ENS 44205: Difference between revisions

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| event date = 05/12/2008 15:00 EDT
| event date = 05/12/2008 15:00 EDT
| last update date = 05/12/2008
| last update date = 05/12/2008
| title = Shut Down Initiated Due To Inoperable Steam Generator Flow Channels  
| title = Shut Down Initiated Due to Inoperable Steam Generator Flow Channels  
| event text = This 4-hour notification is being made to report that Salem Unit 2 has initiated a manual reactor shutdown in accordance with [Technical Specification] 3.0.3. The shutdown was initiated due to all eight steam generator steam flow channels being declared inoperable at 1500 on 5/12/08.  All eight steam flow channels were indicating lower than actual steam flow such that the high steam flow coincident with low steam pressure or low-low Tave would not occur within the allowable values specified in the technical specifications.  Salem Unit 2 is currently in Mode 1. Reactor Coolant System Temperature is 551 degrees Fahrenheit with pressure @ 2235 PSIG.  Salem Unit 2 has no other shutdown Tech. Spec. action statements in effect.  Prior to the initiating event Salem Unit 2 was raising power at 1/2 % per hour after 2R16 refueling outage.
| event text = This 4-hour notification is being made to report that Salem Unit 2 has initiated a manual reactor shutdown in accordance with [Technical Specification] 3.0.3. The shutdown was initiated due to all eight steam generator steam flow channels being declared inoperable at 1500 on 5/12/08.  All eight steam flow channels were indicating lower than actual steam flow such that the high steam flow coincident with low steam pressure or low-low Tave would not occur within the allowable values specified in the technical specifications.  Salem Unit 2 is currently in Mode 1. Reactor Coolant System Temperature is 551 degrees Fahrenheit with pressure @ 2235 PSIG.  Salem Unit 2 has no other shutdown Tech. Spec. action statements in effect.  Prior to the initiating event Salem Unit 2 was raising power at 1/2 % per hour after 2R16 refueling outage.
All ECCS and ESF Systems are available.
All ECCS and ESF Systems are available.

Latest revision as of 22:14, 1 March 2018

ENS 44205 +/-
Where
Salem PSEG icon.png
New Jersey (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Time - Person (Reporting Time:+1.8 h0.075 days <br />0.0107 weeks <br />0.00247 months <br />)
Opened: Gary Meekins
20:48 May 12, 2008
NRC Officer: Pete Snyder
Last Updated: May 12, 2008
44205 - NRC Website
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