY~~3P METHOD OF STATUS%POWER OTHER STATUS~DISCOVERY DISCOVERY DESCRIPTION Q32 E Qs~l0 0 Qs N/A~AQolOperator observation 7 8 9 10 12 13 44 45 46 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY~LOCATION OF RELEASE Q~z Q~zs~A 7 8 9 10 45 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39~00 0 Q>>~Z:.Qss 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41
~r f
~00 0 Qo NA 80 80 80 80 80 80~s ss a 80~a 0 a ss}}
P t
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    't n
 
NRC FORM 386                                                                                                                            U. S. NUCLEAR REGULATORY COMMISSION (7.77) o J   e                                                           LICENSEE EVENT REPORT oeCONTROL BLOCK:                                                                       (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
I                                   6
~o1
'7 M   I     D     C       C       1 14 Q2 15 0   0   0 0     0   0     0 LICENSE NUMBER 0     0     0        OQo4 25      26 1    1      1 LICENSE TYPE 1
30 Q4~Qs 57 CAT 58 8   9         LICENSEE CODE CON'T
[oot)               "o,~LOs0   60            61 G   0     0   0 DOCK ET NUMBE R 3   1   5 68 Oo 69         EVENT DATE              74 QB 75 0      3    1 REPORT DATE 7
80 QB EVENT DESCRIPTION AND PROBABLE CONSEQUENCES                               Q10
~o~             Iiater     s   ra ed         into the inver ter for the                       CD     D'
~O3             in failure of the inverter                               power     supply.           The     inverter         was     switched to the alternate power source and the engine was                                   tested.         The Diesel was                   inoperable for                 36   minutest
  ~OS             This is the               first occurrence                   of this type.
  ~OB
  ~O7
  ~OB                                                                                                                                                                                     80 7       8
                                                                                                                                    '9 SYSTEM               CAUSE         CAUSE                                                           COMP.           VALVE CODE                 CODE       SUBCODE                 COMPONENT CODE                         SUBCODE           SUBCODE
  ~OS 8
                                    ~EE 9            10 Q>>
11 EQu       ~GQio 12            13 G     E     N     E     R   A Q4 18
                                                                                                                                              ~FQ>>             ~ZQ 20 7
SEQUENTIAL                             OCCURRENCE             REPORT                       REVISION Q>>o LERIRO ACTION FUTURE Poor EVENT YEAR
                                      ~78 21          22 EFFECT
                                                              +
23 SHUTDOWN
                                                                              ~01 24 REPORT NO.
7 26 Qx 27 ATTACHMENT
                                                                                                                          ~03 28 CODE 29 NPRDX TYPE
                                                                                                                                                +L 30 PRIME COMP.
Q 31 NO.
QO 32 COMPONENT TAKEN ACTION                     ON PLANT           METHOD                 HOURS 022           SUBMITTED           FORM SUB.         SUPPLIER             MANUFACTURER I A IQ>s ~2Q>e                     ~ZQoo             ~ZQ>>             0     0     0     0             N   Qoo       ~NQoo             ~AQos               S   2 33           34                   35               36             37                     40       41               42                 43               44             47 cAUsE DEscRIPTIQN AND coRREGTIYE AGTIQNs 027 o       This condition                   was     the result of           a   water su             1     ho             c eanin           e The Supervisor responsible                               for this .cleanin                   has been         instructed not to                     use     ressur ized water .cleaning equipment in the                                 vicinity of             any     electrical panels                 ~ ~
3 4
80 7
  ~l5 8   9 FACILITY STATUS
              ~EQ28            ~IO
                                    % POWER 0    Qoo      N/A OTHER STATUS     0       METHOD OF DISCOVERY
                                                                                                  ~aQ31                  N/A DISCOVERY DESCRIPTION Q32 7       8   9               10                 12                                     44       45            46                                                                      80 ACTIVITY CONTENT RELEASED OF RELEASE                             AMOUNT OF ACTIVITY     Q                                                    LOCATION OF RELEASE          Q 6     ~Z       Q33     ~ZQ34                 N   A                                                    N  A 7     8     9               10             11                                         44             45                                                                              80 PERSONNEL EXPOSURES NUMBER               TYPE           DESCRIPTION 039
  ~l7 ~00                     0     Q>>         ZQs 13 NA 80 7       8     9               11       12 PERSONNEL INJURIES NUMBER               DESCRIPTIONQ41
              ~00           0     Qoo 12 NA 80 7       8   9                 11 LOSS OF OR DAMAGE TO FACILITY                 43 TYPE       DESCRIPTION 6         Z   Q42       N   A 8   9           10                                                                                                                                                           80 PUBLICITY                                                                                                                                         NRC USE ONI Y o
ISSUED       DESCRIPTION N/A Q                                                                                                                                             o
              ~Z 044                                                                                                                                                                         r 10                                                                                                                         68    69                          80' 8    9 0
David G. Mizner                                                      PHQNE 616-465-5901 NAME QF PREPARER
 
