Information Notice 2000-09, Steam Generator Tube Failure at Indian Point Unit 2: Difference between revisions

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| issue date = 06/28/2000
| issue date = 06/28/2000
| title = Steam Generator Tube Failure at Indian Point Unit 2
| title = Steam Generator Tube Failure at Indian Point Unit 2
| author name = Marsh L B
| author name = Marsh L
| author affiliation = NRC/NRR/DRIP/REXB
| author affiliation = NRC/NRR/DRIP/REXB
| addressee name =  
| addressee name =  
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{{#Wiki_filter:cc: Holody Urban June 28, 2000 NRC INFORMATION NOTICE 2000-09: STEAM GENERATOR TUBE FAILURE AT INDIAN POINT UNIT 2  
{{#Wiki_filter:cc: Holody
 
Urban
 
UNITED STATES                                          Nick
 
NUCLEAR REGULATORY COMMISSION
 
OFFICE OF NUCLEAR REACTOR REGULATION
 
WASHINGTON, D.C. 20555-0001 June 28, 2000
NRC INFORMATION NOTICE 2000-09: STEAM GENERATOR TUBE FAILURE AT INDIAN
 
POINT UNIT 2


==Addressees==
==Addressees==
All holders of operating licenses for nuclear power reactors except those who have ceased operations and have certified that fuel has been permanently removed from the reactor vesse
All holders of operating licenses for nuclear power reactors except those who have ceased
 
operations and have certified that fuel has been permanently removed from the reactor vessel.


==Purpose==
==Purpose==
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice to inform addressees of a steam generator tube failure at Indian Point Unit 2. NRC investigations of the licensee's steam generator inspection program are ongoing and any potentially generic issues identified will be communicated in a separate generic communication. However, the investigations to date re-emphasize the importance of licensee involvement with ongoing industry efforts to understand and detect steam generator degradation. It is expected that recipients will review the information for applicability to their facilities and consider actions, as appropriate, to avoid similar problems. However, suggestions contained in this information notice are not NRC requirements; therefore, no specific action or written response is require
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice to inform
 
addressees of a steam generator tube failure at Indian Point Unit 2. NRC investigations of the
 
licensee's steam generator inspection program are ongoing and any potentially generic issues
 
identified will be communicated in a separate generic communication. However, the
 
investigations to date re-emphasize the importance of licensee involvement with ongoing
 
industry efforts to understand and detect steam generator degradation. It is expected that
 
recipients will review the information for applicability to their facilities and consider actions, as
 
appropriate, to avoid similar problems. However, suggestions contained in this information
 
notice are not NRC requirements; therefore, no specific action or written response is required.


