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{{#Wiki_filter:NRC FORM 195 V.S.NUCLEAR RFOVLATORV COMMISSION I2 70)o NR DISTRIBUTION FDR PART 50 DOCI(ET MATERIAL | {{#Wiki_filter:NRC FORM 195 V.S. NUCLEAR RFOVLATORV COMMISSION DO TgtgVI 0 E FI I2 70) o FILE NVMOER NR DISTRIBUTION FDR PART 50 DOCI(ET MATERIAL INCIDENT REPORT To: J.G. Keppl er FRDM: Indiana 8 Michigan Power Co. DATE OF DOCUMENT Bridgman, Michigan 6-2-76 R.lJ. Jurgensen DATE RECEIVED 6-10-76 SLETTER NOTOR I Z E D PROP INPUT FORM NUMBER OF COPIES RECEIVED 0ORIGINAI EI V N C LASS I F I E D QCOPV 30 DESCRIPTldN ENCLOSURE Licensee Event Report (%.0. II 76-23) on 5-2-76 Ltr. trans the followihg........ Concerning Various Valves (Isloation) failed to meet acceptable leak rate Specifications...... | ||
- Licensee Event Report (R.O. k'6-24) on 6-76 Concer'ning"Lower. Inlet. Door'-R* opening 'Torque being in excess of Tech. Sepc....... | |||
-Licensee Event Report (R.O.k'6-24)on | (30 Carbon Sisgned Cys. REceived) | ||
Inlet.Door'-R*opening'Torque being in excess of Tech.Sepc....... | ACKNOWLEDGED DO NOT REMOVZ PLANT NA1IE. Cook b 1 NOTE: IF PERSONNEL EXPOSURE IS INVOLVED.. | ||
(30 Carbon Sisgned Cys.REceived)ACKNOWLEDGED DO NOT REMOVZ NOTE: IF PERSONNEL EXPOSURE IS INVOLVED.. | SEND DIRECTLY TO KREGER/J, COLLINS | ||
SEND DIRECTLY TO KREGER/J, COLLINS-- | - SAFETY FOR ACTION/INFORMATION ENVIRO SAB 6-10-76 BRANCH CHIEF: Kniel W 3 CYS FOR ACTION LIC ~ -ASST: Lee W/ CYS ACRS 'YS ENT TO LA INTERNAL DISTRIBUTION NRC PDR ICE 2 SCHROEDER/IPPOLITO NOVAK CHECK IES S . E TEDESCO HACCA EN BAER SHAO VOLLH~BH BUNCH KRE E 0 N EXTERNAL DISTRIBUTION CONTROL NUMBER LPDR: ~ | ||
TIC NSIC 5879" | |||
3 I~ | |||
3 ~ 3 I' 3 Ilt II | |||
' | |||
~ | ~egtffatoty QL cd | ||
@Afar o4 INDIANA 8 NICHIGAN I'DN'E IANy DONALD C. COOK NUCL PL@~>'km P.O. Box 458, Bridgmnn,>hi gran 4SLIC 3 | |||
ig gog7.92 June 2, 1976 ANION 876~ | |||
g~q teton p~g Clerk | |||
<95. %%%lNtK.'t Hr. J.G. Keppler, Regional Direc a ~jg Office of 'Inspection and Enforcement United States Nuclear Regulatory Commission I. | |||
Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Operating License DPR-58 Docket No. 50-315 | |||
'4 P SUPPLEt1EHT TO REPORTABLE OCCURREtfCE RO-50-315 76-23 SUPPLEHENT TO EVEtiT DESCRIPTION THE FOLLOMIt<G VALVES MERE FOUND=TO HAVE EXCESSIVE LEAKAGE: DCR-621 ECR-15 GCR-314 NCR-105 NCR-106 NSW-244-2 NSW-244-3 NSM-244-4 MCR-958 HSW-417-4 NSM-415-1 NSW-415-2 | ==Dear lhr'. Keppler:== | ||
[oO]WHILE It(NCDE 5, DURING ICE CONDENSER INLET DOOR OPENING TORQUE SURVEILLANCE TESTING, 7 0 9 UO | Pursuant to the requirements of Appendix A Technical Specifications and the United States Nuclear Regulatory Commission Regulatory Guide | ||
[oa~j DOOR 1-R Llt>IT WAS EXCEEDED | : 1. 16, Revision 4, Section 2.b, the following reports are submitted: | ||
