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=Text=
{{#Wiki_filter:P~F I ACCELERATED l%TR1BUTION DEMOYSOXTIOY SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:8908140101 DOC.DATE: 89/08/01 NOTARIZED:
{{#Wiki_filter:F                                                  I P~
NO FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe AUTH.NAME AUTHOR AFFILIATION FIES,C.L.Washington Public Power Supply System POWERS,C.M.
ACCELERATED           l%TR1BUTION                       DEMOYSOXTIOY           SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000397
ACCESSION NBR:8908140101                       DOC.DATE: 89/08/01   NOTARIZED: NO           DOCKET FACIL:50-397   WPPSS   Nuclear Project, Unit 2, Washington Public                   Powe   05000397 AUTH. NAME         AUTHOR AFFILIATION FIES,C.L.           Washington Public Power Supply System POWERS,C.M.         Washington Public Power Supply System RECIPIENT AFFILIATION NOTES';
RECIP.NAME


==SUBJECT:==
==SUBJECT:==
LER 89-029-00:on 890703,RWCU
LER   89-029-00:on 890703,RWCU & RCIC sys isolations caused by                               I inadequate test/surveillance procedure.
&RCIC sys isolations caused by inadequate test/surveillance procedure.
W/8         ltr.
W/8 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR 3 ENCL I SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES';I RECIPIENT ID CODE/NAME PD5 LA SAMWORTH,R INTERNAL: ACRS MICHELSON ACRS WYLIE AEOD/DS P/TPAB DEDRO NRR/DEST/CEB 8H NRR/DEST/ICSB 7 NRR/DEST/MTB 9H NRR/DEST/RSB 8E NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NUDOCS-ABSTRACT RES/DSIR/EIB RGN5 FILE 01 EXTERNAL: EG&G WILLIAMS, S L ST LOBBY WARD NRC PDR NSIC MURPHY,G.A COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 4 4 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PD5 PD ACRS MOELLER AEOD/DOA AEOD/ROAB/DS P IRM/DCTS/DAB NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB
DISTRIBUTION CODE: IE22T                     COPIES RECEIVED:LTR 3Incident ENCL I   SIZE:
.8D NRR/DEST/SGB 8D NRR/DLPQ/PEB 10 RPB 10 REG 02 RES/DSR/PRAB FORD BLDG HOY,A LPDR NSIC MAYS,G COPIES LTTR ENCL 1 1 2 2 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 h D, R I S A NOIX'IO ALL"RZDS" RECZPIENIS'LEASE HELP US IO RECCE%ASTE!CXNTACI'HE DOQ3MENI'GHIBOL DESK, KXM Pl-37 (EXT.20079)K)ELIKQRTH KKR NMB FR%MPHtZBUTZCH LISTS FOR DOCUMEKIS RXJ DGNPT NEZDt FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF.COPIES REQUIRED: LTTR 41 ENCL 41 D S ti WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O.Box 968~3000 George washington 11'ay~Richland, 11'ashinglon 99352 Docket No.50-397 August 1, 1989 Document Control Desk U.S.Nuclear Regulatory Commission Washington, D.C.20555  
TITLE: 50.73/50.9 Licensee Event Report (LER),                               Rpt, etc.
RECIPIENT                          COPIES          RECIPIENT         COPIES              h ID CODE/NAME                        LTTR ENCL      ID CODE/NAME     LTTR ENCL PD5 LA                                 1    1    PD5 PD                1    1              D, SAMWORTH,R                             1    1 INTERNAL: ACRS MICHELSON                           1    1    ACRS MOELLER          2    2 ACRS WYLIE                               1  1    AEOD/DOA              1    1 AEOD/DS P/TPAB                           1  1    AEOD/ROAB/DS P        2    2 DEDRO                                   1  1    IRM/DCTS/DAB          1    1 NRR/DEST/CEB 8H                         1  1    NRR/DEST/ESB 8D      1    1 NRR/DEST/ICSB 7                         1  1    NRR/DEST/MEB 9H      1    1 NRR/DEST/MTB 9H                         1  1    NRR/DEST/PSB .8D      1    1 NRR/DEST/RSB 8E                         1  1    NRR/DEST/SGB 8D      1    1 NRR/DLPQ/HFB 10                         1  1    NRR/DLPQ/PEB 10      1    1 NRR/DOEA/EAB 11                         1  1              RPB 10      2    2 NUDOCS-ABSTRACT                         1  1    REG            02    1    1 RES/DSIR/EIB                             1  1    RES/DSR/PRAB          1    1 RGN5     FILE 01                        1  1 EXTERNAL: EG&G WILLIAMS,S                           4   4   FORD BLDG HOY,A       1     1             R L ST LOBBY WARD                          1   1   LPDR                  1     1 NRC PDR                                  1   1   NSIC MAYS,G          1     1             I NSIC MURPHY,G.A                          1   1 S
A D
NOIX 'IO ALL "RZDS" RECZPIENIS'LEASE S
HELP US IO RECCE %ASTE! CXNTACI'HE DOQ3MENI'GHIBOL DESK, KXM Pl-37 (EXT. 20079) K) ELIKQRTH KKR NMB FR% MPHtZBUTZCH LISTS FOR DOCUMEKIS RXJ DGNPT NEZDt FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF. COPIES REQUIRED: LTTR                       41 ENCL   41
 
ti WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ 3000 George washington 11'ay ~ Richland, 11'ashinglon 99352 Docket No. 50-397 August 1, 1989 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555


==Subject:==
==Subject:==
NUCLEAR PLANT NO.2 LICENSEE EVENT REPORT NO.89-029  
NUCLEAR PLANT NO. 2 LICENSEE EVENT REPORT NO. 89-029


==Dear Sir:==
==Dear   Sir:==
Transmitted herewith is Licensee Event Report No.89-029 for the WNP-2 Plant.This report is submitted in response to the report requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrence.
 
