IR 05000461/1997001: Difference between revisions
StriderTol (talk | contribs) (StriderTol Bot change) |
StriderTol (talk | contribs) (StriderTol Bot change) |
||
Line 1: | Line 1: | ||
{{Adams | {{Adams | ||
| number = | | number = ML20149D523 | ||
| issue date = | | issue date = 06/23/1997 | ||
| title = | | title = SALP Rept 50-461/97-01 for Period of 950625-970405 | ||
| author name = | | author name = | ||
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) | | author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) | ||
| addressee name = | | addressee name = | ||
| addressee affiliation = | | addressee affiliation = | ||
| docket = 05000461 | | docket = 05000461 | ||
| license number = | | license number = | ||
| contact person = | | contact person = | ||
| document report number = 50-461-97-01, 50-461-97-1, NUDOCS | | document report number = 50-461-97-01, 50-461-97-1, NUDOCS 9707170166 | ||
| | | package number = ML20149D520 | ||
| document type = | | document type = SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE, TEXT-INSPECTION & AUDIT & I&E CIRCULARS | ||
| page count = | | page count = 7 | ||
}} | }} | ||
Line 19: | Line 19: | ||
=Text= | =Text= | ||
{{#Wiki_filter: | {{#Wiki_filter:1 | ||
. | . | ||
* | |||
. | |||
Clinton Power Station SALP 14 (Report No. 50-461/97001) i L INTRODUCTION The Systematic Assessment of Licensee Performance (SALP) process is used to develop the Nuclear Regulatory Commission's (NRC) conclusions regarding a licensee's safety j performance. Four functional areas are assessed: Plant Operations, Maintenance, | |||
Engineering, and Plarl Support. The SALP report documents the NRC's observations and ' | |||
insights on a licensee s performance and communicates the results to the licensee and the public. It provides a vehicle for clear communication with licensee management that focuses on plant performance relative to safety risk perspectives. The NRC utilizes SALP results when allocating NRC inspection resources at licensee facilities This report is the NRC's assessment of the safety performance at Illinois Power's Clinton Power Station for the SALP 14 period from June 25,1995 through April 5,199 An NRC SALP Board, composed of the individuals listed below, met on April 30,1997, to review the observations and data on performance and to assess performance in i accordance with the guidance in NRC Management Directive 8.6, " Systematic Assessment I of Licensee Performance" Board Chairman - | |||
'J. L.'Caldwell, Director, Division of Reactor Projects, Region ill Board Members G.-H. Marcus,' Director, Projects Directorate 1113, NRR M. N. Leach, Acting Deputy Director, Division of Reactor Safety l G. L. Shear, Acting Deputy Director, Division of Nuclear Meterial Safety 1 Jh PERFORMANCE ANALYSIS ) | |||
A. Plant Ooerations > | |||
, | |||
! | |||
Performance in this functional area was adequate, a decline from performance in the previous period. Areas of decline included procedure use and adherence, quality of | |||
' procedures, control room conduct of operations, and personnel errors. Management was unable to provide satisfactory guidance and oversight to the plant staff to address these problems, especially the procedure related issues, until after significant NRC interventio Further, management fostered an environment which placed excessive emphasis on minimizing equipment and unit outage ' time. The September 5,1996, reactor' recirculation (RR) pump seal failure and follow up to that event revealc<i the extent of decline in these areas. In March through May 1997, the licensee made improvements in_the areas noted above'as part of a recovery program, and NRC inspectors noted improvement _ | |||
9707170166 970623 Y PDR ADOCK 05000461 G -POR | |||
. . _ __ __ _ _ _ . _ . . _ _ _ _ . . _ . _ _ . _ _ . . _ - _ . . - . - . _ _ _ _ . . | |||
.- | |||
; | |||
e p | |||
, .. l | |||
. | . | ||
" | |||
Management failed to provide appropriate control over procedures, and was unable to l | |||
- provide-adequate guidance on procedure use until after significant NRC involvement. This | |||
!- deficiency resulted in a pervasive problem with procedural adherence, with some instances | |||
. amounting to careless disregard for NRC regulations. During the September 5,1996, RR | |||
. | |||
! | ! | ||
- pump seal failure event, operators improperly used procedures which led to a failure of the | |||
,1 RR pump seal and other complications. The NRC identified the procedural adherence | |||
: -issues shortly after the September 5 event. The administrative procedure guiding procedural adherence allowed staff to modify procedures without observing important | |||
; procedural change controls. Licensee management did not articulate to plant staff the | |||
, | , | ||
proper level of procedural adherence control and procedure change requirements until April | |||
: .1997, after NRC inspection activities continued to identify numerous procedural adherence | |||
+ | |||
problems. Appropriate procedural adherence and procedure change policies and programs | |||
; were implemented at the end of the period. | |||
i' | |||
Some operating procedures were not appropriate for the intended evolution. The | |||
' | ' | ||
.. | |||
surveillance procedure for high pressure core spray (HPCS) valve operability allowed the I | |||
' | ' | ||
