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| issue date = 05/26/1994
| issue date = 05/26/1994
| title = LER 94-008-00:on 940426,CROs Observed Slight Reactor Power Fluctuations on Six Aprms.Caused by Degraded Condition of Reactor Recirculation (RRC) FCV Position Transmitter. Replaced RRC FCV Position transmitters.W/940526 Ltr
| title = LER 94-008-00:on 940426,CROs Observed Slight Reactor Power Fluctuations on Six Aprms.Caused by Degraded Condition of Reactor Recirculation (RRC) FCV Position Transmitter. Replaced RRC FCV Position transmitters.W/940526 Ltr
| author name = MACKAMAN C D, PARRISH J V
| author name = Mackaman C, Parrish J
| author affiliation = WASHINGTON PUBLIC POWER SUPPLY SYSTEM
| author affiliation = WASHINGTON PUBLIC POWER SUPPLY SYSTEM
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:~ACCELERATED D STRIBUTION DEMONS ATION SYSTEM S~REGULATORY INFORMATXON DXSTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9406020024 DOC.DATE: 94/05/26 NOTARIZED:
{{#Wiki_filter:~
NO DOCKET FACIL:50-397, WPPSS Nuclear Project, Unit 2, Washington, Public Powe 05000397 AUTH.NAME AUTHOR AFFILIATION MACKAMAN,C.D.
ACCELERATED D STRIBUTION DEMONS                                     ATION SYSTEM S     ~
Washington Public Power Supply System PARRISH,J.V.
REGULATORY INFORMATXON DXSTRIBUTION SYSTEM (RIDS)
Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION
ACCESSION NBR:9406020024             DOC.DATE: 94/05/26       NOTARIZED: NO       DOCKET FACIL:50-397, WPPSS   Nuclear Project, Unit 2, Washington, Public           Powe 05000397 AUTH. NAME           AUTHOR AFFILIATION MACKAMAN,C.D.       Washington Public Power Supply System PARRISH,J.V.       Washington Public Power Supply System RECIP.NAME           RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
LER 94-008-00:on 940426,CROs observed slight reactor power fluctuations on six APRMs.Caused by degraded condition of reactor recirculation (RRC)FCV position transmitter.
LER   94-008-00:on 940426,CROs observed slight reactor power fluctuations on six APRMs.Caused by degraded condition of reactor recirculation (RRC) FCV position transmitter.
Replaced RRC FCV position transmitters.W/940526 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR L ENCL/SIZE: 7 TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES RECIPIENT ID CODE/NAME PDIV-3 PD INTERNAL: ACRS AEOD/DS P/TPAB NRR/DE/EELB NRR/DORS/OEAB NRR/DRCH/HICB NRR/DRIL/RPEB NRRggSS SPLB EG FX 02 RGN4 FI~01 EXTERNAL: EG&G BRYCE,J.H NRC PDR NSIC POORE1W~COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 RECXPIENT ID CODE/NAME CLIFFORD,J AEOD/DOA'EOD/ROAB/DSP NRR/DE/EMEB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRSS/PRPB NRR/DSSA/SRXB RES/DSIR/EIB L ST LOBBY WARD NSIC MURPHY,G.A NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 D R I D NOTE TO ALL"RIDS" RECIPIENTS:
Replaced RRC FCV position transmitters.W/940526 ltr.
D D PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 28 ENCL 28 WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O.Box 968~3000 George Washington Way~Richland, Washington 99352 May 26, 1994 G02-94-125 Docket No.50-397 Document Control Desk U.S.Nuclear Regulatory Commission Washington, D.C.20555  
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR               L TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
ENCL  / SIZE: 7 NOTES RECIPIENT               COPIES          RECXPIENT            COPIES ID CODE/NAME             LTTR ENCL      ID  CODE/NAME      LTTR ENCL PDIV-3 PD                   1    1    CLIFFORD,J              1    1            D INTERNAL: ACRS                           1    1                              1    1 AEOD/DOA'EOD/ROAB/DSP AEOD/DS P/TPAB             1    1                              2    2 NRR/DE/EELB                 1    1    NRR/DE/EMEB              1    1 NRR/DORS/OEAB               1    1    NRR/DRCH/HHFB            1    1 NRR/DRCH/HICB               1    1    NRR/DRCH/HOLB            1    1 NRR/DRIL/RPEB               1    1    NRR/DRSS/PRPB            2    2 NRRggSS   SPLB             1    1    NRR/DSSA/SRXB            1    1 EG   FX           02       1    1    RES/DSIR/EIB            1    1 RGN4     FI~     01        1    1 EXTERNAL: EG&G BRYCE,J.H                 2     2     L ST LOBBY WARD          1   1 NRC PDR                    1     1     NSIC MURPHY,G.A         1   1 NSIC POORE1W    ~          1     1     NUDOCS FULL TXT          1   1 R
I D
D D
NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR             28   ENCL       28
 
WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ 3000 George Washington Way ~ Richland, Washington 99352 May 26, 1994 G02-94-125 Docket No. 50-397 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555


