ML18283B241: Difference between revisions
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{{#Wiki_filter:HI1t: ronhl 195 | {{#Wiki_filter:HI1t: ronhl 195 U.S. NUCLI:AIIfrt:CIUI.AYOIIVCOMhIISSION DOCICIrY NUMOLPA tr-ir'I 50-259 260 I:ILI:. HUihtlrttn MAC DISTB II3UTIOM roll PAR'F ~PO DOCKE1 MATEfIIRL HOll'1'll'l.Y RRPORY TO: FIIPMI TENNESSEL'ALLI-'Y AUTIIOKITX DAYLl Oil DOCUMCNY D'.ATUR,, ALA 2-10>>76 DAYL'C CCI V E0 2-18-76 | ||
.CTTI! It QNo Yontzr D PAOP II'IPUT l.onhl NUMtlrn of- coPIcs ALCrYIvGD Qonto INnL QCOP V UNCLnsslrfr:D 1-OSSCnlf'YION GNCLOSU nfl LETTER TRANS TIIE FOLT.OIrlXNG: HO.'lTIILY REPORT FOR JANUARY 1976 PLANT & COlIPONEiVZ OPEIQ.BXLXTX & | |||
AVAXLABXLXTX ~ TIIXS REPORT TO BE USED XN PREPARING GRAY BOOIC BX PLANS & OPERATXONS. | |||
~TIIXS REPORT TO BE USED XN PREPARING GRAY BOOIC BX PLANS&OPERATXONS. | PLANT HAHE: OWNS Ff RRY 1 & 2 l' 1 FOB ACTION/INFORViATION 2- 19-7 rlcb HXPC | ||
PLANT HAHE: OWNS Ff RRY 1&2 | ~H1< ~YH LO! ACYtOH INTEhNAL OISl RI DU I'ION NRC PDR UGDORMITr.P | ||
~1iMiQZm H1LrHCH CHYH~PL~LPDR/ITIII HS~PA | ~1iMiQZm H1LrHCH CHYH~PL~ | ||
.AS'=.Xl LPDR TXC | |||
/ITIII HS~PA Lf IINRL DISTR IDUTION CpiIITII L I'!UMUI!II 1597 | |||
~~UNIT Beowns Ferry I DATE c.'/"r/7C)COHPLETED BY lla old Halls | ~pg3TI0y | ||
r 1 | ) TENNESSEE VALLEY AUTHORITY Brogans Perry Nuclear Plant P. 0. Box 2000 | ||
BEACTOB RZSEBVZ ShgiDO'Ei} | /P76 1916 Decatur, Alabama 35601 PegU.i~i+."j Pcuilet FI18 Pebruary 10, Qo- Z Eq/pg0 cB3 81976 ~ | ||
HQUBS.~~.~.744 | U.S. kPJCuAR ItCiVLATORY coMMlss K>u | ||
~ Mdl Section | |||
'Nuclear Regulatory Commission Office of Management Information and Program Control Washington, D. C. 20545 Gent:lemen: | |||
.))5)NZT ELECTRICAL PO'~G tiPMZD (tG'H)....; | " | ||
'-2,022 2 489,847 BZACTOB | Enclosed is the January 1976 report on plant and component operability and availability for Browns Perry Nuclear Plant units 1 and '2.. | ||
UI}IT CAPACITY FACTOR (3)................. | Very truly yours, TENNESSEE VALLEY AUTHORITY H. J. Green Plant Superintendent Enclosures CC: Nuclear Regulatory Commission Office of Inspection and Enforcement 230 'Peachtree Street, Rf Suite 818 Atlant:a, Georgia 30303 An Equal Opportunity Employer | ||
0 0 18.7 FORCED OUTAGE RATE (4)~~~~~~.100 100 S}}UTDOWNS SCHEDULED TO BEGIN, IN hEXT 6 HOhT}}S (STATE TYPES DATE AND'DURATION OF EACH): IF SEtUTDOttN AT END OF REPORT PERIOD, ESTD))tTED D:.TE OF STARTUP.Undetermined PLANTS IN TEST STATUS (PRIOR TO COMERCLKL OPERATION! | |||
