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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:' @ 4 004 -
    *
UNITED STATES
          /.' @ 4 004'%'~
/.
                        -                NUCLEAR REGULATORY COMMISSION
'%'~
                                                        REGION il
NUCLEAR REGULATORY COMMISSION
      .' [ ~           o
*
                                                101 MARIETTA STREET, N.W.
.' [ ~
        5              j.
REGION il
        *            't                       AT LANTA, oEoRGI A 30323
o
          *%,         ,/
5
              .....
j.
                Report Numbers:     50-321/88-05 and 50-366/88-05
101 MARIETTA STREET, N.W.
                Licensee: Georgia Power Company
't
                            P. O. Box 4545
AT LANTA, oEoRGI A 30323
                            Atlanta, GA 30302
*
                Docket Numbers:     50-321 and 50-366                   License Numbers:   DPR-57 and NPF-5
*%,
                Facility Name:     Hatch 1 and 2
,/
                Inspection Dates: January 23 - February 19, 1988
.....
                Inspectors:     D )[               adv [m
Report Numbers:
                            Peter Holmes 'Ra , Senior Resi/ent Inspector
50-321/88-05 and 50-366/88-05
                                                                                              /
Licensee: Georgia Power Company
                                                                                          Date Signed
P. O. Box 4545
                                                      &             W
Atlanta, GA 30302
Docket Numbers:
50-321 and 50-366
License Numbers:
DPR-57 and NPF-5
Facility Name:
Hatch 1 and 2
Inspection Dates: January 23 - February 19, 1988
Inspectors:
D )[
adv [m
/
Peter Holmes 'Ra , Senior Resi/ent Inspector
Date Signed
&
W
JohnE.Menning,ResidentIn@ector
Date Sitned
,
,
                            JohnE.Menning,ResidentIn@ector                                Date Sitned
AccompanyingPersgnel:/RanallA.Mussr
                AccompanyingPersgnel:/RanallA.Mussr
$/7!W
                Approved by:    !Muk/         / WWV1             d--
!Muk/
                              Marvin \f/. Sinkule, Chief, Project Section 3B
/ WWV1
                                                                                          $/7!W
d--
                                                                                          Date Signed
Approved by:
                              Division of Reactor Projects
Marvin \\f/. Sinkule, Chief, Project Section 3B
                                                      SUMMARY
Date Signed
                Scope:     This routine inspection was conducted at the site in the areas of
Division of Reactor Projects
                Licensee Action on Previous Enforcement Matters, Operational Safety
SUMMARY
                Verification, Maintenance Observation,             Plant Modification,     Surveillance
Scope:
                Observation,     Radiological     Protection,       Physical   Security,   Reportable
This routine inspection was conducted at the site in the areas of
                Occurrences, and Reactor Operating Events.
Licensee Action
                Results:   Two violations were identified.
on
                  880330o068 8s0310
Previous
                  PDR     ADOCK 0500o321
Enforcement Matters,
                  Q                   DCD
Operational
  t_
Safety
Verification, Maintenance Observation,
Plant Modification,
Surveillance
Observation,
Radiological
Protection,
Physical
Security,
Reportable
Occurrences, and Reactor Operating Events.
Results:
Two violations were identified.
880330o068 8s0310
PDR
ADOCK 0500o321
Q
DCD
t_


- _ __ _       _ _ _ _ -
- _ __ _
          .
_ _ _ _ -
        -              ~
.
.
                            '
-
            .
~
                                  .
.
                                                        REPORT DETAILS
'
            1.             Persons Contacted
.
                            Licensee. Employees
.
                            T. Beckham, Vice President-Plant Hatch
REPORT DETAILS
                          *C. Coggin, Training and Emergency Preparedness Manager
1.
                            D. Davis, Manager General Support
Persons Contacted
                                                                    ~
Licensee. Employees
                            J. - Fitzsimmons, Nuclear Security Manager
T. Beckham, Vice President-Plant Hatch
                          *P. Fornel, Maintenance Manager
*C. Coggin, Training and Emergency Preparedness Manager
                          *0. Fraser, Site Quality Assurance (QA) Manager
D. Davis, Manager General Support
                          *M. Googe, Outages and Planning Manager
~
                          *H. Nix, Plant Manager
J. - Fitzsimmons, Nuclear Security Manager
                          *T. Powers, Engineering Manager
*P. Fornel, Maintenance Manager
                          *D. Read, Plant Support Manager
*0. Fraser, Site Quality Assurance (QA) Manager
                          *H. Sumner, Operations Manager
*M. Googe, Outages and Planning Manager
                          *S. Tipps, Nuclear Safety and Compliance Manager
*H. Nix, Plant Manager
                                                      .
*T. Powers, Engineering Manager
                            R.-Zavadoski, Health Physics and Chemistry Manager
*D. Read, Plant Support Manager
                            Other licensee employees contacted included technicians, operators,
*H. Sumner, Operations Manager
                            mechanics, security force members and office personnel.
*S. Tipps, Nuclear Safety and Compliance Manager
                            NRC Resident Inspectors
.
                          *P. Holmes-Ray
R.-Zavadoski, Health Physics and Chemistry Manager
                          *J. Menning
Other licensee employees contacted included technicians, operators,
                          *R. Musser
mechanics, security force members and office personnel.
                            NRC management on site during inspection period:
NRC Resident Inspectors
                            M. Sinkule, Chief, Project Section 38, Region II
*P. Holmes-Ray
                          * Attended exit interview
*J. Menning
            2.             Exit Interview (30703)
*R. Musser
                            The inspection scope and findings were summarized on February 19, 1988,
NRC management on site during inspection period:
                            with those persons indicated in paragraph 1 above. The licensee did not
M. Sinkule, Chief, Project Section 38, Region II
                            identify as proprietary any of the material provided to or reviewed by the
* Attended exit interview
                            inspectors during this inspection. The licensee acknowledged the findings
2.
                            and took no exception.
Exit Interview (30703)
                            Item Number           Status               Description / Reference Paragraph
The inspection scope and findings were summarized on February 19, 1988,
                            321/88-05-01         Open                 VIOLATION - Bypassing of APRM
with those persons indicated in paragraph 1 above.
                                                                      Downscale Scram Inputs
The licensee did not
                                                                      (paragraph 5)
identify as proprietary any of the material provided to or reviewed by the
inspectors during this inspection. The licensee acknowledged the findings
and took no exception.
Item Number
Status
Description / Reference Paragraph
321/88-05-01
Open
VIOLATION - Bypassing of APRM
Downscale Scram Inputs
(paragraph 5)