Very truly yours, C.M.Powers (M/D 927M)WNP-2 Plant Manager CMP:lg  
Transmitted herewith is Licensee Event Report No. 89-029 for the WNP-2 Plant.
This report is submitted in response to the report requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrence.
Very   truly yours, C.M. Powers (M/D 927M)
WNP-2 Plant Manager CMP:lg


==Enclosure:==
==Enclosure:==


Licensee Event Report No.89-029 cc: Mr.John B.Martin, NRC-Region V Mr.C.J.Bosted, NRC Site (M/D 901A)INPO Records Center-Atlanta, GA Ms.Dottie Sherman, ANI Mr.D.L.Williams, BPA (M/D 399)35'0=140i 05000-~97%9080i pop ADOCK pDC S NAC Form 388 (9.8 3 I LICENSEE EVENT REPORT ILER)U.S.NUCLEAR REGULATORY COMMISSION APPAOVEO OMB NO, 31500104 EXPIAESI BI3)i88 FACILITY NAME (1)DOCKET NUMBER (2)PAGE 13)Washin ton Nuclear Plant-Unit 2 0 5 0 0 03 97>oF0 4""'"'Reactor Water Cleanup and Reactor Core Isolation Cooling System Isolations caused by Inade uate Test/Surveillance Procedure EVFNT DATE 15)LEA NUMBER (8)REPORT DATE (7)OTHER FACILITIES INVOLVED (SI MONTH DAY YE.AR YEAR SEQUENTIAL NUM8%R RE"G~MONT~NUMBER OAY YEAR FACILITY NAMES DOCKET NUMBER(SI 0 5 0 0 0 0 7 0 3 8 9 8 9 029 00 08 01 8 9 0 5 0 0 0 OPF RATING~MODE (8)1 POWER LEVEL)4AiYrrreprr:.".i rir7rrr, Cy@ev.20.402(bl 20.405(e l(1)(i)20.405 (~)I I)I 8 I 20.405(~)(I)liiil 20.405(el(1 l(iv)20,405(~Ill I (v I 20.40S(c)50.381c)(1)S0.38(c)(2)50.73(~l(21(II 50.73(~I(2)(ii)50.73(el(2) liiil LICENSEE CONTACT FOR THIS LER (12I 50.73(el(2) 1iv)50.73 le)12)Hl 50.73(e)12)(viil S0.73lel(2) lviiil(A)50.73(~l(2)(viiil(BI 50.73(~l(2)(cl THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR (): ICnece one or more of tne foriowintl Ill)73.71(5)73.71 (cl OTHER ISoecify in Apstrect oerow end in Ter I, ff RC Perm 366AI NAME C.L.Fies Com liance En ineer AREA CODE 5 0 9 TELEPHONE NUMBER COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFAC TVAER REPORTABLE TO NPADS')ccpnpp/p
Licensee Event Report No. 89-029 cc:   Mr. John B. Martin, NRC - Region V Mr. C.J. Bosted, NRC Site (M/D 901A)
.~fr CAUSE v rKrnt rcSRAirrrfeKCO c'"S(NP'p..rSK69 r SYSTEM COMPON'ENT'ANVFAC.
INPO Records Center - Atlanta, GA Ms. Dottie Sherman,   ANI Mr. D.L. Williams,   BPA (M/D   399) 35'0=140i       %9080i pop    ADOCK    05000-~97 pDC S
TVAER EPORTAB LE TO NPRDS~+~((PP~A~.
 