REPORT THE FOLLOUDtO': | VEI'i'IANE Bromo tiorry I DATE Klvr) opznAnnG srArus: CO!~ZLKTF:D BY: }4rol(} }';ill., | ||
DAT" LAST DAT~REASON FOR FORECAST | r 1~ REPORTING PERIOD: 0000760101 TO 2400760131 GROSS }}OURS Itl REPORTING PERXOD: | ||
*100 GFOSS}}OUPHE Xil FXPORTING Pi'.RIOD | 2 CURRENTLY AUT}}ORIZED PO<G'R LEVEL t'H4t I Ão-tKT 1065 3 POWER LEVEL TO N}IC}}RESTPICTED (XF ANY): N/A 4, 'EASONS FOR RESTRXCTIONS ( IF ANY):. | ||
T}IXS CU IULATXV.E | |||
"! '.IT}} ~ YR-TO DATE TO DATE HOURS REACTOR WAS CRITICAL...........".... 0 0 ' | |||
9,870.02 E}EACTOR RESERVE SHUTDOWN'I HOUBS- ~ . 526.10 7,o HOURS GENERATOR ON-LXHE.. 9,282.80 | |||
: 8. Ul}XT RESCUE S}VJTDOWtl HOURS 0 0 0 9 GROSS THER}}AL PO>W GE}I:-RATED= (t}WH).'..... 0 0 22,036,392 | |||
: 10. GROSS ELECTRICAL POWr Gr. iiMTH) (I "nTH) (5) 0 7,091,570 | |||
: 11. NET FLECTRXCAL POWER GF'iWATZD (t}WH) ~ | |||
-5,756 -5,756 6 )828,416 16.8 | |||
: 12. REACTOR AVAILABILITYFACTOR(l) 0 16.2 46.1 | |||
: 13. UNIT USE FACTOR (2)............. ~ . ~ . ~ ~ ~ .. | |||
0 0 32.6 1}}. U}GT CAPACITY FACTOR (3 ) ~ ~ ~ ~ o ~ e r ~ ~ ~ ~ o ~ ~ | |||
~ ~ | |||
100 100 50.0 FORCED OUTAGE RATE (4) ~ ~ o ~ ~ ~ ~ ~ ~ | |||
S}!UTDOENS SCHEDULFD TO BEGIN W NEXT 6 ~A}0}A}}S (STATE TYPE, DATE AND DURATION OF EACH): | |||
: 17. XF SHUTDOWN AT END OF REPO T PERIOD ESTD}ATED DATE OF START}V'' | |||
: 18. PLANTS IN TEST STATUS (PRIOR TO CO~a~ERCIAL OPERATION) REPORT THE FOLLGHING'ATE LAST . D:TE . Rp SON FOR FORECAST . ACHIEVED DXFFERENCE XNXTIAL CRITXCALITY INXTIAL ELECTRICAL PO}IVER GENERATION COt}t}ERCXAL OPE}}ATION | |||
~ | |||
(1) REACTOR AVAXLABXLITYFACTOR - 1}OURS RLACTOR }'S CRITICAL *100 GROSS l}OURS IN REPORTING PERIOD (2) URIC,'SE FACTO}(.- HOURS GENE}FETOR ON-LINE ~100 GROSS }}OU}}S IN I&PORTING PERXOD (3) UNIT CAPACITY FACTOR - NET ELECTRICAL PO}'ER GFNFRATED CURRENTLY LICENSED POLE}'EVEI "GROSS }}OURS IN REPORTING P" RIOD (4) FORCED OUTAGE "RATE " FORC}'.D OUTAGE }!(>URS + }.00 | |||
}}OU}H G}'.NLAI'.KTOR ON-LINL' FORCED OU'rAGE l}OURS (5) DOES NOT INCLUDE AUXILIARY DXESEL GENERATION | |||
I o | |||
UNIT Mi'QE Browns Ferrv I DATE 2/5/76 Unit. remained in cold shutdown H 1dV>> | |||
