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{{#Wiki_filter:~~L 4~PHILADELPHIA GEAR CORPORATION KING OF PRUSSIA, PENN.19406 LIMITORQUE VALVE CONTROL TEST OF LIMITORQUE'ALVE OPERATOR.TO MEET GENERAL REQUIREMENTS OF AN ELECTRIC VALVE ACTUATOR IN NUCLEAR REACTOR CONTAINMENT ENVIRONMENT TEST REPORT 3'ANUARY 2, 196 9 soo EGG~gogS  
{{#Wiki_filter:~ ~
L 4~
PHILADELPHIA GEAR CORPORATION KING OF PRUSSIA, PENN. 19406 LIMITORQUE VALVE CONTROL TEST OF LIMITORQUE'ALVE OPERATOR
          .TO MEET GENERAL REQUIREMENTS OF AN ELECTRIC VALVE ACTUATOR IN NUCLEAR REACTOR CONTAINMENT ENVIRONMENT TEST REPORT 3'ANUARY 2, 196 9 soo EGG
                                                ~ gogS


TEST REPORT-JANUARY 2, 1969 ENGINEERING ORDER NO.600198 The Limitorque valve operator tested was Model SMB-0 with a 15 foot: pound, 3 phase, 60 cycle, 440 volt motor, w~ith s eg~~igh temperature motor insulation and high temperature resistant non-\,e~r~~~~W metallic components, to withstand the~contemplated steam pressure, high temperature and chemical conditions expected.in.the event of a nuclear reactor failure.within.the,.containment vessel.The Limitorque.
TEST REPORT JANUARY               2, 1969 ENGINEERING ORDER NO.               600198 The   Limitorque valve operator tested                 was Model SMB-0     with a 15   foot: pound,   3 phase, 60   cycle,   440       volt motor,   w~ith s eg~~igh temperature motor insulation     \
operator was wired for a torque seating control for closing direction and position limiting control for open direction.
and ,e high
'I A 2 3/8" diameter by 1/4" pitch, 1/4" lead, left hand stem was used to simulate the stem of a valve being opened and closed The speed of operation was approximately 6" per minute over a 12" travel.L The designed seating thrust to be exerted on the.stem by the Limitorque valve control was 16,500 pounds of thrust in the closed position of the valve stem.A slide wire electric position trans-mitter.was also installed and connected to a remote position receiver outside the test chamber.TESTS TO BE PERFORMED ON OPERATOR 1.Preliminary heat tests on component parts.2.Preliminary heat tests on actuator.3.Preliminary live steam test on actuator.4.Heat aging test of electric motor and electric motor with brake.  
                                              ~ r ~
temperature resistant non-
                                                                            ~       ~ ~ W metallic     components,   to withstand the contemplated steam pressure,
                                                      ~
high temperature and chemical conditions expected .in. the event of a   nuclear reactor failure. within. the,.containment vessel.                     The Limitorque. operator was wired for             a     torque seating control for closing direction and position limiting control for open direction.
                                                                                  'I A 2   3/8" diameter by 1/4" pitch, 1/4" lead,                     left hand stem was used to simulate the       stem of a   valve being opened and closed                 The speed of operation     was approximately 6" per minute over a 12"                     travel.
L The designed     seating thrust to be exerted on the .stem by the Limitorque valve control was 16,500 pounds of thrust in the closed position of the valve stem.           A slide wire electric position trans-mitter   .was also installed and connected to                 a remote position receiver outside the test chamber.
TESTS TO BE PERFORMED ON OPERATOR
: 1.     Preliminary heat tests       on component           parts.
: 2. Preliminary heat tests         on actuator.
: 3. Preliminary live steam test           on     actuator.
: 4. Heat aging     test of electric motor               and electric   motor with brake.
: 5. Shock and  vibration test of actuator to simulate seismic conditions.
: 6. l50 life cycle test  of actuator producing approximately 16,500 pounds  of thrust.
7', Test of Limitorque valve operator and    electric  brake motor under  a  simulated reactor containment post-accident steam and chemical environment.
: l. PRELIMINARY HEAT TESTS ON COMPONENT PARTS The standard    Limitorque operator geared      limit switch    and torque switch was subjected to        a dry heat test for approxi-mately  16  hours at  a  temperature of 375'F.      Periodically during this test, the switches were removed from the oven and actuated by hand. The operation was satisfactory and no mal-occurred. All parts  functioned freely and there      was 'unctions no  binding, jamming, nor abnormal distortion of .parts.            The test  was  successful in    all respects.
: 2. ~  PRELIMINARY HEAT TESTS ON ACTUATOR A completely assembled and operational Limitorque operator was placed. in  an oven where  the temperature    was  maintained at approximately 325'F. for      a duration of    12 hours. The  unit  was electrically    operated every  thirty minutes for    a  period of approximately two minutes per cycle and using the geared            limit switches to stop the actuator at the          full open  and  full closed position of travel.        Indicating light circuits    were also wired
    .to the geared limit switches.
The  test  was  successful in every respect.        There were no malfunctions of the operator and upon inspection of the com--
ponen't parts used,    there  was no  noticeable deterioration or wear.
The  lubricant    used  in  he geared  limit switch did    become hard and caked, however the lubricant used in the Limitorque