  ~ J 4
C
 
NRC FORM 366                                                                                                                            U. S. NUCLEAR REGULATORY COMMISSION (7.77) s LICENSEE EVENT REPORT CONTROL BLOCK:                                                     Ql                 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION1 1                                 6
  ~oi 7        8    9 M     10         C LICENSEE CODE C     1 14 Qo 15 0     0 0     0     0     0 LICENSE NUMBER 0     0     0     0     OQo 25      26 4     1     1 LICENSE TYPE 1     I 30 Qs~Qs 57 CAT 58 CON'T KDi 7
soos~L'..Qs                   0     5     0     0 03         1   5     Qo           2                           QB       0     3     1     7   7     8 QB 8                       60             61             DOCKET NUMBER               68     69       EVENT DATE               74       75       REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES                                 Q10
  ~O2                 Durin         normal o             erations,         Ft/I0-212, the motor o crated                           auxiliar             feed       um     dischar     e valve for             (51   S/6,'ailed to               shut from the Control                       Room.         This constituted degradation
  ~o4                 of   an   operable flow path required by Technical Specification 3.7.1.2.                                                                       The   failure
  ~os                 did not present                     a   substantial safety hazard since the'valve failed in the safest (ful
  ~06                 o en           osition           and redundant             auxiliar           feed     s stems         were o erable.                   This is the.         first
  ~o     7           event of           this nature at the lant.
  ~OB 7         8 9                                                                                                                                                                               80 SYSTEM               CAUSE       CAUSE                                                             COMP.           VALVE CODE                 CODE       SUBCODE                   COMPONENT CODE                       SUBCODE           SUBCODE
  ~OS                                  ~CH             Q>>         8 Q>>     ~C     Q13         V     A     L     V     0     P   Qls     ~AQls           ~Z     Qls 7        8                          9           10           11           12               13                                 18         19               20 SEQUENTIAL                             OCCURRENCE             REPORT                         REVISION Q>>
LER/RO os ACTION FUTURE osr EVENT YEAR
                                        ~78 21          22 EFFECT
                                                                +
23 SHUTDOWN
                                                                              ~01 24 REPORT NO.
8 26
                                                                                                        +w 27
                                                                                                                          ~03 28 ATTACHMENT CODE 29 NPRDR
                                                                                                                                                +L TYPE 30 Q
PRIME COMP.
31 NO.
                                                                                                                                                                                +0 32 COMPONENT TAKEN ACTION                     ON PLANT           METHOD                   HOURS Q22         SUBMITTED           FORM SUB.         SUPPLIER             MANUFACTURER
                  ~EQls ~ZQo                       ~ZQoo             ~ZQ>>               0     0     0   0           N   Qos       ~NQos             ~AQos             ..L   3   0   0   Qos 33           34                   35                 36             37                     40     41                 42                 43               44               47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o           FMO-212         failed to             o   crate     due     to   a loose screw at an electrical connection. in. the..
valve's motor                 o   erator control circuit. This connection                                         was       robabl         not   ti   htened during         initial installation,                       although previous operations with                                     FMO-212 were             success-3             ful .       The       1 pose       screw'as         ti   htened and subse uent                       retest       was       sati sfactory.               No other connections were found to be loose and no                                           further actions are                         1 armed.
7         8     9                                                                                                                                                                           80 FACILITY STATUS E   Qs       ~l0
                                    ~
                                    % POWER 0 Qs OTHER STATUS N/A
                                                                                        ~
                                                                                        ~3P      METHOD OF DISCOVERY
                                                                                                    ~AQol            Operator observation DISCOVERY DESCRIPTION Q32 7       8     9               10                 12       13                             44       45         46                                                                         80 ACTIVITY CONTENT RELEASED OF RELEASE
                ~z      Q ~zs                      ~ A AMOUNT OF ACTIVITY       ~                             N  A LOCATION OF RELEASE         Q 7       8     9               10                                                         44            45                                                                               80 PERSONNEL EXPOSURES NUMBER               TYPE         DESCRIPTION Q39 7        8
                ~00 9
0 Q>>~Z:.Qss 11       12           13                                                                                                                                 80 PERSONNEL INJURIES NUMBER               DESCRIPTIONQ41 7        8
                ~00 9
0 Qo 11        12 NA 80 LOSS OF OR DAMAGE TO FACILITY TYPE        DESCRIPTION                      Q43 zQ-                vA 7        8    9            10                                                                                                                                                            80 PUBLICITY DESCRIPTION        ~S                                                                                                                    NRC  USF. ONLY ISSUED                                                                                                                                                                            ~s ss a
O        LILtQ44 7        8    9            10                                                                                                                        68    69                            80 ~ a Michael S. Brown                                                                  616-465-5901                              0 a
NAME OF PREPARER                                                                                            PHONE:                                                  ss}}