for repair of control cables. CO>PLETED BY REPORT HOh~ - anuary PLANT SHUTDOWNS TYPE 1'iETHOD OF F"FORCED DURATION SHUTTING DOWN HO. DAH S-SCHEDULED HOURS REASON 1 TikE REACTOR 2 CON KNTS 1 760101 744 B B (1) REASON: (2) KTPOD A-EQUIPi~iEHT F~KILURE (EXPLAIN) A-iiBNUA B-KKINT, OR TEST B-~"~EQUAL C-REFUELING "KQ D-RECUIATORY RESTRICTION C"c E-OPERATOR TRAINING AND SCP'iaaf LICENSING EXQlINATION F-ADiiINISTRATIVE G-.OPERATIONAL ERROR (EXPLAIN) | |||
UNIT Beowns Ferry I | |||
~ ~ | |||
DATE c.'/ "r/7C) | |||
COHPLETED BY lla old Halls DAILY UNIT PO':TER OUTPUT kfONTH January DAY AVERAGE DAILY Y"e-net AVERAGE DAILY Htle-net | |||
-5.83 25 -10.13 | |||
-4.96 26 | |||
. -10;46. | |||
-5.46 27 -10.21 4 -5.46 28 | |||
'"9. 17 | |||
-5;13 '-7.46 | |||
, 6. -5.17 30 ~ | |||
-8, 63 | |||
-5.58 -8; 75 7 31 | |||
-7.04 9 -7.75 10 -9.08 11 -8.63 12 -8.63 13 | |||
-8.67 14 | |||
-6.75 15 -8.04 16 | |||
-7.63 17 -7.92 18 .". '-'8.71 | |||
'9 | |||
-8.63 20 -8.29 21 -8.04 | |||
'22 7 ~ 17 | |||
~ w 23 -5.96 24 -9.17 Note: Negative values indicate station use when unit is off line. | |||
r 1 UHZT FigdgE Browns rry II DATE 2/5//6 OPF}}ATIt}G STATUS: BY: lnrori | |||
'OMPLEAT I ~ REPORTING PERIOD: '000760101 TP 2l!00760131 GROSS }lOURS Xt} REPORTrtiG PERI0D: 744 | |||
: 2. CURRENTLY AUT}lORXZED POMER LEVEL t54t: 3293 t&e "alET 1065 3~ PO'F}ER LEVEL TO H}}IC}tRESTRICTED (XF ANY): N/A 4 REASONS FOR RESTRICTIONS ( IF ANY): | |||
~ | |||
THIS CU, fULATIVP | |||
~0! "r}t YR-TO DATE TO MTE 5 )e HOUBS B~KCTOB VAS CBITXCAL............... 0 3, <PiT~ | |||
.6. 6 057.3 | |||
BEACTOB RZSEBVZ ShgiDO'Ei} HQUBS. ~ ~ .~. 744 744 7 e HOURS GZI}:-I}ATOB Ot;-LXli.......,........,.... Oi 0 3,578. 08. | |||
: 8. I) | |||
: 9. GROSS THi%1AL PO~ GZtir~TW (tGlH).....'.. ~ | |||
=8;259,'696 | |||
: 10. .))5) | |||
NZT ELECTRICAL PO'~ G tiPMZD (tG'H)....; '-2,022 2 489,847 2~ BZACTOB AVAILABILITYFACTOB(1) 30.7 13 ~ | |||
- | |||
Ut}XT USZ FACTOR (2)............... | |||
: 14. UI}IT CAPACITY FACTOR (3 )................. 0 0 18.7 FORCED OUTAGE RATE (4) ~ ~ ~ ~ ~ ~ . 100 100 70.6 | |||
,16. S}}UTDOWNS SCHEDULED TO BEGIN, IN hEXT 6 HOhT}}S (STATE TYPES DATE AND ' | |||
DURATION OF EACH): | |||
17- IF SEtUTDOttN AT END OF REPORT PERIOD, ESTD))tTED D:.TE OF STARTUP. Undetermined | |||
: 18. PLANTS IN TEST STATUS (PRIOR TO COMERCLKL OPERATION! REPORT THE FOLLOUDtO': | |||
DAT" LAST DAT ~ REASON FOR | |||
' | |||
FORECAST . ACHIEVED DIFFERENCE XNITIAL CRITICALXTY INITIAL ELECTRICAL POh'ER GENERATION COAQ}ERCIAL OPERATION REACTOR AVAIL~VILITYFACTOR - HOURS R=-DOCTOR 1 AS CRITICAL *100 GROSS }lOURS It} REPORTING PERIOD (2) 1$ I7. USE FACTOR " HOURS GENEFATOR 0'ii-Lr'}E *100 GFOSS }}OUPHE Xil FXPORTING Pi'.RIOD UNXT CAPACXTY FACTOR - NET ELECTRICAL PO}! R C'NER;KTED | |||
