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| issue date = 06/30/1998
| issue date = 06/30/1998
| title = Monthly Operating Rept for June 1998 for Salem,Unit 1. W/980715 Ltr
| title = Monthly Operating Rept for June 1998 for Salem,Unit 1. W/980715 Ltr
| author name = BAKKEN A C, KNIERIEM R B
| author name = Bakken A, Knieriem R
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:e Pu,blic Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236  
{{#Wiki_filter:~1 e
' Nuclear Business Unit U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Attn: Document Control Desk MONTHLY OPERA TING REPORT SALEM UNIT NO. 1 DOCKET NO. 50-272 Gentlemen:
OPS~G Pu,blic Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit LR-N98-0333 July 15, 1998 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Attn: Document Control Desk MONTHLY OPERA TING REPORT SALEM UNIT NO. 1 DOCKET NO. 50-272 Gentlemen:
LR-N98-0333 July 15, 1998 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original Monthly Operating report for June 1998 is attached.  
In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original Monthly Operating report for June 1998 is attached.                               I Sincerely, A. C. Bakken Ill General Manager -
/rbk Enclosures C Mr. H.J. Miller ...... 'J (\  
Salem Operations
/,{* Sincerely, A. C. Bakken Ill General Manager -Salem Operations Regional Administrator USNRC, Region 1 475 Allendale Road King of Prussia, PA 19046 ------900721 oi99-
    /rbk Enclosures
-, PDR ADOCK 05000272 R PDR The power is in your hands. I \\1 \ 95-2168 REV. 6/94 Reporting Period: June 1998 DOCKET NO.: 50-272 UNIT: Salem 1 DATE: 7/15/98 COMPLETED BY: R. Knieriem TELEPHONE:  
                                          ...... 'J (\
(609) 339-1782 OPERATING DATA REPORT Design Electrical Rating (MWe-Net) 1115 Maximum Dependable Capacity (MWe-Net) 1106 Month Year-to-date Cumulative No. of hours reactor was critical 720 2023 106404 No. of hours generator was on line (service 720 1782 102171 hours) Unit reserve shutdown hours 0 0 0 Net Electrical Energy (MWH) 776400 1736476 101873019 UNIT SHUTDOWNS NO. DATE TYPE F=FORCED S=SCHEDULED (1) Reason A -Equipment Failure (Explain) B -Maintenance or Test C -Refueling D -Regulatory Restriction DURATION (HOURS) E -Operator Training/License Examination F -Administrative G -Operational Error (Explain)
                                        \.,~ /,{* ~~j                                                \\1 \
H -Other Summary: REASON METHOD OF (1) SHUTTING DOWN THE REACTOR (2) (2) Method 1 -Manual 2 -Manual Trip/Scram 3 -Automatic Trip/Scram 4 -Continuation 5 -Other (Explain)
C        Mr. H.J. Miller Regional Administrator USNRC, Region 1 475 Allendale Road King of Prussia, PA 19046
CORRECTIVE ACTION/COMMENT Salem Unit 1 began the month of June operating at full power. On June 3, power was reduced to 50% to perform corrective maintenance on the 12 Steam Generator Feed pump. The unit returned to full power on the following day and operated at full power for the remainder of the month. --1 
- -----900721oi99- c,00630--.-~--- -,
PDR       ADOCK 05000272 R                         PDR The power is in your hands.
95-2168 REV. 6/94
 