==Description of Circumstances==
==Description of Circumstances==
On February 15, 2000, at 7:17 p.m., the Indian Point Unit 2 nuclear plant experienced a steam generator tube failure,, which required the declaration of an Alert at 7:29 p.m., and a manual reactor trip at 7:30 p.m. The operators identified that the #24 steam generator was the source of the leak and completed isolation of the #24 steam generator by 8:31 At 9:02 p.m., the operator opened the high-pressure steam dump valves and established an excessive primary plant cooldown rate that caused a rapid reduction in the pressurizer level and required the operators to manually initiate safety injection. The operators reset the safety injection at 9:21 p.m., reduced the reactor coolant system pressure to about 970 psig at 9:32 p.m., and re-commenced a plant cooldown at 11:35 The residual heat removal (RHR) system was placed in service on February 16, 2000, at 12:38 p.m., and primary plant pressure was reduced below the #24 steam generator pressure to terminate the steam generator tube leakage at 2:20 p.m. The plant cooldown continued, and the plant entered cold shutdown at 4:57 p.m. The licensee exited the Alert at 6:50 The NRC sent an Augmented Inspection Team (AIT) on February 18, 2000, to review the causes, safety implications, and licensee actions associated with the event. The AIT developed a sequence of events, determined the risk significance of the event, and assessed the response by the plant staff and management. The cause of the tube failure was outside the scope of this inspection and is currently being reviewed separately by the NRC. The AIT's report is presented in Inspection Report 05000247/2000-02, dated April 28, 2000 (Accession Number ML003710036). Discussion The event was risk significant. It involved a steam generator tube failure that resulted in an initial primary-to-secondary leak of reactor coolant of approximately 146 gallons per minute and required an "Alert" declaration (the second level of emergency action in the NRC-required emergency response plan). The event resulted in a minor radiological release to the environment that was well within regulatory limits. No radioactivity was measured offsite above normal background levels, and the event did not adversely impact the public health and safet The licensee performed the necessary actions to protect the health and safety of the publi Specifically, the operators promptly and appropriately took those actions in the emergency operating procedures to trip the reactor, isolate the affected steam generator, and depressurize the reactor coolant system. Additionally, the necessary event mitigation systems worked properly. Notwithstanding the above actions, the AIT identified performance problems in several broad areas that challenged operators, complicated the event response, delayed achieving the cold shutdown condition, and affected the radiological release. The problems involved operator performance, procedure quality, equipment performance, technical support, and emergency respons Operator Performance Some operator performance problems were noted during the plant cooldown phase involving the following: While attempting to cool down the reactor coolant system (RCS), the reactor operator initiated an excessive cooldown rate that exceeded procedural and Technical Specification limits. The excessive cooldown led to several conditions that complicated the subsequent event response and delayed the RCS cooldow Operators were slow to recognize configuration lineup problems that (1) prevented successful operation of the auxiliary spray system to lower RCS pressure and (2) delayed heatup of the RHR syste Procedure Quality The procedures adequately guided the initial operator response; however, several procedure problems were identified that delayed the cooldown and depressurizing of the RCS. Procedure deficiencies affected Standard Operating Procedures, Emergency Operating Procedures, and Emergency Plan Implementing Procedures. Specific activities included initiation of RHR cooling, initiation of component cooling water alignment, use of auxiliary pressurizer spray, use of methods to monitor RCS temperature to maintain cold shutdown conditions, and initiation of emergency response organization (ERO) notifications. Station personnel were previously aware of the procedure issue involving initiation of RHR cooling but had not corrected the problem before this even Equipment Performance The necessary event mitigation systems, including the reactor protection system, the auxiliary feedwater system, and the safety injection system, functioned properly. However, several longstanding equipment performance problems were identified that challenged operators during this event: Two losses of condenser vacuum resulted from problems with the operation of the automatic steam supply pressure control valve to the steam jet air ejectors, and the #22 condenser vacuum pum The isolation valve seal water system became inoperable during the event and required operator action and an entry into a Technical Specification Limiting Condition for Operation Action Statemen A containment entry was required to install a temporary nitrogen supply to the pressurizer power-operated relief valve to compensate for a design deficiency. This action was required before placing the overpressure protection system in servic The steam generator leak rate monitoring equipment had been degraded for an extended period, and limited the amount of steam generator leak rate information available to the operators before the even The AIT determined that the number and duration of the equipment problems reflected weaknesses in engineering, corrective action processes, and operational support at the statio The licensee's response to a number of the equipment problems identified during the event reflected an acceptance of "working around" the problem rather than fixing i Emergency Response The ERO took the necessary steps to ensure the protection of public health and safety. The operators properly classified the event, and the licensee implemented a thorough peer review of the emergency response to this event. The AIT identified several emergency plan and implementing procedure problems similar to those identified by the licensee's peer review team, including the following: The emergency response staff was slow to activate the emergency facilitie
On February 15, 2000, at 7:17 p.m., the Indian Point Unit 2 nuclear plant experienced a steam
 
generator tube failure,, which required the declaration of an Alert at 7:29 p.m., and a manual
 
reactor trip at 7:30 p.m. The operators identified that the #24 steam generator was the source
 
of the leak and completed isolation of the #24 steam generator by 8:31 p.m.
 
At 9:02 p.m., the operator opened the high-pressure steam dump valves and established an
 
excessive primary plant cooldown rate that caused a rapid reduction in the pressurizer level and
 
required the operators to manually initiate safety injection. The operators reset the safety
 
injection at 9:21 p.m., reduced the reactor coolant system pressure to about 970 psig at 9:32 p.m., and re-commenced a plant cooldown at 11:35 p.m.
 