'100 (3) | |||
CURRENTLY LICENSED POWER LEVEL"-GROSS 110URS Xii }U POPTING PERIOD (4) 1'ORCED OUTAGE RATH - FOFCHD Ot}TAC}'. 110URS 110URS GENE}UeTOR ON" LrtP': } FOFiCED 0}ffACE }10URS (5) DOES NOT INCLUDE AUXILXA}tYDIESE}, GE}KlbYTXON | |||
UNI> N~~ - Bro: ns'.er '.T. | |||
\ | |||
2/5/76 'ATE Unit r mained shutdown for repair of control cables Haro ld Halls CO~X ~TED BY REPORT 140NTH January PLANT SHUTDOMHS TYPE . >!ETHOD OP P-FORCED DURATION S11UTTING DOWN DAT:" S -SC13ZDULED 1jOURS REASON 1 T11E REACTOR 2 COMENTS 760101 744 (I) REASON: (2) >ZTHOD: | |||
'-EQUIP>ENT FAILURE (EXPLAIN) A-~i'ANUAL B-PAINT, OR TEST B-."QiUAL C-REFUELING gc;R,'La! | |||
D-REGULATORY RESTRICTION C- 0. LV E-OPERATOR TRAINING AND SCK4' LICENSING EXAMINATION P-AD~!INISTRATI'LtE G-OPERATIONAL ERROR (EXPLAIN) | |||
( ~ | |||
UNIT owns Ferr IT. | |||
2/S/76 | |||
'llew'0 ld Wa 1 1 s COHPLE TED gy DAILY IP.fIT PO';1ER OUTPUT Omr a<<<<V AVERAGE DAILY K97e-net DAY AVERAGE DAILY %le-net | |||
-4.0 -1.4 | |||
-4.3 26 -1.4 . | |||
-4.3 -l. 9 4 -4.0 28- -20S | |||
-4.3 -2.8 | |||
-4.7 30 -2. 8 | |||
"'7 | |||
. | |||
-4.0 31 -1.8 | |||
-2.6 | |||
-1.6 9. | |||
10 | |||
-1.8 | |||
-1. 6 | |||
-2. 1 13 -2. 6 14 -3.8 1S 3~1 16 3 ~1 17 -2. 9 18 -2.3 19 -1. 7 20 -1. 7 21 -1.5 22 -2.9 | |||
-3.'7 23 24 -1. 5 Hote: Negative values indicate station use when unit is off line. | |||
0 to}} | 0 to}} |
Revision as of 13:50, 20 October 2019
ML18283B241 | |
Person / Time | |
---|---|
Site: | Browns Ferry |
Issue date: | 02/10/1976 |
From: | Green H Tennessee Valley Authority |
To: | Office of Nuclear Reactor Regulation |
References | |
Download: ML18283B241 (14) | |
Text
HI1t: ronhl 195 U.S. NUCLI:AIIfrt:CIUI.AYOIIVCOMhIISSION DOCICIrY NUMOLPA tr-ir'I 50-259 260 I:ILI:. HUihtlrttn MAC DISTB II3UTIOM roll PAR'F ~PO DOCKE1 MATEfIIRL HOll'1'll'l.Y RRPORY TO: FIIPMI TENNESSEL'ALLI-'Y AUTIIOKITX DAYLl Oil DOCUMCNY D'.ATUR,, ALA 2-10>>76 DAYL'C CCI V E0 2-18-76
.CTTI! It QNo Yontzr D PAOP II'IPUT l.onhl NUMtlrn of- coPIcs ALCrYIvGD Qonto INnL QCOP V UNCLnsslrfr:D 1-OSSCnlf'YION GNCLOSU nfl LETTER TRANS TIIE FOLT.OIrlXNG: HO.'lTIILY REPORT FOR JANUARY 1976 PLANT & COlIPONEiVZ OPEIQ.BXLXTX &
AVAXLABXLXTX ~ TIIXS REPORT TO BE USED XN PREPARING GRAY BOOIC BX PLANS & OPERATXONS.