                                                                                                      --1 DOCKET NO.:     50-272 UNIT: Salem 1 DATE:   7/15/98 COMPLETED BY:         R. Knieriem TELEPHONE:       (609) 339-1782 Reporting Period: June 1998 OPERATING DATA REPORT Design Electrical Rating (MWe-Net)                       1115 Maximum Dependable Capacity (MWe-Net)                     1106 Month         Year-to-date       Cumulative No. of hours reactor was critical                         720             2023             106404 No. of hours generator was on line (service               720             1782             102171 hours)
Unit reserve shutdown hours                                 0               0                 0 Net Electrical Energy (MWH)                             776400           1736476           101873019 UNIT SHUTDOWNS NO. DATE       TYPE               DURATION  REASON        METHOD OF        CORRECTIVE F=FORCED           (HOURS)    (1)          SHUTTING        ACTION/COMMENT S=SCHEDULED                                 DOWN THE REACTOR (2)
(1) Reason                                     (2) Method A - Equipment Failure (Explain)                 1 - Manual B - Maintenance or Test                         2 - Manual Trip/Scram C - Refueling                                   3 - Automatic Trip/Scram D - Regulatory Restriction                       4 - Continuation E - Operator Training/License Examination       5 - Other (Explain)
F -Administrative G - Operational Error (Explain)
H -Other Summary:
Salem Unit 1 began the month of June operating at full power. On June 3, power was reduced to 50% to perform corrective maintenance on the 12 Steam Generator Feed pump. The unit returned to full power on the following day and operated at full power for the remainder of the month.
 
*'
*'
* i \ .. . , DOCKET NO.: 50-272 UNIT: Salem 1 DATE: 7715798 COMPLETED BY: R. B. Knieriem TELEPHONE:  
* i
(609) 339-1782  
      \ ..
DOCKET NO.:     50-272 UNIT: Salem 1 DATE:   7715798 COMPLETED BY:         R. B. Knieriem TELEPHONE:       (609) 339-1782


==SUMMARY==
==SUMMARY==
OF CHANGES, TESTS, AND EXPERIMENTS FOR THE SALEM UNIT 1 GENERATING STATION MONTH: June 1998 The following items completed during June 1998 have been evaluated to determine:  
OF CHANGES, TESTS, AND EXPERIMENTS FOR THE SALEM UNIT 1 GENERATING STATION MONTH: June 1998 The following items completed during June 1998 have been evaluated to determine:
-----------1 1. If the probability of occurrence or the consequences of an accident or malfunction of equipment important to safety previously evaluated in the safety analysis report may be increased; or 2. If a possibility for an accident or malfunction of a different type than any evaluated previously in the safety analysis report may be created; or 3. If the margin of safety as defined in the basis for any technical specification is reduced.
: 1. If the probability of occurrence or the consequences of an accident or malfunction of equipment important to safety previously evaluated in the safety analysis report may be increased; or
* The 1 OCFR50.59 Safety Evaluations showed that these items did not create a new safety hazard to the plant; nor did they affect the safe shutdown of the reactor. These items did not change the plant effluent releases and did not alter the existing environmental impact. The 1 OCFR50.59 Safety Evaluations determined that no unreviewed safety or environmental questions are involved.
: 2. If a possibility for an accident or malfunction of a different type than any evaluated previously in the safety analysis report may be created; or
Design Changes -Summary of Safety Evaluations 1 EC-3692, Pkg. 1, Heater Drain Pump Start And Heater Drain Valve (HD-15) Open Interlock Modification This design change provided an anti-reset windup feature and interlocked the starting of the Bleed Steam Heater Drain pumps and their associated Bleed* Steam Heater Drain Pump Discharge air operated globe valves. The change will prevent the Feedwater Heater and Moisture Separator Reheater Drain tank from draining before the HD-15 valve responds to automatic level control. This design change does not negatively impact any accident response nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
: 3. If the margin of safety as defined in the basis for any technical specification is reduced.
Temporary Modifications  
* The 10CFR50.59 Safety Evaluations showed that these items did not create a new safety hazard to the plant; nor did they affect the safe shutdown of the reactor. These items did not change the plant effluent releases and did not alter the existing environmental impact. The 10CFR50.59 Safety Evaluations determined that no unreviewed safety or environmental questions are involved.
-Summary of Safety Evaluations There were no changes in this category implemented during June 1998.
Design Changes - Summary of Safety Evaluations 1EC-3692, Pkg. 1, Heater Drain Pump Start And Heater Drain Valve (HD-15)
-* 'I '* .. ' Procedures  
Open Interlock Modification This design change provided an anti-reset windup feature and interlocked the starting of the Bleed Steam Heater Drain pumps and their associated Bleed*
-Summary of Safety Evaluations  
Steam Heater Drain Pump Discharge air operated globe valves. The change will prevent the Feedwater Heater and Moisture Separator Reheater Drain tank from draining before the HD-15 valve responds to automatic level control.
$alem 'Emergency Plan, Section 15, Revision 5 This change revised Section 15 of the Emergency Plan to clarify how the PSE&G Nuclear Business Unit will conduct accountability drills and defines "limited" accountability.
This design change does not negatively impact any accident response nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.
This change does not negatively impact any accident response nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety.
Temporary Modifications - Summary of Safety Evaluations There were no changes in this category implemented during June 1998.
Therefore, this change does not involve an Unreviewed Safety Question.
 