SUPPLEMENTAL REPORT EXPECTED (14I NO YES III yes, complete fXPECTEO SUBMISSIOiV OATEI ABSTRACT ILimit to f400 sprees, I e., epproeimemfy Afreen si'npie specs typewri Hen Iinnl (18)FXPECTEO SV 8 MISS I 0 N DATE 115I MONTH DAY YEAR On July 3, 1989 at 1022 hours a Reactor Water Cleanup (RWCU)System Isolation occured when RWCU-V-1 closed as part of a Group 7 Nuclear Steam Supply Shutoff System (NS4)isolation.
NAC Form 388                                                                                                                                             U.S. NUCLEAR REGULATORY COMMISSION (9.8 3 I APPAOVEO OMB NO, 31500104 EXPIAESI BI3)i88 LICENSEE EVENT REPORT ILER)
At 1026 hours a similar Reactor Core Isolation Cooling (RCIC)System isolation occurred when RCIC-V-63 closed.Both these isolations occurred as a result of Technical Specification Surveillance Testing per Plant Procedure 7.4.3.2.1.6, Leak Detection Monitor Division II Channel Calibration (CC)/Channel Functional Test (CFT).The root cause of this ESF actuation was less than adequate preparation and review of a surveillance test procedure which had been rewritten to support a plant modification.
FACILITY NAME (1)                                                                                                                               DOCKET NUMBER (2)                           PAGE 13)
This modification had recently been completed during a refueling outage.Immediate corrective action consisted of prompt action by the plant operators to return the impacted systems to service.The surveillance test procedure was also corrected and deviated.Further corrective action will be taken by plant maintenance to strengthen their procedure modification process.In addition, testing and project management procedures will be modified to require, when practical, a more complete check of the modified surveillance prior to plant operation and to allow more time for review and preparation of procedures associated with outage work.Since all ESF systems responded as designed there is no safety significance associated with this event.NRC Form 388 (9 83)
Washin ton Nuclear Plant - Unit 2                                                                                                               0 5   0     0     03 97             >   oF0       4
NRC Form 388A (9.83)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION APPROVEO OMB NO, 3150&104 EXPIRES: 8/31/8$FACILITY NAME (()DOCKET NUMBER (2)YEAR LER NUMBER (8)SEOUENTIAL NUMBER REVISION NUMBER PAGE (3)shin ton Nuclear Plant-Unit 2 TEXT///mOre epeee/4 rei/Oiied.
""'"'Reactor                       Water Cleanup and Reactor Core Isolation Cooling System                                                               Isolations caused by Inade uate Test/Surveillance Procedure EVFNT DATE 15)                         LEA NUMBER (8)                           REPORT DATE (7)                               OTHER FACILITIES INVOLVED (SI SEQUENTIAL        RE"G~                      OAY        YEAR            FACILITYNAMES                        DOCKET NUMBER(SI MONTH         DAY       YE.AR     YEAR               NUM8% R       NUMBER MONT~
Fee eddr'O'OOe/NRC FOnn 3SSA'4)(11)0 5 0 0 0 3 9 7 8 9 0 2 9 0 0 0 2 OF Plant Conditions a)Power Level-83%b)Plant Mode-1 (Power Operation)
0   5   0     0   0 0       7 0 3           8 9 8         9             029             00 08 01                           8   9                                                   0   5   0     0   0 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR (): ICnece one or more of tne foriowintl                    Ill)
Event Descri tion On July 3, 1989 at 1022 hours and again at 1026 hours primary containment isolation valves closed on an isolation signal.Both these events occurred during power ascension following the fourth refueling outage.The first event, a Reactor Water Cleanup (RWCU)System Isolation occurred when RI4:U-V-1 (the inboard containment isolation valve between the reactor vessel and the RNCU System)closed on an NS4 RWCU area high temperature simulated signal causing the operating pump (RWCU-P-lA) to trip.Plant Operators immediately began an investigation into the cause of the isolation which can be the result of any of several events.During their investigation, at 1026 hours, a Reactor Core Isolation Cooling (RCIC)System Isolation occurred on an RCIC Pump Room High Temperature simulated signal causing RCIC-V-63 to close.At that time plant operators traced both isolations to Technical Specification Surveillance (TSS)Testing on the Leak Detection System which had been in progress since 0729 hours.The specific test being performed was TSS 7.4.3.2.1.6, Leak Detection Monitor Division II Channel Calibration (CC)/Channel Functional Test (CFT)for Leak Detection Monitors LD-MON-18 and LD-MON-28.
OPF RATING              ~
The Instrument ana Control (IKC)Technicians had completed Section"AR of the procedure which calibrates LD-MON-18, and were proceeding with Section"BR which tests the relay trip logic on LD-MON-18.
MODE (8)                      20.402(bl                                   20.40S(c)                               50.73(el(2) 1iv)                             73.71(5) 1 POWER                              20.405(e l(1)(i)                             50.381c) (1)                           50.73 le)12) Hl                              73.71 (cl LEVEL 20.405        I
Steps 1 and 2 of Section RBR of the pr'ocedure required bypass key locks for LD-RMS-S3C, LD-RMS-S3D and LD-RMS-S48, to be in the test position.The test position should have placed the downstream trip logic for LD-MON-18 in a configuration where relays RKlBR and RK28R could be tested without an ESF actuation.
(~ ) I ) I8 I                        S0.38(c) (2)                           50.73(e)12)(viil                            OTHER ISoecify in Apstrect oerow end in Ter I, ffRC Perm 20.405( ~ ) (I) liiil                      50.73( ~ l(21(II                        S0.73lel(2) lviiil(A)                       366AI 20.405(el(1 l(iv)                          50.73( ~ I(2) (ii)                      50.73( ~ l(2)(viiil(BI
The I8C Technicians, following procedures as written, proceeded through step 10 of the procedure which simulated a high temperature in the RKU pump and heat exchanger areas, places the leak detection RKlR relay in the RTrip" condition and tests for the proper functioning of the downstream RK1BR relay.With these steps complete they proceeded with steps ll through 15 of the procedure which simulates a high RCIC Equipment Area or Differential Temperature, places the Leak detection RK2" relay in the"trip" condition and tests for proper functioning of the downstream RK28R relay.The Control Room Operators stopped the surveillance testing at this time since it had obviously caused the isolations.
) 4AiYrrreprr:.".i rir7rrr, Cy@ev.      20,405( ~ IllI (v I                        50.73(el(2)  liiil                    50.73( ~ l(2)(cl LICENSEE CONTACT FOR THIS LER (12I NAME                                                                                                                                                                TELEPHONE NUMBER AREA CODE C.L. Fies                Com      liance             En ineer                                                                             5 0         9 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
MANUFAC           REPORTABLE
                                                                                    ')ccpnpp/p                                 COMPON'ENT'ANVFAC.                      EPORTAB LE CAUSE      SYSTEM        COMPONENT                TVAER          TO NPADS
                                                                                                          ~fr CAUSE SYSTEM                            TVAER            TO NPRDS v rKrnt rcSRAirrrfeKCO c'"S(NP
                                                                                                                                                                                      ~+~((PP~A~.
                                                                                    'p..rSK69 r SUPPLEMENTAL REPORT EXPECTED (14I                                                                                   MONTH      DAY      YEAR FXPECTEO SV 8 MISS I0  N DATE 115I YES III yes, complete fXPECTEO SUBMISSIOiV OATEI                                           NO ABSTRACT ILimit to f400 sprees,       I e., epproeimemfy Afreen si'npie specs typewri Hen   Iinnl (18)
On        July 3,              1989       at     1022         hours       a   Reactor                 Water Cleanup         (RWCU)           System         Isolation occured when           RWCU-V-1             closed             as     part of a Group 7 Nuclear                                 Steam         Supply Shutoff System                             (NS4) isolation. At 1026                                       hours a similar Reactor Core                                       Isolation Cooling (RCIC) System isolation occurred when                                       RCIC-V-63 closed.                         Both these isolations occurred as a result of Technical Specification Surveillance Testing per Plant Procedure 7.4.3.2. 1.6, Leak Detection Monitor Division II Channel Calibration (CC )/Channel Functional Test (CFT).
The         root cause of this ESF actuation was less than adequate preparation and review of a surveillance test procedure which had been rewritten to support a plant modification.
This modification had recently been completed during a refueling outage.
Immediate corrective action consisted of prompt action by the plant operators to return the impacted systems to service. The surveillance test procedure was also corrected and deviated.
Further                 corrective action will be taken by plant maintenance to strengthen their procedure                 modification process.                               In addition, testing and project management procedures will be modified to require, when practical, a more complete check of the modified surveillance prior to plant operation and to allow more time for review and preparation of procedures associated with outage work.
Since           all       ESF     systems               responded         as       designed               there is     no     safety significance associated with this event.
NRC Form 388 (9 83)
 