. test to be performed under plant conditions which prevented the operators from obtaining | |||
~ accurate test results. A reactor water cleanup pump failed upon loss of suction flow j during a bus restoration. The pump did not trip because the procedure in use allowed j system operation when pump trip protective features were inoperable. Improper 3 procedural instructions for defeating the reactor core isolation cooling suction transfer logic ; | |||
. | 4' | ||
were identified during procedure use in a plant transient. Recovery of the main condenser l | |||
, | l :following a scram was significantly delayed due, in part, to system restoration procedure | ||
{- problems. 'At the end of the period, the licensee was involved in significant procedure i | |||
' | ' | ||
reviews and upgrades, especially in the areas of operations surveillance, instrument surveillance, and system operating precedure ] | |||
At times management and staff placed excessive emphasis on minimizing equipment and j | |||
. | |||
unit outage time. A plan to support an outage schedule by intentionally defeatin'g the ] | |||
j - primary containment hatch interlock while the reactor was critical was developed by plant j | |||
, staff and was approved by plant management early in the SALP period. NRC intervention ' | |||
: was required to prevent this inappropriate action. Plant management's decision to reduce ; | |||
l' | |||
outage time by maintaining.the plant in hot stand-by following a complicated reactor trip 1 | |||
;. resulted in cycling the safety relief valves approximately 85 times. This decision increased l r the likelihood of a relief valve sticking open, causing an uncontrolled cooldown. In an ! | |||
;. effort to maintain the reactor at power on September 5,1996, plant management | |||
, | , | ||
responded to a degraded seal on the "B" RR pump in a manner which led to seal failure of the pump, a preventable entry into emergency operating procedures, and the declaration of an Unusual Event. After the RR pump seal failure, the unit was shut down in a protracted manner allowing maximum time for the leakage rate to decrease below the Technical | |||
- | |||
Specification limit, which would have allowed continued unit operations. Individual , | |||
; ' operators manipulated the.feedwater system in a manner outside of the approved i procedural guidance to reduce outage time and expedite unit restart following the l September 1996 even l l | |||
' Although conduct of operations in the control room was adequate, a number of errors were identified. Failure to track identified leakage during the RR pump seal failure event complicated the operating crew's ability to evaluate the proper emergency action level Y 2 | |||
; | |||
' | |||
,- ' . , ~ . , . - - - . - - . . , - , . . . - - . - . - . , | |||
~ , - - . - | |||
. | . | ||
. | . | ||
classification. An incorrectly performed valve line-up resulted in a large spill of feedwater ' | |||
which was not identified for two shifts despite repeated control room annunciator indications of high emergency core cooling system sump levels. NRC inspectors identified some instances of inadequate short term relief turnovers, incomplete operator logs and rounds sheets, and informal control room communications. Further, the inspectors identifieil one example of an operator leaving the "at the controls" area without proper relie In addition, there were a number of personnel errors in activities conducted outside the control room area. Multiple errors in preparing, implementing, and clearing a tagout resulted in racking in a high voltage circulating water pump motor breaker contrary to the i requirements of a tagout. An inadvertent reactor protection system trip was initiated when an operator removed intermediate range rnonitor "E" from service with IRM "F" | |||
); | |||
already deenergized. An operator incorrectly positioned the division 11 emergency diesel l generator maintenance switch while performing a tagout, and the second operator failed to j perform an adequate independent verification of the tagou j I | |||
for | Management implemented two partial work stand-downs in February 1997 to address the i excessive number of personnel errors. Following the second February 1997 stand-down, notable improvements in performance were observed by the NRC. Following an NRC inspection debrief involving a March 9,1997, procedure adherence incident, the licensee l made critical changes to procedures governing procedural adherence and the temporary procedure change process, in concert with these actions, other operating, surveillance, | ||
* | * | ||
this | and maintenance procedures were revised to support the emphasis on strict procedural adherence. Late in the period, inspectors observed operators making detailed changes to procedures when surveillance such as diesel generator operability runs could not be performed as written, then proceeding in a controlled deliberate manner to complete the task. Management monitoring and industry peer reviews performed from March through June 1997 resulted in improvement in control room formality and communications near the end of the perio l The Plant Operations area is rated Category ' | ||
B. Maintenance j l | |||
