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| issue date = 06/11/1993
| issue date = 06/11/1993
| title = LER 92-008-01:on 920301,SGTS Fan Flow Limiter Setpoint Error Discovered.Caused by Analysis Deficiencies.Sgts Fan Flow Limiter Setpoint Changed & Rev 2 of Jco Approved W/New Offsite Dose calculations.W/930611 Ltr
| title = LER 92-008-01:on 920301,SGTS Fan Flow Limiter Setpoint Error Discovered.Caused by Analysis Deficiencies.Sgts Fan Flow Limiter Setpoint Changed & Rev 2 of Jco Approved W/New Offsite Dose calculations.W/930611 Ltr
| author name = FULLER R E, PARRISH J V
| author name = Fuller R, Parrish J
| author affiliation = WASHINGTON PUBLIC POWER SUPPLY SYSTEM
| author affiliation = WASHINGTON PUBLIC POWER SUPPLY SYSTEM
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:ACCELE~ED DOCUMENT DIS UTION SYSTEM REGUL RY INFORMATION DISTRIBUT SYSTEM (RIDS)ACCESSION NBR:9306230033 DOC.DATE: 93/06/11 NOTARIZED:
{{#Wiki_filter:ACCELE             ~ED DOCUMENT DIS                           UTION SYSTEM REGUL     RY INFORMATION         DISTRIBUT       SYSTEM (RIDS)
NO FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe AUTH.NAME AUTHOR AFFILIATION FULLER,R.E.
ACCESSION NBR:9306230033             DOC.DATE:     93/06/11   NOTARIZED: NO         DOCKET  ¹ FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public                 Powe 05000397 AUTH. NAME           AUTHOR AFFILIATION FULLER,R.E.         Washington Public Power Supply System PARRISH,J.V.         Washington Public Power Supply System RECIP.NAME           RECIPIENT AFFILIATION
Washington Public Power Supply System PARRISH,J.V.
Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION DOCKET¹05000397


==SUBJECT:==
==SUBJECT:==
LER 92-008-01:on 920301,SGTS fan flow limiter setpoint error discovered.
LER   92-008-01:on 920301,SGTS fan flow limiter setpoint error discovered. Caused by analysis deficiencies.SGTS fan flow limiter setpoint changed & Rev 2 of JCO               approved w/new offsite dose calculations.W/930611 ltr.
Caused by analysis deficiencies.SGTS fan flow limiter setpoint changed&Rev 2 of JCO approved w/new offsite dose calculations.W/930611 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES: RECIPIENT ID CODE/NAME PDV LA CLIFFORD,J INTERNAL: ACNW AEOD/DOA AEOD/ROAB/DSP NRR/DE/EMEB NRR/DRCH/HICB NRR/DRIL/RPEB NRR/DRSS/PRPB NRR/DSSA/SRXB RES/DSIR/EIB EXTERNAL EG&G BRYCE i J~H NRC PDR NSIC POORE,W.COPIES LTTR ENCL 1 1 1 1 2 2 1 1 2 2 1 1 1 1 1 1 2 2 1 1 1 1 2 2 1 1 1 1 RECIPIENT ID CODE/NAME PDV PD ACRS AEOD/DSP/TPAB NRR/DE/EELB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPW/OEAB NRR/DSSA/SPLB EG:F~02 RGN5 FILE 01 L ST LOBBY WARD NSIC MURPHYtG.A NUDOCS FULL TXT COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 ,1 1 NOTE TO ALL"RIDS" RECIPIENTS:
DISTRIBUTION CODE: IE22T           COPIES RECEIVED:LTR           ENCL     SIZE:
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (Exl'.504-2065)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 32 ENCL 32 WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O.Box 968~3000 George Washington Way~Richland, Washington 99352 June 11, 1993 G02-93-151 Docket No.50-397 Document Control Desk U.S.Nuclear Regulatory Commission Washington, D.C.20555  
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
RECIPIENT              COPIES              RECIPIENT         COPIES ID CODE/NAME            LTTR ENCL          ID CODE/NAME       LTTR ENCL PDV LA                       1      1      PDV PD                1    1 CLIFFORD,J                   1      1 INTERNAL: ACNW                         2      2      ACRS                  2    2 AEOD/DOA                     1      1      AEOD/DSP/TPAB          1    1 AEOD/ROAB/DSP                 2      2      NRR/DE/EELB            1    1 NRR/DE/EMEB                  1      1      NRR/DRCH/HHFB          1    1 NRR/DRCH/HICB                1      1      NRR/DRCH/HOLB          1     1 NRR/DRIL/RPEB                1      1      NRR/DRPW/OEAB          1    1 NRR/DRSS/PRPB                2      2      NRR/DSSA/SPLB          1    1 NRR/DSSA/SRXB                1      1      EG:F~         02     1    1 RES/DSIR/EIB                  1      1      RGN5     FILE   01     1    1 EXTERNAL    EG&G BRYCE i J ~ H          2      2      L ST LOBBY WARD       1    1 NRC PDR                      1      1      NSIC MURPHYtG.A       1     1 NSIC POORE,W.                1     1     NUDOCS FULL TXT      ,1     1 NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (Exl'. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR                 32   ENCL   32
 
WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ 3000 George Washington Way ~ Richland, Washington 99352 June 11, 1993 G02-93-151 Docket No. 50-397 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555