5.Shock and vibration test of actuator to simulate seismic conditions.
gear housing remained      pliable    and had  its original consistency.
6.l50 life cycle test of actuator producing approximately 16,500 pounds of thrust.7', Test of Limitorque valve operator and electric brake motor under a simulated reactor containment post-accident steam and chemical environment.  
It was  determined that the grease        in the geared limit switch gear housing should be changed to the          same  grease as in the Limitorque operator gear housing.
3'.. PRELIMINARY LIVE STEPS TEST ON ACTUATOR
        ~
A complete Limitorque actuator was set up          for electrical operation and live steam      was piped    into the conduit taps      on the top of the    limit switch      compartment. One  of the bottom conduit taps    was  left  open  to drain off    any condensate. The operator  was  set up on  a  timer basis for operation over        a  period of approximately nine hours        and  operating every    thirty minutes for  two minutes per cycle.       During  this test, the live steam in the switch compartment        seemed  to have no effect whatever on the function of the. limit switches in'heir control of          the operator at the    full. open  and  full closed    position of travel.
In addition, the    limit switches    were wired up    to indicating lights which operated satisfactorily.
The test was successful and there          was no  noticeable effect on  the function of any of the parts in the          limit switch  com-partment.
: 4. HEAT AGING TEST. OF ELECTRIC MOTOR AND ELECTRIC MOTOR WITH BRAKE The  electric motor for the Limitorque operator to be used in the environment test and another electric motor equipped with a disk type brake were sub'jected to a heat aging test.


l.PRELIMINARY HEAT TESTS ON COMPONENT PARTS The standard Limitorque operator geared limit switch and torque switch was subjected to a dry heat test for approxi-mately 16 hours at a temperature of 375'F.Periodically during this test, the switches were removed from the oven and actuated by hand.The operation was satisfactory and no mal-'unctions occurred.All parts functioned freely and there was no binding, jamming, nor abnormal distortion of.parts.The test was successful in all respects.2.~PRELIMINARY HEAT TESTS ON ACTUATOR A completely assembled and operational Limitorque operator was placed.in an oven where the temperature was maintained at approximately 325'F.for a duration of 12 hours.The unit was electrically operated every thirty minutes for a period of approximately two minutes per cycle and using the geared limit switches to stop the actuator at the full open and full closed position of travel.Indicating light circuits were also wired.to the geared limit switches.The test was successful in every respect.There were no malfunctions of the operator and upon inspection of the com--ponen't parts used, there was no noticeable deterioration or wear.The lubricant used in he geared limit switch did become hard and caked, however the lubricant used in the Limitorque  
Both  electric motors were sent to Reliance, Electric Co. for heat age testing. This test consisted of baking the motors at a temperature of 180'C. for a total of 100 hours to simulate aging the motor to a 40 year        life expectancy. Motor insulation checks were. made and found. to.be      within normal limits. There
    . were no adverse    effects  on the motors and motor    insulation resi'stance measured    'infinity to  ground.
5.. SHOCK AND VIBRATION TEST OF ACTUATOR TO SIMULATE          SEISMIC CONDITIONS The Limitorque operator to be used in the environment test was shipped complete      to the  Lockheed  Electronics Co., in Plain-.
field,  New  Jersey,  for  shock and  vibration testing to simulate seismic conditions.       A copy  of this report is enclosed herewith.
The  test basically consisted of mounting the Limitorque operator on a shock and vibration table to test it at '20 cycles per second vibration at. 1G load for a period of two minutes on one minute off. This would constitute one cycle. The cycle was repeated five times in both the vertical and horizontal axis of the operator.       The  actual test report  and photographs are included here.
The test   was successful and there     was no noticeable effect whatsoever on the Limitorque operator.