  _ _ _ _ _ - - _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _                         . - _ _ _ _ - _ _ - _ - _ - _ _ _ - _ _ _ _ _ _ _ _ - _ - _ - - _ - _ _ _ _ _ _ _ _ _ _                                     _ _ _ _ _ .
_ _ _ _ _ - - _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _
                                                  .
. - _ _ _ _ - _ _ - _ - _ - _ _ _ - _ _ _ _ _ _ _ _ - _ - _ - - _ - _ _ _ _ _ _ _ _ _ _
            .
_ _ _ _ _ .
                                              .
.
                                                      .
.
        .,
.
                                                                *
.
                                                        -
.,
                                                                                                                                                                  2                                                :
2
                                                                                                                                                                                                                    ;
:
                                                                                                                                                                                                                    .
*
                                                          Item Number                                                             Status                           Description / Reference Paragraph
-
                                                          cont'd
;
                                                                                                                                                                    VIOLATION - Inadequate MWO for
.
                                                                                                                                                                                                                    '
Item Number
4                                                         321/88-05-04                                                          Open
Status
                                                                                                                                                                    Vacuum Breaker Maintenance
Description / Reference Paragraph
                                                                                                                                                                    (paragraph 8)
cont'd
321/88-05-04
Open
VIOLATION - Inadequate MWO for
'
4
Vacuum Breaker Maintenance
(paragraph 8)
9
9
                                                          321,366/86-41-01'                                                     Closed                             VIOLATION - Failure to follow
321,366/86-41-01'
                                                                                                                                                                    plant procedures which
Closed
                                                                                                                                                                    resulted in partial loss of water
VIOLATION - Failure to follow
                                                                                                                                                                    from the fuel pools (paragraph 3)              '
plant procedures which
                                                          321,366/88-05-02                                                        Open                              URI - Leak Testing of Test
resulted in partial loss of water
                                                                                                                                                                    Solenoid Valves (paragraph 5)
                                                          321/88-05-03                                                            Open                              URI - Inadequate APRM
                                                                                                                                                                    Surveillance (paragraph 8)
                                                    3.    Licensee Action on Previous Enforcement Matters (92702)
                                                          (Closed) Violation 321,366/86-41-01, Failure to follow plant procedures
                                                                                                                                                                                                                    '
                                                          which resulted in a partial loss of water from the fuel pools.                                                                        The GPC          i
                                                          letter of response dated May 8,1987, was reviewed. Licensee corrective
                                                          action involved replacement of the transfer canal inflatable seal assembly,
                                                          an enhancement of the leak detection system (implemented by DCR 87-99),
                                                          the addition of redundant air supplies to the inflatable seal assembly and
                                                          annunciation in the control rocin for loss of seal air pressure (implemented
                                                          by DCR 87-100), and specific training for operations personnel on the
                                                          spill event.    The inspector reviewed the GPC corrective action package,
4                                                          DCR's 87-99 and 87-100 (and associated MW0s), toured the new seal air                                                                                  ,
i                                                          supply system with the system engineer and determined that the required
f                                                          corrective actions had been performed. Since the actions to correct the
j                                                          specifics of this violation have been completed, this item is closed.                                                                                  ;
                                                    4.    Unresolved Item (URI)*
'
'
                                                          (0 pen) URI 321,366/88-05-02, Leak Testing of Test Solenoid Valves.                                                                                    ,
from the fuel pools (paragraph 3)
i                                                          (0 pen) URI 321/88-05-03, Inadequate APRM Surveillance.
321,366/88-05-02
                                                          (Closed) URI 321,366/87-02-03, Method to Ensure Qualified Personnel are
Open
i                                                         Available to Fill Emergency Organization Positions.
URI - Leak Testing of Test
                                                          In Inspection Report 321,366/87-18 the Emergency Preparedness Section                                                                                  .
Solenoid Valves (paragraph 5)
'                                                         opened IFI 87-18-04, Veri fy Shift Augmentation Times and Violation                                                                                    ;
321/88-05-03
Open
URI - Inadequate APRM
Surveillance (paragraph 8)
3.
Licensee Action on Previous Enforcement Matters (92702)
'
(Closed) Violation 321,366/86-41-01, Failure to follow plant procedures
which resulted in a partial loss of water from the fuel pools.
The GPC
i
letter of response dated May 8,1987, was reviewed. Licensee corrective
action involved replacement of the transfer canal inflatable seal assembly,
an enhancement of the leak detection system (implemented by DCR 87-99),
the addition of redundant air supplies to the inflatable seal assembly and
annunciation in the control rocin for loss of seal air pressure (implemented
by DCR 87-100), and specific training for operations personnel on the
spill event.
The inspector reviewed the GPC corrective action package,
DCR's 87-99 and 87-100 (and associated MW0s), toured the new seal air
4
,
,
                                                          87-18-05, Failure to Maintain a Trained and Qualified Emergency Response
i
i                                                         Staff. These two items cover the same concern as 87-02-03. URI 87-02-03
supply system with the system engineer and determined that the required
                                                          is closed to remove the redundancy.
f
l                                                   "An Unresolved Item is a matter about which more information is required to
corrective actions had been performed.
                                                    determine whether it is acceptable or may involve a violation or deviation.                                                                                   I
Since the actions to correct the
                                                                                                                                                                                                                  i
j
specifics of this violation have been completed, this item is closed.
;
4.
Unresolved Item (URI)*
'
(0 pen) URI 321,366/88-05-02, Leak Testing of Test Solenoid Valves.
,
i
(0 pen) URI 321/88-05-03, Inadequate APRM Surveillance.
(Closed) URI 321,366/87-02-03, Method to Ensure Qualified Personnel are
Available to Fill Emergency Organization Positions.
i
In Inspection Report 321,366/87-18 the Emergency Preparedness Section
.
opened IFI 87-18-04, Veri fy Shift Augmentation Times and Violation
;
'
87-18-05, Failure to Maintain a Trained and Qualified Emergency Response
,
i
Staff.
These two items cover the same concern as 87-02-03. URI 87-02-03
is closed to remove the redundancy.
l
"An Unresolved Item is a matter about which more information is required to
determine whether it is acceptable or may involve a violation or deviation.
I
i


                                                                                    _____- ______ _ ___
_____- ______ _ ___
      .
.
    .     .
,
  ,
.
                    -
.
            .
3
                                                    3
-
        5.     Operational Safety Verification (71707) Units 1 and 2
.
              The inspectors kept themselves informed on a daily basis of the overall
5.
              plant status and any significant safety matters related to plant
Operational Safety Verification (71707) Units 1 and 2
              operations. Daily discussions were held with plant management and various
The inspectors kept themselves informed on a daily basis of the overall
              members of the plant operating staff. The inspectors made frequent visits
plant status and any significant safety matters related to plant
              to the control room. Observations included instrument readings, setpoints
operations. Daily discussions were held with plant management and various
              and recordings, status of operating systems, tags and clearances on
members of the plant operating staff. The inspectors made frequent visits
              equipment, controls and switches, annunciator alarms, adherence to
to the control room. Observations included instrument readings, setpoints
              limiting conditions for operation, temporary alterations in effect, daily
and recordings, status of operating systems, tags and clearances on
              journals and data sheet entries, control room manning, and access
equipment, controls and switches, annunciator alarms, adherence to
              controls. This inspection activity included numerous informal discussions
limiting conditions for operation, temporary alterations in effect, daily
              with operators and their supervisors. Weekly, when on site, selected
journals and data sheet entries, control room manning, and access
              Engineering Safety Feature (ESF) systems were confirmed operable. The
controls. This inspection activity included numerous informal discussions
              confirmation was made by verifying the following:     accessible valve flow
with operators and their supervisors.
              path alignment, power supply breaker and fuse status, instrumentation,
Weekly, when on site, selected
              major component leakage, lubrication, cooling, and general condition.
Engineering Safety Feature (ESF) systems were confirmed operable.
              General plant tours were conducted on at least a weekly basis. Portions
The
              of the control building, turbine building, reactor building, and outside
confirmation was made by verifying the following:
              areas were visited.       Observations included general plant / equipment
accessible valve flow
              conditions, safety related tagout verifications, shif t turnover, sampling
path alignment, power supply breaker and fuse status, instrumentation,
              program, housekeeping and general plant conditions, fire protection
major component leakage, lubrication, cooling, and general condition.
              equipment, control of activities in progress, radiation protection
General plant tours were conducted on at least a weekly basis. Portions
              controls, physical security, problem identification systems, missile
of the control building, turbine building, reactor building, and outside
              hazards, instrumentation and alarms in the control room, and containment
areas were visited.
              isolation.
Observations included general plant / equipment
              On January 28, 1988, the inspector observed tools and other materials in
conditions, safety related tagout verifications, shif t turnover, sampling
              the Unit 1 reactor building in the vicinity of Core Spray System Outboard
program, housekeeping and general plant conditions, fire protection
              Injection Valve 1E21-F004A.     These items had apparently not been removed
equipment, control of activities in progress, radiation protection
              following the completion of maintenance work. This matter was brought to
controls, physical security, problem identification systems, missile
              the attention of the Unit 1 Shift Supervisor.
hazards, instrumentation and alarms in the control room, and containment
              On February 9,     1988, while administering an NRC operator licensing
isolation.
              examination, the examiner noted that Unit I was potentially operating with
On January 28, 1988, the inspector observed tools and other materials in
              less than the minimum number of operable Average Power Range Monitor
the Unit 1 reactor building in the vicinity of Core Spray System Outboard
              (APRM) Downscale scram inputs required by the Technical Specifications
Injection Valve 1E21-F004A.
              (TS). At the time of this observation (approximately 0840) Unit I was
These items had apparently not been removed
              operating in the RUN mode at approximately 100 percent of rated power.
following the completion of maintenance work. This matter was brought to
              The examiner noted that APRM channel A and Intermediate Range Monitor
the attention of the Unit 1 Shift Supervisor.
              (IRM) channel C were both in the bypassed condition. A review of a
On February 9,
              f acility print (H-17789) confirmed that the bypassing of IRM channel C in
1988, while administering an NRC operator licensing
              effect bypassed the Downscale scram input of APRM channel C.       Since APRM
examination, the examiner noted that Unit I was potentially operating with
              channels A, C and E provide input to Reactor Protection system (RPS)
less than the minimum number of operable Average Power Range Monitor
              channel A, only APRM channel E remained available to provide Downscale
(APRM) Downscale scram inputs required by the Technical Specifications
              scram input to this RPS Channel. During power operations Table 3.1-1 of
(TS).
              the TS requires a minimum of two operable channel inputs per RPS channel
At the time of this observation (approximately 0840) Unit I was
              for the APRM Downscale scram function. If the min' um number of operable
operating in the RUN mode at approximately 100 percent of rated power.
              inputs cannot be met for an RPS channel, the affected RPS channel must be
The examiner noted that APRM channel A and Intermediate Range Monitor
              tripped.     The examiner observed that RPS channel A was not tripped. The
(IRM) channel C were both in the bypassed condition.
A review of a
f acility print (H-17789) confirmed that the bypassing of IRM channel C in
effect bypassed the Downscale scram input of APRM channel C.
Since APRM
channels A, C and E provide input to Reactor Protection system (RPS)
channel A, only APRM channel E remained available to provide Downscale
scram input to this RPS Channel.
During power operations Table 3.1-1 of
the TS requires a minimum of two operable channel inputs per RPS channel
for the APRM Downscale scram function. If the min' um number of operable
inputs cannot be met for an RPS channel, the affected RPS channel must be
tripped.
The examiner observed that RPS channel A was not tripped.
The
i
i


