ENS 52655: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by Mark Hawes)
 
(Created page by program invented by StriderTol)
 
Line 16: Line 16:
| event date = 03/31/2017 11:55 EDT
| event date = 03/31/2017 11:55 EDT
| last update date = 03/31/2017
| last update date = 03/31/2017
| title = Pressure Suppression Pool Declared Inoperable Due To Torus High Water Level
| title = Pressure Suppression Pool Declared Inoperable Due to Torus High Water Level
| event text = On March 31, 2017 at 1155 hours [EDT], with the reactor at 97% core thermal power and steady state conditions, operators inadvertently caused water level to rise in the Pressure Suppression Pool (TORUS). Pilgrim Nuclear Power Station (PNPS) was restoring normal system valve line-ups after performing flushing of the suction piping of the Core Spray system in accordance with station procedures. During the process of restoring the appropriate valve line-ups, water was inadvertently transferred to the TORUS from the Condensate Storage Tank. The cause of the event is understood.
| event text = On March 31, 2017 at 1155 hours [EDT], with the reactor at 97% core thermal power and steady state conditions, operators inadvertently caused water level to rise in the Pressure Suppression Pool (TORUS). Pilgrim Nuclear Power Station (PNPS) was restoring normal system valve line-ups after performing flushing of the suction piping of the Core Spray system in accordance with station procedures. During the process of restoring the appropriate valve line-ups, water was inadvertently transferred to the TORUS from the Condensate Storage Tank. The cause of the event is understood.
The Technical Specification (TS) Limiting Condition for Operation (LCO) Action Statement (AS) 3.7.A.5 was entered. The LCO AS was exited at 1540 when TORUS water level was restored to the limits specified in LCO's 3.7.A.1.b and 3.7.A.1.m. Because the TORUS was declared inoperable, PNPS is providing an 8-hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(v)(D), an event or condition that could have prevented fulfillment of a safety function needed to mitigate the consequences of an accident.
The Technical Specification (TS) Limiting Condition for Operation (LCO) Action Statement (AS) 3.7.A.5 was entered. The LCO AS was exited at 1540 when TORUS water level was restored to the limits specified in LCO's 3.7.A.1.b and 3.7.A.1.m. Because the TORUS was declared inoperable, PNPS is providing an 8-hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(v)(D), an event or condition that could have prevented fulfillment of a safety function needed to mitigate the consequences of an accident.

Latest revision as of 21:43, 1 March 2018

ENS 52655 +/-
Where
Pilgrim
Massachusetts (NRC Region 1)
Reporting
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
Time - Person (Reporting Time:+3.32 h0.138 days <br />0.0198 weeks <br />0.00455 months <br />)
Opened: Kenneth Gracia
19:14 Mar 31, 2017
NRC Officer: Vince Klco
Last Updated: Mar 31, 2017
52655 - NRC Website
Loading map...