PLANT HAHE: OWNS Ff RRY 1 & 2 l' 1 FOB ACTION/INFORViATION 2- 19-7 rlcb HXPC
~H1< ~YH LO! ACYtOH INTEhNAL OISl RI DU I'ION NRC PDR UGDORMITr.P
~1iMiQZm H1LrHCH CHYH~PL~
.AS'=.Xl LPDR TXC
/ITIII HS~PA Lf IINRL DISTR IDUTION CpiIITII L I'!UMUI!II 1597
~pg3TI0y
) TENNESSEE VALLEY AUTHORITY Brogans Perry Nuclear Plant P. 0. Box 2000
/P76 1916 Decatur, Alabama 35601 PegU.i~i+."j Pcuilet FI18 Pebruary 10, Qo- Z Eq/pg0 cB3 81976 ~
U.S. kPJCuAR ItCiVLATORY coMMlss K>u
~ Mdl Section
'Nuclear Regulatory Commission Office of Management Information and Program Control Washington, D. C. 20545 Gent:lemen:
"
Enclosed is the January 1976 report on plant and component operability and availability for Browns Perry Nuclear Plant units 1 and '2..
Very truly yours, TENNESSEE VALLEY AUTHORITY H. J. Green Plant Superintendent Enclosures CC: Nuclear Regulatory Commission Office of Inspection and Enforcement 230 'Peachtree Street, Rf Suite 818 Atlant:a, Georgia 30303 An Equal Opportunity Employer
VEI'i'IANE Bromo tiorry I DATE Klvr) opznAnnG srArus: CO!~ZLKTF:D BY: }4rol(} }';ill.,
r 1~ REPORTING PERIOD: 0000760101 TO 2400760131 GROSSOURS Itl REPORTING PERXOD: 2 CURRENTLY AUT}}ORIZED PO<G'R LEVEL t'H4t I Ão-tKT 1065 3 POWER LEVEL TO N}IC}}RESTPICTED (XF ANY): N/A 4, 'EASONS FOR RESTRXCTIONS ( IF ANY):. T}IXS CU IULATXV.E
"! '.IT}} ~ YR-TO DATE TO DATE HOURS REACTOR WAS CRITICAL...........".... 0 0 '
9,870.02 E}EACTOR RESERVE SHUTDOWN'I HOUBS- ~ . 526.10 7,o HOURS GENERATOR ON-LXHE.. 9,282.80
- 8. Ul}XT RESCUE S}VJTDOWtl HOURS 0 0 0 9 GROSS THER}}AL PO>W GE}I:-RATED= (t}WH).'..... 0 0 22,036,392
- 10. GROSS ELECTRICAL POWr Gr. iiMTH) (I "nTH) (5) 0 7,091,570
- 11. NET FLECTRXCAL POWER GF'iWATZD (t}WH) ~
-5,756 -5,756 6 )828,416 16.8
- 12. REACTOR AVAILABILITYFACTOR(l) 0 16.2 46.1
- 13. UNIT USE FACTOR (2)............. ~ . ~ . ~ ~ ~ ..