                                                                        - - - - - _ - - - - - . _ _ _ - - _ - _ - - - - __
- - - - - _ - - - - - . _ _ _ - - _ - _ - - - -
    .
__
  .   i
.
              -
.
        .
i
                                                4
4
-
.
i
i
          examiner discussed his concerns with the Unit 1 Shift Supervisor and noted
examiner discussed his concerns with the Unit 1 Shift Supervisor and noted
          that IRM channel C was subsequently unbypassed.
that IRM channel C was subsequently unbypassed.
          The resident inspector attempted to determine how long APRM channel A and
The resident inspector attempted to determine how long APRM channel A and
          IRM channel C had been simultaneously bypassed in following up on this
IRM channel C had been simultaneously bypassed in following up on this
          matter. This could not be determined from a review of control room log
matter. This could not be determined from a review of control room log
          books. However, on duty operations personnel indicated that the condition
books. However, on duty operations personnel indicated that the condition
          had existed since at least the start of their shift. This event is
had existed since at least the start of their shift.
          considered a violation of TS Table 3.1-1 in that only one APRM channel
This event is
          was available to provide APRM Downscale scram input to RPS channel A and
considered a violation of TS Table 3.1-1 in that only one APRM channel
          the RPS channel was untripped. This matter will be tracked as Violation
was available to provide APRM Downscale scram input to RPS channel A and
          321/88-05-01 - Bypassing of APRM Downscale Scram Inputs.
the RPS channel was untripped.
          At approximately 1500 on February 9,       1988, while conducting an NRC
This matter will be tracked as Violation
          licensed one"/.or examination, the examiner noticed that halon tanks
321/88-05-01 - Bypassing of APRM Downscale Scram Inputs.
          serv 4 *., the Unit 2 Remote Shutdown Panel were discharged.                                 Discussions
At approximately 1500 on February 9,
          wi .n operations personnel revealed that the tanks discharged at 2237 on
1988, while conducting an NRC
          February 8, 1988. Operations personnel also indicated that no action had
licensed one"/.or examination, the examiner noticed that halon tanks
          ,een taken to replenish the halon. Since Unit 2 was in cold shutdown
serv 4 *., the Unit 2 Remote Shutdown Panel were discharged.
          during this time period, halon protection was not required for the Remote
Discussions
          Shutdown Panel. However, the examiner and the resident inspectors were
wi .n operations personnel revealed that the tanks discharged at 2237 on
          concerned that the licensee had taken no action to replenish the halon
February 8, 1988. Operations personnel also indicated that no action had
          almost 17 hours af ter the discharge had taken place. The licensee is
,een taken to replenish the halon.
          currently reviewing this matter. Region II NRC personnel will also review
Since Unit 2 was in cold shutdown
          this matter during a future inspection.
during this time period, halon protection was not required for the Remote
          At 1920 on February 12, 1988, with Unit 1 operating at 100 percent of
Shutdown Panel.
However, the examiner and the resident inspectors were
concerned that the licensee had taken no action to replenish the halon
almost 17 hours af ter the discharge had taken place.
The licensee is
currently reviewing this matter. Region II NRC personnel will also review
this matter during a future inspection.
At 1920 on February 12, 1988, with Unit 1 operating at 100 percent of
rated power, the licensee declared a loss of primary containment integrity
,
,
          rated power, the licensee declared a loss of primary containment integrity
;
;        and entered a 12-hour hot shutdown LCO.     Proper NRC notifications were
and entered a 12-hour hot shutdown LCO.
          made at that time. These actions were precipitated by the results of
Proper NRC notifications were
          local leak rate testing (LLRT) in Unit 2 which is currently in an outage.
made at that time.
;         The licensee had previously been conducting LLRTs on vacuum breaker test
These actions were precipitated by the results of
          solenoid valves 2T48-F342A - L. These test solenoid valves are in lines
local leak rate testing (LLRT) in Unit 2 which is currently in an outage.
;
The licensee had previously been conducting LLRTs on vacuum breaker test
solenoid valves 2T48-F342A - L.
These test solenoid valves are in lines
that supply air to the air operators of torus to drywell vacuum breakers
'
'
          that supply air to the air operators of torus to drywell vacuum breakers
L.
          2T48-F323A    -
These vacuum breakers normally operate in the
                          L.   These vacuum breakers normally operate in the
2T48-F323A
,        self-actuated mode. The air operators exist for the purpose on
-
          demonstrating opening capability on a monthly basis. For containment
self-actuated mode.
          isolation purposes, the licensee considers the air operators to be primary
The air operators exist for the purpose on
;        barriers. Test solenoid valves 2T48-F342A - L are considered outboard
,
i         isolation valves, and are identified as containment isolation valves in
demonstrating opening capability on a monthly basis.
:         the licensee's Pump and Valve Program. Until the current Unit 2 outage,
For containment
isolation purposes, the licensee considers the air operators to be primary
barriers.
Test solenoid valves 2T48-F342A - L are considered outboard
;
i
isolation valves, and are identified as containment isolation valves in
:
the licensee's Pump and Valve Program.
Until the current Unit 2 outage,
!
LLRT's on these valves had been performed with pressure applied on the
!
!
          LLRT's on these valves had been performed with pressure applied on the
side of the F342 valves away from accident pressure. When recently tested
!        side of the F342 valves away from accident pressure. When recently tested
i
i         on the accident side, the valves failed to hold pressure.
on the accident side, the valves failed to hold pressure.
          As a result of the Unit 2 test failures and the similarity of equipment in
As a result of the Unit 2 test failures and the similarity of equipment in
i         Unit 1, the licensee promptly declared a loss of primary containment
i
1         integrity in Unit 1.     The licensee subsequently restored primary containment
Unit 1, the licensee promptly declared a loss of primary containment
l         integrity in Unit 1 by disconnecting and capping the air lines at test
1
;        solenoid valves 1T48-F343A - L. This avoided shutdown of Unit 1 and was
integrity in Unit 1.
          accomplished within the LCO time allowed. The licensee it currently
The licensee subsequently restored primary containment
l
integrity in Unit 1 by disconnecting and capping the air lines at test
solenoid valves 1T48-F343A - L.
This avoided shutdown of Unit 1 and was
;
accomplished within the LCO time allowed.
The licensee it currently


                                                                                              . - _ _ _ _ _ _ - _ _ _ _         _ _ _ _ _ _
. - _ _ _ _ _ _ - _ _ _ _
_
_ _ _ _ _
<
<
                      .
.
                    -     '                                                                                                                 (
(
          .
-
                                                                                                                                            !
'
                                  *
.
                            .
!
                                                                    5
*
                                                                                                                                            ;
5
                              investigating this matter and exploring options for corrective action.
.
,                              Pending completion of the licensee's investigation and -NRC review, the
                                                                                                                                            '
                              matter will be identified as Unresolved Item 321,366/88-05-02 - Leak
                              Testing of Test Solenoid Valves.
                              One violation was identified.
                                                                                                                                            l
                        6.    Maintenance Observation (62703) Units 1 and 2                                                                ,
                              During the report period, the inspectors observed selected maintenance                                        .
                              activities. The observations included a review of the work documents for
                              adequacy, adherence to procedure, proper tagouts, adherence to technical
                              specifications, radiological controls, observation of all or part of the
                              actual work and/or retesting in progress, specified retest requirements,
;                              and adherence to the appropriate quality controls.      The primary maintenance
                              observations during this month are summarized below:
                              Maintenance Activity                                                                      Date
;
;
l                             1.   Preventive maintenance on Limitorque operator                                       1/26/88
investigating this matter and exploring options for corrective action.
                                    on valve 2E32-F001P per procedure                                                                       i
Pending completion of the licensee's investigation and -NRC review, the
                                    52PM-MNT-005-0S (Unit 2)
,
                              2.   Plant service water pump "2A" sequencing                                           1/28/88
matter will be identified as Unresolved Item 321,366/88-05-02 - Leak
                                    timer evaluation per procedure
'
                                    42SP-011188-0J-1-2S.   (Unit 2)
Testing of Test Solenoid Valves.
                              3.   Inspection of "2C" diesel generator per                                             2/3/88             ;
One violation was identified.
l
6.
Maintenance Observation (62703) Units 1 and 2
,
During the report period, the inspectors observed selected maintenance
.
activities.
The observations included a review of the work documents for
adequacy, adherence to procedure, proper tagouts, adherence to technical
specifications, radiological controls, observation of all or part of the
actual work and/or retesting in progress, specified retest requirements,
;
and adherence to the appropriate quality controls.
The primary maintenance
observations during this month are summarized below:
Maintenance Activity
Date
;
l
1.
Preventive maintenance on Limitorque operator
1/26/88
on valve 2E32-F001P per procedure
i
52PM-MNT-005-0S (Unit 2)
2.
Plant service water pump "2A" sequencing
1/28/88
timer evaluation per procedure
42SP-011188-0J-1-2S.
(Unit 2)
3.
Inspection of "2C" diesel generator per
2/3/88
;
procedure 52SV-R43-001-05 (Unit 2)
[
;
;
                                    procedure 52SV-R43-001-05 (Unit 2)                                                                      [
:
:
j                             4.   Inspection of Allis Chalmers Motor                                                 2/8/88
j
j                                   Control Center 2R24-5012 per
4.
                                    procedure 52PM-R24-001-05 (Unit 2)
Inspection of Allis Chalmers Motor
2/8/88
j
Control Center 2R24-5012 per
procedure 52PM-R24-001-05 (Unit 2)
,
,
5.
Removal of Valve 2E11-F005B per
2/9/88
'
'
                              5.    Removal of Valve 2E11-F005B per                                                    2/9/88
l
l                                    Maintenance Work Order 2-87-3462 for
Maintenance Work Order 2-87-3462 for
j                                   Inservice Inspection (Unit 2)
j
                              No violations or deviations were identified.
Inservice Inspection (Unit 2)
No violations or deviations were identified.
!
!
!
!
7.
Plant Modification (37700) Unit 2
;
;
                        7.    Plant Modification (37700) Unit 2
l
l                              The inspectors observed the performance of selected plant modification
The inspectors observed the performance of selected plant modification
                              Design Change Requests (DCRs). The observation included a review of the
Design Change Requests (DCRs). The observation included a review of the
                              DCR for technical adequacy, conformance to Technical Specifications,
DCR for technical adequacy, conformance to Technical Specifications,
                              verification of test instrument calibration, observation of all or part of
verification of test instrument calibration, observation of all or part of
                              the actual surveillances, removal from service and return to service of
the actual surveillances, removal from service and return to service of
T
T
l
l
:
:
l
l
  . _ . _ - - . - -                                                   ..- ,- - -- ,, -
.
.
- - . - -
. - - - - - - -
. . - - - . .
..- ,- - --
,, -