==Subject:==
==Subject:==
NUCLEAR PLANT WNP-2, OPERATING LICENSE NPF-21 LICENSEE EVENT REPORT NO.94-008-00 Transmitted herewith is Licensee Event Report No.94-008-00 for the WNP-2 Plant.This report is submitted in response to the reporting requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrence.
NUCLEAR PLANT WNP-2, OPERATING LICENSE NPF-21 LICENSEE EVENT REPORT NO. 94-008-00 Transmitted herewith is Licensee Event Report No. 94-008-00 for the WNP-2 Plant. This report is submitted in response to the reporting requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrence.
Should you have any questions or desire additional information, please call me or D.A.Swank at (509)377-4563.Sincerely, J.Parrish (Mail Drop 1023)Assistant Managing Director, Operations JVP/CDM/my Enclosure CC: LJ Callan, NRC-RIV KE Perkins, Jr., NRC RIV, Walnut Creek Field Office NS Reynolds, Winston&Strawn NRC Sr.Resident Inspector (Mail Drop 927N, 2 Copies)INPO Records Center-Atlanta, GA DL Williams, BPA (Mail Drop 399)9406020024 940526 PDR ADOCK 05000397 8"'DR LICENSEE EVEIOREPORT (LER)ACILITY NAME (1)Washin ton Nuclear Plant-Unit 2 DOCKET NUMB R ()PAGE (3)0 5 0 0 0 3 9 7 I OF ITLE (4)MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS EVENT DATE 5 MONTH DAY YEAR LER NUMBER SEQUENTIAL NUMBER 6)AA EVI SION UMBER REPORT DATE (7)MONTH DAY YEAR FACILITY NAMES CKE 50 OTHER FACILITIES INVOLVED 8 NUMB 0 0 R (5)0 4 26 94 9 4 00 8 0 0 0 5 2 6 9 4 5 0 00 P ERAT ING ODE (9)MIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or more of the following)(ll)I OWER LEVEL (10)20.402(b)20.405(a)(1)(i) 0.405(a)(1)(ii) 20.405(a)(1)(iii) 20.405(a)(1)(iv) 20.405(a)(1)(v) 20.405(C)50.36(c)(1) 50.36(c)(2) 50.73(a)(2)(i) 50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 50.73(a)(2)(x) 77.71(b)73.73(c)THER (Specify in Abstract elow and in Text, NRC orm 366A)LICENSEE CONTACT FOR THIS LER 12 C.D.Mackaman, Licensing Engineer TELEPHONE NUMBER REA CODE 5 0 9 7 7-4 4 5 1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IH THIS REPORT (13)CAUSE SYSTEM COMPOHEHT MANUFACTURER EPORTABLE jc:,.',4::",;Qh;CAUSE SYSTEM COMPONENT MAHUFACTURER EPORTABLE TO NPRDS BD A D 0 5 2 SUPPLEMENTAL REPORT EXPECTED (14)YES (If yes, cTNpiete EXPECTED SUBMISSIOH DATE)X NO TRACY IIeI EXPECTED SUSHI SSI OH MONTH DA'Y TEAR ATE (15)At 1010 hours on April 26, 1994, with the plant at 50%reactor power and 55%core flow, plant Control Room Operators (CROs)observed slight reactor power fluctuations on the six average power range monitors (APRMs).Based on an indication of potential core instabilities, Control Room personnel manually scrammed the reactor in accordance with Plant Abnormal Operating Procedure PPM 4.12.4.7,"Unintentional Entry Into Region of Potential Core Power Instabilities." Immediate corrective actions were taken by the Control Room staff to bring the plant to a safe shutdown.condition in accordance with Emergency Operating Procedure (EOP)5.1.1,"RPV Control," and Recovery Procedure PPM 3.3.1,"Reactor Scram." The root causes for this event were the degraded condition of a Reactor Recirculation (RRC)flow control valve (FCV)position transmitter and the lack of procedural criteria to determine when to"lock up" the degraded FCV.Further corrective actions include: (1)replacement of the RRC FCV position transmitters, (2)calibration and testing of the replacement FCV position transmitters, and (3)required reading of this Licensee Event Report (LER)by WNP-2 licensed operators.
Should you have any questions or desire additional information, please call me or D.A. Swank at (509) 377-4563.
Sincerely, J   . Parrish (Mail Drop 1023)
Assistant Managing Director, Operations JVP/CDM/my Enclosure CC:     LJ Callan, NRC-RIV KE Perkins, Jr., NRC RIV, Walnut Creek Field Office NS Reynolds, Winston & Strawn NRC Sr. Resident Inspector (Mail Drop 927N, 2 Copies)
INPO Records Center - Atlanta, GA DL Williams, BPA (Mail Drop 399)
PDR 8 "'DR 9406020024 940526 ADOCK 05000397
 
LICENSEE EVEIOREPORT (LER)
ACILITY NAME (1)                                                                                       DOCKET NUMB R ( )                     PAGE (3)
Washin ton Nuclear              Plant - Unit        2                                              0   5   0   0   0   3     9   7   I   OF ITLE (4)
MANUALSCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS EVENT DATE     5                 LER NUMBER   6)             REPORT DATE         (7)                 OTHER  FACILITIES INVOLVED 8 MONTH        DAY    YEAR              SEQUENTIAL      EVI SION    MONTH         DAY   YEAR FACILITY NAMES                                 CKE   NUMB R   (5)
NUMBER          UMBER AA 50  0 0 0 4       26     94       9 4       00   8         0 0       0 5           2 6     9 4                                                 5 0 00 P ERAT ING               MIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF             10 CFR 5: (Check one or more     of the following)     (ll)
ODE    (9)            I OWER   LEVEL                 20.402(b)                     20.405(C)                        50.73(a)(2)(iv)                 77.71(b)
(10)                           20.405(a)(1)(i)               50.36(c)(1)                     50.73(a)(2)(v)                   73.73(c) 0.405(a)(1)(ii)              50.36(c)(2)                     50.73(a)(2)(vii)                 THER    (Specify in Abstract 20.405(a)(1)(iii)             50.73(a)(2)(i)                   50.73(a)(2)(viii)(A)             elow and in Text,    NRC 20.405(a)(1)(iv)               50.73(a)(2)(ii)                   50.73(a)(2)(viii)(B)            orm 366A) 20.405(a)(1)(v)               50.73(a)(2)(iii)                 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER           12 TELEPHONE NUMBER REA CODE C.D. Mackaman, Licensing Engineer                                                                                             -
5   0   9     7     7         4   4   5   1 COMPLETE ONE LINE FOR EACH COMPONENT         FAILURE DESCRIBED IH THIS REPORT   (13)
MANUFACTURER     EPORTABLE   jc:,.',4::", CAUSE   SYSTEM       COMPONENT       MAHUFACTURER       EPORTABLE CAUSE      SYSTEM      COMPOHEHT TO NPRDS
                                                                            ; Qh; BD         A D                             0   5 2 EXPECTED SUSHI SSI OH              DA'Y  TEAR SUPPLEMENTAL REPORT EXPECTED   (14)                                                                   MONTH ATE (15)
YES   (If yes,   cTNpiete   EXPECTED SUBMISSIOH DATE)     X NO TRACY IIeI At 1010 hours on April 26,             1994, with the plant at 50% reactor power and 55% core flow, plant Control Room Operators (CROs) observed slight reactor power fluctuations on the six average power range monitors (APRMs). Based on an indication of potential core instabilities, Control Room personnel manually scrammed the reactor in accordance with Plant Abnormal Operating Procedure PPM 4.12.4.7, "Unintentional Entry Into Region of Potential Core Power Instabilities."
Immediate corrective actions were taken by the Control Room staff to bring the plant to a safe shutdown.
condition in accordance with Emergency Operating Procedure (EOP) 5.1.1, "RPV Control," and Recovery Procedure PPM 3.3.1, "Reactor Scram."
The root causes for this event were the degraded condition of a Reactor Recirculation (RRC) flow control valve (FCV) position transmitter and the lack of procedural criteria to determine when to "lock up" the degraded FCV.
Further corrective actions include: (1) replacement of the RRC FCV position transmitters, (2) calibration and testing of the replacement FCV position transmitters, and (3) required reading of this Licensee Event Report (LER) by WNP-2 licensed operators.
This event posed no threat to the health and safety of either the public or plant personnel.
This event posed no threat to the health and safety of either the public or plant personnel.
LICENSEE EVENT REPOR ER)TEXl CONTINUATION AGILITY NAME (I)Washington Nuclear Plant-Unit 2 OOCKET NUMBER (2)0 5 0 0 0 3 9 7 ear LER NUMBER (8)umber ev.No.4 08 00 AGE (3)2 F 6 ITLE (4)MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS Pl n ndii n Power Level-50%Plant Mode-1{Power Operation)
Even Descri i n At 0831 hours on April 26, 1994, WNP-2 experienced an overload trip of a 480 VAC load center breaker, (E-CB-31/3) and loss of a nonsafety-related 480 VAC motor control center (E-MC-3A).
The loss of the motor control center{MCC)caused a loss of power to the bleed steam (BS)dump and turbine non-return (backflow preventer) valve solenoid pilot valves for Low Pressure (LP)Feedwater Heaters 1A, 2A, 3A, and 4A.The loss of power to the solenoid pilot valves resulted in isolation of extraction steam to the four.LP heaters and opening of the dump valves to the main condenser.
By 0841 hours, reactor feedwater (RFW)inlet temperature had decreased approximately 6.5'ahrenheit.
At 0850 hours, in accordance with Plant Abnormal Operating Procedure PPM 4.2.7.2,"Loss Of Feedwater Heating," plant Control Room Operators (CROs)reduced reactor power from 70%to 50%and core flow from 100%to 55%.At 1010 hours, plant CROs observed slight reactor power fluctuations on the six average power range monitors (APRMs)during an approximate four minute time period.The maximum amplitude of the fluctuations was approximately 8%peak-to-peak and the interval between fluctuations was approximately 20 seconds.Based on the increasing amplitude of the fluctuations, Control Room personnel manually scrammed the reactor less than one minute after the maximum amplitude was experienced using guidance outlined in Plant Abnormal Operating Procedure PPM 4.12.4.7,"Unintentional Entry Into Region of Potential Core Power Instabilities." All control rods fully inserted and no safety relief valves actuated.Plant response to the scram was as expected.The reactor pressure vessel (RPV)level reached a minimum of-15.4 inches and a maximum of+60.1 inches.mmediate rrective A i n Following the reactor scram, the Control Room staff promptly entered Emergency Operating Procedure (EOP)5.1.1,"RPV Control," as required when the RPV level decreased to+13 inches.RPV level was recovered using the RFW pumps and the plant was stabilized in accordance with Recovery Procedure PPM 3.3.1,"Reactor Scram." EOP 5.1.1 was exited at 1043 hours.