UFSAR Change Notices -Summary of Safety Evaluations Salem UFSAR Change Notice S98-020, Section 13.5, Administrative Procedures This UFSAR Change Notice modified section 13.5 of the Salem UFSAR to make it consistent with the Hope Creek UFSAR with regard to the administrative procedure sections and descriptions.
-*   'I '*
Procedures - Summary of Safety Evaluations
                $alem 'Emergency Plan, Section 15, Revision 5 This change revised Section 15 of the Emergency Plan to clarify how the PSE&G Nuclear Business Unit will conduct accountability drills and defines "limited" accountability.
This change does not negatively impact any accident response nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this change does not involve an Unreviewed Safety Question.
UFSAR Change Notices - Summary of Safety Evaluations Salem UFSAR Change Notice S98-020, Section 13.5, Administrative Procedures This UFSAR Change Notice modified section 13.5 of the Salem UFSAR to make it consistent with the Hope Creek UFSAR with regard to the administrative procedure sections and descriptions.
This change does not negatively impact any accident response nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this change does not involve an Unreviewed Safety Question.
This change does not negatively impact any accident response nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this change does not involve an Unreviewed Safety Question.
Deficiency Reports -Summary of Safety Evaluations There were no changes in this category implemented during June 1998. Other -Summary of Safety Evaluations There were no changes in this category implemented during June 1998.}}
Deficiency Reports - Summary of Safety Evaluations There were no changes in this category implemented during June 1998.
Other - Summary of Safety Evaluations There were no changes in this category implemented during June 1998.}}

Latest revision as of 03:53, 3 February 2020

Monthly Operating Rept for June 1998 for Salem,Unit 1. W/980715 Ltr
ML18106A714
Person / Time
Site: Salem PSEG icon.png
Issue date: 06/30/1998
From: Bakken A, Knieriem R
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LR-N98-0333, LR-N98-333, NUDOCS 9807210199
Download: ML18106A714 (4)


Text

~1 e

OPS~G Pu,blic Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit LR-N98-0333 July 15, 1998 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Attn: Document Control Desk MONTHLY OPERA TING REPORT SALEM UNIT NO. 1 DOCKET NO. 50-272 Gentlemen:

In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original Monthly Operating report for June 1998 is attached. I Sincerely, A. C. Bakken Ill General Manager -

Salem Operations

/rbk Enclosures

...... 'J (\

\.,~ /,{* ~~j \\1 \

C Mr. H.J. Miller Regional Administrator USNRC, Region 1 475 Allendale Road King of Prussia, PA 19046

- -----900721oi99- c,00630--.-~--- -,

PDR ADOCK 05000272 R PDR The power is in your hands.