~00 0 T ttA 7 09 11'l2 13 PERSONNEL INJURIES tiUMBEA OESCRIPTtON | R0-50-315/76-23 RO-50-315/76-24 Sincerely, r | ||
[i')~00 | R.M. ge en Plant tan er | ||
/bab cc: R.S. Hunter | |||
-J.E. Dolan G.E. Lien R. Kilburn R.J. Vollen BPI R.C. Callen 1/PSC K.R. Baker RO:III P.W. Steketee, Esq. | |||
R. Walsh, Esq. | |||
G , Charnoff, Esq G. Olson J.N. Hennigan PNSRC R.S..Keith | |||
'Dir., IE (30 copies) | |||
Dir., 1<IPC {3 copies) | |||
~ LICENSES SVSNT aePORTi CONTROL 0LOCK: (PLEASE PRINT ALL REOUIREO INFORIVIATION) 1 0 LtCENSf f LCT NSE EVENT NAhtf LtCLNSE t6uhtIILA IVPL. TYPE 0 0 0 0: 0 0 0 0 4 1 1 1 1 +0+] | |||
~'9 14 15 5 30 31 32 AFT'OAT AfPOAT CAT EOOAY kuhIOIA fVENT OA'If Aft'CAT OATF | |||
'0 TYPE SOUSE OOCKET | |||
[oagcow T L050 03 15/ 0 5 O 8 Z 6 ~0 7 0 57 59 74 75 EVENT DESCRIPTION Jog WHILE IN t'lODE 5 DURING SURVEILLANCE TESTIttG OF CONTAINMENT ISOLATION VALVES VARIOUS UD AC l P TYP . AK' P 7 0 9 UD toOj R N A P IFICATIOt<S PARAGRAPH 3.6.1.2.b. | |||
UO roO5j 7 0 9 roOsj (RO-50-31 5/76- 23) | |||
I'fv 7 0 9 PfdV F SvSTT M CAUSE COht FUN TNT COht PON'I k T COCE COOE COMPONEt4T COOE SUPPLEA ht Ahui*CI UPf A VOLATION | |||
[oar] ~SD 6 V' L V 6 X ~0 X 9 9 9 7 0 9 10 11 12 17 43 48 CAUSE OESCRlPTION EXCESSI EAKAGE DUE T DEPOSIT BUILDUP ON VALVE SEATS AND WEAR BY VALVE OPERA N 7 0 9 UO | |||
~o9 ALL VALVES WITH EXCESSIVE LEAK RATES WERE REPAIRED AND RETESTED; TOTAL LEAKAGE WAS 7 0 9 UO Q~o WI TH I N SPECIFICATION. | |||
7 09 f htETHOO OF STATt1S POWER OTHER STATUS OTSCOVF AY 01SCOVEAY OESCIVPIlON | |||
[ll1] 6 ~00 0 NA 44 B SURVEILLANCE TESTING 7 0 9 10 12 13 40 FOPhl OF ACT lVITY CO') T EN T AFLEASfo OF PELE*Sf At tOUtTT OF ACTIVITY LOCATlON Of AELEASE Jig ' | |||
~Z Z NA NA 7 0 10 11 44 45 PERSONNEL EXPOSURES 7 | |||
EG3 0 9 LILLI~ 11 LZJ 12 13 PERSONNEL INJURIES feuhtS=A OESCA1PTtON | |||
[i)4] ~00 0 tlA 7 09 11 12 PROBABLE COttSEQUEttCES Jig> NA 9 00 LOSS OR DAMAGE TO FACILITY T v PE OESCA:P T TON Z NZ 7 8 9 10 PUULICITY tIA 7 8 9 t'DDITIONAL I'ACTORS pg I ttA 7 | |||
7 gH 09 l~ UO JACK RISCHLIttG p~,ig.~616 465 59~01 368) | |||
G>0 ddI 46 1 | |||
'4 P SUPPLEt1EHT TO REPORTABLE OCCURREtfCE RO-50-315 76- 23 SUPPLEHENT TO EVEtiT DESCRIPTION THE FOLLOMIt<G VALVES MERE FOUND=TO HAVE EXCESSIVE LEAKAGE: | |||
DCR-621 MCR-905 ECR-15 HSW-415-3 GCR-314 NSW-415-4 NCR-105 WCR-922 NCR-106 WCR-921 NSW-244-2 HSW-417-3 NSW-244-3 VCR-106 NSM-244-4 VCR-206 MCR-958 SI-189 HSW-417-4 N-102 NSM-415-1 SH-1 NSW-415-2 | |||
t>> | |||
l,i | |||
CONTROL BLOCK: | |||
~ LICENSEE EVENT REIoORI (PLEASE PAINT ALL AEOUIREO INFORMATION) | |||
LiCKNSTE LtCI ttSE. IVTNT NL'VE LL IttSE tiUMBLR TYPE I v I'E toOjI t1 I D C C 1 0 0 0 0 0 0 4 t i l l ~03 | |||
~ | |||
) | |||
7 09 14 15 20 Jo 31 32 Afponr ntpont CLTT Gonv OOCKK t t'UMrB'LR f VINT Ontf ntPORT OATK | |||