Latest revision as of 18:53, 20 October 2019

LER 1978-017-03L & LER 1978-018-03L Re Failure of Inverter Power Supply
ML18219C209
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 03/17/1978
From: Shaller D
Indiana Michigan Power Co
To: James Keppler
NRC/RGN-III
References
LER 1978-017-03L, LER 1978-018-03L
Download: ML18219C209 (7)


Text

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REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS) t DISTRIBUTION FOR INCOMING MATERIAL 50-315 J REC: KEPPLER J G ORG: SHALLER D V DOCDATE: 03/17/78 NRC IN 4 MI PWR DATE RCVD: 03/22/78 DOCTYPE: LETTER NOTARIZED: NO COPIES RECEIVED

SUBJECT:

LTR 1 ENCL 1 LICENSEE EVENT REPT <RO 50-315/78-017/03L-0) ON 02/15/78 CONCERNING WATER SPRAYED INTO THE INVERTOR FOR THE CD DIESEL GENERATOR SPEED GOVENOR RESULTED IN FAILURE QF THE INVERTER POWER SUPPLY... W/ATT LER 78-018/03L-0.

PLANT NAME: COOK UNIT 1 REVIEWER INITIAL: X JM DISTRIBUTOR INITIAL:

DISTRIBUTION OF THIS MATERIAL IS AS FOLLOWS INCIDENT REPORTS (DISTRIBUTION CQDE A002)