gear housing remained pliable and had its original consistency.
  , ~
It was determined that the grease in the geared limit switch gear housing should be changed to the same grease as in the Limitorque operator gear housing.3'..PRELIMINARY LIVE STEPS TEST ON ACTUATOR~A complete Limitorque actuator was set up for electrical operation and live steam was piped into the conduit taps on the top of the limit switch compartment.
        ~
One of the bottom conduit taps was left open to drain off any condensate.
      ~
The operator was set up on a timer basis for operation over a period of approximately nine hours and operating every thirty minutes for two minutes per cycle.During this test, the live steam in the switch compartment seemed to have no effect whatever on the function of the.limit switches in'heir control of the operator at the full.open and full closed position of travel.In addition, the limit switches were wired up to indicating lights which operated satisfactorily.
6 ~ 150 LIFE CYCLE TEST OF LIMITORQUE OPERATOR PRODUCING APPROXIMATELY 16,500 POUNDS THRUST The Limitorque operator     was shipped   to the Franklin Institute Research Laboratories,       Philadelphia, Pennsylvania.
The test was successful and there was no noticeable effect on the function of any of the parts in the limit switch com-partment.4.HEAT AGING TEST.OF ELECTRIC MOTOR AND ELECTRIC MOTOR WITH BRAKE The electric motor for the Limitorque operator to be used in the environment test and another electric motor equipped with a disk type brake were sub'jected to a heat aging test.
The operator was mounted on a stand       inside the test chamber and a 150 cycle load test     was made on   the unit. This   test consisted of stroking the     2 3/8" diameter valve stem     a total of approximately   12 inches in two minutes.       The valve stem in the full closed   position produced     a thrust of   16,500 pounds on a rigid plate securely bolted to       the test chamber.     The thrust was measured   by the   same strain-gauge recording instru-ment used   in the actual environmental test conducted by the Franklin Institute.     The unit was wired up so that the closing (y.           direction and the open   position geared limit switch stopped the unit in the   full open   position. The speed   of. travel was 6 inches per minute.
 
After the   life cycle   testing   was completed,   the unit   was inspected and -found to be in excellent condition.           There was no noticeable wear   on any of the parts.
Both electric motors were sent to Reliance, Electric Co.for heat age testing.This test consisted of baking the motors at a temperature of 180'C.for a total of 100 hours to simulate aging the motor to a 40 year life expectancy.
I The same   electric motor which had been heat age tested at Reliance Electric Co.
Motor insulation checks were.made and found.to.be within normal limits.There.were no adverse effects on the motors and motor insulation resi'stance measured'infinity to ground.5..SHOCK AND VIBRATION TEST OF ACTUATOR TO SIMULATE SEISMIC CONDITIONS The Limitorque operator to be used in the environment test was shipped complete to the Lockheed Electronics Co., in Plain-.field, New Jersey, for shock and vibration testing to simulate seismic conditions.
was used for this life Cycle test.         There was no noticeable adverse effect on the electric motor and it. functioned properly.
A copy of this report is enclosed herewith.The test basically consisted of mounting the Limitorque operator on a shock and vibration table to test it at'20 cycles per second vibration at.1G load for a period of two minutes on one minute off.This would constitute one cycle.The cycle was repeated five times in both the vertical and horizontal axis of the operator.The actual test report and photographs are included here.The test was successful and there was no noticeable effect whatsoever on the Limitorque operator.
: 7. TEST OF LIMITORQUE VALVE OPERATOR UNDER SIMULATED 'REACTOR CONTAINMENT POST-ACCIDENT STEAM AND CHEMICAL ENVIRONMENT The attached report of the Franklin         Institute Research Laboratories describes the       actual testing under this environ-
 