1 LICENSEE EVENT REPOR ER), TEXT CONTINUATION AGILITY NAME'1)Washington Nuclear Plant-Unit 2 OOCKET NUMBER (2)0 5 0 0 0 3 9 7 LER NUMBER (8)ear umber ev.No.08 00 AGE (3)3 OF 6 ITLE (4)MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS Fu her Ev lua i n d orr ive Action F h rEv lu tion 1.Pursuant to'0CFR50.72(b)(2)(ii), this event was reported to the NRC Operations Center via the Emergency Notification System (ENS)at 1111 hours as an unplanned manual actuation of the Reactor Protection System (RPS).This event is also being reported in accordance with 10CFR50.73(a)(2)(iv) as an unplanned manual actuation of the RPS.2.The overload trip of Load Center Breaker E-CB-31/3 and loss of Motor Control Center E-MC-3A occurred while performing a test run of a new turbine building exhaust fan (TEA-FN-1C) motor with it coupled to the fan, The motor had been upgraded from 100 HP to 200 HP as part of a plant modification (BDC 92-0220-0).
LICENSEE EVENT REPOR             ER)
The overload trip condition was caused by concurrently running the new fan motor and an old fan (TEA-FN-1A) motor while both were still powered from the same MCC.Due to E-MC-3A loading limitations, later steps in the modification installation sequence provided for the relocation of the TEA-FN-1A motor power feed to another MCC.The field engineer did not recognize that the modification sequence of running the old and the new fan motors concurrently on the same MCC would cause an overload of the MCC.Problem Evaluation Report (PER)294-0324 was initiated following the loss of E-MC-3A and an Incident Review Board (IRB)was convened to investigate the event.As an immediate action, an Engineering"Time Out" was taken on April 27, 1994 to review ongoing design changes with Project Engineers, System Engineers, Design Engineers, and Operations personnel to ensure adequate implementation and test planning.A formal root cause analysis was subsequently performed for the PER and a corrective action plan was developed to preclude the recurrence of a similar event.3, Following the scram, investigation of the observed reactor power fluctuations showed that they were not the result of reactor core instability or oscillations.
TEXl CONTINUATION AGILITY NAME (I)                             OOCKET NUMBER (2)                 LER NUMBER (8)        AGE  (3) ear     umber       ev. No.
The power fluctuations were caused by a degraded position transmitter (RRC-POT-26A) for a Reactor Recirculation (RRC)System flow control valve (FCV)(RRC-FCV-60A).
Washington Nuclear Plant - Unit 2 0  5  0  0  0 3 9  7 4        08      00        2    F  6 ITLE (4)
The position transmitter produced slight perturbations in the output signal that caused small step changes in actual FCV position.These valve position changes caused corresponding changes in reactor core flow and power.When the FCV was in operation at rated power and flow conditions, slight perturbations in the position transmitter output signal do not result in significant changes in reactor core flow because the valve is near full open.However, these same transmitter output perturbations can cause relatively significant changes in reactor core flow when the FCV is near its lower limit such as the 55%flow condition that existed during this event.
MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS Pl n      ndii  n Power Level - 50%
LICENSEE EVENT REPOR ER)TEXT CONTINUATION AGILITY NANE (1)DOCKET NUNBER (2)Washington Nucleai Plant-Unit 2 ear LER NUMBER (8)umber ev.No.AGE (3)4 008 D ITLE (4)MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS 4 F 6 4.Indications of RRC-FCV-60A position fluctuations were previously identified on August 16, 1993.As a result of the investigation, a Work Order was initiated and scheduled to replace RRC-FCV-60A position transmitter RRC-POT-26A.
Plant Mode - 1 {Power Operation)
As an interim measure until'ransmitter replacement, the system engineer provided recommendations in an Interoffice Memorandum (IOM)for operating RRC-FCV-60A in the degraded condition.
Even Descri    i n At 0831 hours on April 26, 1994, WNP-2 experienced an overload trip of a 480 VAC load center breaker, (E-CB-31/3) and loss of a nonsafety-related 480 VAC motor control center (E-MC-3A). The loss of the motor control center {MCC) caused a loss of power to the bleed steam (BS) dump and turbine non-return (backflow preventer) valve solenoid pilot valves for Low Pressure (LP) Feedwater Heaters 1A, 2A, 3A, and 4A. The loss of power to the solenoid pilot valves resulted in isolation of extraction steam to the four
One of the recommendations was for the FCV hydraulic power unit (HPU)to be shutdown after the valve was placed in the desired position.This action establishes a hydraulic"lock up" of the valve and prevents the valve operator from moving the valve.Operating Procedure PPM 2.2.1,"Reactor Recirculation System," was revised to incorporate the recommendations for interim operation of RRC-FCV-60A; however, the procedure revision did not provide criteria for determining when to"lock up" the FCV other than to say: "[a]fter[the FCV]is in the desired position..
. LP heaters and opening of the dump valves to the main condenser. By 0841 hours, reactor feedwater (RFW) inlet temperature had decreased approximately 6.5'ahrenheit. At 0850 hours, in accordance with Plant Abnormal Operating Procedure PPM 4.2.7.2, "Loss Of Feedwater Heating," plant Control Room Operators (CROs) reduced reactor power from 70% to 50% and core flow from 100% to 55%.
~." 5.RRC-FCV-60A had been maintained in a"lock up" condition most of the time, except during plant maneuvering, since August 1993.However, approximately two weeks before this event, maintenance activities began to replace control rod solenoid scram pilot valves (SSPVs).With the plant power maneuvering requirements necessary to support this maintenance effort, Operations crew management decided not to"lock up" RRC-FCV-60A after each power maneuver.During this two week time period, the FCV was observed to have been operating normally, with no indications of spurious valve position changes.After reducing reactor power to 50%and core flow to 55%(and having taken the FCV out of"lock up")in response to the E-MC-3A outage and loss of the LP feedwater heaters, Operations crew management decided not to"lock up" RRC-FCV-60A until the plant was returned to the power and flow conditions that existed prior to the event.They expected to promptly recover from the MCC outage, restore the lost heaters, and increase reactor power and flow to the previous values of approximately 70%and 100%, respectively; then they would"lock up" the FCV.The Supply System believes that the decision not to"lock up" RRC-FCV-60A was consistent with procedure provisions.
At 1010 hours, plant CROs observed slight reactor power fluctuations on the six average power range monitors (APRMs) during an approximate four minute time period. The maximum amplitude of the fluctuations was approximately 8% peak-to-peak and the interval between fluctuations was approximately 20 seconds. Based on the increasing amplitude of the fluctuations, Control Room personnel manually scrammed the reactor less than one minute after the maximum amplitude was experienced using guidance outlined in Plant Abnormal Operating Procedure PPM 4.12.4.7, "Unintentional Entry Into Region of Potential Core Power Instabilities." All control rods fully inserted and no safety relief valves actuated.
However, this event did reveal that there was insufficient criteria in the governing procedure for determining when to"lock up" the FCV.The action to manually scram the reactor was consistent with Supply System expectations as conveyed to the plant staff through procedures and training.However, for instances such as in this event, where there are no clear indications that reactor core oscillations are occurring, the Supply System has concluded that refined guidance and training may be prudent to assure additional confirmatory information is taken into consideration prior to scramming the reactor.Efforts are underway to evaluate and implement, if appropriate, additional guidance and training for unexplained power oscillations.
Plant response to the scram was as expected. The reactor pressure vessel (RPV) level reached a minimum of -15.4 inches and a maximum of +60.1 inches.
LICENSEE EVENT REPORT R)TEXT CONTINUATION
mmediate      rrective A i n Following the reactor scram, the Control Room staff promptly entered Emergency Operating Procedure (EOP) 5.1.1, "RPV Control," as required when the RPV level decreased to +13 inches. RPV level was recovered using the RFW pumps and the plant was stabilized in accordance with Recovery Procedure PPM 3.3.1, "Reactor Scram." EOP 5.1.1 was exited at 1043 hours.
~AGILITY NAHE (1)Washington Nuclear Plant-Unit 2 DOCKET NUHBER (2)0 5 0 0 0 3 9 7 LER NUHBER (8)ear umber ev.No.4 08 00 AGE (3)5 F 6 ITLE (4)MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS The primary root cause for this event (manual scram)was the degraded condition of FCV position transmitter RRC-POT-26A.
 