NRC Form 388A                                                                                                     U.S. NUCLEAR REGULATORY COMMISSION (9.83)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                                 APPROVEO OMB NO, 3150&104 EXPIRES: 8/31/8$
FACILITY NAME (()                                                       DOCKET NUMBER (2)               LER NUMBER (8)                     PAGE (3)
YEAR  SEOUENTIAL        REVISION NUMBER        NUMBER shin ton Nuclear Plant - Unit                             2   0  5  0  0    0  3 9 7  8 9      0 2    9        0 0 0      2 OF TEXT ///mOre epeee/4 rei/Oiied. Fee eddr'O'OOe/NRC FOnn 3SSA'4) (11)
Plant Conditions a)        Power Level                -  83%
b)       Plant         Mode         - 1   (Power Operation)
Event Descri                   tion On   July 3, 1989 at 1022 hours and again at 1026 hours primary containment isolation valves closed on an isolation signal.                                   Both these events occurred during power ascension following the fourth refueling outage.                                     The first event, a Reactor Water Cleanup (RWCU) System Isolation occurred when RI4:U-V-1 (the inboard containment isolation valve between the reactor vessel and the RNCU System) closed on an NS4 RWCU area               high temperature simulated signal causing the operating pump (RWCU-P-lA) to trip. Plant Operators immediately began an investigation into the cause of the isolation which can be the result of any of several events.                                                       During their investigation, at 1026 hours, a Reactor Core Isolation Cooling (RCIC) System Isolation occurred on an RCIC Pump Room High Temperature simulated signal causing RCIC-V-63 to close.                                 At that time plant operators traced both isolations to Technical Specification Surveillance (TSS) Testing on the Leak Detection System which had been in progress since 0729 hours.                                     The specific test being performed was TSS 7.4.3.2. 1.6, Leak Detection Monitor Division II Channel Calibration (CC )/Channel Functional Test (CFT) for Leak Detection Monitors LD-MON-18 and LD-MON-28. The Instrument ana Control ( IKC) Technicians had completed Section "AR of the procedure which calibrates LD-MON-18, and were proceeding with Section "BR which tests the relay trip logic on LD-MON-18. Steps 1 and 2 of Section RBR of the pr'ocedure required bypass key locks for LD-RMS-S3C, LD-RMS-S3D and LD-RMS-S48, to be in the test position. The test position should have placed the downstream trip logic for LD-MON-18 in a configuration where relays RKlBR and RK28R could be tested without an ESF actuation.                         The I8C Technicians,           following procedures as written, proceeded through step 10 of the procedure which simulated a high temperature in the RKU pump and heat exchanger                             areas, places the leak detection RKlR relay in the RTrip" condition and tests for the proper functioning of the downstream RK1BR relay. With these steps complete they proceeded with steps ll through 15 of the procedure which simulates a high RCIC Equipment Area or Differential Temperature, places the Leak detection RK2" relay in the "trip" condition and tests for proper functioning of the downstream RK28R relay. The Control Room Operators stopped the surveillance testing at this time since                         it   had obviously caused the isolations.
Immediate Corrective Action Investigation by the Plant Operators and I8C Technicians revealed that the wrong switches had been called out in Steps 1 and 2 of Section RBR of the procedure.
Immediate Corrective Action Investigation by the Plant Operators and I8C Technicians revealed that the wrong switches had been called out in Steps 1 and 2 of Section RBR of the procedure.
Consequently the testing of LD-MON-18 caused the RWCU and RCIC isolation.
Consequently the testing of LD-MON-18 caused the RWCU and RCIC isolation.                                                           The switches identified were those needed for Section RE" of the procedure and were associated with LD-MON-28. The procedure was deviated to call out the correct switches, LD-RMS-S18 and LD-RMS-S28. Part 8 of the procedure was then completed successfully. The entire surveillance was successfully completed at 1627 hours.
The switches identified were those needed for Section RE" of the procedure and were associated with LD-MON-28.
NRC FORM SBBA                                                                                                                 'V.ST CPOI 1988 f20-SS9 (9 83)
The procedure was deviated to call out the correct switches, LD-RMS-S18 and LD-RMS-S28.
 