The residual heat removal (RHR) system was placed in service on February 16, 2000, at 12:38 p.m., and primary plant pressure was reduced below the #24 steam generator pressure to
 
terminate the steam generator tube leakage at 2:20 p.m. The plant cooldown continued, and
 
the plant entered cold shutdown at 4:57 p.m. The licensee exited the Alert at 6:50 p.m.
 
The NRC sent an Augmented Inspection Team (AIT) on February 18, 2000, to review the
 
causes, safety implications, and licensee actions associated with the event. The AIT developed
 
a sequence of events, determined the risk significance of the event, and assessed the response
 
by the plant staff and management. The cause of the tube failure was outside the scope of this
 
inspection and is currently being reviewed separately by the NRC. The AIT's report is
 
presented in Inspection Report 05000247/2000-02, dated April 28, 2000 (Accession Number
 
ML003710036).
 
Discussion
 
The event was risk significant. It involved a steam generator tube failure that resulted in an
 
initial primary-to-secondary leak of reactor coolant of approximately 146 gallons per minute and
 
required an "Alert" declaration (the second level of emergency action in the NRC-required
 
emergency response plan). The event resulted in a minor radiological release to the
 
environment that was well within regulatory limits. No radioactivity was measured offsite above
 
normal background levels, and the event did not adversely impact the public health and safety.
 
The licensee performed the necessary actions to protect the health and safety of the public.
 
Specifically, the operators promptly and appropriately took those actions in the emergency
 
operating procedures to trip the reactor, isolate the affected steam generator, and depressurize
 
the reactor coolant system. Additionally, the necessary event mitigation systems worked
 
properly. Notwithstanding the above actions, the AIT identified performance problems in
 
several broad areas that challenged operators, complicated the event response, delayed
 
achieving the cold shutdown condition, and affected the radiological release. The problems
 
involved operator performance, procedure quality, equipment performance, technical support, and emergency response.
 
Operator Performance
 
Some operator performance problems were noted during the plant cooldown phase involving
 
the following:
          While attempting to cool down the reactor coolant system (RCS), the reactor operator
 
initiated an excessive cooldown rate that exceeded procedural and Technical
 
Specification limits. The excessive cooldown led to several conditions that complicated
 
the subsequent event response and delayed the RCS cooldown.
 
Operators were slow to recognize configuration lineup problems that (1) prevented
 
successful operation of the auxiliary spray system to lower RCS pressure and
 
(2) delayed heatup of the RHR system.
 
Procedure Quality
 
The procedures adequately guided the initial operator response; however, several procedure
 
problems were identified that delayed the cooldown and depressurizing of the RCS. Procedure
 
deficiencies affected Standard Operating Procedures, Emergency Operating Procedures, and
 
Emergency Plan Implementing Procedures. Specific activities included initiation of RHR
 
cooling, initiation of component cooling water alignment, use of auxiliary pressurizer spray, use
 
of methods to monitor RCS temperature to maintain cold shutdown conditions, and initiation of
 
IN2000-09 emergency response organization (ERO) notifications. Station personnel were previously
 
aware of the procedure issue involving initiation of RHR cooling but had not corrected the
 
problem before this event.
 
===Equipment Performance===
The necessary event mitigation systems, including the reactor protection system, the auxiliary
 
feedwater system, and the safety injection system, functioned properly. However, several
 
longstanding equipment performance problems were identified that challenged operators during
 
this event:
        Two losses of condenser vacuum resulted from problems with the operation of the
 
automatic steam supply pressure control valve to the steam jet air ejectors, and the #22 condenser vacuum pump.
 
The isolation valve seal water system became inoperable during the event and required
 
operator action and an entry into a Technical Specification Limiting Condition for
 
Operation Action Statement.
 
A containment entry was required to install a temporary nitrogen supply to the
 
pressurizer power-operated relief valve to compensate for a design deficiency. This
 
action was required before placing the overpressure protection system in service.
 
The steam generator leak rate monitoring equipment had been degraded for an
 
extended period, and limited the amount of steam generator leak rate information
 
available to the operators before the event.
 
The AIT determined that the number and duration of the equipment problems reflected
 
weaknesses in engineering, corrective action processes, and operational support at the station.
 