==Subject:==
==Subject:==
NUCLEAR PLANT WNP-2, OPERATING LICENSE NPF-21 LICENSEE EVENT REPORT NO.92-008-01 Transmitted herewith is Licensee Event Report No.92-008-01 for the WNP-2 Plant.This report is submitted in response to the report requirements of 10CFR50.73 and incorporates only minor administrative changes.Sincerely, J.V.Parrish (Mail Drop 1023)Assistant Managing Director, Operations JVP/REF/jd Enclosure CC: Mr.B.H.Faulkenberry, NRC-Region V Mr.R.Barr, NRC Resident Inspector (Mail Drop 901A, 2 Copies)INPO Records Center-Atlanta, GA Mr.D.L.Williams, BPA (Mail Drop 399)~, t-q.;o.-)9306230033 9306fi PDR ADQCK 05000397 S PDR ACILITY NAHE (I)LICENSEE T REPORT (LER)OOC ET UHB R ()PAGE (3)0 5 0 0 0 3 9 7 C.ITLE (4)Standby Gas Treatment System Fan Flow Limiter Setpoint Error HONTH DAY YEAR YEAR SEQUENT]AL NUMBER E VIS ION UHBER HONTH OAY YEAR FACILITY NAHES'E 8 R (S)0 3 0 0 0 8 0 6 PERA ING H IS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or narc of the fo low ng)(I 0.402(b)20.405(a)(1)(i) 0.405(a)(1)(ii) 0.405(a)(l)(iii) 0.405(a)(1)(iv) 0.405(a)(1)(v)0.405(C)50.36(c)(1) 50.36(c)(2) 50.73(a)(2)(i) 0.73(a)(2)(ii) 50.73(a)(2)(iii) 0.73(a)(2)(iv) 0.73(a)(2)(v) 0.73(a)(2)(vii) 0.73(a)(2)(viii)(A).
NUCLEAR PLANT WNP-2, OPERATING LICENSE NPF-21 LICENSEE EVENT REPORT NO. 92-008-01 Transmitted herewith is Licensee Event Report No. 92-008-01 for the WNP-2 Plant. This report is submitted in response to the report requirements of 10CFR50.73 and incorporates only minor administrative changes.
0.73(a)(2)(viii)(B) 0.73(a)(2)(x) 77.71(b)3.73(c)THER (Specify in Abstract elow and in Text,'RC orm 366A)LICENSEE CONTACT FOR THIS LER 12 R.E;Fuller, Compliance Engineer REA CODE lELEPNOHE NUMBER 0 9 7 7-4 1 4 8 COMPLETE ONE LIHE FOR EACH COMPONENT FAILURE DESCRIBED IH THIS REPORT (13)CAUSE S'YSTEH COMPOHEHT HANUFACTURER EPORTABLE CAUSE SYSTEM COMPOHEHT HAHUFACTURER EPORTABLE 0 NPRDS SUPPLEMENTAL REPORT EXPECTED (14)YES (If yes, conyiete EXPECTED SUBHISSIOH DAlE)X NO XPECTED SUBMISSIOH MOHTN DAY'YEAR ATE (15)ABSTRACI'16)
Sincerely, J. V. Parrish   (Mail Drop 1023)
On March 1, 1992, a Plant Technical Engineer determined the setpoint for the Standby Gas Treatment (SGT)System fan flow limiters could trip the fan motor thermal overloads (TOL)and prevent the SGT System from performing its safety function under highly unlikely design conditions.
Assistant Managing Director, Operations JVP/REF/jd Enclosure CC:     Mr. B. H. Faulkenberry, NRC - Region V Mr. R. Barr, NRC Resident Inspector (Mail Drop 901A, 2 Copies)
Operability determination of the SGT System at the setpoint used the wrong instrument reference calibration condition and did not consider instrument loop uncertainties.
INPO Records Center - Atlanta, GA Mr. D. L. Williams, BPA (Mail Drop 399)
The setpoint error was discovered by the Engineer during a review of the SGT System.The SGT System was declared inoperable and the Technical Specification Action Statement (TSAS)3.6.5.3(b) for the SGT System was entered.The NRC was verbally notified at 1545 hours PST on March 1, 1992, per 10 CFR 50.72(b)(2)(iii)(C).
          ~, t-q.; o.-)
9306230033 9306fi PDR     ADQCK 05000397 S                       PDR
 
LICENSEE                 T REPORT (LER)
ACILITY NAHE    (I)                                                                          OOC ET   UHB R   ( )                   PAGE   (3) 0   5   0   0     0   3   9   7 C. ITLE   (4)
Standby Gas Treatment System Fan Flow Limiter Setpoint Error HONTH     DAY     YEAR     YEAR     SEQUENT]AL     E VIS ION   HONTH   OAY   YEAR FACILITY NAHES'                                   E       8 R   (S)
NUMBER          UHBER 0   3   0                           0   0   8                 0   6 PERA ING                 H IS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR     5: (Check one or narc     of the fo   low ng) (   I 0.402(b)                       0.405(C)                 0.73(a)(2)(iv)                 77.71(b) 20.405(a)(1)(i)               50.36(c)(1)               0.73(a)(2)(v)                    3.73(c) 0.405(a)(1)(ii)               50.36(c)(2)               0.73(a)(2)(vii)                 THER (Specify in Abstract 0.405(a)(l)(iii)             50.73(a)(2)(i)             0.73(a)(2)(viii)(A).            elow and in Text,'RC 0.405(a)(1)(iv)               0.73(a)(2)(ii)           0.73(a)(2)(viii)(B)              orm 366A) 0.405(a) (1) (v)             50.73(a)(2)(iii)           0.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER     12 lELEPNOHE NUMBER R. E;       Fuller,         Compliance Engineer                                             REA CODE 0     9     7   7         4   1   4     8 COMPLETE ONE LIHE FOR EACH COMPONENT FAILURE DESCRIBED IH THIS REPORT       (13)
CAUSE     S'YSTEH       COMPOHEHT     HANUFACTURER   EPORTABLE           CAUSE   SYSTEM     COMPOHEHT         HAHUFACTURER     EPORTABLE 0   NPRDS SUPPLEMENTAL REPORT EXPECTED   (14)                                 XPECTED SUBMISSIOH      MOHTN    DAY    'YEAR ATE (15)
YES (If yes,   conyiete   EXPECTED SUBHISSIOH DAlE)   X   NO ABSTRACI'16)
On March 1, 1992, a Plant Technical Engineer determined the setpoint for the Standby Gas Treatment (SGT) System fan flow limiters could trip the fan motor thermal overloads (TOL) and prevent the SGT System from performing its safety function under highly unlikely design conditions. Operability determination of the SGT System at the setpoint used the wrong instrument reference calibration condition and did not consider instrument loop uncertainties. The setpoint error was discovered by the Engineer during a review of the SGT System.
The SGT System was declared inoperable and the Technical Specification Action Statement (TSAS) 3.6.5.3(b) for the SGT System was entered. The NRC was verbally notified at 1545 hours PST on March 1, 1992, per 10 CFR 50.72(b)(2)(iii)(C).
The root cause of this condition was Analysis Deficiencies.
The root cause of this condition was Analysis Deficiencies.
Review of systems for possible similar actual versus standard flow problems has been completed and outstanding issues resolved.Investigation into instrument setpoint accuracy is ongoing..The safety significance of this condition is considered negligible.
Review of systems for possible similar actual versus standard flow problems has been completed and outstanding issues resolved. Investigation into instrument setpoint accuracy is ongoing..
The likelihood of a sustained low voltage condition occurring during an accident that would require the SGT System to perform its safety function coincident with worst-case operating conditions is considered very low.
The safety significance of this condition is considered negligible. The likelihood of a sustained low voltage condition occurring during an accident that would require the SGT System to perform its safety function coincident with worst-case operating conditions is considered very low.
LICENSEE EVENT REPO (LER)TEXT CONTINUATION ACILITY NAME (I)Mashington Nuclear Plant--Unit 2 OOCKET NUMBER (2)0 5 0 0 0 3 9 7 LER NUMBER (8)Year umber ev.No.2 008 01 AGE (3)2 F 7 ITLE (4)Standby Gas Treatment System Fan Flow Limiter Set oint Error Plant n i i n Power Level-0%Plant Mode-4 (Cold Shutdown)ven De ri in On March 1, 1992, a Plant Technical Engineer determined the setpoint for the Standby Gas Treatment (SGT)System fan flow limiters could trip the fan motor thermal overloads (TOL)and prevent the SGT System from performing its safety function under highly unlikely design conditions.
 