Part 8 of the procedure was then completed successfully.
RC Farm 366A                                                                                                             U.S. NUCLEAR REGULATORY COMMISSION 94)3)
The entire surveillance was successfully completed at 1627 hours.NRC FORM SBBA (9 83)'V.ST CPOI 1988 f20-SS9 RC Farm 366A 94)3)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION APPROVEO OMB NO.3160&)04 EXPIRES: 8/31/88 FACILITY NAME (1)OOCKET NUMBER (2)YEAR LER NUMBER (6)SEGVSNZIAL NVMSSR REVISION NVMSSR PAGE (3)Washin ton Nuclear Plant-Unit 2<<<<o 3 9 7 TEXT (If more space js rerfoiied, rrse additional ffRC Form 3664's)(12)8 9 0 2 9 0 0 0 3 OF The RCIC System was returned to Standby Status at 1039 hours.The RNCU system was brought back into service at 1515 hours after the required verification of pump bowl temperatures prior to pump restart.There was a delay in gaining access to the RKU, pump room caused by an inadvertently removed step off pad.Further Evaluation and Corrective Action A.Further Evaluation 1.This event is being reported per the requirements of 10CFR50.73(a)(2)(iv) as an"event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF)...2.There were no structures, components or systems that were inoperable at the start of this event that contributed to the event.3.The root cause of this event was less than adequate attention to detail in the preparation and review of the surveillance procedure.
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                                       APPROVEO OMB NO. 3160&)04 EXPIRES: 8/31/88 FACILITY NAME (1)                                                                 OOCKET NUMBER (2)             LER NUMBER (6)                       PAGE (3)
A contributing factor was the fact that the surveillance procedure was drafted and reviewed during the outage when schedule and time constraints are very intense.a)The initial draft of the procedures by the Project Engineer had the correct by-pass switches called out for LD-MON-1B.
YEAR    SEGVSNZIAL      REVISION NVMSSR        NVMSSR Washin ton Nuclear TEXT (Ifmore space js rerfoiied, rrse additional Plant - Unit ffRC Form 3664's) (12) 2      <<<<            o 3  9 7  8 9     0 2     9         0 0 0         3 OF The RCIC System was                               returned to Standby Status at 1039 hours. The RNCU system was brought back into service at 1515 hours after the required verification of pump bowl temperatures prior to pump restart.                                       There was a delay in gaining access to the RKU, pump room caused by an inadvertently removed step off pad.
A subsequent revision to the draft by the I&C Engineer caused the incorrect switches to be placed in Section"B" of the procedure.
Further Evaluation and Corrective Action A.         Further Evaluation
b)c)Reviews of this revision by the Project Engineer and the I&C Engineers did not discover the deficiency in Section RBU.A contributing factor to this less than adequate review was the ongoing outage which started in mid April when the I&C Engineers had a large number of competing outage tasks to perform.Temporary Test Procedure 8.3.139, WNP-2 Leak Detection Moni tor Preoperational Test was written in May 1989 to check out operation of the NUNC Leak Detection Moni tors being installed during the refueling outage.The test included the performance of TSS Test 7.4.3.2.1.6 as part of its procedure.
: 1.           This event is being reported per the requirements of 10CFR50.73(a)(2)(iv) as an "event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF). . .
The test was completed on June 10, 1989 without discovering the error associated with the bypass switches associated with LD-MON-1B.
: 2.           There were no                     structures,   components     or systems   that   were       inoperable at the     start of this event that contributed to the event.
A review of the test showed that the procedure calls for the bypassing of all ten isolation functions associated with the Leak Detection System.These bypasses were in place prior to and during the performance of the surveillance test part of the procedure.
: 3.           The     root cause of this event was less than adequate attention to detail in the preparation and review of the surveillance procedure. A contributing factor was the fact that the surveillance procedure was drafted and reviewed during the outage when schedule and time constraints are very intense.
Thus, individual operation of the bypass switches in the manner they were intended to be used in the subsequent surveillance were not verified during the performance of the test.d)The review of the surveillance contained in the test procedure should have identified and corrected the error with the bypass switches.NRC FORM 36SA (94)31'V.S.CPOI 1966 920$69r00010 NRC Form 388A (94)3)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION APPROVEO OM8 NO, 3150&104 EXPIRES: 8/31/88 FACILITY NAME (1)OOCKET NUMBER (2)LER NUMBER (8)PAGE (3)YEAR 99.v SEOI/ENTIAL NUMBER REVISION NUMBER Washin ton Nuclear Plant-Unit 2 TEXT///moro 4poco/4/or/IIPod.
a)         The     initial draft of the procedures by the Project Engineer had the correct by-pass switches called out for LD-MON-1B. A subsequent revision to the draft by the I&C Engineer caused the incorrect switches to be placed in Section "B" of the procedure.
Ir>>odd/dorM//VRC Form SSSAS/(17)0 5 0 0 0 3 9 7 8 9 0 2 9 000 4 OF 0 4 B.Further Corrective Action 1.Maintenance Engineers will receive additional training on the use of the"Maintenance Department Procedure Writers Guide." 2.Plant Procedure PPM 1.5.7, Post Maintenance/Modification Testing will be modified.Where practical, in situations where a plant modification resul ts in a change to an Operations or Surveillance Test it will be performed as a Section of the preoperational test.3.Project management procedures (1.16 Series)will be modified to require more advance planning for plant modification work.Where practical, draft revisions to test and surveillance procedures will be scheduled and completed prior to the start of the refueling outage.This will provide improved management visibility of the procedure/software modification workload allowing appropriate time for preparation and review.Safety Si nificance There is no safety significance associated with the event.During all tests that were performed associated with the installation of the new leak detection equipment the equipment and the downstream logic performed its safety function as designed.This event posed no threat to the health and safety of the public or Plant personnel.
b)         Reviews           of this revision           by the Project Engineer and the I&C Engineers             did   not   discover the deficiency in Section RBU.                                   A contributing factor to this less than adequate review was the ongoing outage which started in mid April when the I&C Engineers had a large number of competing outage tasks to perform.
Similar Events A review of previous LERs identified 87-009 as a similar event.It involved an ESF actuation caused by an oversight associated with a procedure revision as a result of a plant modification.
c)          Temporary Test Procedure                     8.3.139, WNP-2 Leak Detection Moni tor Preoperational Test was written in May 1989 to check out operation of the NUNC Leak Detection Moni tors being installed during the refueling outage. The test included the performance of TSS Test 7.4.3.2.1.6 as part of its procedure. The test was completed on June 10,     1989 without discovering the error associated                         with the bypass switches associated with LD-MON-1B. A review of the test showed that the procedure calls for the bypassing of all ten isolation functions associated with the Leak Detection System.                         These bypasses were in place prior to and during the performance of the surveillance test part of the procedure.                     Thus, individual operation of the bypass switches in the manner they were intended to be used in the subsequent surveillance were not verified during the performance of the test.
Corrective action was very specific to the event.EIIS Information Text Reference EI IS Reference System Component Reactor Water Cleanup Reactor Core Isolation Cooling Nuclear Steam Supply Shutoff System RWCU-V-1 RWCU-P-lA Leak Detection RC IC-V-63 LD-MON-18 LD-MON-28 LO-RMS-53C LD-RMS-53D LD-RMS-548 LD-RMS-518 LD-RMS-528 CE BN BD CE CE IJ BN IJ IJ IJ IJ IJ IJ IJ V P V MON MON HS HS HS HS HS NRC FORM 300A 19 33)*V.ST CPOI 1988 520-589 000)0}}
d)           The review of the surveillance contained in the test procedure should have identified and corrected the error with the bypass switches.
NRC FORM 36SA                                                                                                                         'V.S. CPOI 1966 920 $ 69r00010 (94)31
 