                                                                                _ _______ _ __
_ _______ _ __
    .
.
  *     *
*
*
.
6
*
.
the system or components affected, and review of the data for acceptability
based upon the acceptance criteria.
The primary DCR observations are
summarized below:
DCR
Date
.
.
                  *
86-235
          .                                        6
2/2/88
            the system or components affected, and review of the data for acceptability
81-008
            based upon the acceptance criteria.        The primary DCR observations are
2/8/88
            summarized below:
No violations or deviations were identified.
                    DCR                                  Date                                        .
8.
                    86-235                               2/2/88
Surveillance Testing Observations (61726) Units 1 and 2
                    81-008                               2/8/88
The inspectors observed the performance of selected surveillances.
            No violations or deviations were identified.
The
      8.     Surveillance Testing Observations (61726) Units 1 and 2
observation included a review of the procedure for technical adequacy,
            The inspectors observed the performance of selected surveillances. The
conformance to Technical Specifications, verification of test instrument
            observation included a review of the procedure for technical adequacy,
calibration, observation of all or part of the actual surveillances,
            conformance to Technical Specifications, verification of test instrument
removal from service and return to service of the system or components
            calibration, observation of all or part of the actual surveillances,
affected, and review of the data for acceptability based upon the
            removal from service and return to service of the system or components
acceptance criteria. The primary surveillance testing observations during
            affected, and review of the data for acceptability based upon the
this month are summarized below:
            acceptance criteria. The primary surveillance testing observations during
Surevillance Testing Activity
            this month are summarized below:
Date
            Surevillance Testing Activity                                                     Date
1.
              1.   Reactor Core Isolation Cooling System                                     2/2/88
Reactor Core Isolation Cooling System
                    Pump Rated Flow Testing per
2/2/88
                    procedure 345V-E51-002-1S (Unit 1)
Pump Rated Flow Testing per
            2.     Functional Testing of Offgas Vent Pipe                                     2/4/88
procedure 345V-E51-002-1S (Unit 1)
                    Radiation Monitor per procedure
2.
                    575V-011-010-1 (Unit 1)
Functional Testing of Offgas Vent Pipe
            3.     Post Maintenance Functional Testing of                                     2/11/88
2/4/88
                    "2" Diesel Generator per procedure
Radiation Monitor per procedure
                    52SV-R43-001-05 (Unit 2)
575V-011-010-1 (Unit 1)
            4.     Functional Testing and Calibration of APRMs                               2/15/88
3.
                    345V-C51-002-15 (Unit 1)
Post Maintenance Functional Testing of
            On February 15, 1988, at 1720, the licensee discovered that the
2/11/88
              surveillance for Average Power Range Monitors (APRM) did not test all
"2" Diesel Generator per procedure
              contacts in the trip logic. The downscale and the flow biased high flux
52SV-R43-001-05 (Unit 2)
              trip contacts had not been included in the surveillance procedure and
4.
              therefore had not been tested weekly as required by Technical Specifications).
Functional Testing and Calibration of APRMs
              The APRMs were declared inoperable at 1720, 2-15-88 and the LC0 atiion required
2/15/88
              by TS 3.1, Table 3.1-1, Scram Number 8 was entered. This required action
345V-C51-002-15 (Unit 1)
            was to reduce power to the IRM range and to have the Mode Switch in Hot
On February 15, 1988, at 1720, the licensee discovered that the
              Standby within eight hours. The licensee requested that the NRC grant
surveillance for Average Power Range Monitors (APRM) did not test all
              discretionary enforcement to extend the LCO time for about eleven hours
contacts in the trip logic. The downscale and the flow biased high flux
              (until 12:00 noon, 2-16-88) to allow time for procedure development and
trip contacts had not been included in the surveillance procedure and
              testing of the APRM trips. The request was processed through proper
therefore had not been tested weekly as required by Technical Specifications).
              channels and discussed. Since the LC0 time limit of eight hours was rot
The APRMs were declared inoperable at 1720, 2-15-88 and the LC0 atiion required
              exceeded, the discretionary enforcement was not utilized due to clearing
by TS 3.1, Table 3.1-1, Scram Number 8 was entered. This required action
was to reduce power to the IRM range and to have the Mode Switch in Hot
Standby within eight hours.
The licensee requested that the NRC grant
discretionary enforcement to extend the LCO time for about eleven hours
(until 12:00 noon, 2-16-88) to allow time for procedure development and
testing of the APRM trips.
The request was processed through proper
channels and discussed. Since the LC0 time limit of eight hours was rot
exceeded, the discretionary enforcement was not utilized due to clearing


                                                                                              I
I
        .                                                                                     :
:
      '   *
.
    .
*
                  *
'
            .                                     7
.
                                                                                              i
7
              of the LCO.     The Senior Resident Inspector reviewed the procedure and
*
              witnessed the testing of one of the APRMs. All APRMs were tested
.
*
i
                                                                                              ;
of the LCO.
              satisfactorily and the LCO cleared .by 2302, 2-15-88.           This item,
The Senior Resident Inspector reviewed the procedure and
              Inadequate APRM Surveillance, will be tracked as URI 321/88-05-03. As
witnessed the testing of one of the APRMs.
              discussed in Region II Reports 321,366/87-29 and 321,366/87-33, several
All APRMs were tested
              Unit 1 torus to drywell vacuum breakers failed to test satisfactorily
;
              during recent monthly operability testing.     More specifically, vacuum
*
              breakers 1T48-F323 C and F did not test properly on November 11, 1987, and
satisfactorily and the LCO cleared .by 2302, 2-15-88.
              vacuum breaker 1T48-F323E stuck open during testing on December 11, 1987.
This item,
  ,
Inadequate APRM Surveillance, will be tracked as URI 321/88-05-03. As
              Vacuum breaker li:.e-F323E eventually did close when the test switch at the
discussed in Region II Reports 321,366/87-29 and 321,366/87-33, several
              local panel for vacuum breaker IT48-F323F was depressed. The licensee
Unit 1 torus to drywell vacuum breakers failed to test satisfactorily
              subsequently initiated a program to identify and correct wiring problems
during recent monthly operability testing.
              in the test circuitry for these vacuum breakers.       Required corrective
More specifically, vacuum
              actions were taken under Maintenance Work Orders (MW0s) 1-87-8123,
breakers 1T48-F323 C and F did not test properly on November 11, 1987, and
              1-87-7516, 1-87-7517 and 1-87-7950 during the month of January 1988. In
vacuum breaker 1T48-F323E stuck open during testing on December 11, 1987.
              essence, the licensee found that solenoid valves in the air test lines for
Vacuum breaker li:.e-F323E eventually did close when the test switch at the
              IT48-F323C, E and F had been incorrectly wired and that individual wire
,
              conductor labels for these solenoid valves were incorrect. The solenoid
local panel for vacuum breaker IT48-F323F was depressed.
              valves (designated IT48-F342 C, E and F) are two-way valves that remain
The licensee
              open after the test button is released to assure that all air is relieved
subsequently initiated a program to identify and correct wiring problems
in the test circuitry for these vacuum breakers.
Required corrective
actions were taken under Maintenance Work Orders (MW0s) 1-87-8123,
1-87-7516, 1-87-7517 and 1-87-7950 during the month of January 1988.
In
essence, the licensee found that solenoid valves in the air test lines for
IT48-F323C, E and F had been incorrectly wired and that individual wire
conductor labels for these solenoid valves were incorrect. The solenoid
valves (designated IT48-F342 C, E and F) are two-way valves that remain
open after the test button is released to assure that all air is relieved
from the test line.
'
.
.
              from the test line.                                                              '
The licensee conducted a broader investigation af the vacuum breaker
              The licensee conducted a broader investigation af the vacuum breaker
testing problems to determine the root cause and identify any additional
              testing problems to determine the root cause and identify any additional
needed corrective actions. The resident inspectors reviewed the report of
              needed corrective actions. The resident inspectors reviewed the report of
this investigation dated February 5,1988.
It was determined that the
!
1
1
              this investigation dated February 5,1988. It was determined that the            !
i
i            wiring discrepancies causing the testing problems were introduced in
wiring discrepancies causing the testing problems were introduced in
,            October of 1987 during the performance of MWO 1-86-7823. This MWO was
October of 1987 during the performance of MWO 1-86-7823. This MWO was
,
I
generated primarily to mark and stow a spare cable and verify the wiring
I
I
              generated primarily to mark and stow a spare cable and verify the wiring
of a new cable.
I            of a new cable. Personnel performing this work noticed and documented
Personnel performing this work noticed and documented
i
improper conductor termination at test solenoid valves 1T48-F342C, E and
              improper conductor termination at test solenoid valves 1T48-F342C, E and
i
,            F. Unfortunately, MWO instructions to correct the observed wiring discrepa-
F.
i             ncies were inadequate, and subsequent corrective maintenance actually introduced [
Unfortunately, MWO instructions to correct the observed wiring discrepa-
'
,
              wiring errors into the test circuitry.   The operability testing difficulties
i
              of vacuum breakers IT48-F323C, E, and F were subsequently experienced in
ncies were inadequate, and subsequent corrective maintenance actually introduced
j            November and December of 1987.
[
              Technical Specification 6.8.1.a.     requires that written procedures be
wiring errors into the test circuitry.
              established, implemented and maintained covering the activities recommended     ,
The operability testing difficulties
              in Appendix "A" of Regulatory Guide 1.33, Revision 2,         February 1978.     ,
'
              Appendix "A" recommends that maintenance that can af fect the performance       l
of vacuum breakers IT48-F323C, E, and F were subsequently experienced in
              of safety-related equipment be properly preplanned and performed in             ;
November and December of 1987.
              accordance with written procedures, documented instructions, or drawings
j
Technical Specification 6.8.1.a.
requires that written procedures be
established, implemented and maintained covering the activities recommended
,
in Appendix
"A" of Regulatory Guide 1.33, Revision 2,
February 1978.
,
Appendix "A" recommends that maintenance that can af fect the performance
l
of safety-related equipment be properly preplanned and performed in
;
accordance with written procedures, documented instructions, or drawings
appropriate to the circumstances.
The rewiring of solenoid valves
,
,
              appropriate to the circumstances.      The rewiring of solenoid valves
l            IT48-F342C,E and F in October 1987 is considered to be a violation of TS        ;
              6.8.1.a. in that the instructions of MWO 1-86-7823 were inadequate and
l
l
              resulted in improper wiring of the three vacuum breaker test soler.oid
IT48-F342C,E and F in October 1987 is considered to be a violation of TS
              valves.   This matter will be tracked as Violation 321/88-05-04           -
;
              Inadequate MWO for Vacuum Breaker Maintenance.     In reviewing this matter
l
              the inspectors noted that the incorrect wiring of the test solenoid valves
6.8.1.a. in that the instructions of MWO 1-86-7823 were inadequate and
              did not impair the ability of the torus to drywell vacuum breakers to
resulted in improper wiring of the three vacuum breaker test soler.oid
              function in the normal, self-actuated mode,
valves.
              One violation was identified.
This matter will be tracked as Violation 321/88-05-04
-
Inadequate MWO for Vacuum Breaker Maintenance.
In reviewing this matter
the inspectors noted that the incorrect wiring of the test solenoid valves
did not impair the ability of the torus to drywell vacuum breakers to
function in the normal, self-actuated mode,
One violation was identified.
L
L