FOR ACTION: BR CHIEF b ENCER++W/4 ENCL INTERNAL: EG FILE44W NRC PDR++W/ENCL NCL MIPC4+Wf3 .ENCL SCHROEDER/I PPOL I TO++W/ENCL HGUSTON++W/ENCL NGVAI<fCHECK+4EWlENCL GR IMES4 +W/ENCL KNIGHT+~W/ENCL BUTLER++W/ENCL IHAIWAUER+4W/ENCL TEDESCO~~W/ENCL EI SENHUT++W/ENCL BAER++W/ENCL SHAG~~~~W/ ENCL VOLLMER/BUNCH++W/ENCL KREGERl J. COLL I NS++W/ENCL ROSA++W/ENCL K SEYFRIT/ IE++WfENCL EXTERNAL: LPDR'S ST. JOSEPH'I ++W/ENCL TIC4~+WfENCL NS I C+~W/ENCL ACRS CAT B4+Wf 16 ENCL COPIES NOT SUBMITTED PER REGULATORY GUIDE 10.1 DISTRIBUTION: LTR 45 ENCL 45 CONTROL NBR: 78083007 SIZE: lP+iP+iP THE END

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~erleen Itteotrla lower dO'ONALD QSCd C. COOK NUCLEAR PLANT P.O. Box 458, Bridgman, Michigan 49106 March 17, 1978 Mr., J. G. Keppler, Regional Director .

Office of In specti on and Enforcement United States Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Operating License DPR-58 Docket No. 50-315

Dear Mr. Keppler:

Pursuant to the requirements of Appendix A..Technical Specifications the following reports are submitted:

RO 78-017/03L-0 RO 78-018/03L-O Since rely, D. V. Shaller Plant Manager

/pk cc: J. E. Dolan R. W. Jurgensen G. E. Lien R. Kilburn R. J. Vollen BPI K. R. Baker RO:III R. C. Callen MPSC P. W. Steketee, Esq.

R. Walsh, Esq.

G. Charnoff, Esq.

G. Olson J. M. Hennigan PNSRC J. F. Stietzel Dir', IE (30 copies)

Dir., MIPC (3 copies) pf

~r f

P t

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't n

NRC FORM 386 U. S. NUCLEAR REGULATORY COMMISSION (7.77) o J e LICENSEE EVENT REPORT oeCONTROL BLOCK: (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

I 6

~o1

'7 M I D C C 1 14 Q2 15 0 0 0 0 0 0 0 LICENSE NUMBER 0 0 0 OQo4 25 26 1 1 1 LICENSE TYPE 1

30 Q4~Qs 57 CAT 58 8 9 LICENSEE CODE CON'T

[oot) "o,~LOs0 60 61 G 0 0 0 DOCK ET NUMBE R 3 1 5 68 Oo 69 EVENT DATE 74 QB 75 0 3 1 REPORT DATE 7

80 QB EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10

~o~ Iiater s ra ed into the inver ter for the CD D'

~O3 in failure of the inverter power supply. The inverter was switched to the alternate power source and the engine was tested. The Diesel was inoperable for 36 minutest

~OS This is the first occurrence of this type.

~OB

~O7

~OB 80 7 8

'9 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~OS 8

~EE 9 10 Q>>

11 EQu ~GQio 12 13 G E N E R A Q4 18

~FQ>> ~ZQ 20 7

SEQUENTIAL OCCURRENCE REPORT REVISION Q>>o LERIRO ACTION FUTURE Poor EVENT YEAR

~78 21 22 EFFECT

+

23 SHUTDOWN

~01 24 REPORT NO.

7 26 Qx 27 ATTACHMENT

~03 28 CODE 29 NPRDX TYPE

+L 30 PRIME COMP.

Q 31 NO.

QO 32 COMPONENT TAKEN ACTION ON PLANT METHOD HOURS 022 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER I A IQ>s ~2Q>e ~ZQoo ~ZQ>> 0 0 0 0 N Qoo ~NQoo ~AQos S 2 33 34 35 36 37 40 41 42 43 44 47 cAUsE DEscRIPTIQN AND coRREGTIYE AGTIQNs 027 o This condition was the result of a water su 1 ho c eanin e The Supervisor responsible for this .cleanin has been instructed not to use ressur ized water .cleaning equipment in the vicinity of any electrical panels ~ ~