Operability determination of the SGT System at the.setpoint used the wrong instrument reference calibration condition and did not consider instrument loop uncertainties.
LICENSEE EVENT REPO                   (LER)
The setpoint error was discovered by the Engineer during a review of the SGT System.The SGT fan flow limiter setpoint was 5600 ICFM (Indicated Cubic Feet per Minute)on the flow recorders, SGT-FR-2A1, 2A2, 2B1, 2B2.The analysis showed that the mass flow rate at the setpoint under extreme air stream conditions combined with instrument loop uncertainties could be higher than intended.Further, the analysis determined that the high mass flow rate under the combination of extremely unlikely design conditions (low voltage)could cause the SGT System fan motor TOLs to trip.Immediate orrective Action The SGT System was declared inoperable and the Techriical Specification Action Statement (TSAS)3.6.5.3b for the SGT System was entered.This condition precludes fuel handling activities, core alterations', or operations with a potential for draining the reactor vessel.The NRC was verbally notified at 1545 hours PST on March 1, 1992, per 10 CFR 50.72(b)(2)(iii)(C) as a condition alone that could have prevented the fulfillment of the safety function of stru'ctures or systems needed to control the release of the radioactive material.Further Ev 1 ti n n rrective A ti n A.AA~h This event is considered reportable per 10 CFR 50.73(a)(2)(v)(C) as a condition alone that could have prevented the fulfillment of the safety function of structures and systems that are needed to control the release of radioactive material.The SGT System may not have performed its safety function under the combination of extremely unlikely design conditions.
TEXT CONTINUATION ACILITY NAME   (I)                                   OOCKET NUMBER   (2)               LER NUMBER (8)         AGE (3)
2.There were no structures, components, or systems inoperable prior to the discovery of the condition which contributed to the condition.
Year     umber       ev. No.
LICENSEE EVENT REPO (LER)TEXT CONTINUATION ACILITY HCAE (1)Mashington Huclear Plant-Unit 2 DOCKET HUHBER (2)0 5 0 0 0 3 9 7 Year 2 008 LER HUHBER (8)umber ev.Ho.AGE (3)3 F 7 ITLE (4)Standb Gas Treatment System Fan Fl'ow Limiter Set oint Error 3.To obtain a relative change in mass flow rate of compressible fluids for different conditions, the indicated volumetric flow rate of the air stream condition is corrected to a reference condition, i.e., temperature, pressure, and relative humidity.If the air stream conditions are at precisely the same conditions the instrumentation was calibrated to, the relative changes in indicated volumetric flow rate are proportional to the relative changes in mass flow rate.The SGT System flow rate instrumentation was calibrated at air stream conditions of 212'F, 16.73 psia, and 0%RH.Prior calculations incorrectly assumed the reference air stream calibration condition was 90'F, 14.89 psia, and 0%RH.The indicated flow rate on the recorders at air stream temperatures below approximately 120'F is lower than the corresponding standard flow rate.At air temperatures above approximately 120'F the indicated flow rate is higher than the standard flow rate.As the air stream temperature decreases for a constant indicated flow rate, the corresponding standard flow rate increases.
Mashington Nuclear Plant    --Unit 2 0  5  0    0  0 3 9 7 2     008         01       2   F 7 ITLE (4)
An increase in standard flow rate corresponds to an increase in mass flow rate.As the mass flow rate through a fan increases, the current draw on the motor increases.
Standby Gas Treatment System Fan Flow               Limiter Set oint Error Plant     n ii n Power Level - 0%
In addition to the error in assumed calibration condition, instrument loop inaccuracies also had not been considered.
Plant Mode - 4 (Cold Shutdown) ven De       ri   in On March 1, 1992, a Plant Technical Engineer determined the setpoint for the Standby Gas Treatment (SGT) System fan flow limiters could trip the fan motor thermal overloads (TOL) and prevent the SGT System from performing its safety function under highly unlikely design conditions. Operability determination of the SGT System at the.setpoint used the wrong instrument reference calibration condition and did not consider instrument loop uncertainties. The setpoint error was discovered by the Engineer during a review of the SGT System.
This error also contributed to underestimation of mass flow.I The rated TOL trip point for the SGT fan motors (36.5 amps)is based on a temperature of 104'F.As the temperature of the TOL decreases, the trip point increases.
The SGT fan flow limiter setpoint was 5600 ICFM (Indicated Cubic Feet per Minute) on the flow recorders, SGT-FR-2A1, 2A2, 2B1, 2B2. The analysis showed that the mass flow rate at the setpoint under extreme air stream conditions combined with instrument loop uncertainties could be higher than intended. Further, the analysis determined that the high mass flow rate under the combination of extremely unlikely design conditions (low voltage) could cause the SGT System fan motor TOLs to trip.
Operability of the SGT System with respect to fan motor TOLs is dependent upon the worst combination of demand flow rate through a fan, air stream conditions, instrument loop uncertainties, motor terminal voltage, and TOL temperature.
Immediate         orrective Action The SGT System was declared inoperable and the Techriical Specification Action Statement (TSAS) 3.6.5.3b for the SGT System was entered. This condition precludes fuel handling activities, core alterations', or operations with a potential for draining the reactor vessel. The NRC was verbally notified at 1545 hours PST on March 1, 1992, per 10 CFR 50.72(b)(2)(iii)(C) as a condition alone that could have prevented the fulfillment of the safety function of stru'ctures or systems needed to control the release of the radioactive material.
For the 5600 ICFM flow limiter setpoint, the worst case demand flow rate was determined to be 6340 SCFM.The corresponding current draw on the fan motor was determined to be 38 amps at 400 VAC, i.e., low voltage conditions.(Low voltage conditions are defined to be the motor terminal voltage when the network voltage is just above the undervoltage transfer relay setpoint and the associated emergency bus is supporting all of its LOCA loads.)Therefore, the setpoint of 5600 ICFM could result in tripping of all of the SGT System fan motors and failure of the SGT System under highly unlikely extended low voltage conditions."
Further Ev     1   ti n n       rrective A ti n A.       AA~h This event is considered reportable per 10 CFR 50.73(a)(2)(v)(C) as a condition alone that could have prevented the fulfillment of the safety function of structures and systems that are needed to control the release of radioactive material. The SGT System may not have performed its safety function under the combination of extremely unlikely design conditions.
: 2.         There were no structures, components, or systems inoperable prior to the discovery of the condition which contributed to the condition.
 
LICENSEE EVENT REPO               (LER)
TEXT CONTINUATION ACILITY HCAE (1)                                 DOCKET HUHBER  (2)              LER HUHBER (8)        AGE (3)
Year    umber      ev. Ho.
Mashington Huclear Plant - Unit 2 0   5   0   0   0 3   9 7 2     008                   3   F 7 ITLE (4)
Standb     Gas   Treatment System Fan Fl'ow Limiter Set oint Error
: 3.     To obtain a relative change in mass flow rate of compressible fluids for different conditions, the indicated volumetric flow rate of the air stream condition is corrected to a reference condition, i.e., temperature, pressure, and relative humidity. If the air stream conditions are at precisely the same conditions the instrumentation was calibrated to, the relative changes in indicated volumetric flow rate are proportional to the relative changes in mass flow rate.
The SGT System flow rate instrumentation was calibrated at air stream conditions of 212'F, 16.73 psia, and 0% RH. Prior calculations incorrectly assumed the reference air stream calibration condition was 90'F, 14.89 psia, and 0% RH.
The indicated flow rate on the recorders at air stream temperatures below approximately 120'F is lower than the corresponding standard flow rate. At air temperatures above approximately 120'F the indicated flow rate is higher than the standard flow rate. As the air stream temperature decreases for a constant indicated flow rate, the corresponding standard flow rate increases. An increase in standard flow rate corresponds to an increase in mass flow rate. As the mass flow rate through a fan increases, the current draw on the motor increases.
In addition to the error in assumed calibration condition, instrument loop inaccuracies also had not been considered. This error also contributed to underestimation of mass flow.
I The rated TOL trip point for the SGT fan motors (36.5 amps) is based on a temperature of 104'F. As the temperature of the TOL decreases, the trip point increases.
Operability of the SGT System with respect to fan motor TOLs is dependent upon the worst combination of demand flow rate through a fan, air stream conditions, instrument loop uncertainties, motor terminal voltage, and TOL temperature. For the 5600 ICFM flow limiter setpoint, the worst case demand flow rate was determined to be 6340 SCFM. The corresponding current draw on the fan motor was determined to be 38 amps at 400 VAC, i.e., low voltage conditions. (Low voltage conditions are defined to be the motor terminal voltage when the network voltage is just above the undervoltage transfer relay setpoint and the associated emergency bus is supporting all of its LOCA loads.) Therefore, the setpoint of 5600 ICFM could result in tripping of all of the SGT System fan motors and failure of the SGT System under highly unlikely extended low voltage conditions."
 