,~~~6~150 LIFE CYCLE TEST OF LIMITORQUE OPERATOR PRODUCING APPROXIMATELY 16,500 POUNDS THRUST The Limitorque operator was shipped to the Franklin Institute Research Laboratories, Philadelphia, Pennsylvania.
The operator was mounted on a stand inside the test chamber and a 150 cycle load test was made on the unit.This test consisted of stroking the 2 3/8" diameter valve stem a total of approximately 12 inches in two minutes.The valve stem in the full closed position produced a thrust of 16,500 pounds on a rigid plate securely bolted to the test chamber.The thrust was measured by the same strain-gauge recording instru-ment used in the actual environmental test conducted by the Franklin Institute.
The unit was wired up so that the closing (y.direction and the open position geared limit switch stopped the unit in the full open position.The speed of.travel was 6 inches per minute.After the life cycle testing was completed, the unit was inspected and-found to be in excellent condition.
There was no noticeable wear on any of the parts.The same electric I motor which had been heat age tested at Reliance Electric Co.was used for this life Cycle test.There was no noticeable adverse effect on the electric motor and it.functioned properly.7.TEST OF LIMITORQUE VALVE OPERATOR UNDER SIMULATED'REACTOR CONTAINMENT POST-ACCIDENT STEAM AND CHEMICAL ENVIRONMENT The attached report of the Franklin Institute Research Laboratories describes the actual testing under this environ-  


w mental condition.
w mental condition.
After the test.was completed, the Limitorque operator was shipped back to Philadelphia Gear Corporation, King of Prussia,'ennsylvania where it was disassembled and all.parts were inspected.'hotographs are included showing the various-parts of the operator.All parts, including the electric motor, slide were position'ransmitter,.
After the test. was completed,     the Limitorque operator was shipped back   to Philadelphia     Gear Corporation, King     of Prussia,'ennsylvania       where it was disassembled   and all. parts were   inspected.'hotographs       are included showing the various
seals, bearings, gears, and shafts, were inspected and no noticeable wear was noted.However, the gear frame.of the geared limit.switch had corroded and caused a minor failure.The geared limit switch frame had been attacked by the boric acid in the steam atmosphere.
  - parts of the operator.       All parts, including     the electric motor, slide were     position'ransmitter,. seals, bearings, gears, and shafts, were inspected and no noticeable wear was noted. However, the gear frame .of the geared       limit. switch had corroded and caused a minor         failure.
This caused the gear frame to corrode and..resulted in binding, up of the shafts of the geared limit switch where they extend through the geared limit switch housing.This caused the malfunction of the switch as described in the Franklin Institute Research Labor-atories'eport.
The geared limit switch     frame had been attacked by the boric acid in the     steam atmosphere.       This caused the gear frame to corrode and..resulted in binding,     up of the shafts of the geared limit switch     where they extend through the geared limit switch   housing. This caused the malfunction of the switch as described in the Franklin         Institute Research   Labor-atories'eport.       A material change     has been instituted to correct this corrosive action of the material used in that particular switch. On all present 'orders being processed, and on all future units to     be shipped   to meet environmental conditions such   as this, the   gear frame housing of the geared
A material change has been instituted to correct this corrosive action of the material used in that particular switch.On all present'orders being processed, and on all future units to be shipped to meet environmental conditions such as this, the gear frame housing of the geared'limit switch will be a bronze material which is not subject l to corrosion by boric acid solutions.
    'limit switch will be     a bronze material which     is not subject l
The motor insulation resistance after all testing was 1,000 megohms across all'three motor terminals to ground at 500 volts.}}
to corrosion   by boric acid solutions.       The motor   insulation resistance after   all testing     was 1,000 megohms across     all
    'three motor terminals to ground at         500 volts.}}