Performance in this functional area declined during this assessment period, but remained j good overall. With notable exceptions, safety related plant equipment was well maintained. The licensee's maintenance program appropriately identified a number of systems requiring additional monitoring, and ensured those systems were receiving j additional attention. However, problems with procedure adherence, procedure and work i package quality, work control, and timely resolution of equipment concerns were evident j throughout the perio Timely resolution of known material condition concerns was lacking in sorra instance While the Clinton facility has historically performed wellin maintaining safaty systems, some long term deGcient conditions have been allowed to exist with respect to balance-of- ; | |||
plant equipment. Examoles included the drywell floor drain sump monitoring system, "B" ! | |||
circulating water purnp starting problems, and control room deficiencies. Extensive NRC l | |||
! | |||
i | |||
: | |||
ll l | |||
j | |||
! | |||
. | . | ||
- | - | ||
. | . | ||
A intervention was required to ensure adequate resolution of some material condition deficiencies including control room correctives, feedwater check valves and safety related breaker problem A number of long-standing material condition issues were pursued during the extended refueling outage. Significant reductions were made in the number of control room deficiencies, a problem identified in the previous SALP period, with over 400 items resolved. Near the end of the period, operators and staff were aggressively identifying additional items, and maintenance staff was actively working to correct them. A concentrated effort on the outboard feedwater isolation check valves resulted in dramatically reduced as left leakage rates. In May and June 1997, the licensee expended considerable resources to ensure operational readiness for safety related breaker Although most routine maintenance activities were conducted safely, maintenance i procedures did not always provide sufficient control of activities in some important area l inadequate procedures resulted in diesel generator preconditioning during performance of I monthly surveillance, damage to the reactor recirculation piping due to the implementation of freeze seals, and failure to meet procedural requirements regarding Use History Analyses, in addition, the Division 111 emergency diesel generator was inoperable for almost a year, in part due to maintenance personnel not questioning a large discrepancy between as-found and as-left relay calibration data, in response to the problems, the ! | |||
licensee initiated an extensive review and revision of existing maintenance procedure l Deficiencies in work packages and work planning complicated some maintenance task j Work planning deficiencies included lack of contingency planning, inadequate tagouts, and l J | |||
failure to provide parts required to complete activities. The reactor trip of April 1996 was l | |||
'due, in part, to the work package for switchyard work which was deficient in that it failed l to differentiate design differences in switchyard breakers and to provide an impact matrix l to discuss the risk of this maintenance on losing a reserve auxiliary transformer at powe l A second reactor trip in June 1996 was attributed to personnel error while performing l maintenance in a difficult environnien At the end of the period, the licensee was working on improving the maintenance work control process, improving surveillance procedures, and in ensuring proper procedure adherence. NRC observed improved procedure adherence and that procedures were being changed when problems were identifie The Maintenance area is rated Category C,, Enaineerina Overall performance in engineering was adequate. Strengths noted during the previous SALP in self-assessment, design, and response to high-priority issues were absent from the current SALP period. Problems with resolution of long-term issues, corrective actions, and inconsistent management oversight that existed in the last period continued. In addition, weaknesses in root cause investigation and corrective action, design control, operability evaluations,10 CFR 50.59 evaluations, and procedure compliance surfaced during the SALP perio , | |||
_ | |||
not | |||
. ~ . - . - . ~ - - . - . . _ - . - - . - - ~ . _ . ~ _ . - . - - . . - . - . - . . | |||
. | . | ||
. . | .. | ||
. .. . .. | l Root cause investigations and corrective action for equipment problems were often not appropriate or timely.'' In particular, a long term common mode failure problem associated with hardened grease in electrical breakers and difficulties with drywall sump leakage monitoring instrumentation noted in the last SALP were neither aggressively pursued nor | ||