LICENSEE EVENT REPOP(LER)
LICENSEE EVENT REPOP(LER)
TEXT CONTINUATION FACILITY NANE (I)Washington.
TEXT CONTINUATION FACILITY NANE   (I)                                 OOCKET NUMBER   (2)               LER NUNBER (8)       AGE (3)
Nuclear Plant-Unit 2 OOCKET NUMBER (2)0 5 0 0 0 3 9 7 LER NUNBER (8)Year umber'v.No.2 008 I AGE (3)4 F 7 ITLE (4)Standby Gas Treatment Syste'm Fan Flow Limiter Set oint Error 4, A Justification for Continued Operation (JCO), Revision I, regarding Secondary Containment operability was in effect at the time the setpoint error was discovered.
Washington. Nuclear Plant - Unit 2 Year    umber'v.      No.
Upon review of WNP-2 calculations of Secondary Containment drawdown time following a postulated LOOP/LOCA, the analyses were found to be nonconservative.
0  5  0    0  0 3 9  7 2    008          I      4   F 7 ITLE (4)
The original analyses did not consider an adequate time delay for Secondary Containment drawdown to-0.25-inch w.g.Also, adverse environmental conditions that increase Secondary Containment leakage were not considered in the analyses.To achieve an acceptable drawdown time under the worst case conditions, the SGT System maximum allowed flow rate needed to be increased.
Standby Gas Treatment Syste'm Fan Flow             Limiter Set oint Error 4,     A Justification for Continued Operation (JCO), Revision I, regarding Secondary Containment operability was in effect at the time the setpoint error was discovered. Upon review of WNP-2 calculations of Secondary Containment drawdown time following a postulated LOOP/LOCA, the analyses were found to be nonconservative. The original analyses did not consider an adequate time delay for Secondary Containment drawdown to -0.25-inch w.g.
The JCO was based on the SGT System fan flow limiter setpoint of 5600 ICFM.In most cases, the actual standard flow through the SGT trains will be higher than the indicated flow.If the indicated value is not corrected to standard conditions with reference to the actual instrument calibration condition, erroneously low and inconsistent mass flow rate values will be used.In addition, the SGT fan flow limiter accuracy error (430 ICFM5600 ICFM)needs to be included in any evaluation that relies on the setpoint value.The indicated recorder readings were corrected with reference to the wrong instrument calibration condition.'his resulted in predicting low mass flow rate values.In addition, the instrument loop uncertainties were not evaluated to determine the highest probable mass flow rate based on SGT System measurements.
Also, adverse environmental conditions that increase Secondary Containment leakage were not considered in the analyses. To achieve an acceptable drawdown time under the worst case conditions, the SGT System maximum allowed flow rate needed to be increased. The JCO was based on the SGT System fan flow limiter setpoint of 5600 ICFM.
The nonconservative low mass flow rate data were then used in surveillance tests to determine the acceptability of Reactor Building leakage.This could have potentially resulted in underpredicting the time to reach a negative 0.25-inch w.g.Reactor building pressure.A\f S*S<<idf'f f S SGTSy d~fiyd Sll and possible erroneous Reactor Building leakage data, the JCO, Revision 1, was declared invalid.New evaluations were initiated to determine the appropriate SGT System flow limiter setpoint value and verify acceptable Secondary Containment leakage.5.The root cause of this condition was Analysis Deficiencies.
In most cases, the actual standard flow through the SGT trains will be higher than the indicated flow. If the indicated value is not corrected to standard conditions with reference to the actual instrument calibration condition, erroneously low and inconsistent mass flow rate values will be used. In addition, the SGT fan flow limiter accuracy error (430 ICFM 5600 ICFM) needs to be included in any evaluation that relies on the setpoint value.
The Instrument Setpoint Change Request gSCR)analysis that supported the change of the SGT System setpoint from 4457.ICFM to 5600 ICFM corrected the indicated flow values with reference to the wrong instrument calibration condition and did not include instrument loop uncertainties.
The indicated recorder readings were corrected with reference to the wrong instrument calibration condition.'his resulted in predicting low mass flow rate values. In addition, the instrument loop uncertainties were not evaluated to determine the highest probable mass flow rate based on SGT System measurements. The nonconservative low mass flow rate data were then used in surveillance tests to determine the acceptability of Reactor Building leakage. This could have potentially resulted in underpredicting the time to reach a negative 0.25-inch w.g. Reactor building pressure.
These errors led to incorrect conclusions regarding actual mass flow.Hence, the impact of mass flow rate on fan motor loads was not properly evaluated.
A         \   f S*S <<idf'f           f S   SGTSy       d   ~fiyd                 Sll and possible erroneous Reactor Building leakage data, the JCO, Revision 1, was declared invalid. New evaluations were initiated to determine the appropriate SGT System flow limiter setpoint value and verify acceptable Secondary Containment leakage.
LICENSEE EVENT REPO (LER)TEXT CONTINUATION AGILITY NAME (I)Washington Nuclear Plant-Unit 2 OOCKET NUMBER (2)0 5 0 0 0 3 9 7 Tear LER NUHBER (8)umber ev.No.2 08 01 AGE (3)5 F 7 ITLE (4)Standby Gas Treatment System Fan Flow Limiter Set oint Error 6.The Revisions 0 and 1 of the JCO had determined that 10CFR100 and GDC19 dose limits could be satisfied provided the Reactor Building drawdown to-0.25-inch w.g.occurred within 10 minutes.Based on corrections of indicated flow values to standard conditions with reference to the correct instrument calibration condition, consideration of instrument loop uncertainties, low voltage, charcoal bed residence time and adverse environmental conditions, the new fan flow limiter setpoint was determined to be 5380 ICFM.The minimum flow rate based on combination of the uncertainties in the negative direction satisfies the 10 minute drawdown requirement.
: 5.     The root cause of this condition was Analysis Deficiencies. The Instrument Setpoint Change Request gSCR) analysis that supported the change of the SGT System setpoint from 4457 .
The worst case demand flow rate for the fan motor TOLs at the new setpoint was calculated to be 6340 SCFM based on combination of the uncertainties in the positive direction, and air stream conditions of 60'F, 14.89 psia, and 0%RH.The TOL trip margin was assumed not to increase with decreasing building air temperature.
ICFM to 5600 ICFM corrected the indicated flow values with reference to the wrong instrument calibration condition and did not include instrument loop uncertainties. These errors led to incorrect conclusions regarding actual mass flow. Hence, the impact of mass flow rate on fan motor loads was not properly evaluated.
The peak current draw on the fan motor was determined to be 39 amps at 400 VAC.7.The TOLs for the fan motors were replaced with TOLs having a trip point of 45 amps.The fan 40A motor fuses were also replaced with 45A rated fuses.Therefore, the SGT System was determined capable of performing its safety function under all design conditions at the new flow limiter setpoint of 5380 ICFM.8.9.The SGT System fan flow limiter setpoint was changed to 5380 ICFM.To achieve Secondary Containment drawdown within 10 minutes at the new fan flow limiter setpoint under all design basis conditions, the Standby Service Water (SSW)pond temperature must be maintained at or below 72'F.All appropriate Plant procedures were changed to ensure the temperature of the SSW ponds would be maintained in compliance with the JCO while the Plant is in Modes 1, 2, 3, or 4.10.Review of other systems for possible errors related to indicated flow (CFM)versus standard flow (SCFM)has been completed.
 