0 0 32.6 1}}. U}GT CAPACITY FACTOR (3 ) ~ ~ ~ ~ o ~ e r ~ ~ ~ ~ o ~ ~
~ ~
100 100 50.0 FORCED OUTAGE RATE (4) ~ ~ o ~ ~ ~ ~ ~ ~ S}!UTDOENS SCHEDULFD TO BEGIN W NEXT 6 ~A}0}A}}S (STATE TYPE, DATE AND DURATION OF EACH):
- 17. XF SHUTDOWN AT END OF REPO T PERIOD ESTD}ATED DATE OF START}V
- 18. PLANTS IN TEST STATUS (PRIOR TO CO~a~ERCIAL OPERATION) REPORT THE FOLLGHING'ATE LAST . D:TE . Rp SON FOR FORECAST . ACHIEVED DXFFERENCE XNXTIAL CRITXCALITY INXTIAL ELECTRICAL PO}IVER GENERATION COt}t}ERCXAL OPE}}ATION
~ (1) REACTOR AVAXLABXLITYFACTOR - 1}OURS RLACTOR }'S CRITICAL *100 GROSS l}OURS IN REPORTING PERIOD (2) URIC,'SE FACTO}(.- HOURS GENE}FETOR ON-LINE ~100 GROSS }}OU}}S IN I&PORTING PERXOD (3) UNIT CAPACITY FACTOR - NET ELECTRICAL PO}'ER GFNFRATED CURRENTLY LICENSED POLE}'EVEI "GROSS }}OURS IN REPORTING P" RIOD (4) FORCED OUTAGE "RATE " FORC}'.D OUTAGE }!(>URS + }.00
}}OU}H G}'.NLAI'.KTOR ON-LINL' FORCED OU'rAGE l}OURS (5) DOES NOT INCLUDE AUXILIARY DXESEL GENERATION
I o
UNIT Mi'QE Browns Ferrv I DATE 2/5/76 Unit. remained in cold shutdown H 1dV>> for repair of control cables. CO>PLETED BY REPORT HOh~ - anuary PLANT SHUTDOWNS TYPE 1'iETHOD OF F"FORCED DURATION SHUTTING DOWN HO. DAH S-SCHEDULED HOURS REASON 1 TikE REACTOR 2 CON KNTS 1 760101 744 B B (1) REASON: (2) KTPOD A-EQUIPi~iEHT F~KILURE (EXPLAIN) A-iiBNUA B-KKINT, OR TEST B-~"~EQUAL C-REFUELING "KQ D-RECUIATORY RESTRICTION C"c E-OPERATOR TRAINING AND SCP'iaaf LICENSING EXQlINATION F-ADiiINISTRATIVE G-.OPERATIONAL ERROR (EXPLAIN)
UNIT Beowns Ferry I
~ ~
DATE c.'/ "r/7C) COHPLETED BY lla old Halls DAILY UNIT PO':TER OUTPUT kfONTH January DAY AVERAGE DAILY Y"e-net AVERAGE DAILY Htle-net
-5.83 25 -10.13 -4.96 26 . -10;46. -5.46 27 -10.21 4 -5.46 28 '"9. 17 -5;13 '-7.46
, 6. -5.17 30 ~
-8, 63 -5.58 -8; 75 7 31 -7.04 9 -7.75 10 -9.08 11 -8.63 12 -8.63 13 -8.67 14 -6.75 15 -8.04 16 -7.63 17 -7.92 18 .". '-'8.71 '9 -8.63 20 -8.29 21 -8.04
'22 7 ~ 17
~ w 23 -5.96 24 -9.17 Note: Negative values indicate station use when unit is off line.
r 1 UHZT FigdgE Browns rry II DATE 2/5//6 OPF}}ATIt}G STATUS: BY: lnrori
'OMPLEAT I ~ REPORTING PERIOD: '000760101 TP 2l!00760131 GROSS }lOURS Xt} REPORTrtiG PERI0D: 744
- 2. CURRENTLY AUT}lORXZED POMER LEVEL t54t: 3293 t&e "alET 1065 3~ PO'F}ER LEVEL TO H}}IC}tRESTRICTED (XF ANY): N/A 4 REASONS FOR RESTRICTIONS ( IF ANY):
~
THIS CU, fULATIVP
~0! "r}t YR-TO DATE TO MTE 5 )e HOUBS B~KCTOB VAS CBITXCAL............... 0 3, <PiT~ .6. 6 057.3
BEACTOB RZSEBVZ ShgiDO'Ei} HQUBS. ~ ~ .~. 744 744 7 e HOURS GZI}:-I}ATOB Ot;-LXli.......,........,.... Oi 0 3,578. 08.