.. . | ' corrected. Most notably, the licensee failed to properly evaluate the condition of 480V, 4160V, and 6.9Kv breakers even after hardened grease had been identified in the breakers. There were examples late in the period where aggressive actions were take For example, the licensee's identification and response to instrument inaccuracies in surveillance and degraded voltage associated with the 345Kv supply through the reserve auxiliary transformer were considered positiv Some design activities resulted in inadequate designs and design errors resulting in significant problems in a number of areas. Several design changes were unsuccessful and had to be modified for important plant equipment to operate satisfactorily, including the drywell leakage monitoring system and a regulating transformer installation in the auxiliary power system to address degraded voltage concern I The operability evaluation program lacked appropriate guidance for engineers and I operators, the program could not easily retrieve previous evaluations, and actions i recommended by the operability evaluations were not always complete nor were they tracked. Some operability evaluations appeared to focus on justifying system operability rather than objectively evaluating the situation against system operability and consistency with the USAR. Specific examples included incorrect motor operator valve weights used , | ||
in seismic analyses and control room chiller auto-start load on the diesel. generato Safety evaluations conducted per 10 CFR 50.59 were not always performed as required and when' performed the' evaluations were at times inadequate. Of greatest concern was the use of engineering generated " Action Plans" which.were used to direct operators to ) | |||
perform special tests on' reactor systems without appropriate safety evaluations'or required ] | |||
reviews. Examples of 10 CFR 50.59 deficiencies included: a special test which isolated j the cycled condensate system from the residual heat removal (RHR) system resulting in l RHR inoperability; disabled annunciators for demineralizer differential pressure; and the l removal of emergency diesel generator air start system dryer check valve springs. An | |||
. improved safety evaluation program was developed as corrective action for these problems. The improved program included training for all engineering and operations personnel on the purpose of 10 CFR 50.59, designation of specially trained and selected ] | |||
individuals to review all safety evaluations, and increased emphasis on safety evaluation ! | |||
A number of examples of failure to follow procedures were noted during several l inspections. One of the most significant contributed to the RHR inoperability example noted previously, which involved engineers indicating it was acceptable to combine steps from disparate procedures without further review. The problem appeared to be the cause or a significant contributor to a variety of engineering weaknesses identified during the SALP period. | |||
of | |||
. | g . Late in the assessment period, the licensee took a number of steps to identify additional i problems and correct known deficiencies. Shortly after the Operational Safety Team ( Inspeiction results were published, the licensee's Engineering Department contracted for an b l L 5 l | ||
I | |||
. .. . - . .-. : | |||
. - - - . -- | |||
. . | |||
The | outside organization to review all engineering activities. In addition, third party focused reviewswere conducted for areas where program improvements had been implemented, including operability and 10 CFR 50.59 evaluations. The changes in these two specific programs were viewed as significant improvements in the Engineering Department's methods for conducting busines , | ||
The Engineering area is rated Category E Plant Suocort Plant Support performance, although adequate, declined during this assessment period primarily due to a significant performance decline in radiation protection (RP). Deficiencies identified in RP mirrored those identified in other areas. Specifically, problems were identified in licensee workers' sensitivity towards and understanding of radiological controls and alarms, and procedural adequacy and adherence. While the problems did not result in any overexposures to licensee personnel or its contractors, the issues were indicative of management controls not being effectively implemented in the radiation protection area which led to a programmatic breakdown. Similar problems with procedural adherence and understanding requirements were also evident in the Security functional area. These problems impacted effective irnp;cmentation of several access cortrol programs, a response activity, and some barrier control activities. Emergency preparedness performance was good, but afsc declined. Several examples were noted where emergency plan requirements were neither implemented in a timely manner nor well understood by plant staf Radiation protection program management failed to recognize that a lack of sensitivity towards and understanding of radiological controls and alarms existed among the work force. This was exemplified by a number of staff actiens including: two occasions where a worker or workers secured the supply gas to a porta! contamination monitor, rendering the monitor inoperable; an apparent deliberate contamination of an RP technician; and worker (s) identified to be sleeping and smoking in the radiologically controlled area, in adoition, procedural adherence and adequacy problems contributed to several radiological events. The events included, contamination of three workers during resin sluicing, pressurization of a radiological waste transfer line prior to having performed an adequate radiological survey, and inadvertent entry of three workers into the drywell in violation of a Radiation Safety Work Plan (RSWP). Although none of the events resulted in worker overexposures, the inadvertent entry into the drywall put the workers at risk of a potentially lethat exposure had fuel handling resumed and a mishap occurred while they were in the upper levels of the drywell. Some aspects of the radiation protection program remained good, such as ALARA planning and controls, and reactor water chemistry; however, the above problems indicated that most of the radiation protection program is in need of significant improvemen Security and Emergency preparedness (EP) performance declined but were considered good. In addition to a lack of understanding of security and EP plan requirements, these areas exhibited weaknesses similar to those in the other areas with regard to procedural adherence and adequacy. In the security area, these problems impacted effective | |||