Outstanding issues are resolved.Secondary Containment leakage was determined to be acceptable using SGT System indicated flow data corrected to the correct instrument reference calibration condition.
LICENSEE EVENT REPO               (LER)
12.Revision 2 of the JCO was approved with new offsite dose calculations at the new fan flow limiter setpoint.The revised JCO was discussed with the NRC.However, NRC approval was not required based on a 10 CFR 50.59 review that determined an Unreviewed Safety Question did not exist, LICENSEE EVENT REPOR LER)TEXT CONTINUATION ACILITY NAHE (1)Washington Nuclear Plant-Unit 2'OCKET NUHBER (2)0 5 0 0'0 3 9 7 Year LER NUMBER (8)umber , ev.No.2 008 1 AGE (3)6 F 7 ITLE (4)Standby Gas Treatment System Fan Flow Limiter Set oint Error B.hr rr iv Aci n Evaluation of setpoints for equipment in harsh environments has been completed per the WNP-2 Setpoint Methodology Program.Although beyond the scope of our original Setpoint Methodology Program, the Supply System is planning to extend its review to selected nonharsh environment setpoints.
TEXT CONTINUATION AGILITY NAME (I)                               OOCKET NUMBER   (2)               LER NUHBER (8)        AGE (3)
Progress of this effort will be dependent on resource availability and overall corporate priorities.
Tear     umber       ev. No.
Based on current planning, this is estimated to be a 4-1/2 year effort.~ff The safety significance of this condition is considered negligible.
Washington Nuclear Plant - Unit 2 0  5  0    0  0 3 9 7 2        08        01        5   F 7 ITLE (4)
The likelihood of a low voltage condition occurring on the network during an accident that would require the SGT System to perform its safety function coincident with abnormally high switchgear room temperatures is considered very low.In addition, the voltage would have to remain just above the setpoint of the degraded voltage relay for an extended period time.Under nominal operating conditions the existing SGT System fan TOLs would not have been expected to trip.Any postulated accident requiring SGT would probably occur when the Reactor Building motor control center room temperature would be near its average value of 75'F.The corresponding current draw on the fan motor would be 38 amps at the fan flow limiter setpoint of 5600 ICFM and 400 VAC.The TOL trip limit is 36.5 amps at 104'F.At 75'F building air temperature, the trip limit increases approximately 15%or to 42 amps.The fan motor fuses were rated at 40 amps.Therefore, it is highly unlikely the SGT System would have failed to perform its safety function with the previous limiter setpoint at 5600 ICFM.There is similar margin under design basis conditions.
Standby Gas Treatment System Fan Flow             Limiter Set oint Error
imilar Events LER 92-02 describes a condition where the indicated flow measurements for the Main Steam Leakage Control (MSLC)System were being used to satisfy the Technical Specification surveillance requirements.
: 6. The Revisions 0 and 1 of the JCO had determined that 10CFR100 and GDC19 dose limits could be satisfied provided the Reactor Building drawdown to -0.25-inch w.g. occurred within 10 minutes. Based on corrections of indicated flow values to standard conditions with reference to the correct instrument calibration condition, consideration of instrument loop uncertainties, low voltage, charcoal bed residence time and adverse environmental conditions, the new fan flow limiter setpoint was determined to be 5380 ICFM. The minimum flow rate based on combination of the uncertainties in the negative direction satisfies the 10 minute drawdown requirement.
The Technical Specifications required flow test values at standard conditions.
The worst case demand flow rate for the fan motor TOLs at the new setpoint was calculated to be 6340 SCFM based on combination of the uncertainties in the positive direction, and air stream conditions of 60'F, 14.89 psia, and 0% RH. The TOL trip margin was assumed not to increase with decreasing building air temperature. The peak current draw on the fan motor was determined to be 39 amps at 400 VAC.
Therefore, the indicated values should have been corrected to standard conditions.
: 7. The TOLs for the fan motors were replaced with TOLs having a trip point of 45 amps. The fan 40A motor fuses were also replaced with 45A rated fuses. Therefore, the SGT System was determined capable of performing its safety function under all design conditions at the new flow limiter setpoint of 5380 ICFM.
LIC~ENSEE EVENT REPO (LER)TEXT CONTINUATION"AGILITY NAME (I)Washington Nuclear Plant-Unit 2 DOCKET NUMBER (2)0 5 0 0 0 3 9 7 Year LER NUMBER (8)umber ev.Ho.0 8 AGE (3)7 F 7 ITLE (4)Standby Gas Treatment System Fan Flow Limiter Set oint Error EII Inform i n Tx Rfern Main Steam System Flow Indicator Standby.Gas Treatment System Fan Standby Gas Treatment System Fan Thermal Overloads Standby Gas Treatment System Flow Limiters Standby Gas Treatment System Flow Indicator$ggem SB BH BH BH BH Ref ren g~m~nn FI FAN FU FCO FI
: 8. The SGT System fan flow limiter setpoint was changed to 5380 ICFM.
: 9. To achieve Secondary Containment drawdown within 10 minutes at the new fan flow limiter setpoint under all design basis conditions, the Standby Service Water (SSW) pond temperature must be maintained at or below 72'F. All appropriate Plant procedures were changed to ensure the temperature of the SSW ponds would be maintained in compliance with the JCO while the Plant is in Modes 1, 2, 3, or 4.
: 10. Review of other systems for possible errors related to indicated flow (CFM) versus standard flow (SCFM) has been completed. Outstanding issues are resolved.
Secondary Containment leakage was determined to be acceptable using SGT System indicated flow data corrected to the correct instrument reference calibration condition.
: 12. Revision 2 of the JCO was approved with new offsite dose calculations at the new fan flow limiter setpoint. The revised JCO was discussed with the NRC. However, NRC approval was not required based on a 10 CFR 50.59 review that determined an Unreviewed Safety Question did not exist,
 