A secondary root cause was insufficient procedural criteria for determining when to"lock up" the degraded FCV.i her rr tive Ac i n 1.Replacement of RRC-FCV-60A and 60B position transmitters will be completed prior to plant startup from the Spring 1994 Refueling Outage (R9).2.Calibration and testing of the replacement FCV position transmitters will be completed prior to plant startup from R9.3.This Licensee Event Report (LER)will be required to be read by WNP-2 licensed operators prior to plant startup from R9.Jlffi ifi A manual reactor scram is the required immediate action in response to unexplained observed power oscillations.
1 LICENSEE EVENT REPOR                  ER)
Although an actual RPV low level condition did exist when the water level decreased to-15.4 inches following the reactor scram, the transient was well within the bounds of the WNP-2 safety analysis.This event posed no threat to the health and safety of either the public or plant personnel.
        , TEXT CONTINUATION AGILITY NAME'1)                                  OOCKET NUMBER  (2)               LER NUMBER (8)         AGE (3) ear    umber      ev. No.
imil r Event LERs 89-031 and 93-002 reported events where degraded RRC flow control valve system controls contributed to reactor scrams.The degraded system controls in these previous events involved inappropriate setpoints and the negative effects of component interactions following system design changes, modifications, and maintenance.
Washington Nuclear Plant - Unit            2 0  5  0    0  0 3 9  7 08        00        3  OF  6 ITLE (4)
The degraded system controls were not attributed to control circuit or component failures.Thus, these previous event LERs did not include corrective actions that would be expected to prevent the conditions described in this LER.
MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS Fu her Ev lua i n        d  orr  ive Action F    h  rEv  lu tion
lt E LICENSEE EVENT REPORlER)TEXT CONTINUATION AGILITY NAME (I)Washington Nuclear Plant-Unit 2 OOCKET NUMBER (2)0 5 0 0 0 3 9 7 LER NUMBER (8)ear umber ev.Mo.4 08 0 AGE (3)6 F 6 ITLE (4)MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS R f R f~/em Qgmmgnent Reactor Recirculation (RRC)System Flow Control Valve (RRC-FCV-60A)
: 1. Pursuant  to'0CFR50.72(b)(2)(ii), this event was reported to the NRC Operations Center via the Emergency Notification System (ENS) at 1111 hours as an unplanned manual actuation of the Reactor Protection System (RPS). This event is also being reported in accordance with 10CFR50.73(a)(2)(iv) as an unplanned manual actuation of the RPS.
Position Transmitter (RRC-POT-26A)
: 2. The overload trip of Load Center Breaker E-CB-31/3 and loss of Motor Control Center E-MC-3A occurred while performing a test run of a new turbine building exhaust fan (TEA-FN-1C) motor with it coupled to the fan, The motor had been upgraded from 100 HP to 200 HP as part of a plant modification (BDC 92-0220-0). The overload trip condition was caused by concurrently running the new fan motor and an old fan (TEA-FN-1A) motor while both were still powered from the same MCC. Due to E-MC-3A loading limitations, later steps in the modification installation sequence provided for the relocation of the TEA-FN-1A motor power feed to another MCC. The field engineer did not recognize that the modification sequence of running the old and the new fan motors concurrently on the same MCC would cause an overload of the MCC.
Load Center Breaker (E-CB-31/3)
Problem Evaluation Report (PER) 294-0324 was initiated following the loss of E-MC-3A and an Incident Review Board (IRB) was convened to investigate the event. As an immediate action, an Engineering "Time Out" was taken on April 27, 1994 to review ongoing design changes with Project Engineers, System Engineers, Design Engineers, and Operations personnel to ensure adequate implementation and test planning. A formal root cause analysis was subsequently performed for the PER and a corrective action plan was developed to preclude the recurrence of a similar event.
Motor Control Center (E-MC-3A)Reactor Protection System (RPS)Average Power Range Monitors (APRMs)Reactor Feedwater (RF%)System Low Pressure (LP)Feedwater Heaters Bleed Steam (BS)Dump Valve Turbine Non-Return Valve AD AD AD EC EC JC JC SJ SM SM SM FCV ZT BKR (52)MCC MON HX FSV FSV2}}
3, Following the scram, investigation of the observed reactor power fluctuations showed that they were not the result of reactor core instability or oscillations. The power fluctuations were caused by a degraded position transmitter (RRC-POT-26A) for a Reactor Recirculation (RRC) System flow control valve (FCV) (RRC-FCV-60A). The position transmitter produced slight perturbations in the output signal that caused small step changes in actual FCV position. These valve position changes caused corresponding changes in reactor core flow and power.
When the FCV was in operation at rated power and flow conditions, slight perturbations in the position transmitter output signal do not result in significant changes in reactor core flow because the valve is near full open. However, these same transmitter output perturbations can cause relatively significant changes in reactor core flow when the FCV is near its lower limit such as the 55% flow condition that existed during this event.
 