NRC Form 388A                                                                                                         U.S. NUCLEAR REGULATORY COMMISSION (94)3)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION                                     APPROVEO OM8 NO, 3150&104 EXPIRES: 8/31/88 FACILITY NAME (1)                                                       OOCKET NUMBER (2)                 LER NUMBER (8)                       PAGE (3)
YEAR       SEOI/ENTIAL      REVISION 99 .v   NUMBER         NUMBER Washin ton Nuclear                       Plant - Unit       2  0  5  0  0    0 3  9 7  8 9          0 2     9        000          4 OF 0      4 TEXT ///moro 4poco /4/or/IIPod. Ir>> odd/dorM//VRC Form SSSAS/ (17)
B.         Further Corrective Action
: 1.         Maintenance Engineers will receive additional training on the use                                           of the "Maintenance Department Procedure Writers Guide."
: 2.         Plant Procedure PPM 1.5.7, Post Maintenance/Modification Testing will be modified. Where practical, in situations where a plant modification resul ts in a change to an Operations or Surveillance Test performed as a Section of the preoperational test.
it      will be
: 3.         Project management procedures (1.16 Series) will be modified to require more advance planning for plant modification work. Where practical, draft revisions to test and surveillance procedures will be scheduled and completed prior to the start of the refueling outage.                                 This will provide improved management visibility of the procedure/software                                         modification workload allowing appropriate time for preparation and review.
Safety Si nificance There         is     no     safety significance associated               with the event. During all tests that were performed associated with the installation                                 of the new leak detection equipment the equipment and the downstream logic performed                                 its safety function as designed.
This event posed no threat to the health and safety of the public or Plant personnel.
Similar Events A   review of previous LERs identified 87-009 as a similar event. It involved an ESF actuation caused by an oversight associated with a procedure revision as a result of a plant modification.                           Corrective action was very specific to the event.
EIIS Information Text Reference                                                                           EI IS Reference System             Component Reactor Water Cleanup                                                                             CE Reactor Core Isolation Cooling                                                                     BN Nuclear Steam Supply Shutoff System                                                                 BD RWCU-V-1                                                                                           CE                      V RWCU-P-lA                                                                                         CE                      P Leak Detection                                                                                     IJ RC IC- V-63                                                                                         BN                      V LD-MON-18                                                                                           IJ                  MON LD-MON-28                                                                                           IJ                  MON LO-RMS-53C                                                                                         IJ                    HS LD-RMS-53D                                                                                         IJ                    HS LD-RMS-548                                                                                         IJ                    HS LD-RMS-518                                                                                         IJ                    HS LD-RMS-528                                                                                           IJ                   HS NRC FORM 300A                                                                                                                   *V.ST CPOI 1988 520-589 000)0 19 33)}}

Latest revision as of 07:59, 4 February 2020

LER 89-029-00:on 890703,RWCU & RCIC Sys Isolation Occurred When RWCU-V-1 Closed as Part of Group 7 Nuclear Steam Supply Shutoff Sys Isolation.Caused by Inadequate Preparation & Review of Surveillance Test procedure.W/890801 Ltr
ML17285A657
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 08/01/1989
From: Fies C, Powers C
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-89-029, LER-89-29, NUDOCS 8908140101
Download: ML17285A657 (6)


Text

F I P~

ACCELERATED l%TR1BUTION DEMOYSOXTIOY SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:8908140101 DOC.DATE: 89/08/01 NOTARIZED: NO DOCKET FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH. NAME AUTHOR AFFILIATION FIES,C.L. Washington Public Power Supply System POWERS,C.M. Washington Public Power Supply System RECIPIENT AFFILIATION NOTES';

RECIP.NAME

SUBJECT:

LER 89-029-00:on 890703,RWCU & RCIC sys isolations caused by I inadequate test/surveillance procedure.

W/8 ltr.

DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR 3Incident ENCL I SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), Rpt, etc.

RECIPIENT COPIES RECIPIENT COPIES h ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 1 PD5 PD 1 1 D, SAMWORTH,R 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLIE 1 1 AEOD/DOA 1 1 AEOD/DS P/TPAB 1 1 AEOD/ROAB/DS P 2 2 DEDRO 1 1 IRM/DCTS/DAB 1 1 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB .8D 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D 1 1 NRR/DLPQ/HFB 10 1 1 NRR/DLPQ/PEB 10 1 1 NRR/DOEA/EAB 11 1 1 RPB 10 2 2 NUDOCS-ABSTRACT 1 1 REG 02 1 1 RES/DSIR/EIB 1 1 RES/DSR/PRAB 1 1 RGN5 FILE 01 1 1 EXTERNAL: EG&G WILLIAMS,S 4 4 FORD BLDG HOY,A 1 1 R L ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC MAYS,G 1 1 I NSIC MURPHY,G.A 1 1 S

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HELP US IO RECCE %ASTE! CXNTACI'HE DOQ3MENI'GHIBOL DESK, KXM Pl-37 (EXT. 20079) K) ELIKQRTH KKR NMB FR% MPHtZBUTZCH LISTS FOR DOCUMEKIS RXJ DGNPT NEZDt FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF. COPIES REQUIRED: LTTR 41 ENCL 41

ti WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ 3000 George washington 11'ay ~ Richland, 11'ashinglon 99352 Docket No. 50-397 August 1, 1989 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555

Subject:

NUCLEAR PLANT NO. 2 LICENSEE EVENT REPORT NO.89-029

Dear Sir:

Transmitted herewith is Licensee Event Report No.89-029 for the WNP-2 Plant.