Latest revision as of 08:07, 30 October 2019

Rept Re Limitorque Valve Operator Test for Meeting General Requirements of Electrical Valve Actuator in Nuclear Reactor Containment Environ.Prepared by Philadelphia Gear Corp
ML17053A853
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 01/02/1969
From:
FRANKLIN INSTITUTE
To:
Shared Package
ML17053A854 List:
References
NUDOCS 7907300160
Download: ML17053A853 (16)


Text

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L 4~

PHILADELPHIA GEAR CORPORATION KING OF PRUSSIA, PENN. 19406 LIMITORQUE VALVE CONTROL TEST OF LIMITORQUE'ALVE OPERATOR

.TO MEET GENERAL REQUIREMENTS OF AN ELECTRIC VALVE ACTUATOR IN NUCLEAR REACTOR CONTAINMENT ENVIRONMENT TEST REPORT 3'ANUARY 2, 196 9 soo EGG

~ gogS

TEST REPORT JANUARY 2, 1969 ENGINEERING ORDER NO. 600198 The Limitorque valve operator tested was Model SMB-0 with a 15 foot: pound, 3 phase, 60 cycle, 440 volt motor, w~ith s eg~~igh temperature motor insulation \

and ,e high

~ r ~

temperature resistant non-

~ ~ ~ W metallic components, to withstand the contemplated steam pressure,

~

high temperature and chemical conditions expected .in. the event of a nuclear reactor failure. within. the,.containment vessel. The Limitorque. operator was wired for a torque seating control for closing direction and position limiting control for open direction.

'I A 2 3/8" diameter by 1/4" pitch, 1/4" lead, left hand stem was used to simulate the stem of a valve being opened and closed The speed of operation was approximately 6" per minute over a 12" travel.

L The designed seating thrust to be exerted on the .stem by the Limitorque valve control was 16,500 pounds of thrust in the closed position of the valve stem. A slide wire electric position trans-mitter .was also installed and connected to a remote position receiver outside the test chamber.

TESTS TO BE PERFORMED ON OPERATOR

1. Preliminary heat tests on component parts.
2. Preliminary heat tests on actuator.
3. Preliminary live steam test on actuator.
4. Heat aging test of electric motor and electric motor with brake.
5. Shock and vibration test of actuator to simulate seismic conditions.
6. l50 life cycle test of actuator producing approximately 16,500 pounds of thrust.

7', Test of Limitorque valve operator and electric brake motor under a simulated reactor containment post-accident steam and chemical environment.

l. PRELIMINARY HEAT TESTS ON COMPONENT PARTS The standard Limitorque operator geared limit switch and torque switch was subjected to a dry heat test for approxi-mately 16 hours at a temperature of 375'F. Periodically during this test, the switches were removed from the oven and actuated by hand. The operation was satisfactory and no mal-occurred. All parts functioned freely and there was 'unctions no binding, jamming, nor abnormal distortion of .parts. The test was successful in all respects.
2. ~ PRELIMINARY HEAT TESTS ON ACTUATOR A completely assembled and operational Limitorque operator was placed. in an oven where the temperature was maintained at approximately 325'F. for a duration of 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The unit was electrically operated every thirty minutes for a period of approximately two minutes per cycle and using the geared limit switches to stop the actuator at the full open and full closed position of travel. Indicating light circuits were also wired

.to the geared limit switches.

The test was successful in every respect. There were no malfunctions of the operator and upon inspection of the com--

ponen't parts used, there was no noticeable deterioration or wear.

The lubricant used in he geared limit switch did become hard and caked, however the lubricant used in the Limitorque

gear housing remained pliable and had its original consistency.

It was determined that the grease in the geared limit switch gear housing should be changed to the same grease as in the Limitorque operator gear housing.

3'.. PRELIMINARY LIVE STEPS TEST ON ACTUATOR

~

A complete Limitorque actuator was set up for electrical operation and live steam was piped into the conduit taps on the top of the limit switch compartment. One of the bottom conduit taps was left open to drain off any condensate. The operator was set up on a timer basis for operation over a period of approximately nine hours and operating every thirty minutes for two minutes per cycle. During this test, the live steam in the switch compartment seemed to have no effect whatever on the function of the. limit switches in'heir control of the operator at the full. open and full closed position of travel.