; implementation of several access control programs, a response activity, and some barrier l l | |||
! | |||
V | |||
_ .. __ _ _ _ _ -._ | |||
. | |||
._ . _ _ | |||
. | |||
. | |||
. | . | ||
O-controls activities. In the EP area, the lack of staff unde.rstanding of the EP plan was I evidenced by a lack of classification conservatism during the September 5,1996 even Additionally, the EP staff was not aggressive in evaluating actual events, in updating the Updated Safety Analysis Report, and in completing timely corrective action for identified backup Meteorological tower instrumentation failures. How3ver, these problems did not affect the overall excellent performance during the 1996 annual exercis Following the end of this SALP period a follow up inspection into the radiation protection f area identified the beginnings of improvements in the area. Some improvement was ) | |||
observed in the awareness among licensee staff of radiation protection requirements and practices. Some improvements were also observed in planning and execution of work, with an emphasis on applying lessons learned. Management expectations on procedure adherence and supervisory oversight of work activities had been emphasized during special training session The Plant Support area is rated Category I | |||
\ | |||
l l | |||
l i | |||
l l | |||
: | |||
l 7- | |||
: | |||
-. | |||
}} | }} |
Revision as of 16:42, 11 December 2021
ML20149D523 | |
Person / Time | |
---|---|
Site: | Clinton |
Issue date: | 06/23/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
To: | |
Shared Package | |
ML20149D520 | List: |
References | |
50-461-97-01, 50-461-97-1, NUDOCS 9707170166 | |
Download: ML20149D523 (7) | |
Text
1
.
.
Clinton Power Station SALP 14 (Report No. 50-461/97001) i L INTRODUCTION The Systematic Assessment of Licensee Performance (SALP) process is used to develop the Nuclear Regulatory Commission's (NRC) conclusions regarding a licensee's safety j performance. Four functional areas are assessed: Plant Operations, Maintenance,
Engineering, and Plarl Support. The SALP report documents the NRC's observations and '
insights on a licensee s performance and communicates the results to the licensee and the public. It provides a vehicle for clear communication with licensee management that focuses on plant performance relative to safety risk perspectives. The NRC utilizes SALP results when allocating NRC inspection resources at licensee facilities This report is the NRC's assessment of the safety performance at Illinois Power's Clinton Power Station for the SALP 14 period from June 25,1995 through April 5,199 An NRC SALP Board, composed of the individuals listed below, met on April 30,1997, to review the observations and data on performance and to assess performance in i accordance with the guidance in NRC Management Directive 8.6, " Systematic Assessment I of Licensee Performance" Board Chairman -
'J. L.'Caldwell, Director, Division of Reactor Projects, Region ill Board Members G.-H. Marcus,' Director, Projects Directorate 1113, NRR M. N. Leach, Acting Deputy Director, Division of Reactor Safety l G. L. Shear, Acting Deputy Director, Division of Nuclear Meterial Safety 1 Jh PERFORMANCE ANALYSIS )
A. Plant Ooerations >
,
!
Performance in this functional area was adequate, a decline from performance in the previous period. Areas of decline included procedure use and adherence, quality of
' procedures, control room conduct of operations, and personnel errors. Management was unable to provide satisfactory guidance and oversight to the plant staff to address these problems, especially the procedure related issues, until after significant NRC interventio Further, management fostered an environment which placed excessive emphasis on minimizing equipment and unit outage ' time. The September 5,1996, reactor' recirculation (RR) pump seal failure and follow up to that event revealc<i the extent of decline in these areas. In March through May 1997, the licensee made improvements in_the areas noted above'as part of a recovery program, and NRC inspectors noted improvement _
9707170166 970623 Y PDR ADOCK 05000461 G -POR
. . _ __ __ _ _ _ . _ . . _ _ _ _ . . _ . _ _ . _ _ . . _ - _ . . - . - . _ _ _ _ . .
.-
e p
, .. l
.
"
Management failed to provide appropriate control over procedures, and was unable to l
- provide-adequate guidance on procedure use until after significant NRC involvement. This
!- deficiency resulted in a pervasive problem with procedural adherence, with some instances
. amounting to careless disregard for NRC regulations. During the September 5,1996, RR
!