  ._ _ _       __--_ --___ _ __               _ _ -
._ _ _
              .
__--_ --___ _ __
            -
_ _ -
          ..
.
-
..
,
<
.
8
,
,
<                                        .
                                  ,
                                                                          8
i.
i.
                          9.       .ESF System Walkdown (71710)
9.
                                    The inspectors routinely conducted partial walkdowns of ESF systems. Valve
.ESF System Walkdown (71710)
                                    and breaker / switch lineups and equipment conditions were randomly verified
The inspectors routinely conducted partial walkdowns of ESF systems. Valve
                                    both locally- and in the control room to ensure that . lineups were in.
and breaker / switch lineups and equipment conditions were randomly verified
                                    accordance with operability requirements and that equipment material
both locally- and in the control room to ensure that . lineups were in.
                                    conditions were satisfactory. The Unit 1 Residual Heat Removal system "A"
accordance with operability requirements and that equipment material
                                    loop was walked down in detail.
conditions were satisfactory. The Unit 1 Residual Heat Removal system "A"
                                    Within the areas inspected, no violations or deviations were identified.
loop was walked down in detail.
a                           10.     Radiological Protection (71709) Units 1 and 2
Within the areas inspected, no violations or deviations were identified.
a
10.
Radiological Protection (71709) Units 1 and 2
;
;
                                    The resident inspectors reviewed aspects of the licensee's radiological
The resident inspectors reviewed aspects of the licensee's radiological
                                    protection program in the course of the monthly activities.           The
protection program in the course of the monthly activities.
                                    performance of health physics and other personnel was observed on various
The
                                    shifts to include:     involvement of health physics supervision, use of
performance of health physics and other personnel was observed on various
                                    radiation work permits, use of personnel monitoring equipment, control of
shifts to include:
                                    high radiation areas, use of friskers and personal contamination monitors,
involvement of health physics supervision, use of
                                    and posting and labeling.
radiation work permits, use of personnel monitoring equipment, control of
                                    No violations or deviations were noted.
high radiation areas, use of friskers and personal contamination monitors,
and posting and labeling.
No violations or deviations were noted.
,
,
                            11.     Physical Security (71881) Units 1 and 2
11.
Physical Security (71881) Units 1 and 2
,
,
                                    In the course of the monthly activities, the resident inspectors included
In the course of the monthly activities, the resident inspectors included
                                    a review of the licensee's physical security program. The performance of
,
,
a review of the licensee's physical security program. The performance of
'
'
                                    various shifts of the security force was observed in the conduct of daily
various shifts of the security force was observed in the conduct of daily
!                                   activities to include: availability of supervision, availability of armed
!
activities to include: availability of supervision, availability of armed
response personnel, protected soc vital access controls, searching of
'
'
                                    response personnel, protected soc vital access controls, searching of
personnel, packages and vehit 'es, badge issuance and retrieval, escorting
                                    personnel, packages and vehit 'es, badge issuance and retrieval, escorting
1
1                                   of visitors, patrols and compensatory pests.
of visitors, patrols and compensatory pests.
1
1
,
On February 18, 1988, the resident inspectors toure, the new security
                                    On February 18, 1988, the resident inspectors toure, the new security
,
j                                   building and observed operations in progress.
j
building and observed operations in progress.
'
'
                                    No violations or deviations were noted.
No violations or deviations were noted.
l                             12.   Reportable Occurrences (90712 & 92700) Unit 1 and 2
l
                                    A number of Licensee Event Reports (LERs) were reviewed for potential
12.
                                    generic impact, to detect trends, and to determine whether corrective
Reportable Occurrences (90712 & 92700) Unit 1 and 2
                                    actions appeared appropriate. Events which were reported immediately were
A number of Licensee Event Reports (LERs) were reviewed for potential
                                    also reviewed as they occurred to determine that Technical Specifications
generic impact, to detect trends, and to determine whether corrective
                                    were being met and the public health and safety were of utmost consideration.
actions appeared appropriate. Events which were reported immediately were
                                    Unit 1: 86-11, Personnel Error Causes ESF Actuation.     The events of
also reviewed as they occurred to determine that Technical Specifications
                                                      this LER were cited as Violation 86-03-03. The licensee's
were being met and the public health and safety were of utmost consideration.
                                                      corrective action was raviewed and the violation closed in
Unit 1: 86-11, Personnel Error Causes ESF Actuation.
                                                      Inspection Report 86-28. This LER is closed.
The events of
this LER were cited as Violation 86-03-03. The licensee's
corrective action was raviewed and the violation closed in
Inspection Report 86-28.
This LER is closed.