LICENSEE EVENT REPOR                  ER)
TEXT CONTINUATION AGILITY NANE (1)                                  DOCKET NUNBER (2)                  LER NUMBER (8)          AGE            (3) ear      umber      ev. No.
Washington Nucleai Plant - Unit            2 4      008          D        4              F  6 ITLE (4)
MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS
: 4. Indications of RRC-FCV-60A position fluctuations were previously identified on August 16, 1993. As a result of the investigation, a Work Order was initiated and scheduled to replace RRC-FCV-60A position transmitter RRC-POT-26A. As an interim measure until replacement, the system engineer provided recommendations in an Interoffice          'ransmitter Memorandum (IOM) for operating RRC-FCV-60A in the degraded condition. One of the recommendations was for the FCV hydraulic power unit (HPU) to be shutdown after the valve was placed in the desired position. This action establishes a hydraulic "lock up" of the valve and prevents the valve operator from moving the valve. Operating Procedure PPM 2.2.1, "Reactor Recirculation System," was revised to incorporate the recommendations for interim operation of RRC-FCV-60A; however, the procedure revision did not provide criteria for determining when to "lock up" the FCV other than to say: "[a]fter [the FCV] is in the desired position.. ."      ~
: 5. RRC-FCV-60A had been maintained in a "lock up" condition most of the time, except during plant maneuvering, since August 1993. However, approximately two weeks before this event, maintenance activities began to replace control rod solenoid scram pilot valves (SSPVs). With the plant power maneuvering requirements necessary to support this maintenance effort, Operations crew management decided not to "lock up" RRC-FCV-60A after each power maneuver. During this two week time period, the FCV was observed to have been operating normally, with no indications of spurious valve position changes.
After reducing reactor power to 50% and core flow to 55% (and having taken the FCV out of "lock up") in response to the E-MC-3A outage and loss of the LP feedwater heaters, Operations crew management decided not to "lock up" RRC-FCV-60A until the plant was returned to the power and flow conditions that existed prior to the event. They expected to promptly recover from the MCC outage, restore the lost heaters, and increase reactor power and flow to the previous values of approximately 70% and 100%, respectively; then they would "lock up" the FCV. The Supply System believes that the decision not to "lock up" RRC-FCV-60A was consistent with procedure provisions. However, this event did reveal that there was insufficient criteria in the governing procedure for determining when to "lock up" the FCV.
The action to manually scram the reactor was consistent with Supply System expectations as conveyed to the plant staff through procedures and training. However, for instances such as in this event, where there are no clear indications that reactor core oscillations are occurring, the Supply System has concluded that refined guidance and training may be prudent to assure additional confirmatory information is taken into consideration prior to scramming the reactor.
Efforts are underway to evaluate and implement, if appropriate, additional guidance and training for unexplained power oscillations.
 