LICENSEE EVENT REPOR             LER)
TEXT CONTINUATION ACILITY NAHE (1)                               'OCKET NUHBER (2)                 LER NUMBER (8)       AGE (3)
                          - Unit                                            Year      umber   , ev. No.
Washington Nuclear Plant        2 0  5  0    0'0  3 9  7 2      008         1       6   F 7 ITLE (4)
Standby Gas Treatment System Fan Flow           Limiter Set oint Error B.           hr     rr   iv Aci n Evaluation of setpoints for equipment in harsh environments has been completed per the WNP-2 Setpoint Methodology Program. Although beyond the scope of our original Setpoint Methodology Program, the Supply System is planning to extend its review to selected nonharsh environment setpoints. Progress of this effort will be dependent on resource availability and overall corporate
  ~ff      priorities. Based on current planning, this is estimated to be a 4-1/2 year effort.
The safety significance of this condition is considered negligible. The likelihood of a low voltage condition occurring on the network during an accident that would require the SGT System to perform its safety function coincident with abnormally high switchgear room temperatures is considered very low. In addition, the voltage would have to remain just above the setpoint of the degraded voltage relay for an extended period time.
Under nominal operating conditions the existing SGT System fan TOLs would not have been expected to trip. Any postulated accident requiring SGT would probably occur when the Reactor Building motor control center room temperature would be near its average value of 75'F. The corresponding current draw on the fan motor would be 38 amps at the fan flow limiter setpoint of 5600 ICFM and 400 VAC. The TOL trip limit is 36.5 amps at 104'F. At 75'F building air temperature, the trip limit increases approximately 15% or to 42 amps. The fan motor fuses were rated at 40 amps. Therefore, it is highly unlikely the SGT System would have failed to perform its safety function with the previous limiter setpoint at 5600 ICFM. There is similar margin under design basis conditions.
imilar Events LER 92-02 describes a condition where the indicated flow measurements for the Main Steam Leakage Control (MSLC) System were being used to satisfy the Technical Specification surveillance requirements.
The Technical Specifications required flow test values at standard conditions. Therefore, the indicated values should have been corrected to standard conditions.
 
LIC~ENSEE EVENT REPO           (LER)
TEXT CONTINUATION "AGILITY NAME (I)                           DOCKET NUMBER (2)             LER NUMBER (8)         AGE (3)
Year    umber       ev. Ho.
Washington Nuclear Plant - Unit 2 0  5  0  0  0 3 9 7 0 8                 7   F 7 ITLE (4)
Standby Gas Treatment System Fan Flow     Limiter Set oint Error EII Inform     i n Tx Rfern                                                             Ref ren
                                                                  $ ggem        g~m~nn Main Steam System Flow Indicator                             SB              FI Standby. Gas Treatment System Fan                           BH              FAN Standby Gas Treatment System Fan Thermal Overloads           BH                FU Standby Gas Treatment System Flow Limiters                   BH              FCO Standby Gas Treatment System Flow Indicator                   BH               FI
 
(,}}
(,}}

Latest revision as of 07:26, 4 February 2020

LER 92-008-01:on 920301,SGTS Fan Flow Limiter Setpoint Error Discovered.Caused by Analysis Deficiencies.Sgts Fan Flow Limiter Setpoint Changed & Rev 2 of Jco Approved W/New Offsite Dose calculations.W/930611 Ltr
ML17290A459
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 06/11/1993
From: Fuller R, Parrish J
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
GO2-93-151, LER-92-008-01, LER-92-8-1, NUDOCS 9306230033
Download: ML17290A459 (10)


Text

ACCELE ~ED DOCUMENT DIS UTION SYSTEM REGUL RY INFORMATION DISTRIBUT SYSTEM (RIDS)

ACCESSION NBR:9306230033 DOC.DATE: 93/06/11 NOTARIZED: NO DOCKET ¹ FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH. NAME AUTHOR AFFILIATION FULLER,R.E. Washington Public Power Supply System PARRISH,J.V. Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 92-008-01:on 920301,SGTS fan flow limiter setpoint error discovered. Caused by analysis deficiencies.SGTS fan flow limiter setpoint changed & Rev 2 of JCO approved w/new offsite dose calculations.W/930611 ltr.

DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PDV LA 1 1 PDV PD 1 1 CLIFFORD,J 1 1 INTERNAL: ACNW 2 2 ACRS 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRIL/RPEB 1 1 NRR/DRPW/OEAB 1 1 NRR/DRSS/PRPB 2 2 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 EG:F~ 02 1 1 RES/DSIR/EIB 1 1 RGN5 FILE 01 1 1 EXTERNAL EG&G BRYCE i J ~ H 2 2 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHYtG.A 1 1 NSIC POORE,W. 1 1 NUDOCS FULL TXT ,1 1 NOTE TO ALL"RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (Exl'. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 32 ENCL 32

WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ 3000 George Washington Way ~ Richland, Washington 99352 June 11, 1993 G02-93-151 Docket No. 50-397 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555

Subject:

NUCLEAR PLANT WNP-2, OPERATING LICENSE NPF-21 LICENSEE EVENT REPORT NO. 92-008-01 Transmitted herewith is Licensee Event Report No. 92-008-01 for the WNP-2 Plant. This report is submitted in response to the report requirements of 10CFR50.73 and incorporates only minor administrative changes.

Sincerely, J. V. Parrish (Mail Drop 1023)

Assistant Managing Director, Operations JVP/REF/jd Enclosure CC: Mr. B. H. Faulkenberry, NRC - Region V Mr. R. Barr, NRC Resident Inspector (Mail Drop 901A, 2 Copies)

INPO Records Center - Atlanta, GA Mr. D. L. Williams, BPA (Mail Drop 399)

~, t-q.; o.-)

9306230033 9306fi PDR ADQCK 05000397 S PDR

LICENSEE T REPORT (LER)

ACILITY NAHE (I) OOC ET UHB R ( ) PAGE (3) 0 5 0 0 0 3 9 7 C. ITLE (4)

Standby Gas Treatment System Fan Flow Limiter Setpoint Error HONTH DAY YEAR YEAR SEQUENT]AL E VIS ION HONTH OAY YEAR FACILITY NAHES' E 8 R (S)

NUMBER UHBER 0 3 0 0 0 8 0 6 PERA ING H IS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or narc of the fo low ng) ( I 0.402(b) 0.405(C) 0.73(a)(2)(iv) 77.71(b) 20.405(a)(1)(i) 50.36(c)(1) 0.73(a)(2)(v) 3.73(c) 0.405(a)(1)(ii) 50.36(c)(2) 0.73(a)(2)(vii) THER (Specify in Abstract 0.405(a)(l)(iii) 50.73(a)(2)(i) 0.73(a)(2)(viii)(A). elow and in Text,'RC 0.405(a)(1)(iv) 0.73(a)(2)(ii) 0.73(a)(2)(viii)(B) orm 366A) 0.405(a) (1) (v) 50.73(a)(2)(iii) 0.73(a)(2)(x)

LICENSEE CONTACT FOR THIS LER 12 lELEPNOHE NUMBER R. E; Fuller, Compliance Engineer REA CODE 0 9 7 7 4 1 4 8 COMPLETE ONE LIHE FOR EACH COMPONENT FAILURE DESCRIBED IH THIS REPORT (13)

CAUSE S'YSTEH COMPOHEHT HANUFACTURER EPORTABLE CAUSE SYSTEM COMPOHEHT HAHUFACTURER EPORTABLE 0 NPRDS SUPPLEMENTAL REPORT EXPECTED (14) XPECTED SUBMISSIOH MOHTN DAY 'YEAR ATE (15)

YES (If yes, conyiete EXPECTED SUBHISSIOH DAlE) X NO ABSTRACI'16)

On March 1, 1992, a Plant Technical Engineer determined the setpoint for the Standby Gas Treatment (SGT) System fan flow limiters could trip the fan motor thermal overloads (TOL) and prevent the SGT System from performing its safety function under highly unlikely design conditions. Operability determination of the SGT System at the setpoint used the wrong instrument reference calibration condition and did not consider instrument loop uncertainties. The setpoint error was discovered by the Engineer during a review of the SGT System.