The licensee's response to a number of the equipment problems identified during the event
 
reflected an acceptance of "working around" the problem rather than fixing it.
 
===Emergency Response===
The ERO took the necessary steps to ensure the protection of public health and safety. The
 
operators properly classified the event, and the licensee implemented a thorough peer review of
 
the emergency response to this event. The AIT identified several emergency plan and
 
implementing procedure problems similar to those identified by the licensee's peer review team, including the following:
        The emergency response staff was slow to activate the emergency facilities.
 
*      The licensee was slow to establish accountability (i.e., identify the location) of
 
emergency response personnel.
 
IN2000-09 The emergency response data system -(ERDS) was inoperable for the first several hours
 
of the event as a result of a pre-existing equipment problem.
 
Problems were noted in the implementation of the media response plan.
 
Problems were identified involving the timeliness and quality of technical support
 
provided to the operators.
 
The licensee developed and was in the process of implementing an emergency response
 
improvement plan before the event.
 
This information notice requires no specific action or written response. However, recipients are
 
reminded that they are required to consider industry-wide operating experience (including NRC
 
information notices) when practical when setting goals and performing periodic evaluations
 
under Section 50.65, "Requirements for monitoring the effectiveness of maintenance at nuclear
 
power plants," of Part 50 of Title 10 of the Code of Federal Regulations. If you have any
 
questions about the information in this notice, please contact the one of the technical contacts
 
listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.
 
/Ledyard B. Mars , Chief
 
Events Assessment, Generic Communications
 
and Non-Power Reactors Branch
 
Division of Regulatory Improvement Programs
 
Office of Nuclear Reactor Regulation
 
Technical contacts:    Eric Benner, NRR                Lawrence Doerflein, Region I
 
301-415-1171                    610-337-5378 E-mail: eibl0.nrc..qov          E-mail: ltdOnrc.gov
 
Peter Eselgroth, Region I      Raymond Lorson, Region I
 
610-337-5234                    603-474-3589 E-mail: pwemnrc.aov            E-mail: rklO.nrc.aov
 
Attachment: List of Recently Issued NRC Information Notices
 
Attachment LIST OF RECENTLY ISSUED
 
NRC INFORMATION NOTICES
 
Information                                            Date of
 
Notice No.                Subject                      Issuance    Issued to
 
2000-08            Inadequate Assessment of the        5/15/2000  All holders of operating licensees
 
Effect of Differential                          for nuclear power reactors
 
Temperatures on Safety
 
Related Pumps
 
2000-07            National Institute for              4/10/2000  All holders of operating licenses
 
for nuclear power reactors,non
 
Occupational Safety and
 
power reactors, and all fuel cycle
 
Health Respirator User Notice:
                                                                    and materiallicensees required to
 
Special Precaustions for Using
 
have an NRC-approved
 
Certain Self-Contained
 
emergency plan
 
Breathing Apparatus Air
 
Cylinders
 
3/22/2000  All holders of operating licenses
 
2000-06            Offsite Power Voltage
 
for nuclear power reactors, Inadequacies
 
except those who have
 
permanently ceased operations
 
and have certified that fuel has
 
been permanently removed from
 
the reactor
 
3/06/2000  All medical licensees
 
2000-05            Recent Medical
 
Misadministrations Resulting
 
from Inattention to Detail
 
1999 Enforcement Sanctions          2/25/2000  All NRC licensees
 
2000-04 for Deliberate Violations of
 
NRC Employee Protection
 
Requirements
 
High-Efficiency Particulate Air      2/22/2000  All NRC licensed fuel-cycled
 
2000-03                                                            conversion, enrichment, and
 