This report is submitted in response to the report requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrence.

Very truly yours, C.M. Powers (M/D 927M)

WNP-2 Plant Manager CMP:lg

Enclosure:

Licensee Event Report No.89-029 cc: Mr. John B. Martin, NRC - Region V Mr. C.J. Bosted, NRC Site (M/D 901A)

INPO Records Center - Atlanta, GA Ms. Dottie Sherman, ANI Mr. D.L. Williams, BPA (M/D 399) 35'0=140i %9080i pop ADOCK 05000-~97 pDC S

NAC Form 388 U.S. NUCLEAR REGULATORY COMMISSION (9.8 3 I APPAOVEO OMB NO, 31500104 EXPIAESI BI3)i88 LICENSEE EVENT REPORT ILER)

FACILITY NAME (1) DOCKET NUMBER (2) PAGE 13)

Washin ton Nuclear Plant - Unit 2 0 5 0 0 03 97 > oF0 4

""'"'Reactor Water Cleanup and Reactor Core Isolation Cooling System Isolations caused by Inade uate Test/Surveillance Procedure EVFNT DATE 15) LEA NUMBER (8) REPORT DATE (7) OTHER FACILITIES INVOLVED (SI SEQUENTIAL RE"G~ OAY YEAR FACILITYNAMES DOCKET NUMBER(SI MONTH DAY YE.AR YEAR NUM8% R NUMBER MONT~

0 5 0 0 0 0 7 0 3 8 9 8 9 029 00 08 01 8 9 0 5 0 0 0 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR (): ICnece one or more of tne foriowintl Ill)

OPF RATING ~

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On July 3, 1989 at 1022 hours a Reactor Water Cleanup (RWCU) System Isolation occured when RWCU-V-1 closed as part of a Group 7 Nuclear Steam Supply Shutoff System (NS4) isolation. At 1026 hours a similar Reactor Core Isolation Cooling (RCIC) System isolation occurred when RCIC-V-63 closed. Both these isolations occurred as a result of Technical Specification Surveillance Testing per Plant Procedure 7.4.3.2. 1.6, Leak Detection Monitor Division II Channel Calibration (CC )/Channel Functional Test (CFT).

The root cause of this ESF actuation was less than adequate preparation and review of a surveillance test procedure which had been rewritten to support a plant modification.

This modification had recently been completed during a refueling outage.

Immediate corrective action consisted of prompt action by the plant operators to return the impacted systems to service. The surveillance test procedure was also corrected and deviated.

Further corrective action will be taken by plant maintenance to strengthen their procedure modification process. In addition, testing and project management procedures will be modified to require, when practical, a more complete check of the modified surveillance prior to plant operation and to allow more time for review and preparation of procedures associated with outage work.

Since all ESF systems responded as designed there is no safety significance associated with this event.

NRC Form 388 (9 83)

NRC Form 388A U.S. NUCLEAR REGULATORY COMMISSION (9.83)

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO OMB NO, 3150&104 EXPIRES: 8/31/8$

FACILITY NAME (() DOCKET NUMBER (2) LER NUMBER (8) PAGE (3)

YEAR SEOUENTIAL REVISION NUMBER NUMBER shin ton Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 8 9 0 2 9 0 0 0 2 OF TEXT ///mOre epeee/4 rei/Oiied. Fee eddr'O'OOe/NRC FOnn 3SSA'4) (11)

Plant Conditions a) Power Level - 83%

b) Plant Mode - 1 (Power Operation)

Event Descri tion On July 3, 1989 at 1022 hours0.0118 days <br />0.284 hours <br />0.00169 weeks <br />3.88871e-4 months <br /> and again at 1026 hours0.0119 days <br />0.285 hours <br />0.0017 weeks <br />3.90393e-4 months <br /> primary containment isolation valves closed on an isolation signal. Both these events occurred during power ascension following the fourth refueling outage. The first event, a Reactor Water Cleanup (RWCU) System Isolation occurred when RI4:U-V-1 (the inboard containment isolation valve between the reactor vessel and the RNCU System) closed on an NS4 RWCU area high temperature simulated signal causing the operating pump (RWCU-P-lA) to trip. Plant Operators immediately began an investigation into the cause of the isolation which can be the result of any of several events. During their investigation, at 1026 hours0.0119 days <br />0.285 hours <br />0.0017 weeks <br />3.90393e-4 months <br />, a Reactor Core Isolation Cooling (RCIC) System Isolation occurred on an RCIC Pump Room High Temperature simulated signal causing RCIC-V-63 to close. At that time plant operators traced both isolations to Technical Specification Surveillance (TSS) Testing on the Leak Detection System which had been in progress since 0729 hours0.00844 days <br />0.203 hours <br />0.00121 weeks <br />2.773845e-4 months <br />. The specific test being performed was TSS 7.4.3.2. 1.6, Leak Detection Monitor Division II Channel Calibration (CC )/Channel Functional Test (CFT) for Leak Detection Monitors LD-MON-18 and LD-MON-28. The Instrument ana Control ( IKC) Technicians had completed Section "AR of the procedure which calibrates LD-MON-18, and were proceeding with Section "BR which tests the relay trip logic on LD-MON-18. Steps 1 and 2 of Section RBR of the pr'ocedure required bypass key locks for LD-RMS-S3C, LD-RMS-S3D and LD-RMS-S48, to be in the test position. The test position should have placed the downstream trip logic for LD-MON-18 in a configuration where relays RKlBR and RK28R could be tested without an ESF actuation. The I8C Technicians, following procedures as written, proceeded through step 10 of the procedure which simulated a high temperature in the RKU pump and heat exchanger areas, places the leak detection RKlR relay in the RTrip" condition and tests for the proper functioning of the downstream RK1BR relay. With these steps complete they proceeded with steps ll through 15 of the procedure which simulates a high RCIC Equipment Area or Differential Temperature, places the Leak detection RK2" relay in the "trip" condition and tests for proper functioning of the downstream RK28R relay. The Control Room Operators stopped the surveillance testing at this time since it had obviously caused the isolations.