- pump seal failure event, operators improperly used procedures which led to a failure of the
,1 RR pump seal and other complications. The NRC identified the procedural adherence
- -issues shortly after the September 5 event. The administrative procedure guiding procedural adherence allowed staff to modify procedures without observing important
- procedural change controls. Licensee management did not articulate to plant staff the
,
proper level of procedural adherence control and procedure change requirements until April
- .1997, after NRC inspection activities continued to identify numerous procedural adherence
+
problems. Appropriate procedural adherence and procedure change policies and programs
- were implemented at the end of the period.
i'
Some operating procedures were not appropriate for the intended evolution. The
'
..
surveillance procedure for high pressure core spray (HPCS) valve operability allowed the I
'
. test to be performed under plant conditions which prevented the operators from obtaining
~ accurate test results. A reactor water cleanup pump failed upon loss of suction flow j during a bus restoration. The pump did not trip because the procedure in use allowed j system operation when pump trip protective features were inoperable. Improper 3 procedural instructions for defeating the reactor core isolation cooling suction transfer logic ;
4'
were identified during procedure use in a plant transient. Recovery of the main condenser l
l :following a scram was significantly delayed due, in part, to system restoration procedure
{- problems. 'At the end of the period, the licensee was involved in significant procedure i
'
reviews and upgrades, especially in the areas of operations surveillance, instrument surveillance, and system operating precedure ]
At times management and staff placed excessive emphasis on minimizing equipment and j
.
unit outage time. A plan to support an outage schedule by intentionally defeatin'g the ]
j - primary containment hatch interlock while the reactor was critical was developed by plant j
, staff and was approved by plant management early in the SALP period. NRC intervention '
- was required to prevent this inappropriate action. Plant management's decision to reduce ;
l'
outage time by maintaining.the plant in hot stand-by following a complicated reactor trip 1
- . resulted in cycling the safety relief valves approximately 85 times. This decision increased l r the likelihood of a relief valve sticking open, causing an uncontrolled cooldown. In an !
- . effort to maintain the reactor at power on September 5,1996, plant management
,
responded to a degraded seal on the "B" RR pump in a manner which led to seal failure of the pump, a preventable entry into emergency operating procedures, and the declaration of an Unusual Event. After the RR pump seal failure, the unit was shut down in a protracted manner allowing maximum time for the leakage rate to decrease below the Technical
-
Specification limit, which would have allowed continued unit operations. Individual ,
- ' operators manipulated the.feedwater system in a manner outside of the approved i procedural guidance to reduce outage time and expedite unit restart following the l September 1996 even l l
' Although conduct of operations in the control room was adequate, a number of errors were identified. Failure to track identified leakage during the RR pump seal failure event complicated the operating crew's ability to evaluate the proper emergency action level Y 2
,- ' . , ~ . , . - - - . - - . . , - , . . . - - . - . - . ,
.
.
classification. An incorrectly performed valve line-up resulted in a large spill of feedwater '
which was not identified for two shifts despite repeated control room annunciator indications of high emergency core cooling system sump levels. NRC inspectors identified some instances of inadequate short term relief turnovers, incomplete operator logs and rounds sheets, and informal control room communications. Further, the inspectors identifieil one example of an operator leaving the "at the controls" area without proper relie In addition, there were a number of personnel errors in activities conducted outside the control room area. Multiple errors in preparing, implementing, and clearing a tagout resulted in racking in a high voltage circulating water pump motor breaker contrary to the i requirements of a tagout. An inadvertent reactor protection system trip was initiated when an operator removed intermediate range rnonitor "E" from service with IRM "F"
);
already deenergized. An operator incorrectly positioned the division 11 emergency diesel l generator maintenance switch while performing a tagout, and the second operator failed to j perform an adequate independent verification of the tagou j I
Management implemented two partial work stand-downs in February 1997 to address the i excessive number of personnel errors. Following the second February 1997 stand-down, notable improvements in performance were observed by the NRC. Following an NRC inspection debrief involving a March 9,1997, procedure adherence incident, the licensee l made critical changes to procedures governing procedural adherence and the temporary procedure change process, in concert with these actions, other operating, surveillance,
and maintenance procedures were revised to support the emphasis on strict procedural adherence. Late in the period, inspectors observed operators making detailed changes to procedures when surveillance such as diesel generator operability runs could not be performed as written, then proceeding in a controlled deliberate manner to complete the task. Management monitoring and industry peer reviews performed from March through June 1997 resulted in improvement in control room formality and communications near the end of the perio l The Plant Operations area is rated Category '
B. Maintenance j l
Performance in this functional area declined during this assessment period, but remained j good overall. With notable exceptions, safety related plant equipment was well maintained. The licensee's maintenance program appropriately identified a number of systems requiring additional monitoring, and ensured those systems were receiving j additional attention. However, problems with procedure adherence, procedure and work i package quality, work control, and timely resolution of equipment concerns were evident j throughout the perio Timely resolution of known material condition concerns was lacking in sorra instance While the Clinton facility has historically performed wellin maintaining safaty systems, some long term deGcient conditions have been allowed to exist with respect to balance-of- ;
plant equipment. Examoles included the drywell floor drain sump monitoring system, "B" !
circulating water purnp starting problems, and control room deficiencies. Extensive NRC l
!
i
ll l
j
!