The SGT System was declared inoperable and the Technical Specification Action Statement (TSAS) 3.6.5.3(b) for the SGT System was entered. The NRC was verbally notified at 1545 hours0.0179 days <br />0.429 hours <br />0.00255 weeks <br />5.878725e-4 months <br /> PST on March 1, 1992, per 10 CFR 50.72(b)(2)(iii)(C).

The root cause of this condition was Analysis Deficiencies.

Review of systems for possible similar actual versus standard flow problems has been completed and outstanding issues resolved. Investigation into instrument setpoint accuracy is ongoing..

The safety significance of this condition is considered negligible. The likelihood of a sustained low voltage condition occurring during an accident that would require the SGT System to perform its safety function coincident with worst-case operating conditions is considered very low.

LICENSEE EVENT REPO (LER)

TEXT CONTINUATION ACILITY NAME (I) OOCKET NUMBER (2) LER NUMBER (8) AGE (3)

Year umber ev. No.

Mashington Nuclear Plant --Unit 2 0 5 0 0 0 3 9 7 2 008 01 2 F 7 ITLE (4)

Standby Gas Treatment System Fan Flow Limiter Set oint Error Plant n ii n Power Level - 0%

Plant Mode - 4 (Cold Shutdown) ven De ri in On March 1, 1992, a Plant Technical Engineer determined the setpoint for the Standby Gas Treatment (SGT) System fan flow limiters could trip the fan motor thermal overloads (TOL) and prevent the SGT System from performing its safety function under highly unlikely design conditions. Operability determination of the SGT System at the.setpoint used the wrong instrument reference calibration condition and did not consider instrument loop uncertainties. The setpoint error was discovered by the Engineer during a review of the SGT System.

The SGT fan flow limiter setpoint was 5600 ICFM (Indicated Cubic Feet per Minute) on the flow recorders, SGT-FR-2A1, 2A2, 2B1, 2B2. The analysis showed that the mass flow rate at the setpoint under extreme air stream conditions combined with instrument loop uncertainties could be higher than intended. Further, the analysis determined that the high mass flow rate under the combination of extremely unlikely design conditions (low voltage) could cause the SGT System fan motor TOLs to trip.

Immediate orrective Action The SGT System was declared inoperable and the Techriical Specification Action Statement (TSAS) 3.6.5.3b for the SGT System was entered. This condition precludes fuel handling activities, core alterations', or operations with a potential for draining the reactor vessel. The NRC was verbally notified at 1545 hours0.0179 days <br />0.429 hours <br />0.00255 weeks <br />5.878725e-4 months <br /> PST on March 1, 1992, per 10 CFR 50.72(b)(2)(iii)(C) as a condition alone that could have prevented the fulfillment of the safety function of stru'ctures or systems needed to control the release of the radioactive material.

Further Ev 1 ti n n rrective A ti n A. AA~h This event is considered reportable per 10 CFR 50.73(a)(2)(v)(C) as a condition alone that could have prevented the fulfillment of the safety function of structures and systems that are needed to control the release of radioactive material. The SGT System may not have performed its safety function under the combination of extremely unlikely design conditions.

2. There were no structures, components, or systems inoperable prior to the discovery of the condition which contributed to the condition.

LICENSEE EVENT REPO (LER)

TEXT CONTINUATION ACILITY HCAE (1) DOCKET HUHBER (2) LER HUHBER (8) AGE (3)

Year umber ev. Ho.

Mashington Huclear Plant - Unit 2 0 5 0 0 0 3 9 7 2 008 3 F 7 ITLE (4)

Standb Gas Treatment System Fan Fl'ow Limiter Set oint Error

3. To obtain a relative change in mass flow rate of compressible fluids for different conditions, the indicated volumetric flow rate of the air stream condition is corrected to a reference condition, i.e., temperature, pressure, and relative humidity. If the air stream conditions are at precisely the same conditions the instrumentation was calibrated to, the relative changes in indicated volumetric flow rate are proportional to the relative changes in mass flow rate.

The SGT System flow rate instrumentation was calibrated at air stream conditions of 212'F, 16.73 psia, and 0% RH. Prior calculations incorrectly assumed the reference air stream calibration condition was 90'F, 14.89 psia, and 0% RH.

The indicated flow rate on the recorders at air stream temperatures below approximately 120'F is lower than the corresponding standard flow rate. At air temperatures above approximately 120'F the indicated flow rate is higher than the standard flow rate. As the air stream temperature decreases for a constant indicated flow rate, the corresponding standard flow rate increases. An increase in standard flow rate corresponds to an increase in mass flow rate. As the mass flow rate through a fan increases, the current draw on the motor increases.

In addition to the error in assumed calibration condition, instrument loop inaccuracies also had not been considered. This error also contributed to underestimation of mass flow.

I The rated TOL trip point for the SGT fan motors (36.5 amps) is based on a temperature of 104'F. As the temperature of the TOL decreases, the trip point increases.

Operability of the SGT System with respect to fan motor TOLs is dependent upon the worst combination of demand flow rate through a fan, air stream conditions, instrument loop uncertainties, motor terminal voltage, and TOL temperature. For the 5600 ICFM flow limiter setpoint, the worst case demand flow rate was determined to be 6340 SCFM. The corresponding current draw on the fan motor was determined to be 38 amps at 400 VAC, i.e., low voltage conditions. (Low voltage conditions are defined to be the motor terminal voltage when the network voltage is just above the undervoltage transfer relay setpoint and the associated emergency bus is supporting all of its LOCA loads.) Therefore, the setpoint of 5600 ICFM could result in tripping of all of the SGT System fan motors and failure of the SGT System under highly unlikely extended low voltage conditions."

LICENSEE EVENT REPOP(LER)

TEXT CONTINUATION FACILITY NANE (I) OOCKET NUMBER (2) LER NUNBER (8) AGE (3)

Washington. Nuclear Plant - Unit 2 Year umber'v. No.

0 5 0 0 0 3 9 7 2 008 I 4 F 7 ITLE (4)

Standby Gas Treatment Syste'm Fan Flow Limiter Set oint Error 4, A Justification for Continued Operation (JCO), Revision I, regarding Secondary Containment operability was in effect at the time the setpoint error was discovered. Upon review of WNP-2 calculations of Secondary Containment drawdown time following a postulated LOOP/LOCA, the analyses were found to be nonconservative. The original analyses did not consider an adequate time delay for Secondary Containment drawdown to -0.25-inch w.g.

