05000323/FIN-2017003-01: Difference between revisions

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| identified by = NRC
| identified by = NRC
| Inspection procedure = IP 71111.15
| Inspection procedure = IP 71111.15
| Inspector = C Newport, J Reynoso, G Kolcum, M Phalen, J O,'Donnell M, Hair
| Inspector = C Newport, J Reynoso, G Kolcum, M Phalen, J O, 'Donnellm Haire
| CCA = H.13
| CCA = H.13
| INPO aspect = DM.1
| INPO aspect = DM.1
| description = The inspectors identified a non- cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for the failure of the licensee to identify and correct a condition adverse to quality. Specifically, the licensee failed to implement prompt corrective actions related to a nitrogen leak from a component associated with safety -related pressurizer power -operated relief valve (PORV) , PCV -455C . The nitrogen leak subsequently resulted in the PORV being declared inoperable, as well as the declaration of an Alert emergency action level classification due the Unit 2 containment atmosphere exceeding habitability limits. The licensees failure to implement prompt corrective action to correct excessive nitrogen leakage into the Unit 2 containment was a performance deficiency.  The finding was more than minor because it was associated with the equipment performance attribute of the mitigating systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  Specifically, the excessive nitrogen leakage resulted in the inoperability of safety -related PORV PCV -455C for greater than technical specification allowed outage time and atmospheric conditions in Unit 2 containment that were an immediate danger to life and health, prompting an Alert emergency declaration. Using NRC Manual Chapter 0609, Significance Determination Process, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, and Appendix A, Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined the finding screened as having very low significance (Green) because: (1) it was not a design deficiency; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and (4) did not result in the loss of a high safety -significant non -technical specification train. The finding was assigned a human performance cross -cutting aspect associated with consistent processes, in  that the licensee did not use a systematic approach in properly assessing the potential risk significance of an increasing trend of nitrogen leakage inside containment [H.13] .  
| description = The inspectors identified a non- cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for the failure of the licensee to identify and correct a condition adverse to quality. Specifically, the licensee failed to implement prompt corrective actions related to a nitrogen leak from a component associated with safety -related pressurizer power -operated relief valve (PORV) , PCV -455C . The nitrogen leak subsequently resulted in the PORV being declared inoperable, as well as the declaration of an Alert emergency action level classification due the Unit 2 containment atmosphere exceeding habitability limits. The licensees failure to implement prompt corrective action to correct excessive nitrogen leakage into the Unit 2 containment was a performance deficiency.  The finding was more than minor because it was associated with the equipment performance attribute of the mitigating systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  Specifically, the excessive nitrogen leakage resulted in the inoperability of safety -related PORV PCV -455C for greater than technical specification allowed outage time and atmospheric conditions in Unit 2 containment that were an immediate danger to life and health, prompting an Alert emergency declaration. Using NRC Manual Chapter 0609, Significance Determination Process, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, and Appendix A, Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined the finding screened as having very low significance (Green) because: (1) it was not a design deficiency; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and (4) did not result in the loss of a high safety -significant non -technical specification train. The finding was assigned a human performance cross -cutting aspect associated with consistent processes, in  that the licensee did not use a systematic approach in properly assessing the potential risk significance of an increasing trend of nitrogen leakage inside containment [H.13] .  
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Revision as of 20:56, 20 February 2018

01
Site: Diablo Canyon Pacific Gas & Electric icon.png
Report IR 05000323/2017003 Section 1R15
Date counted Sep 30, 2017 (2017Q3)
Type: NCV: Green
cornerstone Mitigating Systems
Identified by: NRC identified
Inspection Procedure: IP 71111.15
Inspectors (proximate) C Newport
J Reynoso
G Kolcum
M Phalen
J O
'Donnellm Haire
Violation of: 10 CFR 50 Appendix B

10 CFR 50 Appendix B Criterion XVI

Technical Specification
CCA H.13, Consistent Process
INPO aspect DM.1
'