.
-
.
A intervention was required to ensure adequate resolution of some material condition deficiencies including control room correctives, feedwater check valves and safety related breaker problem A number of long-standing material condition issues were pursued during the extended refueling outage. Significant reductions were made in the number of control room deficiencies, a problem identified in the previous SALP period, with over 400 items resolved. Near the end of the period, operators and staff were aggressively identifying additional items, and maintenance staff was actively working to correct them. A concentrated effort on the outboard feedwater isolation check valves resulted in dramatically reduced as left leakage rates. In May and June 1997, the licensee expended considerable resources to ensure operational readiness for safety related breaker Although most routine maintenance activities were conducted safely, maintenance i procedures did not always provide sufficient control of activities in some important area l inadequate procedures resulted in diesel generator preconditioning during performance of I monthly surveillance, damage to the reactor recirculation piping due to the implementation of freeze seals, and failure to meet procedural requirements regarding Use History Analyses, in addition, the Division 111 emergency diesel generator was inoperable for almost a year, in part due to maintenance personnel not questioning a large discrepancy between as-found and as-left relay calibration data, in response to the problems, the !
licensee initiated an extensive review and revision of existing maintenance procedure l Deficiencies in work packages and work planning complicated some maintenance task j Work planning deficiencies included lack of contingency planning, inadequate tagouts, and l J
failure to provide parts required to complete activities. The reactor trip of April 1996 was l
'due, in part, to the work package for switchyard work which was deficient in that it failed l to differentiate design differences in switchyard breakers and to provide an impact matrix l to discuss the risk of this maintenance on losing a reserve auxiliary transformer at powe l A second reactor trip in June 1996 was attributed to personnel error while performing l maintenance in a difficult environnien At the end of the period, the licensee was working on improving the maintenance work control process, improving surveillance procedures, and in ensuring proper procedure adherence. NRC observed improved procedure adherence and that procedures were being changed when problems were identifie The Maintenance area is rated Category C,, Enaineerina Overall performance in engineering was adequate. Strengths noted during the previous SALP in self-assessment, design, and response to high-priority issues were absent from the current SALP period. Problems with resolution of long-term issues, corrective actions, and inconsistent management oversight that existed in the last period continued. In addition, weaknesses in root cause investigation and corrective action, design control, operability evaluations,10 CFR 50.59 evaluations, and procedure compliance surfaced during the SALP perio ,
_
. ~ . - . - . ~ - - . - . . _ - . - - . - - ~ . _ . ~ _ . - . - - . . - . - . - . .
.
..
l Root cause investigations and corrective action for equipment problems were often not appropriate or timely. In particular, a long term common mode failure problem associated with hardened grease in electrical breakers and difficulties with drywall sump leakage monitoring instrumentation noted in the last SALP were neither aggressively pursued nor
' corrected. Most notably, the licensee failed to properly evaluate the condition of 480V, 4160V, and 6.9Kv breakers even after hardened grease had been identified in the breakers. There were examples late in the period where aggressive actions were take For example, the licensee's identification and response to instrument inaccuracies in surveillance and degraded voltage associated with the 345Kv supply through the reserve auxiliary transformer were considered positiv Some design activities resulted in inadequate designs and design errors resulting in significant problems in a number of areas. Several design changes were unsuccessful and had to be modified for important plant equipment to operate satisfactorily, including the drywell leakage monitoring system and a regulating transformer installation in the auxiliary power system to address degraded voltage concern I The operability evaluation program lacked appropriate guidance for engineers and I operators, the program could not easily retrieve previous evaluations, and actions i recommended by the operability evaluations were not always complete nor were they tracked. Some operability evaluations appeared to focus on justifying system operability rather than objectively evaluating the situation against system operability and consistency with the USAR. Specific examples included incorrect motor operator valve weights used ,
in seismic analyses and control room chiller auto-start load on the diesel. generato Safety evaluations conducted per 10 CFR 50.59 were not always performed as required and when' performed the' evaluations were at times inadequate. Of greatest concern was the use of engineering generated " Action Plans" which.were used to direct operators to )
perform special tests on' reactor systems without appropriate safety evaluations'or required ]
reviews. Examples of 10 CFR 50.59 deficiencies included: a special test which isolated j the cycled condensate system from the residual heat removal (RHR) system resulting in l RHR inoperability; disabled annunciators for demineralizer differential pressure; and the l removal of emergency diesel generator air start system dryer check valve springs. An
. improved safety evaluation program was developed as corrective action for these problems. The improved program included training for all engineering and operations personnel on the purpose of 10 CFR 50.59, designation of specially trained and selected ]
individuals to review all safety evaluations, and increased emphasis on safety evaluation !