In addition, the limit switches were wired up to indicating lights which operated satisfactorily.

The test was successful and there was no noticeable effect on the function of any of the parts in the limit switch com-partment.

4. HEAT AGING TEST. OF ELECTRIC MOTOR AND ELECTRIC MOTOR WITH BRAKE The electric motor for the Limitorque operator to be used in the environment test and another electric motor equipped with a disk type brake were sub'jected to a heat aging test.

Both electric motors were sent to Reliance, Electric Co. for heat age testing. This test consisted of baking the motors at a temperature of 180'C. for a total of 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> to simulate aging the motor to a 40 year life expectancy. Motor insulation checks were. made and found. to.be within normal limits. There

. were no adverse effects on the motors and motor insulation resi'stance measured 'infinity to ground.

5.. SHOCK AND VIBRATION TEST OF ACTUATOR TO SIMULATE SEISMIC CONDITIONS The Limitorque operator to be used in the environment test was shipped complete to the Lockheed Electronics Co., in Plain-.

field, New Jersey, for shock and vibration testing to simulate seismic conditions. A copy of this report is enclosed herewith.

The test basically consisted of mounting the Limitorque operator on a shock and vibration table to test it at '20 cycles per second vibration at. 1G load for a period of two minutes on one minute off. This would constitute one cycle. The cycle was repeated five times in both the vertical and horizontal axis of the operator. The actual test report and photographs are included here.

The test was successful and there was no noticeable effect whatsoever on the Limitorque operator.

, ~

~

~

6 ~ 150 LIFE CYCLE TEST OF LIMITORQUE OPERATOR PRODUCING APPROXIMATELY 16,500 POUNDS THRUST The Limitorque operator was shipped to the Franklin Institute Research Laboratories, Philadelphia, Pennsylvania.

The operator was mounted on a stand inside the test chamber and a 150 cycle load test was made on the unit. This test consisted of stroking the 2 3/8" diameter valve stem a total of approximately 12 inches in two minutes. The valve stem in the full closed position produced a thrust of 16,500 pounds on a rigid plate securely bolted to the test chamber. The thrust was measured by the same strain-gauge recording instru-ment used in the actual environmental test conducted by the Franklin Institute. The unit was wired up so that the closing (y. direction and the open position geared limit switch stopped the unit in the full open position. The speed of. travel was 6 inches per minute.

After the life cycle testing was completed, the unit was inspected and -found to be in excellent condition. There was no noticeable wear on any of the parts.

I The same electric motor which had been heat age tested at Reliance Electric Co.

was used for this life Cycle test. There was no noticeable adverse effect on the electric motor and it. functioned properly.

7. TEST OF LIMITORQUE VALVE OPERATOR UNDER SIMULATED 'REACTOR CONTAINMENT POST-ACCIDENT STEAM AND CHEMICAL ENVIRONMENT The attached report of the Franklin Institute Research Laboratories describes the actual testing under this environ-

w mental condition.

After the test. was completed, the Limitorque operator was shipped back to Philadelphia Gear Corporation, King of Prussia,'ennsylvania where it was disassembled and all. parts were inspected.'hotographs are included showing the various

- parts of the operator. All parts, including the electric motor, slide were position'ransmitter,. seals, bearings, gears, and shafts, were inspected and no noticeable wear was noted. However, the gear frame .of the geared limit. switch had corroded and caused a minor failure.

The geared limit switch frame had been attacked by the boric acid in the steam atmosphere. This caused the gear frame to corrode and..resulted in binding, up of the shafts of the geared limit switch where they extend through the geared limit switch housing. This caused the malfunction of the switch as described in the Franklin Institute Research Labor-atories'eport. A material change has been instituted to correct this corrosive action of the material used in that particular switch. On all present 'orders being processed, and on all future units to be shipped to meet environmental conditions such as this, the gear frame housing of the geared

'limit switch will be a bronze material which is not subject l

to corrosion by boric acid solutions. The motor insulation resistance after all testing was 1,000 megohms across all

'three motor terminals to ground at 500 volts.