- 8. I)
- 9. GROSS THi%1AL PO~ GZtir~TW (tGlH).....'.. ~
=8;259,'696
- 10. .))5)
NZT ELECTRICAL PO'~ G tiPMZD (tG'H)....; '-2,022 2 489,847 2~ BZACTOB AVAILABILITYFACTOB(1) 30.7 13 ~
-
Ut}XT USZ FACTOR (2)...............
- 14. UI}IT CAPACITY FACTOR (3 )................. 0 0 18.7 FORCED OUTAGE RATE (4) ~ ~ ~ ~ ~ ~ . 100 100 70.6
,16. S}}UTDOWNS SCHEDULED TO BEGIN, IN hEXT 6 HOhT}}S (STATE TYPES DATE AND ' DURATION OF EACH): 17- IF SEtUTDOttN AT END OF REPORT PERIOD, ESTD))tTED D:.TE OF STARTUP. Undetermined
- 18. PLANTS IN TEST STATUS (PRIOR TO COMERCLKL OPERATION! REPORT THE FOLLOUDtO':
DAT" LAST DAT ~ REASON FOR
'
FORECAST . ACHIEVED DIFFERENCE XNITIAL CRITICALXTY INITIAL ELECTRICAL POh'ER GENERATION COAQ}ERCIAL OPERATION REACTOR AVAIL~VILITYFACTOR - HOURS R=-DOCTOR 1 AS CRITICAL *100 GROSS }lOURS It} REPORTING PERIOD (2) 1$ I7. USE FACTOR " HOURS GENEFATOR 0'ii-Lr'}E *100 GFOSS }}OUPHE Xil FXPORTING Pi'.RIOD UNXT CAPACXTY FACTOR - NET ELECTRICAL PO}! R C'NER;KTED
'100 (3)
CURRENTLY LICENSED POWER LEVEL"-GROSS 110URS Xii }U POPTING PERIOD (4) 1'ORCED OUTAGE RATH - FOFCHD Ot}TAC}'. 110URS 110URS GENE}UeTOR ON" LrtP': } FOFiCED 0}ffACE }10URS (5) DOES NOT INCLUDE AUXILXA}tYDIESE}, GE}KlbYTXON
UNI> N~~ - Bro: ns'.er '.T.
\
2/5/76 'ATE Unit r mained shutdown for repair of control cables Haro ld Halls CO~X ~TED BY REPORT 140NTH January PLANT SHUTDOMHS TYPE . >!ETHOD OP P-FORCED DURATION S11UTTING DOWN DAT:" S -SC13ZDULED 1jOURS REASON 1 T11E REACTOR 2 COMENTS 760101 744 (I) REASON: (2) >ZTHOD:
'-EQUIP>ENT FAILURE (EXPLAIN) A-~i'ANUAL B-PAINT, OR TEST B-."QiUAL C-REFUELING gc;R,'La!
D-REGULATORY RESTRICTION C- 0. LV E-OPERATOR TRAINING AND SCK4' LICENSING EXAMINATION P-AD~!INISTRATI'LtE G-OPERATIONAL ERROR (EXPLAIN)
( ~ UNIT owns Ferr IT. 2/S/76
'llew'0 ld Wa 1 1 s COHPLE TED gy DAILY IP.fIT PO';1ER OUTPUT Omr a<<<<V AVERAGE DAILY K97e-net DAY AVERAGE DAILY %le-net -4.0 -1.4 -4.3 26 -1.4 . -4.3 -l. 9 4 -4.0 28- -20S -4.3 -2.8 -4.7 30 -2. 8
"'7 .
-4.0 31 -1.8 -2.6 -1.6 9.
10
-1.8 -1. 6 -2. 1 13 -2. 6 14 -3.8 1S 3~1 16 3 ~1 17 -2. 9 18 -2.3 19 -1. 7 20 -1. 7 21 -1.5 22 -2.9 -3.'7 23 24 -1. 5 Hote: Negative values indicate station use when unit is off line.
0 to}}