Filter Exceeds Mass Limit
 
fabrication facilities
 
Before Reaching Expected
 
Differential Pressure
 
2/22/2000  All NRC licensed fuel-cycled
 
2000-02            Failure of Criticality Safety
 
conversion, enrichment, and
 
Control to Prevent Uranium                      fabrication facilities
 
Dioxide (U0 2) Powder
 
Accumulation


* The licensee was slow to establish accountability (i.e., identify the location) of emergency response personne The emergency response data system -(ERDS) was inoperable for the first several hours of the event as a result of a pre-existing equipment proble Problems were noted in the implementation of the media response pla Problems were identified involving the timeliness and quality of technical support provided to the operator The licensee developed and was in the process of implementing an emergency response improvement plan before the even This information notice requires no specific action or written response. However, recipients are reminded that they are required to consider industry-wide operating experience (including NRC information notices) when practical when setting goals and performing periodic evaluations under Section 50.65, "Requirements for monitoring the effectiveness of maintenance at nuclear power plants," of Part 50 of Title 10 of the Code of Federal Regulations. If you have any questions about the information in this notice, please contact the one of the technical contacts listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manage /Ledyard B. Mars , Chief Events Assessment, Generic Communications and Non-Power Reactors Branch Division of Regulatory Improvement Programs Office of Nuclear Reactor Regulation Technical contacts: Eric Benner, NRR Lawrence Doerflein, Region I 301-415-1171 610-337-5378 E-mail: eibl0.nrc..qov E-mail: ltdOnrc.gov Peter Eselgroth, Region I Raymond Lorson, Region I 610-337-5234 603-474-3589 E-mail: pwemnrc.aov E-mail: rklO.nrc.aov
OL = operating License


===Attachment:===
CP = Construction Permit}}
List of Recently Issued NRC Information Notices Attachment LIST OF RECENTLY ISSUED NRC INFORMATION NOTICESInformation Date of Notice No. Subject Issuance Issued to 2000-08 Inadequate Assessment of the 5/15/2000 All holders of operating licenseesEffect of Differential Temperatures on SafetyRelated Pumps National Institute for Occupational Safety and Health Respirator User Notice: Special Precaustions for Using Certain Self-Contained Breathing Apparatus Air Cylinders Offsite Power Voltage Inadequacies Recent Medical Misadministrations Resulting from Inattention to Detail 1999 Enforcement Sanctions for Deliberate Violations of NRC Employee Protection Requirements High-Efficiency Particulate Air Filter Exceeds Mass Limit Before Reaching Expected Differential Pressure Failure of Criticality Safety Control to Prevent Uranium Dioxide (U02) Powder Accumulation4/10/2000 3/22/2000 3/06/20002/25/20002/22/2000 2/22/2000for nuclear power reactorsAll holders of operating licenses for nuclear power reactors,nonpower reactors, and all fuel cycle and materiallicensees required to have an NRC-approved emergency plan All holders of operating licenses for nuclear power reactors, except those who have permanently ceased operations and have certified that fuel has been permanently removed from the reactor All medical licenseesAll NRC licenseesAll NRC licensed fuel-cycled conversion, enrichment, and fabrication facilities All NRC licensed fuel-cycled conversion, enrichment, and fabrication facilitiesOL = operating License CP = Construction Permit2000-07 2000-06 2000-052000-042000-03 2000-02}}


{{Information notice-Nav}}
{{Information notice-Nav}}

Latest revision as of 05:46, 24 November 2019

Steam Generator Tube Failure at Indian Point Unit 2
ML011930011
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 06/28/2000
From: Marsh L
Operational Experience and Non-Power Reactors Branch
To:
References
FOIA/PA-2001-0256 IN-00-009
Download: ML011930011 (5)


cc: Holody

Urban

UNITED STATES Nick

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, D.C. 20555-0001 June 28, 2000

NRC INFORMATION NOTICE 2000-09: STEAM GENERATOR TUBE FAILURE AT INDIAN

POINT UNIT 2

Addressees

All holders of operating licenses for nuclear power reactors except those who have ceased

operations and have certified that fuel has been permanently removed from the reactor vessel.

Purpose

The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice to inform

addressees of a steam generator tube failure at Indian Point Unit 2. NRC investigations of the

licensee's steam generator inspection program are ongoing and any potentially generic issues

identified will be communicated in a separate generic communication. However, the

investigations to date re-emphasize the importance of licensee involvement with ongoing

industry efforts to understand and detect steam generator degradation. It is expected that

recipients will review the information for applicability to their facilities and consider actions, as

appropriate, to avoid similar problems. However, suggestions contained in this information

notice are not NRC requirements; therefore, no specific action or written response is required.