LICENSEE EVENT REPORT                  R)
TEXT CONTINUATION
~ AGILITY NAHE (1)                                   DOCKET NUHBER  (2)                   LER NUHBER (8)        AGE (3) ear     umber       ev. No.
Washington Nuclear Plant - Unit            2 9
0  5  0  0  0 3     7 4        08      00        5  F 6 ITLE (4)
MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS The primary root cause for this event (manual scram) was the degraded condition of FCV position transmitter RRC-POT-26A. A secondary root cause was insufficient procedural criteria for determining when to "lock up" the degraded FCV.
i her    rr tive Ac i  n
: 1. Replacement    of RRC-FCV-60A and        60B position transmitters  will be completed prior to plant startup from  the Spring  1994  Refueling  Outage (R9).
: 2. Calibration and testing    of the replacement FCV position transmitters will be completed prior to plant startup from R9.
: 3. This Licensee Event Report (LER)        will be required to be  read by WNP-2 licensed operators prior to plant startup from R9.
Jlffi ifi A manual reactor scram is the required immediate action in response to unexplained observed power oscillations. Although an actual RPV low level condition did exist when the water level decreased to -15.4 inches following the reactor scram, the transient was well within the bounds of the WNP-2 safety analysis. This event posed no threat to the health and safety of either the public or plant personnel.
imil r Event LERs 89-031 and 93-002 reported events where degraded RRC flow control valve system controls contributed to reactor scrams. The degraded system controls in these previous events involved inappropriate setpoints and the negative effects of component interactions following system design changes, modifications, and maintenance. The degraded system controls were not attributed to control circuit or component failures. Thus, these previous event LERs did not include corrective actions that would be expected to prevent the conditions described in this LER.
 
lt E
 
LICENSEE EVENT REPORl              ER)
TEXT CONTINUATION AGILITY NAME (I)                              OOCKET NUMBER  (2)              LER NUMBER (8)        AGE (3) ear    umber      ev. Mo.
Washington Nuclear Plant - Unit        2 0 3 9 0  5  0  0          7 4      08          0      6  F  6 ITLE (4)
MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS R f                                                      R  f
                                                                    ~/em            Qgmmgnent Reactor Recirculation (RRC) System                      AD Flow Control Valve (RRC-FCV-60A)                        AD              FCV Position Transmitter (RRC-POT-26A)                      AD                ZT Load Center Breaker (E-CB-31/3)                          EC            BKR (52)
Motor Control Center (E-MC-3A)                          EC              MCC Reactor Protection System (RPS)                          JC Average Power Range Monitors (APRMs)                    JC              MON Reactor Feedwater (RF%) System                          SJ Low Pressure (LP) Feedwater Heaters                      SM                HX Bleed Steam (BS) Dump Valve                              SM              FSV Turbine Non-Return Valve                                 SM             FSV2}}

Latest revision as of 13:35, 29 October 2019

LER 94-008-00:on 940426,CROs Observed Slight Reactor Power Fluctuations on Six Aprms.Caused by Degraded Condition of Reactor Recirculation (RRC) FCV Position Transmitter. Replaced RRC FCV Position transmitters.W/940526 Ltr
ML17290B194
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 05/26/1994
From: Mackaman C, Parrish J
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
GO2-94-125, LER-94-008, LER-94-8, NUDOCS 9406020024
Download: ML17290B194 (10)


Text

~

ACCELERATED D STRIBUTION DEMONS ATION SYSTEM S ~

REGULATORY INFORMATXON DXSTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9406020024 DOC.DATE: 94/05/26 NOTARIZED: NO DOCKET FACIL:50-397, WPPSS Nuclear Project, Unit 2, Washington, Public Powe 05000397 AUTH. NAME AUTHOR AFFILIATION MACKAMAN,C.D. Washington Public Power Supply System PARRISH,J.V. Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 94-008-00:on 940426,CROs observed slight reactor power fluctuations on six APRMs.Caused by degraded condition of reactor recirculation (RRC) FCV position transmitter.

Replaced RRC FCV position transmitters.W/940526 ltr.

DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR L TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

ENCL / SIZE: 7 NOTES RECIPIENT COPIES RECXPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PDIV-3 PD 1 1 CLIFFORD,J 1 1 D INTERNAL: ACRS 1 1 1 1 AEOD/DOA'EOD/ROAB/DSP AEOD/DS P/TPAB 1 1 2 2 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRIL/RPEB 1 1 NRR/DRSS/PRPB 2 2 NRRggSS SPLB 1 1 NRR/DSSA/SRXB 1 1 EG FX 02 1 1 RES/DSIR/EIB 1 1 RGN4 FI~ 01 1 1 EXTERNAL: EG&G BRYCE,J.H 2 2 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHY,G.A 1 1 NSIC POORE1W ~ 1 1 NUDOCS FULL TXT 1 1 R

I D

D D

NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 28 ENCL 28

WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ 3000 George Washington Way ~ Richland, Washington 99352 May 26, 1994 G02-94-125 Docket No. 50-397 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555

Subject:

NUCLEAR PLANT WNP-2, OPERATING LICENSE NPF-21 LICENSEE EVENT REPORT NO. 94-008-00 Transmitted herewith is Licensee Event Report No. 94-008-00 for the WNP-2 Plant. This report is submitted in response to the reporting requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrence.

Should you have any questions or desire additional information, please call me or D.A. Swank at (509) 377-4563.

Sincerely, J . Parrish (Mail Drop 1023)

Assistant Managing Director, Operations JVP/CDM/my Enclosure CC: LJ Callan, NRC-RIV KE Perkins, Jr., NRC RIV, Walnut Creek Field Office NS Reynolds, Winston & Strawn NRC Sr. Resident Inspector (Mail Drop 927N, 2 Copies)

INPO Records Center - Atlanta, GA DL Williams, BPA (Mail Drop 399)

PDR 8 "'DR 9406020024 940526 ADOCK 05000397

LICENSEE EVEIOREPORT (LER)

ACILITY NAME (1) DOCKET NUMB R ( ) PAGE (3)

Washin ton Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 I OF ITLE (4)

MANUALSCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS EVENT DATE 5 LER NUMBER 6) REPORT DATE (7) OTHER FACILITIES INVOLVED 8 MONTH DAY YEAR SEQUENTIAL EVI SION MONTH DAY YEAR FACILITY NAMES CKE NUMB R (5)

NUMBER UMBER AA 50 0 0 0 4 26 94 9 4 00 8 0 0 0 5 2 6 9 4 5 0 00 P ERAT ING MIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or more of the following) (ll)

ODE (9) I OWER LEVEL 20.402(b) 20.405(C) 50.73(a)(2)(iv) 77.71(b)

(10) 20.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.73(c) 0.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii) THER (Specify in Abstract 20.405(a)(1)(iii) 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) elow and in Text, NRC 20.405(a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) orm 366A) 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)

LICENSEE CONTACT FOR THIS LER 12 TELEPHONE NUMBER REA CODE C.D. Mackaman, Licensing Engineer -