[oagcour ~L 0 5 0 0 3 1 5 0 5 0 6 7 6 0 6 0 I 7 6 7 0 57 50 59 00 60 09 74 75 UO EVENT OESCRIPTION | |||
[oO] WHILE It( NCDE 5, DURING ICE CONDENSER INLET DOOR OPENING TORQUE SURVEILLANCE TESTING, 7 0 9 UO LOWER INLET DOOR 1-R OPENING TORQUE WAS FOUND IN EXCESS'OF TECHNICAL SPECIFICATION 7 0 9 UO Qpjn PARAGRAPH 4.6.5.3.1 b3 LllklT OF 195 ItlCkt POUNDS. LOWER INLET DOOR 3-L. INITIAL 7 0 9 UO Jag OPENlt,G TOR UE WAS FOUr(D TO BE IN EXCESS OF TECHNICAL SPECIFICATION PARAGRAPH 4.6.5.3.1 7 0 9 toOQ bl Llt1IT OF 675 It(CH POUt<DS. DOOR 1-R SPRING TEttSIOt< (SEE SUPPLEtkENT) (RO-50-315/76<i0 7 0 9 Pnnr E SYSTKti CAUSE CCrrtrt 4 O4'I COLrPONINT COOK CODE COVPONENT CODE 'Uf R MLtuUt LOT UrrtR | |||
[nn') ~so F X X X X X X W 1 2 0 7 0 0 10 11 12 17 43 44 CAUSE OESCRIPTION | |||
[oa~j DOOR 1-R Llt>IT WAS EXCEEDED DUE TO SPRING TENSION DRIFT. DOOR 3-L INITIAL OPENING 7 0 9 00 X EEDED L"ItlITS BECAUSE OF AN ICE BUILDUP FROtl CONDENSATION ON THE LOWER SILL. | |||
7 0 9 | |||
~1O 7 09 TLCtLITY MEIHOO OF STLTUS POtttf n otiiKA sTntUs OISCOVf A V otscovf AY of scn'.ptIQN | |||
~00 UO'u) | |||
Lsj o NA SURVEILLANCE TESTING 7 0 9 10 12 13 45 40 FOtttl OF ACTIVITY CO@TENT aMourtt of nctiv:tv LOfnttON OF RELKnSE NA 7 0 9 10 11 nn 45 PERSONNEL EXPOSURES tiUMBER TYPE OESCRlPTtON | |||
~00 0 T ttA 7 09 11 'l2 13 PERSONNEL INJURIES tiUMBEA OESCRIPTtON | |||
[i')0 9~00 7 | |||
0 11 12 ttA UU PROBABLE CONSEQUENCES t115j tiA 7 0'9 Uo LOSS OR DAMAGE TO FACILITY T'vpE oEscnpooti tIIsj Z tlA 7 09 10 PUULICITY | |||
[lli) t'iA 0 9 AOOITIONAL FACTORS rtA Qg I 7 8 9 9] NA 7 04J J. RISCHLlttG P>IOIIE{616)4G5 5901(368 Gt'4t e tt I ~ a 0 1 | |||
SUPPLEt'iEt<T TO REPORTABLE OCCURRENCE RO-50-315/76- 4 SUPPLEMENT TO EVENT DESCRIPTION WAS ADJUSTED TO PROVIDE A 189 INCH POUND OPENING TORQUE. DOOR 3-L BOTTOM SILL WAS CLEANED At40 INITIAL OPEttING TORQUE h'AS REMEASURED AT, 287 INCH | |||
'POUNDS.}} |
Latest revision as of 19:17, 2 February 2020
ML18219C352 | |
Person / Time | |
---|---|
Site: | Cook |
Issue date: | 06/02/1976 |
From: | Jurgensen R American Electric Power Service Corp, Indiana Michigan Power Co, (Formerly Indiana & Michigan Power Co) |
To: | James Keppler NRC/IE, NRC/RGN-III |
References | |
LER-1976-023-00, LER-1976-024-00 | |
Download: ML18219C352 (10) | |
Text
NRC FORM 195 V.S. NUCLEAR RFOVLATORV COMMISSION DO TgtgVI 0 E FI I2 70) o FILE NVMOER NR DISTRIBUTION FDR PART 50 DOCI(ET MATERIAL INCIDENT REPORT To: J.G. Keppl er FRDM: Indiana 8 Michigan Power Co. DATE OF DOCUMENT Bridgman, Michigan 6-2-76 R.lJ. Jurgensen DATE RECEIVED 6-10-76 SLETTER NOTOR I Z E D PROP INPUT FORM NUMBER OF COPIES RECEIVED 0ORIGINAI EI V N C LASS I F I E D QCOPV 30 DESCRIPTldN ENCLOSURE Licensee Event Report (%.0. II 76-23) on 5-2-76 Ltr. trans the followihg........ Concerning Various Valves (Isloation) failed to meet acceptable leak rate Specifications......