Description of Circumstances

On February 15, 2000, at 7:17 p.m., the Indian Point Unit 2 nuclear plant experienced a steam

generator tube failure,, which required the declaration of an Alert at 7:29 p.m., and a manual reactor trip at 7:30 p.m. The operators identified that the #24 steam generator was the source

of the leak and completed isolation of the #24 steam generator by 8:31 p.m.

At 9:02 p.m., the operator opened the high-pressure steam dump valves and established an

excessive primary plant cooldown rate that caused a rapid reduction in the pressurizer level and

required the operators to manually initiate safety injection. The operators reset the safety

injection at 9:21 p.m., reduced the reactor coolant system pressure to about 970 psig at 9:32 p.m., and re-commenced a plant cooldown at 11:35 p.m.

The residual heat removal (RHR) system was placed in service on February 16, 2000, at 12:38 p.m., and primary plant pressure was reduced below the #24 steam generator pressure to

terminate the steam generator tube leakage at 2:20 p.m. The plant cooldown continued, and

the plant entered cold shutdown at 4:57 p.m. The licensee exited the Alert at 6:50 p.m.

The NRC sent an Augmented Inspection Team (AIT) on February 18, 2000, to review the

causes, safety implications, and licensee actions associated with the event. The AIT developed

a sequence of events, determined the risk significance of the event, and assessed the response

by the plant staff and management. The cause of the tube failure was outside the scope of this

inspection and is currently being reviewed separately by the NRC. The AIT's report is

presented in Inspection Report 05000247/2000-02, dated April 28, 2000 (Accession Number

ML003710036).

Discussion

The event was risk significant. It involved a steam generator tube failure that resulted in an

initial primary-to-secondary leak of reactor coolant of approximately 146 gallons per minute and

required an "Alert" declaration (the second level of emergency action in the NRC-required

emergency response plan). The event resulted in a minor radiological release to the

environment that was well within regulatory limits. No radioactivity was measured offsite above

normal background levels, and the event did not adversely impact the public health and safety.

The licensee performed the necessary actions to protect the health and safety of the public.

Specifically, the operators promptly and appropriately took those actions in the emergency

operating procedures to trip the reactor, isolate the affected steam generator, and depressurize

the reactor coolant system. Additionally, the necessary event mitigation systems worked

properly. Notwithstanding the above actions, the AIT identified performance problems in

several broad areas that challenged operators, complicated the event response, delayed

achieving the cold shutdown condition, and affected the radiological release. The problems

involved operator performance, procedure quality, equipment performance, technical support, and emergency response.

Operator Performance

Some operator performance problems were noted during the plant cooldown phase involving

the following:

While attempting to cool down the reactor coolant system (RCS), the reactor operator

initiated an excessive cooldown rate that exceeded procedural and Technical

Specification limits. The excessive cooldown led to several conditions that complicated

the subsequent event response and delayed the RCS cooldown.

Operators were slow to recognize configuration lineup problems that (1) prevented

successful operation of the auxiliary spray system to lower RCS pressure and

(2) delayed heatup of the RHR system.

Procedure Quality

The procedures adequately guided the initial operator response; however, several procedure

problems were identified that delayed the cooldown and depressurizing of the RCS. Procedure

deficiencies affected Standard Operating Procedures, Emergency Operating Procedures, and

Emergency Plan Implementing Procedures. Specific activities included initiation of RHR

cooling, initiation of component cooling water alignment, use of auxiliary pressurizer spray, use

of methods to monitor RCS temperature to maintain cold shutdown conditions, and initiation of

IN2000-09 emergency response organization (ERO) notifications. Station personnel were previously

aware of the procedure issue involving initiation of RHR cooling but had not corrected the

problem before this event.

Equipment Performance

The necessary event mitigation systems, including the reactor protection system, the auxiliary

feedwater system, and the safety injection system, functioned properly. However, several

longstanding equipment performance problems were identified that challenged operators during

this event:

Two losses of condenser vacuum resulted from problems with the operation of the

automatic steam supply pressure control valve to the steam jet air ejectors, and the #22 condenser vacuum pump.