5 0 9 7 7 4 4 5 1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IH THIS REPORT (13)

MANUFACTURER EPORTABLE jc:,.',4::", CAUSE SYSTEM COMPONENT MAHUFACTURER EPORTABLE CAUSE SYSTEM COMPOHEHT TO NPRDS

Qh; BD A D 0 5 2 EXPECTED SUSHI SSI OH DA'Y TEAR SUPPLEMENTAL REPORT EXPECTED (14) MONTH ATE (15)

YES (If yes, cTNpiete EXPECTED SUBMISSIOH DATE) X NO TRACY IIeI At 1010 hours0.0117 days <br />0.281 hours <br />0.00167 weeks <br />3.84305e-4 months <br /> on April 26, 1994, with the plant at 50% reactor power and 55% core flow, plant Control Room Operators (CROs) observed slight reactor power fluctuations on the six average power range monitors (APRMs). Based on an indication of potential core instabilities, Control Room personnel manually scrammed the reactor in accordance with Plant Abnormal Operating Procedure PPM 4.12.4.7, "Unintentional Entry Into Region of Potential Core Power Instabilities."

Immediate corrective actions were taken by the Control Room staff to bring the plant to a safe shutdown.

condition in accordance with Emergency Operating Procedure (EOP) 5.1.1, "RPV Control," and Recovery Procedure PPM 3.3.1, "Reactor Scram."

The root causes for this event were the degraded condition of a Reactor Recirculation (RRC) flow control valve (FCV) position transmitter and the lack of procedural criteria to determine when to "lock up" the degraded FCV.

Further corrective actions include: (1) replacement of the RRC FCV position transmitters, (2) calibration and testing of the replacement FCV position transmitters, and (3) required reading of this Licensee Event Report (LER) by WNP-2 licensed operators.

This event posed no threat to the health and safety of either the public or plant personnel.

LICENSEE EVENT REPOR ER)

TEXl CONTINUATION AGILITY NAME (I) OOCKET NUMBER (2) LER NUMBER (8) AGE (3) ear umber ev. No.

Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 4 08 00 2 F 6 ITLE (4)

MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS Pl n ndii n Power Level - 50%

Plant Mode - 1 {Power Operation)

Even Descri i n At 0831 hours0.00962 days <br />0.231 hours <br />0.00137 weeks <br />3.161955e-4 months <br /> on April 26, 1994, WNP-2 experienced an overload trip of a 480 VAC load center breaker, (E-CB-31/3) and loss of a nonsafety-related 480 VAC motor control center (E-MC-3A). The loss of the motor control center {MCC) caused a loss of power to the bleed steam (BS) dump and turbine non-return (backflow preventer) valve solenoid pilot valves for Low Pressure (LP) Feedwater Heaters 1A, 2A, 3A, and 4A. The loss of power to the solenoid pilot valves resulted in isolation of extraction steam to the four

. LP heaters and opening of the dump valves to the main condenser. By 0841 hours0.00973 days <br />0.234 hours <br />0.00139 weeks <br />3.200005e-4 months <br />, reactor feedwater (RFW) inlet temperature had decreased approximately 6.5'ahrenheit. At 0850 hours0.00984 days <br />0.236 hours <br />0.00141 weeks <br />3.23425e-4 months <br />, in accordance with Plant Abnormal Operating Procedure PPM 4.2.7.2, "Loss Of Feedwater Heating," plant Control Room Operators (CROs) reduced reactor power from 70% to 50% and core flow from 100% to 55%.

At 1010 hours0.0117 days <br />0.281 hours <br />0.00167 weeks <br />3.84305e-4 months <br />, plant CROs observed slight reactor power fluctuations on the six average power range monitors (APRMs) during an approximate four minute time period. The maximum amplitude of the fluctuations was approximately 8% peak-to-peak and the interval between fluctuations was approximately 20 seconds. Based on the increasing amplitude of the fluctuations, Control Room personnel manually scrammed the reactor less than one minute after the maximum amplitude was experienced using guidance outlined in Plant Abnormal Operating Procedure PPM 4.12.4.7, "Unintentional Entry Into Region of Potential Core Power Instabilities." All control rods fully inserted and no safety relief valves actuated.

Plant response to the scram was as expected. The reactor pressure vessel (RPV) level reached a minimum of -15.4 inches and a maximum of +60.1 inches.

mmediate rrective A i n Following the reactor scram, the Control Room staff promptly entered Emergency Operating Procedure (EOP) 5.1.1, "RPV Control," as required when the RPV level decreased to +13 inches. RPV level was recovered using the RFW pumps and the plant was stabilized in accordance with Recovery Procedure PPM 3.3.1, "Reactor Scram." EOP 5.1.1 was exited at 1043 hours0.0121 days <br />0.29 hours <br />0.00172 weeks <br />3.968615e-4 months <br />.

1 LICENSEE EVENT REPOR ER)

, TEXT CONTINUATION AGILITY NAME'1) OOCKET NUMBER (2) LER NUMBER (8) AGE (3) ear umber ev. No.

Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 08 00 3 OF 6 ITLE (4)

MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS Fu her Ev lua i n d orr ive Action F h rEv lu tion

1. Pursuant to'0CFR50.72(b)(2)(ii), this event was reported to the NRC Operations Center via the Emergency Notification System (ENS) at 1111 hours0.0129 days <br />0.309 hours <br />0.00184 weeks <br />4.227355e-4 months <br /> as an unplanned manual actuation of the Reactor Protection System (RPS). This event is also being reported in accordance with 10CFR50.73(a)(2)(iv) as an unplanned manual actuation of the RPS.
2. The overload trip of Load Center Breaker E-CB-31/3 and loss of Motor Control Center E-MC-3A occurred while performing a test run of a new turbine building exhaust fan (TEA-FN-1C) motor with it coupled to the fan, The motor had been upgraded from 100 HP to 200 HP as part of a plant modification (BDC 92-0220-0). The overload trip condition was caused by concurrently running the new fan motor and an old fan (TEA-FN-1A) motor while both were still powered from the same MCC. Due to E-MC-3A loading limitations, later steps in the modification installation sequence provided for the relocation of the TEA-FN-1A motor power feed to another MCC. The field engineer did not recognize that the modification sequence of running the old and the new fan motors concurrently on the same MCC would cause an overload of the MCC.