Immediate Corrective Action Investigation by the Plant Operators and I8C Technicians revealed that the wrong switches had been called out in Steps 1 and 2 of Section RBR of the procedure.

Consequently the testing of LD-MON-18 caused the RWCU and RCIC isolation. The switches identified were those needed for Section RE" of the procedure and were associated with LD-MON-28. The procedure was deviated to call out the correct switches, LD-RMS-S18 and LD-RMS-S28. Part 8 of the procedure was then completed successfully. The entire surveillance was successfully completed at 1627 hours0.0188 days <br />0.452 hours <br />0.00269 weeks <br />6.190735e-4 months <br />.

NRC FORM SBBA 'V.ST CPOI 1988 f20-SS9 (9 83)

RC Farm 366A U.S. NUCLEAR REGULATORY COMMISSION 94)3)

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO OMB NO. 3160&)04 EXPIRES: 8/31/88 FACILITY NAME (1) OOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

YEAR SEGVSNZIAL REVISION NVMSSR NVMSSR Washin ton Nuclear TEXT (Ifmore space js rerfoiied, rrse additional Plant - Unit ffRC Form 3664's) (12) 2 <<<< o 3 9 7 8 9 0 2 9 0 0 0 3 OF The RCIC System was returned to Standby Status at 1039 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.953395e-4 months <br />. The RNCU system was brought back into service at 1515 hours0.0175 days <br />0.421 hours <br />0.0025 weeks <br />5.764575e-4 months <br /> after the required verification of pump bowl temperatures prior to pump restart. There was a delay in gaining access to the RKU, pump room caused by an inadvertently removed step off pad.

Further Evaluation and Corrective Action A. Further Evaluation

1. This event is being reported per the requirements of 10CFR50.73(a)(2)(iv) as an "event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF). . .
2. There were no structures, components or systems that were inoperable at the start of this event that contributed to the event.
3. The root cause of this event was less than adequate attention to detail in the preparation and review of the surveillance procedure. A contributing factor was the fact that the surveillance procedure was drafted and reviewed during the outage when schedule and time constraints are very intense.

a) The initial draft of the procedures by the Project Engineer had the correct by-pass switches called out for LD-MON-1B. A subsequent revision to the draft by the I&C Engineer caused the incorrect switches to be placed in Section "B" of the procedure.

b) Reviews of this revision by the Project Engineer and the I&C Engineers did not discover the deficiency in Section RBU. A contributing factor to this less than adequate review was the ongoing outage which started in mid April when the I&C Engineers had a large number of competing outage tasks to perform.

c) Temporary Test Procedure 8.3.139, WNP-2 Leak Detection Moni tor Preoperational Test was written in May 1989 to check out operation of the NUNC Leak Detection Moni tors being installed during the refueling outage. The test included the performance of TSS Test 7.4.3.2.1.6 as part of its procedure. The test was completed on June 10, 1989 without discovering the error associated with the bypass switches associated with LD-MON-1B. A review of the test showed that the procedure calls for the bypassing of all ten isolation functions associated with the Leak Detection System. These bypasses were in place prior to and during the performance of the surveillance test part of the procedure. Thus, individual operation of the bypass switches in the manner they were intended to be used in the subsequent surveillance were not verified during the performance of the test.

d) The review of the surveillance contained in the test procedure should have identified and corrected the error with the bypass switches.

NRC FORM 36SA 'V.S. CPOI 1966 920 $ 69r00010 (94)31

NRC Form 388A U.S. NUCLEAR REGULATORY COMMISSION (94)3)

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO OM8 NO, 3150&104 EXPIRES: 8/31/88 FACILITY NAME (1) OOCKET NUMBER (2) LER NUMBER (8) PAGE (3)

YEAR SEOI/ENTIAL REVISION 99 .v NUMBER NUMBER Washin ton Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 8 9 0 2 9 000 4 OF 0 4 TEXT ///moro 4poco /4/or/IIPod. Ir>> odd/dorM//VRC Form SSSAS/ (17)

B. Further Corrective Action

1. Maintenance Engineers will receive additional training on the use of the "Maintenance Department Procedure Writers Guide."
2. Plant Procedure PPM 1.5.7, Post Maintenance/Modification Testing will be modified. Where practical, in situations where a plant modification resul ts in a change to an Operations or Surveillance Test performed as a Section of the preoperational test.

it will be

3. Project management procedures (1.16 Series) will be modified to require more advance planning for plant modification work. Where practical, draft revisions to test and surveillance procedures will be scheduled and completed prior to the start of the refueling outage. This will provide improved management visibility of the procedure/software modification workload allowing appropriate time for preparation and review.

Safety Si nificance There is no safety significance associated with the event. During all tests that were performed associated with the installation of the new leak detection equipment the equipment and the downstream logic performed its safety function as designed.

This event posed no threat to the health and safety of the public or Plant personnel.

Similar Events A review of previous LERs identified 87-009 as a similar event. It involved an ESF actuation caused by an oversight associated with a procedure revision as a result of a plant modification. Corrective action was very specific to the event.

EIIS Information Text Reference EI IS Reference System Component Reactor Water Cleanup CE Reactor Core Isolation Cooling BN Nuclear Steam Supply Shutoff System BD RWCU-V-1 CE V RWCU-P-lA CE P Leak Detection IJ RC IC- V-63 BN V LD-MON-18 IJ MON LD-MON-28 IJ MON LO-RMS-53C IJ HS LD-RMS-53D IJ HS LD-RMS-548 IJ HS LD-RMS-518 IJ HS LD-RMS-528 IJ HS NRC FORM 300A *V.ST CPOI 1988 520-589 000)0 19 33)