- Licensee Event Report (R.O. k'6-24) on 6-76 Concer'ning"Lower. Inlet. Door'-R* opening 'Torque being in excess of Tech. Sepc.......
(30 Carbon Sisgned Cys. REceived)
ACKNOWLEDGED DO NOT REMOVZ PLANT NA1IE. Cook b 1 NOTE: IF PERSONNEL EXPOSURE IS INVOLVED..
SEND DIRECTLY TO KREGER/J, COLLINS
- SAFETY FOR ACTION/INFORMATION ENVIRO SAB 6-10-76 BRANCH CHIEF: Kniel W 3 CYS FOR ACTION LIC ~ -ASST: Lee W/ CYS ACRS 'YS ENT TO LA INTERNAL DISTRIBUTION NRC PDR ICE 2 SCHROEDER/IPPOLITO NOVAK CHECK IES S . E TEDESCO HACCA EN BAER SHAO VOLLH~BH BUNCH KRE E 0 N EXTERNAL DISTRIBUTION CONTROL NUMBER LPDR: ~
3 I~
3 ~ 3 I' 3 Ilt II
~egtffatoty QL cd
@Afar o4 INDIANA 8 NICHIGAN I'DN'E IANy DONALD C. COOK NUCL PL@~>'km P.O. Box 458, Bridgmnn,>hi gran 4SLIC 3
ig gog7.92 June 2, 1976 ANION 876~
g~q teton p~g Clerk
<95. %%%lNtK.'t Hr. J.G. Keppler, Regional Direc a ~jg Office of 'Inspection and Enforcement United States Nuclear Regulatory Commission I.
Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Operating License DPR-58 Docket No. 50-315
Dear lhr'. Keppler:
Pursuant to the requirements of Appendix A Technical Specifications and the United States Nuclear Regulatory Commission Regulatory Guide
- 1. 16, Revision 4, Section 2.b, the following reports are submitted:
R0-50-315/76-23 RO-50-315/76-24 Sincerely, r
R.M. ge en Plant tan er
/bab cc: R.S. Hunter
-J.E. Dolan G.E. Lien R. Kilburn R.J. Vollen BPI R.C. Callen 1/PSC K.R. Baker RO:III P.W. Steketee, Esq.
R. Walsh, Esq.
G , Charnoff, Esq G. Olson J.N. Hennigan PNSRC R.S..Keith
'Dir., IE (30 copies)
Dir., 1<IPC {3 copies)
~ LICENSES SVSNT aePORTi CONTROL 0LOCK: (PLEASE PRINT ALL REOUIREO INFORIVIATION) 1 0 LtCENSf f LCT NSE EVENT NAhtf LtCLNSE t6uhtIILA IVPL. TYPE 0 0 0 0: 0 0 0 0 4 1 1 1 1 +0+]
~'9 14 15 5 30 31 32 AFT'OAT AfPOAT CAT EOOAY kuhIOIA fVENT OA'If Aft'CAT OATF
'0 TYPE SOUSE OOCKET
[oagcow T L050 03 15/ 0 5 O 8 Z 6 ~0 7 0 57 59 74 75 EVENT DESCRIPTION Jog WHILE IN t'lODE 5 DURING SURVEILLANCE TESTIttG OF CONTAINMENT ISOLATION VALVES VARIOUS UD AC l P TYP . AK' P 7 0 9 UD toOj R N A P IFICATIOt NA 9 00 LOSS OR DAMAGE TO FACILITY T v PE OESCA:P T TON Z NZ 7 8 9 10 PUULICITY tIA 7 8 9 t'DDITIONAL I'ACTORS pg I ttA 7
7 gH 09 l~ UO JACK RISCHLIttG p~,ig.~616 465 59~01 368)
G>0 ddI 46 1
'4 P SUPPLEt1EHT TO REPORTABLE OCCURREtfCE RO-50-315 76- 23 SUPPLEHENT TO EVEtiT DESCRIPTION THE FOLLOMIt<G VALVES MERE FOUND=TO HAVE EXCESSIVE LEAKAGE:
DCR-621 MCR-905 ECR-15 HSW-415-3 GCR-314 NSW-415-4 NCR-105 WCR-922 NCR-106 WCR-921 NSW-244-2 HSW-417-3 NSW-244-3 VCR-106 NSM-244-4 VCR-206 MCR-958 SI-189 HSW-417-4 N-102 NSM-415-1 SH-1 NSW-415-2
t>>
l,i
CONTROL BLOCK:
~ LICENSEE EVENT REIoORI (PLEASE PAINT ALL AEOUIREO INFORMATION)
LiCKNSTE LtCI ttSE. IVTNT NL'VE LL IttSE tiUMBLR TYPE I v I'E toOjI t1 I D C C 1 0 0 0 0 0 0 4 t i l l ~03
~
)
7 09 14 15 20 Jo 31 32 Afponr ntpont CLTT Gonv OOCKK t t'UMrB'LR f VINT Ontf ntPORT OATK
[oagcour ~L 0 5 0 0 3 1 5 0 5 0 6 7 6 0 6 0 I 7 6 7 0 57 50 59 00 60 09 74 75 UO EVENT OESCRIPTION
[oO] WHILE It( NCDE 5, DURING ICE CONDENSER INLET DOOR OPENING TORQUE SURVEILLANCE TESTING, 7 0 9 UO LOWER INLET DOOR 1-R OPENING TORQUE WAS FOUND IN EXCESS'OF TECHNICAL SPECIFICATION 7 0 9 UO Qpjn PARAGRAPH 4.6.5.3.1 b3 LllklT OF 195 ItlCkt POUNDS. LOWER INLET DOOR 3-L. INITIAL 7 0 9 UO Jag OPENlt,G TOR UE WAS FOUr(D TO BE IN EXCESS OF TECHNICAL SPECIFICATION PARAGRAPH 4.6.5.3.1 7 0 9 toOQ bl Llt1IT OF 675 It(CH POUt<DS. DOOR 1-R SPRING TEttSIOt< (SEE SUPPLEtkENT) (RO-50-315/76<i0 7 0 9 Pnnr E SYSTKti CAUSE CCrrtrt 4 O4'I COLrPONINT COOK CODE COVPONENT CODE 'Uf R MLtuUt LOT UrrtR
[nn') ~so F X X X X X X W 1 2 0 7 0 0 10 11 12 17 43 44 CAUSE OESCRIPTION
[oa~j DOOR 1-R Llt>IT WAS EXCEEDED DUE TO SPRING TENSION DRIFT. DOOR 3-L INITIAL OPENING 7 0 9 00 X EEDED L"ItlITS BECAUSE OF AN ICE BUILDUP FROtl CONDENSATION ON THE LOWER SILL.
7 0 9
~1O 7 09 TLCtLITY MEIHOO OF STLTUS POtttf n otiiKA sTntUs OISCOVf A V otscovf AY of scn'.ptIQN
~00 UO'u)
Lsj o NA SURVEILLANCE TESTING 7 0 9 10 12 13 45 40 FOtttl OF ACTIVITY CO@TENT aMourtt of nctiv:tv LOfnttON OF RELKnSE NA 7 0 9 10 11 nn 45 PERSONNEL EXPOSURES tiUMBER TYPE OESCRlPTtON
~00 0 T ttA 7 09 11 'l2 13 PERSONNEL INJURIES tiUMBEA OESCRIPTtON
[i')0 9~00 7
0 11 12 ttA UU PROBABLE CONSEQUENCES t115j tiA 7 0'9 Uo LOSS OR DAMAGE TO FACILITY T'vpE oEscnpooti tIIsj Z tlA 7 09 10 PUULICITY
[lli) t'iA 0 9 AOOITIONAL FACTORS rtA Qg I 7 8 9 9] NA 7 04J J. RISCHLlttG P>IOIIE{616)4G5 5901(368 Gt'4t e tt I ~ a 0 1
SUPPLEt'iEt<T TO REPORTABLE OCCURRENCE RO-50-315/76- 4 SUPPLEMENT TO EVENT DESCRIPTION WAS ADJUSTED TO PROVIDE A 189 INCH POUND OPENING TORQUE. DOOR 3-L BOTTOM SILL WAS CLEANED At40 INITIAL OPEttING TORQUE h'AS REMEASURED AT, 287 INCH
'POUNDS.