95-2168 REV. 6/94

--1 DOCKET NO.: 50-272 UNIT: Salem 1 DATE: 7/15/98 COMPLETED BY: R. Knieriem TELEPHONE: (609) 339-1782 Reporting Period: June 1998 OPERATING DATA REPORT Design Electrical Rating (MWe-Net) 1115 Maximum Dependable Capacity (MWe-Net) 1106 Month Year-to-date Cumulative No. of hours reactor was critical 720 2023 106404 No. of hours generator was on line (service 720 1782 102171 hours)

Unit reserve shutdown hours 0 0 0 Net Electrical Energy (MWH) 776400 1736476 101873019 UNIT SHUTDOWNS NO. DATE TYPE DURATION REASON METHOD OF CORRECTIVE F=FORCED (HOURS) (1) SHUTTING ACTION/COMMENT S=SCHEDULED DOWN THE REACTOR (2)

(1) Reason (2) Method A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual Trip/Scram C - Refueling 3 - Automatic Trip/Scram D - Regulatory Restriction 4 - Continuation E - Operator Training/License Examination 5 - Other (Explain)

F -Administrative G - Operational Error (Explain)

H -Other Summary:

Salem Unit 1 began the month of June operating at full power. On June 3, power was reduced to 50% to perform corrective maintenance on the 12 Steam Generator Feed pump. The unit returned to full power on the following day and operated at full power for the remainder of the month.

  • '
  • i

\ ..

DOCKET NO.: 50-272 UNIT: Salem 1 DATE: 7715798 COMPLETED BY: R. B. Knieriem TELEPHONE: (609) 339-1782

SUMMARY

OF CHANGES, TESTS, AND EXPERIMENTS FOR THE SALEM UNIT 1 GENERATING STATION MONTH: June 1998 The following items completed during June 1998 have been evaluated to determine:

1. If the probability of occurrence or the consequences of an accident or malfunction of equipment important to safety previously evaluated in the safety analysis report may be increased; or
2. If a possibility for an accident or malfunction of a different type than any evaluated previously in the safety analysis report may be created; or
3. If the margin of safety as defined in the basis for any technical specification is reduced.
  • The 10CFR50.59 Safety Evaluations showed that these items did not create a new safety hazard to the plant; nor did they affect the safe shutdown of the reactor. These items did not change the plant effluent releases and did not alter the existing environmental impact. The 10CFR50.59 Safety Evaluations determined that no unreviewed safety or environmental questions are involved.

Design Changes - Summary of Safety Evaluations 1EC-3692, Pkg. 1, Heater Drain Pump Start And Heater Drain Valve (HD-15)

Open Interlock Modification This design change provided an anti-reset windup feature and interlocked the starting of the Bleed Steam Heater Drain pumps and their associated Bleed*

Steam Heater Drain Pump Discharge air operated globe valves. The change will prevent the Feedwater Heater and Moisture Separator Reheater Drain tank from draining before the HD-15 valve responds to automatic level control.

This design change does not negatively impact any accident response nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this design change does not involve an Unreviewed Safety Question.

Temporary Modifications - Summary of Safety Evaluations There were no changes in this category implemented during June 1998.

-* 'I '*

Procedures - Summary of Safety Evaluations

$alem 'Emergency Plan, Section 15, Revision 5 This change revised Section 15 of the Emergency Plan to clarify how the PSE&G Nuclear Business Unit will conduct accountability drills and defines "limited" accountability.

This change does not negatively impact any accident response nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this change does not involve an Unreviewed Safety Question.

UFSAR Change Notices - Summary of Safety Evaluations Salem UFSAR Change Notice S98-020, Section 13.5, Administrative Procedures This UFSAR Change Notice modified section 13.5 of the Salem UFSAR to make it consistent with the Hope Creek UFSAR with regard to the administrative procedure sections and descriptions.

This change does not negatively impact any accident response nor does it increase the probability or consequences of either an accident or a malfunction of equipment important to safety. Therefore, this change does not involve an Unreviewed Safety Question.

Deficiency Reports - Summary of Safety Evaluations There were no changes in this category implemented during June 1998.

Other - Summary of Safety Evaluations There were no changes in this category implemented during June 1998.