A number of examples of failure to follow procedures were noted during several l inspections. One of the most significant contributed to the RHR inoperability example noted previously, which involved engineers indicating it was acceptable to combine steps from disparate procedures without further review. The problem appeared to be the cause or a significant contributor to a variety of engineering weaknesses identified during the SALP period.
g . Late in the assessment period, the licensee took a number of steps to identify additional i problems and correct known deficiencies. Shortly after the Operational Safety Team ( Inspeiction results were published, the licensee's Engineering Department contracted for an b l L 5 l
I
. .. . - . .-. :
. - - - . --
. .
outside organization to review all engineering activities. In addition, third party focused reviewswere conducted for areas where program improvements had been implemented, including operability and 10 CFR 50.59 evaluations. The changes in these two specific programs were viewed as significant improvements in the Engineering Department's methods for conducting busines ,
The Engineering area is rated Category E Plant Suocort Plant Support performance, although adequate, declined during this assessment period primarily due to a significant performance decline in radiation protection (RP). Deficiencies identified in RP mirrored those identified in other areas. Specifically, problems were identified in licensee workers' sensitivity towards and understanding of radiological controls and alarms, and procedural adequacy and adherence. While the problems did not result in any overexposures to licensee personnel or its contractors, the issues were indicative of management controls not being effectively implemented in the radiation protection area which led to a programmatic breakdown. Similar problems with procedural adherence and understanding requirements were also evident in the Security functional area. These problems impacted effective irnp;cmentation of several access cortrol programs, a response activity, and some barrier control activities. Emergency preparedness performance was good, but afsc declined. Several examples were noted where emergency plan requirements were neither implemented in a timely manner nor well understood by plant staf Radiation protection program management failed to recognize that a lack of sensitivity towards and understanding of radiological controls and alarms existed among the work force. This was exemplified by a number of staff actiens including: two occasions where a worker or workers secured the supply gas to a porta! contamination monitor, rendering the monitor inoperable; an apparent deliberate contamination of an RP technician; and worker (s) identified to be sleeping and smoking in the radiologically controlled area, in adoition, procedural adherence and adequacy problems contributed to several radiological events. The events included, contamination of three workers during resin sluicing, pressurization of a radiological waste transfer line prior to having performed an adequate radiological survey, and inadvertent entry of three workers into the drywell in violation of a Radiation Safety Work Plan (RSWP). Although none of the events resulted in worker overexposures, the inadvertent entry into the drywall put the workers at risk of a potentially lethat exposure had fuel handling resumed and a mishap occurred while they were in the upper levels of the drywell. Some aspects of the radiation protection program remained good, such as ALARA planning and controls, and reactor water chemistry; however, the above problems indicated that most of the radiation protection program is in need of significant improvemen Security and Emergency preparedness (EP) performance declined but were considered good. In addition to a lack of understanding of security and EP plan requirements, these areas exhibited weaknesses similar to those in the other areas with regard to procedural adherence and adequacy. In the security area, these problems impacted effective
- implementation of several access control programs, a response activity, and some barrier l l
!
V
_ .. __ _ _ _ _ -._
.
._ . _ _
.
O-controls activities. In the EP area, the lack of staff unde.rstanding of the EP plan was I evidenced by a lack of classification conservatism during the September 5,1996 even Additionally, the EP staff was not aggressive in evaluating actual events, in updating the Updated Safety Analysis Report, and in completing timely corrective action for identified backup Meteorological tower instrumentation failures. How3ver, these problems did not affect the overall excellent performance during the 1996 annual exercis Following the end of this SALP period a follow up inspection into the radiation protection f area identified the beginnings of improvements in the area. Some improvement was )
observed in the awareness among licensee staff of radiation protection requirements and practices. Some improvements were also observed in planning and execution of work, with an emphasis on applying lessons learned. Management expectations on procedure adherence and supervisory oversight of work activities had been emphasized during special training session The Plant Support area is rated Category I
\
l l
l i
l l
l 7-
-.