                                                                                _ _ _ _ _ _ _ _ _ - _ _ _ _ .
_ _ _ _ _ _ _ _ _ - _ _ _ _ .
    .
.
  .     .
.
.
,
,
              '
9
                                                9
'
                  87-01, Spurious Ground Fault Trips Turbine Overspeed Device
87-01, Spurious Ground Fault Trips Turbine Overspeed Device
                          Causing Reactor SCRAM. The licensee's response to to this
Causing Reactor SCRAM. The licensee's response to to this
                          event was reviewed and appeared adaquate. No fault was
event was reviewed and appeared adaquate.
                            located in the turbine overspeed device and the device has
No fault was
                          operated properly during Unit 1 power operations. This LER
located in the turbine overspeed device and the device has
                            is closed.
operated properly during Unit 1 power operations. This LER
                    87-02, Ground Condition Trips Main Generator and Turbine
is closed.
                            Resulting in Reactor SCRAM. A loose wire was located and
87-02, Ground Condition Trips Main Generator and Turbine
                            repaired. Checks were made for other loose components or
Resulting in Reactor SCRAM. A loose wire was located and
                          ground conditions with none found. A review for possible
repaired.
                            additional preventative measures is continuing.   This LER
Checks were made for other loose components or
                            is closed.
ground conditions with none found. A review for possible
                    87-05. Blocked Air Port Prevents Damper Closure Resulting in
additional preventative measures is continuing.
                            Improper ESF Actuation. This event was caused by a missing
This LER
                            locknut on the damper control valve bleed off port
is closed.
                            adjusting screw. The nut was replaced, the screw properly
87-05. Blocked Air Port Prevents Damper Closure Resulting in
                            adjusted and locked and the other dampers inr.oected for
Improper ESF Actuation. This event was caused by a missing
                            loose or missing locknuts. This LER is closed.
locknut on the damper control valve bleed off port
          Unit 2: 86-20, Primary Containment Penetrations Failed LLRT. All failed
adjusting screw. The nut was replaced, the screw properly
                            penetrations were repaired and retested prior to Unit 2
adjusted and locked and the other dampers inr.oected for
                            startup.   This LER is closed.
loose or missing locknuts.
                    87-05, Leaking Valves Cause RWCU Isolation (Group 5). The leaking
This LER is closed.
                            valves were located and isolated and the Group 5 isolation
Unit 2: 86-20, Primary Containment Penetrations Failed LLRT. All failed
                            signal reset.   There is a continuing RWCU upgrade in
penetrations were repaired and retested prior to Unit 2
                            progress to which this problem has been added. This LER is
startup.
                            closed.
This LER is closed.
      13. Operating Reactor Events (93702) Unit 2
87-05, Leaking Valves Cause RWCU Isolation (Group 5).
          As discussed in Report 321,366/88-01, the maximum reactor coolant system
The leaking
          cooldown rate of 100 degrees F per hour specified in Technical
valves were located and isolated and the Group 5 isolation
          Specification 3.4.6.1 was exceeded during the shutdown of Unit 2 on
signal reset.
          January 13, 1988. The licensee determined that a cooldown from about 520
There is a continuing RWCU upgrade in
          to 375 degrees F occurred in one hour. The associated technical specification
progress to which this problem has been added. This LER is
          Action Statement required the licensee to perform an engineering
closed.
          evaluation to determine the effects of the out-of-limit condition on the
13. Operating Reactor Events (93702) Unit 2
          fracture toughness properties of the r6 actor coolant system and to determine
As discussed in Report 321,366/88-01, the maximum reactor coolant system
          that the reactor coolant system remains acceptable for continued
cooldown rate of 100 degrees F per hour specified in Technical
          operation.   An engineering evaluation, performed by General Electric
Specification 3.4.6.1 was exceeded during the shutdown of Unit 2 on
          Company for the licensee, addressed the potential cor.cerns of brittle
January 13, 1988. The licensee determined that a cooldown from about 520
          fracture, allowable stress and f atigue.     The evaluation concluded that
to 375 degrees F occurred in one hour.
          brittle fracture was not a concern, and that the impact of the transient
The associated technical specification
          on maximum stress and fatigue were less severe than those evaluated for
Action Statement required the licensee to perform an engineering
          the design basis single relief valve blowdown event. In summary, it was
evaluation to determine the effects of the out-of-limit condition on the
          concluded that there were no structural integrity concerns with continued
fracture toughness properties of the r6 actor coolant system and to determine
          operation of Unit 2.
that the reactor coolant system remains acceptable for continued
operation.
An engineering evaluation, performed by General Electric
Company for the licensee, addressed the potential cor.cerns of brittle
fracture, allowable stress and f atigue.
The evaluation concluded that
brittle fracture was not a concern, and that the impact of the transient
on maximum stress and fatigue were less severe than those evaluated for
the design basis single relief valve blowdown event.
In summary, it was
concluded that there were no structural integrity concerns with continued
operation of Unit 2.


                                                                      _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _
                                                                                                                      . _ _ ,
. _ _ ,
      .
.
    .     .
.
  ,
.
                *
,
                                                10
10
            The resident inspectors reviewed the General Electric engineering evaluation
*
            dated January 18, 1988.
The resident inspectors reviewed the General Electric engineering evaluation
            Within the areas inspected, no violations or deviations were identified.
dated January 18, 1988.
        14. Information Meeting with Local Officials, (94600)
Within the areas inspected, no violations or deviations were identified.
            On February 2,1988, the Chief of Region II Projects Section 3B and the
14.
            resident inspectors held an information meeting with the Appling County
Information Meeting with Local Officials, (94600)
            Board of Commissioners. The NRC representatives provided the Board with a
On February 2,1988, the Chief of Region II Projects Section 3B and the
            description of the NRC organization and responsibilities, a summary of
resident inspectors held an information meeting with the Appling County
            plant status and the business telephone numbers of appropriate NRC
Board of Commissioners. The NRC representatives provided the Board with a
            contacts. Additionally, the Hatch resident inspectors were introduced and
description of the NRC organization and responsibilities, a summary of
            the inspection program was briefly described. Information available in
plant status and the business telephone numbers of appropriate NRC
            the local Public Document Rnom was also discussed. The NRC representatives
contacts. Additionally, the Hatch resident inspectors were introduced and
            responded to questions posed by the Board at the conclusien of this
the inspection program was briefly described.
            information meeting.
Information available in
the local Public Document Rnom was also discussed. The NRC representatives
responded to questions posed by the Board at the conclusien of this
information meeting.
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Latest revision as of 11:29, 11 December 2024

Insp Repts 50-321/88-05 & 50-366/88-05 on 880123-0219. Violations Noted.Major Areas Inspected:Licensee Action on Previous Enforcement Matters,Maint Observation,Operational Safety Verification,Plant Mods & Physical Security
ML20148H711
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 03/07/1988
From: Holmesray P, Menning J, Sinkule M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20148H683 List:
References
50-321-88-05, 50-321-88-5, 50-366-88-05, 50-366-88-5, NUDOCS 8803300068
Download: ML20148H711 (11)


See also: IR 05000321/1988005

Text

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION il

o

5

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101 MARIETTA STREET, N.W.

't

AT LANTA, oEoRGI A 30323

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,/

.....

Report Numbers:

50-321/88-05 and 50-366/88-05

Licensee: Georgia Power Company

P. O. Box 4545

Atlanta, GA 30302

Docket Numbers:

50-321 and 50-366

License Numbers:

DPR-57 and NPF-5

Facility Name:

Hatch 1 and 2

Inspection Dates: January 23 - February 19, 1988

Inspectors:

D )[

adv [m

/

Peter Holmes 'Ra , Senior Resi/ent Inspector

Date Signed

&

W

JohnE.Menning,ResidentIn@ector

Date Sitned

,

AccompanyingPersgnel:/RanallA.Mussr

$/7!W

!Muk/

/ WWV1

d--

Approved by:

Marvin \\f/. Sinkule, Chief, Project Section 3B

Date Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine inspection was conducted at the site in the areas of

Licensee Action

on

Previous

Enforcement Matters,

Operational

Safety

Verification, Maintenance Observation,

Plant Modification,

Surveillance

Observation,

Radiological

Protection,

Physical

Security,

Reportable

Occurrences, and Reactor Operating Events.

Results:

Two violations were identified.

880330o068 8s0310

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REPORT DETAILS

1.

Persons Contacted

Licensee. Employees

T. Beckham, Vice President-Plant Hatch

D. Davis, Manager General Support

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J. - Fitzsimmons, Nuclear Security Manager

  • P. Fornel, Maintenance Manager
  • 0. Fraser, Site Quality Assurance (QA) Manager
  • M. Googe, Outages and Planning Manager
  • H. Nix, Plant Manager
  • T. Powers, Engineering Manager
  • D. Read, Plant Support Manager
  • H. Sumner, Operations Manager
  • S. Tipps, Nuclear Safety and Compliance Manager

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R.-Zavadoski, Health Physics and Chemistry Manager

Other licensee employees contacted included technicians, operators,

mechanics, security force members and office personnel.

NRC Resident Inspectors

  • P. Holmes-Ray
  • J. Menning
  • R. Musser

NRC management on site during inspection period:

M. Sinkule, Chief, Project Section 38, Region II

  • Attended exit interview

2.

Exit Interview (30703)

The inspection scope and findings were summarized on February 19, 1988,

with those persons indicated in paragraph 1 above.

The licensee did not

identify as proprietary any of the material provided to or reviewed by the

inspectors during this inspection. The licensee acknowledged the findings

and took no exception.

Item Number

Status

Description / Reference Paragraph

321/88-05-01

Open

VIOLATION - Bypassing of APRM

Downscale Scram Inputs

(paragraph 5)

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Item Number

Status

Description / Reference Paragraph

cont'd

321/88-05-04

Open

VIOLATION - Inadequate MWO for

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Vacuum Breaker Maintenance

(paragraph 8)

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321,366/86-41-01'

Closed

VIOLATION - Failure to follow

plant procedures which

resulted in partial loss of water

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from the fuel pools (paragraph 3)

321,366/88-05-02

Open

URI - Leak Testing of Test

Solenoid Valves (paragraph 5)

321/88-05-03

Open

URI - Inadequate APRM

Surveillance (paragraph 8)

3.

Licensee Action on Previous Enforcement Matters (92702)

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(Closed) Violation 321,366/86-41-01, Failure to follow plant procedures

which resulted in a partial loss of water from the fuel pools.

The GPC

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letter of response dated May 8,1987, was reviewed. Licensee corrective

action involved replacement of the transfer canal inflatable seal assembly,

an enhancement of the leak detection system (implemented by DCR 87-99),

the addition of redundant air supplies to the inflatable seal assembly and

annunciation in the control rocin for loss of seal air pressure (implemented

by DCR 87-100), and specific training for operations personnel on the

spill event.