The isolation valve seal water system became inoperable during the event and required

operator action and an entry into a Technical Specification Limiting Condition for

Operation Action Statement.

A containment entry was required to install a temporary nitrogen supply to the

pressurizer power-operated relief valve to compensate for a design deficiency. This

action was required before placing the overpressure protection system in service.

The steam generator leak rate monitoring equipment had been degraded for an

extended period, and limited the amount of steam generator leak rate information

available to the operators before the event.

The AIT determined that the number and duration of the equipment problems reflected

weaknesses in engineering, corrective action processes, and operational support at the station.

The licensee's response to a number of the equipment problems identified during the event

reflected an acceptance of "working around" the problem rather than fixing it.

Emergency Response

The ERO took the necessary steps to ensure the protection of public health and safety. The

operators properly classified the event, and the licensee implemented a thorough peer review of

the emergency response to this event. The AIT identified several emergency plan and

implementing procedure problems similar to those identified by the licensee's peer review team, including the following:

The emergency response staff was slow to activate the emergency facilities.

  • The licensee was slow to establish accountability (i.e., identify the location) of

emergency response personnel.

IN2000-09 The emergency response data system -(ERDS) was inoperable for the first several hours

of the event as a result of a pre-existing equipment problem.

Problems were noted in the implementation of the media response plan.

Problems were identified involving the timeliness and quality of technical support

provided to the operators.

The licensee developed and was in the process of implementing an emergency response

improvement plan before the event.

This information notice requires no specific action or written response. However, recipients are

reminded that they are required to consider industry-wide operating experience (including NRC

information notices) when practical when setting goals and performing periodic evaluations

under Section 50.65, "Requirements for monitoring the effectiveness of maintenance at nuclear

power plants," of Part 50 of Title 10 of the Code of Federal Regulations. If you have any

questions about the information in this notice, please contact the one of the technical contacts

listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.

/Ledyard B. Mars , Chief

Events Assessment, Generic Communications

and Non-Power Reactors Branch

Division of Regulatory Improvement Programs

Office of Nuclear Reactor Regulation

Technical contacts: Eric Benner, NRR Lawrence Doerflein, Region I

301-415-1171 610-337-5378 E-mail: eibl0.nrc..qov E-mail: ltdOnrc.gov

Peter Eselgroth, Region I Raymond Lorson, Region I

610-337-5234 603-474-3589 E-mail: pwemnrc.aov E-mail: rklO.nrc.aov

Attachment: List of Recently Issued NRC Information Notices

Attachment LIST OF RECENTLY ISSUED

NRC INFORMATION NOTICES

Information Date of

Notice No. Subject Issuance Issued to

2000-08 Inadequate Assessment of the 5/15/2000 All holders of operating licensees

Effect of Differential for nuclear power reactors

Temperatures on Safety

Related Pumps

2000-07 National Institute for 4/10/2000 All holders of operating licenses

for nuclear power reactors,non

Occupational Safety and

power reactors, and all fuel cycle

Health Respirator User Notice:

and materiallicensees required to

Special Precaustions for Using

have an NRC-approved

Certain Self-Contained

emergency plan

Breathing Apparatus Air

Cylinders

3/22/2000 All holders of operating licenses

2000-06 Offsite Power Voltage

for nuclear power reactors, Inadequacies

except those who have

permanently ceased operations

and have certified that fuel has

been permanently removed from

the reactor

3/06/2000 All medical licensees

2000-05 Recent Medical

Misadministrations Resulting

from Inattention to Detail

1999 Enforcement Sanctions 2/25/2000 All NRC licensees

2000-04 for Deliberate Violations of

NRC Employee Protection

Requirements

High-Efficiency Particulate Air 2/22/2000 All NRC licensed fuel-cycled

2000-03 conversion, enrichment, and

Filter Exceeds Mass Limit

fabrication facilities

Before Reaching Expected

Differential Pressure

2/22/2000 All NRC licensed fuel-cycled

2000-02 Failure of Criticality Safety

conversion, enrichment, and

Control to Prevent Uranium fabrication facilities

Dioxide (U0 2) Powder

Accumulation

OL = operating License

CP = Construction Permit