3 4

80 7

~l5 8 9 FACILITY STATUS

~EQ28 ~IO

% POWER 0 Qoo N/A OTHER STATUS 0 METHOD OF DISCOVERY

~aQ31 N/A DISCOVERY DESCRIPTION Q32 7 8 9 10 12 44 45 46 80 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY Q LOCATION OF RELEASE Q 6 ~Z Q33 ~ZQ34 N A N A 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION 039

~l7 ~00 0 Q>> ZQs 13 NA 80 7 8 9 11 12 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41

~00 0 Qoo 12 NA 80 7 8 9 11 LOSS OF OR DAMAGE TO FACILITY 43 TYPE DESCRIPTION 6 Z Q42 N A 8 9 10 80 PUBLICITY NRC USE ONI Y o

ISSUED DESCRIPTION N/A Q o

~Z 044 r 10 68 69 80' 8 9 0

David G. Mizner PHQNE 616-465-5901 NAME QF PREPARER

~ J 4

C

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7.77) s LICENSEE EVENT REPORT CONTROL BLOCK: Ql (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION1 1 6

~oi 7 8 9 M 10 C LICENSEE CODE C 1 14 Qo 15 0 0 0 0 0 0 LICENSE NUMBER 0 0 0 0 OQo 25 26 4 1 1 LICENSE TYPE 1 I 30 Qs~Qs 57 CAT 58 CON'T KDi 7

soos~L'..Qs 0 5 0 0 03 1 5 Qo 2 QB 0 3 1 7 7 8 QB 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10

~O2 Durin normal o erations, Ft/I0-212, the motor o crated auxiliar feed um dischar e valve for (51 S/6,'ailed to shut from the Control Room. This constituted degradation

~o4 of an operable flow path required by Technical Specification 3.7.1.2. The failure

~os did not present a substantial safety hazard since the'valve failed in the safest (ful

~06 o en osition and redundant auxiliar feed s stems were o erable. This is the. first

~o 7 event of this nature at the lant.

~OB 7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~OS ~CH Q>> 8 Q>> ~C Q13 V A L V 0 P Qls ~AQls ~Z Qls 7 8 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION Q>>

LER/RO os ACTION FUTURE osr EVENT YEAR

~78 21 22 EFFECT

+

23 SHUTDOWN

~01 24 REPORT NO.

8 26

+w 27

~03 28 ATTACHMENT CODE 29 NPRDR

+L TYPE 30 Q

PRIME COMP.

31 NO.

+0 32 COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER

~EQls ~ZQo ~ZQoo ~ZQ>> 0 0 0 0 N Qos ~NQos ~AQos ..L 3 0 0 Qos 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o FMO-212 failed to o crate due to a loose screw at an electrical connection. in. the..

valve's motor o erator control circuit. This connection was robabl not ti htened during initial installation, although previous operations with FMO-212 were success-3 ful . The 1 pose screw'as ti htened and subse uent retest was sati sfactory. No other connections were found to be loose and no further actions are 1 armed.

7 8 9 80 FACILITY STATUS E Qs ~l0

~

% POWER 0 Qs OTHER STATUS N/A

~

~3P METHOD OF DISCOVERY

~AQol Operator observation DISCOVERY DESCRIPTION Q32 7 8 9 10 12 13 44 45 46 80 ACTIVITY CONTENT RELEASED OF RELEASE

~z Q ~zs ~ A AMOUNT OF ACTIVITY ~ N A LOCATION OF RELEASE Q 7 8 9 10 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39 7 8

~00 9

0 Q>>~Z:.Qss 11 12 13 80 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41 7 8

~00 9

0 Qo 11 12 NA 80 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION Q43 zQ- vA 7 8 9 10 80 PUBLICITY DESCRIPTION ~S NRC USF. ONLY ISSUED ~s ss a

O LILtQ44 7 8 9 10 68 69 80 ~ a Michael S. Brown 616-465-5901 0 a

NAME OF PREPARER PHONE: ss