The inspector reviewed the GPC corrective action package,

DCR's 87-99 and 87-100 (and associated MW0s), toured the new seal air

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supply system with the system engineer and determined that the required

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corrective actions had been performed.

Since the actions to correct the

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specifics of this violation have been completed, this item is closed.

4.

Unresolved Item (URI)*

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(0 pen) URI 321,366/88-05-02, Leak Testing of Test Solenoid Valves.

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(0 pen) URI 321/88-05-03, Inadequate APRM Surveillance.

(Closed) URI 321,366/87-02-03, Method to Ensure Qualified Personnel are

Available to Fill Emergency Organization Positions.

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In Inspection Report 321,366/87-18 the Emergency Preparedness Section

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opened IFI 87-18-04, Veri fy Shift Augmentation Times and Violation

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87-18-05, Failure to Maintain a Trained and Qualified Emergency Response

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Staff.

These two items cover the same concern as 87-02-03. URI 87-02-03

is closed to remove the redundancy.

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"An Unresolved Item is a matter about which more information is required to

determine whether it is acceptable or may involve a violation or deviation.

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5.

Operational Safety Verification (71707) Units 1 and 2

The inspectors kept themselves informed on a daily basis of the overall

plant status and any significant safety matters related to plant

operations. Daily discussions were held with plant management and various

members of the plant operating staff. The inspectors made frequent visits

to the control room. Observations included instrument readings, setpoints

and recordings, status of operating systems, tags and clearances on

equipment, controls and switches, annunciator alarms, adherence to

limiting conditions for operation, temporary alterations in effect, daily

journals and data sheet entries, control room manning, and access

controls. This inspection activity included numerous informal discussions

with operators and their supervisors.

Weekly, when on site, selected

Engineering Safety Feature (ESF) systems were confirmed operable.

The

confirmation was made by verifying the following:

accessible valve flow

path alignment, power supply breaker and fuse status, instrumentation,

major component leakage, lubrication, cooling, and general condition.

General plant tours were conducted on at least a weekly basis. Portions

of the control building, turbine building, reactor building, and outside

areas were visited.

Observations included general plant / equipment

conditions, safety related tagout verifications, shif t turnover, sampling

program, housekeeping and general plant conditions, fire protection

equipment, control of activities in progress, radiation protection

controls, physical security, problem identification systems, missile

hazards, instrumentation and alarms in the control room, and containment

isolation.

On January 28, 1988, the inspector observed tools and other materials in

the Unit 1 reactor building in the vicinity of Core Spray System Outboard

Injection Valve 1E21-F004A.

These items had apparently not been removed

following the completion of maintenance work. This matter was brought to

the attention of the Unit 1 Shift Supervisor.

On February 9,

1988, while administering an NRC operator licensing

examination, the examiner noted that Unit I was potentially operating with

less than the minimum number of operable Average Power Range Monitor

(APRM) Downscale scram inputs required by the Technical Specifications

(TS).

At the time of this observation (approximately 0840) Unit I was

operating in the RUN mode at approximately 100 percent of rated power.

The examiner noted that APRM channel A and Intermediate Range Monitor

(IRM) channel C were both in the bypassed condition.

A review of a

f acility print (H-17789) confirmed that the bypassing of IRM channel C in

effect bypassed the Downscale scram input of APRM channel C.

Since APRM

channels A, C and E provide input to Reactor Protection system (RPS)

channel A, only APRM channel E remained available to provide Downscale

scram input to this RPS Channel.

During power operations Table 3.1-1 of

the TS requires a minimum of two operable channel inputs per RPS channel

for the APRM Downscale scram function. If the min' um number of operable

inputs cannot be met for an RPS channel, the affected RPS channel must be

tripped.

The examiner observed that RPS channel A was not tripped.

The

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examiner discussed his concerns with the Unit 1 Shift Supervisor and noted

that IRM channel C was subsequently unbypassed.

The resident inspector attempted to determine how long APRM channel A and

IRM channel C had been simultaneously bypassed in following up on this

matter. This could not be determined from a review of control room log

books. However, on duty operations personnel indicated that the condition

had existed since at least the start of their shift.

This event is

considered a violation of TS Table 3.1-1 in that only one APRM channel

was available to provide APRM Downscale scram input to RPS channel A and

the RPS channel was untripped.

This matter will be tracked as Violation

321/88-05-01 - Bypassing of APRM Downscale Scram Inputs.

At approximately 1500 on February 9,

1988, while conducting an NRC

licensed one"/.or examination, the examiner noticed that halon tanks

serv 4 *., the Unit 2 Remote Shutdown Panel were discharged.

Discussions

wi .n operations personnel revealed that the tanks discharged at 2237 on

February 8, 1988. Operations personnel also indicated that no action had

,een taken to replenish the halon.

Since Unit 2 was in cold shutdown

during this time period, halon protection was not required for the Remote

Shutdown Panel.

However, the examiner and the resident inspectors were

concerned that the licensee had taken no action to replenish the halon

almost 17 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br /> af ter the discharge had taken place.

The licensee is

currently reviewing this matter. Region II NRC personnel will also review

this matter during a future inspection.

At 1920 on February 12, 1988, with Unit 1 operating at 100 percent of

rated power, the licensee declared a loss of primary containment integrity

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and entered a 12-hour hot shutdown LCO.

Proper NRC notifications were

made at that time.

These actions were precipitated by the results of

local leak rate testing (LLRT) in Unit 2 which is currently in an outage.

The licensee had previously been conducting LLRTs on vacuum breaker test

solenoid valves 2T48-F342A - L.

These test solenoid valves are in lines

that supply air to the air operators of torus to drywell vacuum breakers

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These vacuum breakers normally operate in the

2T48-F323A

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self-actuated mode.

The air operators exist for the purpose on

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demonstrating opening capability on a monthly basis.

For containment

isolation purposes, the licensee considers the air operators to be primary

barriers.

Test solenoid valves 2T48-F342A - L are considered outboard

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isolation valves, and are identified as containment isolation valves in

the licensee's Pump and Valve Program.

Until the current Unit 2 outage,

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LLRT's on these valves had been performed with pressure applied on the

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side of the F342 valves away from accident pressure. When recently tested

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on the accident side, the valves failed to hold pressure.

As a result of the Unit 2 test failures and the similarity of equipment in

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Unit 1, the licensee promptly declared a loss of primary containment

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integrity in Unit 1.

The licensee subsequently restored primary containment

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integrity in Unit 1 by disconnecting and capping the air lines at test

solenoid valves 1T48-F343A - L.

This avoided shutdown of Unit 1 and was

accomplished within the LCO time allowed.

The licensee it currently

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investigating this matter and exploring options for corrective action.

Pending completion of the licensee's investigation and -NRC review, the

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matter will be identified as Unresolved Item 321,366/88-05-02 - Leak

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Testing of Test Solenoid Valves.

One violation was identified.

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6.

Maintenance Observation (62703) Units 1 and 2

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During the report period, the inspectors observed selected maintenance

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activities.

The observations included a review of the work documents for

adequacy, adherence to procedure, proper tagouts, adherence to technical

specifications, radiological controls, observation of all or part of the

actual work and/or retesting in progress, specified retest requirements,

and adherence to the appropriate quality controls.

The primary maintenance

observations during this month are summarized below:

Maintenance Activity

Date

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1.

Preventive maintenance on Limitorque operator

1/26/88

on valve 2E32-F001P per procedure

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52PM-MNT-005-0S (Unit 2)

2.

Plant service water pump "2A" sequencing

1/28/88

timer evaluation per procedure

42SP-011188-0J-1-2S.

(Unit 2)

3.

Inspection of "2C" diesel generator per

2/3/88

procedure 52SV-R43-001-05 (Unit 2)

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4.

Inspection of Allis Chalmers Motor

2/8/88

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Control Center 2R24-5012 per

procedure 52PM-R24-001-05 (Unit 2)

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5.

Removal of Valve 2E11-F005B per

2/9/88

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Maintenance Work Order 2-87-3462 for

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Inservice Inspection (Unit 2)

No violations or deviations were identified.

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7.

Plant Modification (37700) Unit 2

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The inspectors observed the performance of selected plant modification

Design Change Requests (DCRs). The observation included a review of the

DCR for technical adequacy, conformance to Technical Specifications,

verification of test instrument calibration, observation of all or part of

the actual surveillances, removal from service and return to service of

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the system or components affected, and review of the data for acceptability

based upon the acceptance criteria.

The primary DCR observations are

summarized below:

DCR

Date

.86-235

2/2/88

81-008

2/8/88

No violations or deviations were identified.

8.

Surveillance Testing Observations (61726) Units 1 and 2

The inspectors observed the performance of selected surveillances.

The

observation included a review of the procedure for technical adequacy,

conformance to Technical Specifications, verification of test instrument

calibration, observation of all or part of the actual surveillances,

removal from service and return to service of the system or components

affected, and review of the data for acceptability based upon the

acceptance criteria. The primary surveillance testing observations during

this month are summarized below:

Surevillance Testing Activity

Date

1.

Reactor Core Isolation Cooling System

2/2/88

Pump Rated Flow Testing per

procedure 345V-E51-002-1S (Unit 1)

2.

Functional Testing of Offgas Vent Pipe

2/4/88

Radiation Monitor per procedure

575V-011-010-1 (Unit 1)

3.