Problem Evaluation Report (PER) 294-0324 was initiated following the loss of E-MC-3A and an Incident Review Board (IRB) was convened to investigate the event. As an immediate action, an Engineering "Time Out" was taken on April 27, 1994 to review ongoing design changes with Project Engineers, System Engineers, Design Engineers, and Operations personnel to ensure adequate implementation and test planning. A formal root cause analysis was subsequently performed for the PER and a corrective action plan was developed to preclude the recurrence of a similar event.

3, Following the scram, investigation of the observed reactor power fluctuations showed that they were not the result of reactor core instability or oscillations. The power fluctuations were caused by a degraded position transmitter (RRC-POT-26A) for a Reactor Recirculation (RRC) System flow control valve (FCV) (RRC-FCV-60A). The position transmitter produced slight perturbations in the output signal that caused small step changes in actual FCV position. These valve position changes caused corresponding changes in reactor core flow and power.

When the FCV was in operation at rated power and flow conditions, slight perturbations in the position transmitter output signal do not result in significant changes in reactor core flow because the valve is near full open. However, these same transmitter output perturbations can cause relatively significant changes in reactor core flow when the FCV is near its lower limit such as the 55% flow condition that existed during this event.

LICENSEE EVENT REPOR ER)

TEXT CONTINUATION AGILITY NANE (1) DOCKET NUNBER (2) LER NUMBER (8) AGE (3) ear umber ev. No.

Washington Nucleai Plant - Unit 2 4 008 D 4 F 6 ITLE (4)

MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS

4. Indications of RRC-FCV-60A position fluctuations were previously identified on August 16, 1993. As a result of the investigation, a Work Order was initiated and scheduled to replace RRC-FCV-60A position transmitter RRC-POT-26A. As an interim measure until replacement, the system engineer provided recommendations in an Interoffice 'ransmitter Memorandum (IOM) for operating RRC-FCV-60A in the degraded condition. One of the recommendations was for the FCV hydraulic power unit (HPU) to be shutdown after the valve was placed in the desired position. This action establishes a hydraulic "lock up" of the valve and prevents the valve operator from moving the valve. Operating Procedure PPM 2.2.1, "Reactor Recirculation System," was revised to incorporate the recommendations for interim operation of RRC-FCV-60A; however, the procedure revision did not provide criteria for determining when to "lock up" the FCV other than to say: "[a]fter [the FCV] is in the desired position.. ." ~
5. RRC-FCV-60A had been maintained in a "lock up" condition most of the time, except during plant maneuvering, since August 1993. However, approximately two weeks before this event, maintenance activities began to replace control rod solenoid scram pilot valves (SSPVs). With the plant power maneuvering requirements necessary to support this maintenance effort, Operations crew management decided not to "lock up" RRC-FCV-60A after each power maneuver. During this two week time period, the FCV was observed to have been operating normally, with no indications of spurious valve position changes.

After reducing reactor power to 50% and core flow to 55% (and having taken the FCV out of "lock up") in response to the E-MC-3A outage and loss of the LP feedwater heaters, Operations crew management decided not to "lock up" RRC-FCV-60A until the plant was returned to the power and flow conditions that existed prior to the event. They expected to promptly recover from the MCC outage, restore the lost heaters, and increase reactor power and flow to the previous values of approximately 70% and 100%, respectively; then they would "lock up" the FCV. The Supply System believes that the decision not to "lock up" RRC-FCV-60A was consistent with procedure provisions. However, this event did reveal that there was insufficient criteria in the governing procedure for determining when to "lock up" the FCV.

The action to manually scram the reactor was consistent with Supply System expectations as conveyed to the plant staff through procedures and training. However, for instances such as in this event, where there are no clear indications that reactor core oscillations are occurring, the Supply System has concluded that refined guidance and training may be prudent to assure additional confirmatory information is taken into consideration prior to scramming the reactor.

Efforts are underway to evaluate and implement, if appropriate, additional guidance and training for unexplained power oscillations.

LICENSEE EVENT REPORT R)

TEXT CONTINUATION

~ AGILITY NAHE (1) DOCKET NUHBER (2) LER NUHBER (8) AGE (3) ear umber ev. No.

Washington Nuclear Plant - Unit 2 9

0 5 0 0 0 3 7 4 08 00 5 F 6 ITLE (4)

MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS The primary root cause for this event (manual scram) was the degraded condition of FCV position transmitter RRC-POT-26A. A secondary root cause was insufficient procedural criteria for determining when to "lock up" the degraded FCV.

i her rr tive Ac i n

1. Replacement of RRC-FCV-60A and 60B position transmitters will be completed prior to plant startup from the Spring 1994 Refueling Outage (R9).
2. Calibration and testing of the replacement FCV position transmitters will be completed prior to plant startup from R9.
3. This Licensee Event Report (LER) will be required to be read by WNP-2 licensed operators prior to plant startup from R9.

Jlffi ifi A manual reactor scram is the required immediate action in response to unexplained observed power oscillations. Although an actual RPV low level condition did exist when the water level decreased to -15.4 inches following the reactor scram, the transient was well within the bounds of the WNP-2 safety analysis. This event posed no threat to the health and safety of either the public or plant personnel.

imil r Event LERs89-031 and 93-002 reported events where degraded RRC flow control valve system controls contributed to reactor scrams. The degraded system controls in these previous events involved inappropriate setpoints and the negative effects of component interactions following system design changes, modifications, and maintenance. The degraded system controls were not attributed to control circuit or component failures. Thus, these previous event LERs did not include corrective actions that would be expected to prevent the conditions described in this LER.

lt E

LICENSEE EVENT REPORl ER)

TEXT CONTINUATION AGILITY NAME (I) OOCKET NUMBER (2) LER NUMBER (8) AGE (3) ear umber ev. Mo.

Washington Nuclear Plant - Unit 2 0 3 9 0 5 0 0 7 4 08 0 6 F 6 ITLE (4)

MANUAL SCRAM DUE TO OBSERVED REACTOR CORE POWER FLUCTUATIONS R f R f

~/em Qgmmgnent Reactor Recirculation (RRC) System AD Flow Control Valve (RRC-FCV-60A) AD FCV Position Transmitter (RRC-POT-26A) AD ZT Load Center Breaker (E-CB-31/3) EC BKR (52)

Motor Control Center (E-MC-3A) EC MCC Reactor Protection System (RPS) JC Average Power Range Monitors (APRMs) JC MON Reactor Feedwater (RF%) System SJ Low Pressure (LP) Feedwater Heaters SM HX Bleed Steam (BS) Dump Valve SM FSV Turbine Non-Return Valve SM FSV2