05000335/FIN-2012007-04: Difference between revisions

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{{finding
{{finding
| title = Failure To Implement Vendor Technical Manual Recommendations To Inspect Edg Immersion Heaters
| title = Failure to Implement Vendor Technical Manual Recommendations to Inspect EDG Immersion Heaters
| docket = 05000335, 05000389
| docket = 05000335, 05000389
| inspection report = IR 05000335/2012007
| inspection report = IR 05000335/2012007
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| identified by = Self-Revealing
| identified by = Self-Revealing
| Inspection procedure = IP 71152
| Inspection procedure = IP 71152
| Inspector = A Butcavage, D Rich, L Lake, R Reyes, T Hoegg, Hopper J, Reyes J, Sowa R, Ng R, Taylor T, Chandler T, Morrisse
| Inspector = A Butcavage, D Rich, L Lake, R Reyes, T Hoegg, Hopperj Reyes, J Sowa, R Ng, R Taylor, T Chandler, T Morrissey
| CCA = H.5
| CCA = H.5
| INPO aspect = WP.1
| INPO aspect = WP.1
| description = A self-revealing potentially greater than Green AV of Technical Specification 6.8.1.a was identified for failure to establish adequate maintenance procedures associated with the emergency diesel generator (EDG) system. Specifically, station personnel failed to establish preventative maintenance inspections of diesel immersion heaters in accordance with vendor manual recommendations. As a result, the Unit 1 1A EDG was immediately rendered inoperable for 43.5 hours due to a failed immersion heater that resulted in a leak of the 1A2 EDG jacket water system. The licensee replaced the heater with an onsite spare. The finding was considered more than minor because it impacted the Reactor Safety Mitigating Systems Cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences and affected the cornerstone attribute of equipment performance. The issue was placed in the licensees corrective action program as condition report 1751214. The cause of this finding was related to the Work Control component of the Human Performance cross-cutting area due to the failure to plan work activities to ensure long term equipment availability. Specifically, maintenance scheduling was more reactive than preventative.
| description = A self-revealing potentially greater than Green AV of Technical Specification 6.8.1.a was identified for failure to establish adequate maintenance procedures associated with the emergency diesel generator (EDG) system. Specifically, station personnel failed to establish preventative maintenance inspections of diesel immersion heaters in accordance with vendor manual recommendations. As a result, the Unit 1 1A EDG was immediately rendered inoperable for 43.5 hours due to a failed immersion heater that resulted in a leak of the 1A2 EDG jacket water system. The licensee replaced the heater with an onsite spare. The finding was considered more than minor because it impacted the Reactor Safety Mitigating Systems Cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences and affected the cornerstone attribute of equipment performance. The issue was placed in the licensees corrective action program as condition report 1751214. The cause of this finding was related to the Work Control component of the Human Performance cross-cutting area due to the failure to plan work activities to ensure long term equipment availability. Specifically, maintenance scheduling was more reactive than preventative.
}}
}}

Latest revision as of 20:47, 20 February 2018

04
Site: Saint Lucie NextEra Energy icon.png
Report IR 05000335/2012007 Section 4OA2
Date counted Jun 30, 2012 (2012Q2)
Type: NCV: Green
cornerstone Mitigating Systems
Identified by: Self-revealing
Inspection Procedure: IP 71152
Inspectors (proximate) A Butcavage
D Rich
L Lake
R Reyes
T Hoegg
Hopperj Reyes
J Sowa
R Ng
R Taylor
T Chandler
T Morrissey
CCA H.5, Work Management
INPO aspect WP.1
'