Post Maintenance Functional Testing of

2/11/88

"2" Diesel Generator per procedure

52SV-R43-001-05 (Unit 2)

4.

Functional Testing and Calibration of APRMs

2/15/88

345V-C51-002-15 (Unit 1)

On February 15, 1988, at 1720, the licensee discovered that the

surveillance for Average Power Range Monitors (APRM) did not test all

contacts in the trip logic. The downscale and the flow biased high flux

trip contacts had not been included in the surveillance procedure and

therefore had not been tested weekly as required by Technical Specifications).

The APRMs were declared inoperable at 1720, 2-15-88 and the LC0 atiion required

by TS 3.1, Table 3.1-1, Scram Number 8 was entered. This required action

was to reduce power to the IRM range and to have the Mode Switch in Hot

Standby within eight hours.

The licensee requested that the NRC grant

discretionary enforcement to extend the LCO time for about eleven hours

(until 12:00 noon, 2-16-88) to allow time for procedure development and

testing of the APRM trips.

The request was processed through proper

channels and discussed. Since the LC0 time limit of eight hours was rot

exceeded, the discretionary enforcement was not utilized due to clearing

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of the LCO.

The Senior Resident Inspector reviewed the procedure and

witnessed the testing of one of the APRMs.

All APRMs were tested

satisfactorily and the LCO cleared .by 2302, 2-15-88.

This item,

Inadequate APRM Surveillance, will be tracked as URI 321/88-05-03. As

discussed in Region II Reports 321,366/87-29 and 321,366/87-33, several

Unit 1 torus to drywell vacuum breakers failed to test satisfactorily

during recent monthly operability testing.

More specifically, vacuum

breakers 1T48-F323 C and F did not test properly on November 11, 1987, and

vacuum breaker 1T48-F323E stuck open during testing on December 11, 1987.

Vacuum breaker li:.e-F323E eventually did close when the test switch at the

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local panel for vacuum breaker IT48-F323F was depressed.

The licensee

subsequently initiated a program to identify and correct wiring problems

in the test circuitry for these vacuum breakers.

Required corrective

actions were taken under Maintenance Work Orders (MW0s) 1-87-8123,

1-87-7516, 1-87-7517 and 1-87-7950 during the month of January 1988.

In

essence, the licensee found that solenoid valves in the air test lines for

IT48-F323C, E and F had been incorrectly wired and that individual wire

conductor labels for these solenoid valves were incorrect. The solenoid

valves (designated IT48-F342 C, E and F) are two-way valves that remain

open after the test button is released to assure that all air is relieved

from the test line.

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The licensee conducted a broader investigation af the vacuum breaker

testing problems to determine the root cause and identify any additional

needed corrective actions. The resident inspectors reviewed the report of

this investigation dated February 5,1988.

It was determined that the

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wiring discrepancies causing the testing problems were introduced in

October of 1987 during the performance of MWO 1-86-7823. This MWO was

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generated primarily to mark and stow a spare cable and verify the wiring

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of a new cable.

Personnel performing this work noticed and documented

improper conductor termination at test solenoid valves 1T48-F342C, E and

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F.

Unfortunately, MWO instructions to correct the observed wiring discrepa-

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ncies were inadequate, and subsequent corrective maintenance actually introduced

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wiring errors into the test circuitry.

The operability testing difficulties

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of vacuum breakers IT48-F323C, E, and F were subsequently experienced in

November and December of 1987.

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Technical Specification 6.8.1.a.

requires that written procedures be

established, implemented and maintained covering the activities recommended

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in Appendix

"A" of Regulatory Guide 1.33, Revision 2,

February 1978.

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Appendix "A" recommends that maintenance that can af fect the performance

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of safety-related equipment be properly preplanned and performed in

accordance with written procedures, documented instructions, or drawings

appropriate to the circumstances.

The rewiring of solenoid valves

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IT48-F342C,E and F in October 1987 is considered to be a violation of TS

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6.8.1.a. in that the instructions of MWO 1-86-7823 were inadequate and

resulted in improper wiring of the three vacuum breaker test soler.oid

valves.

This matter will be tracked as Violation 321/88-05-04

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Inadequate MWO for Vacuum Breaker Maintenance.

In reviewing this matter

the inspectors noted that the incorrect wiring of the test solenoid valves

did not impair the ability of the torus to drywell vacuum breakers to

function in the normal, self-actuated mode,

One violation was identified.

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9.

.ESF System Walkdown (71710)

The inspectors routinely conducted partial walkdowns of ESF systems. Valve

and breaker / switch lineups and equipment conditions were randomly verified

both locally- and in the control room to ensure that . lineups were in.

accordance with operability requirements and that equipment material

conditions were satisfactory. The Unit 1 Residual Heat Removal system "A"

loop was walked down in detail.

Within the areas inspected, no violations or deviations were identified.

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10.

Radiological Protection (71709) Units 1 and 2

The resident inspectors reviewed aspects of the licensee's radiological

protection program in the course of the monthly activities.

The

performance of health physics and other personnel was observed on various

shifts to include:

involvement of health physics supervision, use of

radiation work permits, use of personnel monitoring equipment, control of

high radiation areas, use of friskers and personal contamination monitors,

and posting and labeling.

No violations or deviations were noted.

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11.

Physical Security (71881) Units 1 and 2

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In the course of the monthly activities, the resident inspectors included

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a review of the licensee's physical security program. The performance of

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various shifts of the security force was observed in the conduct of daily

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activities to include: availability of supervision, availability of armed

response personnel, protected soc vital access controls, searching of

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personnel, packages and vehit 'es, badge issuance and retrieval, escorting

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of visitors, patrols and compensatory pests.

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On February 18, 1988, the resident inspectors toure, the new security

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building and observed operations in progress.

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No violations or deviations were noted.

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12.

Reportable Occurrences (90712 & 92700) Unit 1 and 2

A number of Licensee Event Reports (LERs) were reviewed for potential

generic impact, to detect trends, and to determine whether corrective

actions appeared appropriate. Events which were reported immediately were

also reviewed as they occurred to determine that Technical Specifications

were being met and the public health and safety were of utmost consideration.

Unit 1: 86-11, Personnel Error Causes ESF Actuation.

The events of

this LER were cited as Violation 86-03-03. The licensee's

corrective action was raviewed and the violation closed in

Inspection Report 86-28.

This LER is closed.

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87-01, Spurious Ground Fault Trips Turbine Overspeed Device

Causing Reactor SCRAM. The licensee's response to to this

event was reviewed and appeared adaquate.

No fault was

located in the turbine overspeed device and the device has

operated properly during Unit 1 power operations. This LER

is closed.

87-02, Ground Condition Trips Main Generator and Turbine

Resulting in Reactor SCRAM. A loose wire was located and

repaired.

Checks were made for other loose components or

ground conditions with none found. A review for possible

additional preventative measures is continuing.

This LER

is closed.

87-05. Blocked Air Port Prevents Damper Closure Resulting in

Improper ESF Actuation. This event was caused by a missing

locknut on the damper control valve bleed off port

adjusting screw. The nut was replaced, the screw properly

adjusted and locked and the other dampers inr.oected for

loose or missing locknuts.

This LER is closed.

Unit 2: 86-20, Primary Containment Penetrations Failed LLRT. All failed

penetrations were repaired and retested prior to Unit 2

startup.

This LER is closed.

87-05, Leaking Valves Cause RWCU Isolation (Group 5).

The leaking

valves were located and isolated and the Group 5 isolation

signal reset.

There is a continuing RWCU upgrade in

progress to which this problem has been added. This LER is

closed.

13. Operating Reactor Events (93702) Unit 2

As discussed in Report 321,366/88-01, the maximum reactor coolant system

cooldown rate of 100 degrees F per hour specified in Technical Specification 3.4.6.1 was exceeded during the shutdown of Unit 2 on

January 13, 1988. The licensee determined that a cooldown from about 520

to 375 degrees F occurred in one hour.

The associated technical specification

Action Statement required the licensee to perform an engineering

evaluation to determine the effects of the out-of-limit condition on the

fracture toughness properties of the r6 actor coolant system and to determine

that the reactor coolant system remains acceptable for continued

operation.

An engineering evaluation, performed by General Electric

Company for the licensee, addressed the potential cor.cerns of brittle

fracture, allowable stress and f atigue.

The evaluation concluded that

brittle fracture was not a concern, and that the impact of the transient

on maximum stress and fatigue were less severe than those evaluated for

the design basis single relief valve blowdown event.

In summary, it was

concluded that there were no structural integrity concerns with continued

operation of Unit 2.

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The resident inspectors reviewed the General Electric engineering evaluation

dated January 18, 1988.

Within the areas inspected, no violations or deviations were identified.

14.

Information Meeting with Local Officials, (94600)

On February 2,1988, the Chief of Region II Projects Section 3B and the

resident inspectors held an information meeting with the Appling County

Board of Commissioners. The NRC representatives provided the Board with a

description of the NRC organization and responsibilities, a summary of

plant status and the business telephone numbers of appropriate NRC

contacts. Additionally, the Hatch resident inspectors were introduced and

the inspection program was briefly described.

Information available in

the local Public Document Rnom was also discussed. The NRC representatives

responded to questions posed by the Board at the conclusien of this

information meeting.

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