Also, adverse environmental conditions that increase Secondary Containment leakage were not considered in the analyses. To achieve an acceptable drawdown time under the worst case conditions, the SGT System maximum allowed flow rate needed to be increased. The JCO was based on the SGT System fan flow limiter setpoint of 5600 ICFM.

In most cases, the actual standard flow through the SGT trains will be higher than the indicated flow. If the indicated value is not corrected to standard conditions with reference to the actual instrument calibration condition, erroneously low and inconsistent mass flow rate values will be used. In addition, the SGT fan flow limiter accuracy error (430 ICFM 5600 ICFM) needs to be included in any evaluation that relies on the setpoint value.

The indicated recorder readings were corrected with reference to the wrong instrument calibration condition.'his resulted in predicting low mass flow rate values. In addition, the instrument loop uncertainties were not evaluated to determine the highest probable mass flow rate based on SGT System measurements. The nonconservative low mass flow rate data were then used in surveillance tests to determine the acceptability of Reactor Building leakage. This could have potentially resulted in underpredicting the time to reach a negative 0.25-inch w.g. Reactor building pressure.

A \ f S*S <<idf'f f S SGTSy d ~fiyd Sll and possible erroneous Reactor Building leakage data, the JCO, Revision 1, was declared invalid. New evaluations were initiated to determine the appropriate SGT System flow limiter setpoint value and verify acceptable Secondary Containment leakage.

5. The root cause of this condition was Analysis Deficiencies. The Instrument Setpoint Change Request gSCR) analysis that supported the change of the SGT System setpoint from 4457 .

ICFM to 5600 ICFM corrected the indicated flow values with reference to the wrong instrument calibration condition and did not include instrument loop uncertainties. These errors led to incorrect conclusions regarding actual mass flow. Hence, the impact of mass flow rate on fan motor loads was not properly evaluated.

LICENSEE EVENT REPO (LER)

TEXT CONTINUATION AGILITY NAME (I) OOCKET NUMBER (2) LER NUHBER (8) AGE (3)

Tear umber ev. No.

Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 2 08 01 5 F 7 ITLE (4)

Standby Gas Treatment System Fan Flow Limiter Set oint Error

6. The Revisions 0 and 1 of the JCO had determined that 10CFR100 and GDC19 dose limits could be satisfied provided the Reactor Building drawdown to -0.25-inch w.g. occurred within 10 minutes. Based on corrections of indicated flow values to standard conditions with reference to the correct instrument calibration condition, consideration of instrument loop uncertainties, low voltage, charcoal bed residence time and adverse environmental conditions, the new fan flow limiter setpoint was determined to be 5380 ICFM. The minimum flow rate based on combination of the uncertainties in the negative direction satisfies the 10 minute drawdown requirement.

The worst case demand flow rate for the fan motor TOLs at the new setpoint was calculated to be 6340 SCFM based on combination of the uncertainties in the positive direction, and air stream conditions of 60'F, 14.89 psia, and 0% RH. The TOL trip margin was assumed not to increase with decreasing building air temperature. The peak current draw on the fan motor was determined to be 39 amps at 400 VAC.

7. The TOLs for the fan motors were replaced with TOLs having a trip point of 45 amps. The fan 40A motor fuses were also replaced with 45A rated fuses. Therefore, the SGT System was determined capable of performing its safety function under all design conditions at the new flow limiter setpoint of 5380 ICFM.
8. The SGT System fan flow limiter setpoint was changed to 5380 ICFM.
9. To achieve Secondary Containment drawdown within 10 minutes at the new fan flow limiter setpoint under all design basis conditions, the Standby Service Water (SSW) pond temperature must be maintained at or below 72'F. All appropriate Plant procedures were changed to ensure the temperature of the SSW ponds would be maintained in compliance with the JCO while the Plant is in Modes 1, 2, 3, or 4.
10. Review of other systems for possible errors related to indicated flow (CFM) versus standard flow (SCFM) has been completed. Outstanding issues are resolved.

Secondary Containment leakage was determined to be acceptable using SGT System indicated flow data corrected to the correct instrument reference calibration condition.

12. Revision 2 of the JCO was approved with new offsite dose calculations at the new fan flow limiter setpoint. The revised JCO was discussed with the NRC. However, NRC approval was not required based on a 10 CFR 50.59 review that determined an Unreviewed Safety Question did not exist,

LICENSEE EVENT REPOR LER)

TEXT CONTINUATION ACILITY NAHE (1) 'OCKET NUHBER (2) LER NUMBER (8) AGE (3)

- Unit Year umber , ev. No.

Washington Nuclear Plant 2 0 5 0 0'0 3 9 7 2 008 1 6 F 7 ITLE (4)

Standby Gas Treatment System Fan Flow Limiter Set oint Error B. hr rr iv Aci n Evaluation of setpoints for equipment in harsh environments has been completed per the WNP-2 Setpoint Methodology Program. Although beyond the scope of our original Setpoint Methodology Program, the Supply System is planning to extend its review to selected nonharsh environment setpoints. Progress of this effort will be dependent on resource availability and overall corporate

~ff priorities. Based on current planning, this is estimated to be a 4-1/2 year effort.

The safety significance of this condition is considered negligible. The likelihood of a low voltage condition occurring on the network during an accident that would require the SGT System to perform its safety function coincident with abnormally high switchgear room temperatures is considered very low. In addition, the voltage would have to remain just above the setpoint of the degraded voltage relay for an extended period time.

Under nominal operating conditions the existing SGT System fan TOLs would not have been expected to trip. Any postulated accident requiring SGT would probably occur when the Reactor Building motor control center room temperature would be near its average value of 75'F. The corresponding current draw on the fan motor would be 38 amps at the fan flow limiter setpoint of 5600 ICFM and 400 VAC. The TOL trip limit is 36.5 amps at 104'F. At 75'F building air temperature, the trip limit increases approximately 15% or to 42 amps. The fan motor fuses were rated at 40 amps. Therefore, it is highly unlikely the SGT System would have failed to perform its safety function with the previous limiter setpoint at 5600 ICFM. There is similar margin under design basis conditions.

imilar Events LER 92-02 describes a condition where the indicated flow measurements for the Main Steam Leakage Control (MSLC) System were being used to satisfy the Technical Specification surveillance requirements.

The Technical Specifications required flow test values at standard conditions. Therefore, the indicated values should have been corrected to standard conditions.

LIC~ENSEE EVENT REPO (LER)

TEXT CONTINUATION "AGILITY NAME (I) DOCKET NUMBER (2) LER NUMBER (8) AGE (3)

Year umber ev. Ho.

Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 0 8 7 F 7 ITLE (4)

Standby Gas Treatment System Fan Flow Limiter Set oint Error EII Inform i n Tx Rfern Ref ren

$ ggem g~m~nn Main Steam System Flow Indicator SB FI Standby. Gas Treatment System Fan BH FAN Standby Gas Treatment System Fan Thermal Overloads BH FU Standby Gas Treatment System Flow Limiters BH FCO Standby Gas Treatment System Flow Indicator BH FI

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