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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML20214K521 + (ML20214K521)
- ML20214K522 + (ML20214K522)
- IA-86-601, Final Response to FOIA Request for Minutes of Nmss,Div of Fuel Cycle Matl Safety,860624 Meeting in Washington,Dc Re Members of New Mgt Team for Syncor.Nrc Has No Records Subj to Request + (ML20214K523)
- ML20214K523 + (ML20214K523)
- ML20214K524 + (ML20214K524)
- ML20214K526 + (ML20214K526)
- ML20214K527 + (ML20214K527)
- IR 05000321/1986043 + (ML20214K528)
- ML20214K529 + (ML20214K529)
- ML20214K530 + (ML20214K530)
- 05000354/LER-1987-020, :on 870421,while Shift Chemistry Technician Attempting to Place RWCU Filter/Demineralizer B in Hold Mode,Steam Leak Isolation Timer Initiated on High Differential Flow.Caused by Personnel Error + (ML20214K531)
- ML20214K532 + (ML20214K532)
- IA-86-370, Forwards Enforcement Conference Outline,Util Nuclear Operations Improvement Plan,Slides on Nuclear Operations Improvement Plan & Slides on Jul 1985 Rod Pull Error from 860509 Preliminary Enforcement Conference + (ML20214K533)
- ML20214K533 + (ML20214K533)
- ML20214K534 + (ML20214K534)
- ML20214K536 + (ML20214K536)
- IR 05000424/1986094 + (ML20214K537)
- ML20214K539 + (ML20214K539)
- RBG-25975, Ro:On 870413,personnel Discovered Core Thermal Power Not Changing Proportionally to Core Flow Changes.Caused by Feedwater Averaging Function of Computer Program Not Updating Points Values.Procedure EDP-CC-0001 Implemented + (ML20214K540)
- ML20214K543 + (ML20214K543)
- ML20214K544 + (ML20214K544)
- ML20214K545 + (ML20214K545)
- ML20214K546 + (ML20214K546)
- ML20214K547 + (ML20214K547)
- PY-CEI-NRR-0655, Forwards Application Fee for Processing Exigent Tech Spec Change Request Made in + (ML20214K548)
- ML20214K549 + (ML20214K549)
- ML20214K551 + (ML20214K551)
- ML20214K553 + (ML20214K553)
- IR 05000424/1986104 + (ML20214K558)
- ML20214K559 + (ML20214K559)
- RBG-25976, Special Rept:On 870420,during Surveillance Test Procedure STP-000-0001, Daily Operations Logs, Main Steam Tunnel Temps Exceeded Tech Spec 3/4.7.8 Limit for Over 8 H.Cause Undetermined.Tech Spec Change Request Being Developed + (ML20214K563)
- 05000265/LER-1986-008-01, :on 860525,while Unit Operating in Run Mode, Core Spray Sys Room Cooler 2-5748A Discovered W/Frayed Belts & Core Spray Room Cooler 2A Declared Inoperable.Caused by Normal Wear of Belts.Belts Replaced + (ML20214K564)
- TXX-4958, Interim Deficiency Rept CP-86-36 Re Scope of Plant Mods Resulting from Pipe Support Reverification Program.Initially Reported on 860609.Encl Lists Support Mods Initiated to Date.Next Rept by 860926 + (ML20214K566)
- ML20214K567 + (ML20214K567)
- ML20214K569 + (ML20214K569)
- ML20214K570 + (ML20214K570)
- AECM-86-0358, Forwards Rev 13 to Physical Security Plan.Rev Also Contains 10CFR50.54 Amends,Indicating Name Change from Middle South Energy,Inc to Sys Energy Resources,Inc.Rev Withheld (Ref 10CFR2.790 & 73.21) + (ML20214K572)
- ML20214K575 + (ML20214K575)
- ML20214K577 + (ML20214K577)
- PY-CEI-NRR-0654, Forwards Rev 7 to Emergency Plan.Rev Incorporates Improvements in Emergency Preparedness Program + (ML20214K579)
- ML20214K580 + (ML20214K580)
- ML20214K583 + (ML20214K583)
- TXX-4959, Interim Deficiency Rept CP-86-41 Re Effects of Operational Status of Plant Equipment During Mode 4 Operations.Initially Reported on 860626.Westinghouse Owners Group Developing Program to Address Concern.Next Rept by 861029 + (ML20214K584)
- ML20214K586 + (ML20214K586)
- PY-CEI-NRR-0522, Forwards LERs 86-036-00,86-037-00 & 86-038-00 + (ML20214K587)
- 05000325/LER-1987-001-01, :on 870126,discovered That HPCI Turbine Steam Supply Inboard Primary Containment Isolation Valve E41-F002 Would Not Open.Caused by Failure of Auxiliary Contact Block Assembly.Contact Assemblies Replaced + (ML20214K589)
- 05000324/LER-1987-006-02, :on 870424,operability Testing of HPCI Sys Revealed HPCI Sys Pump Flow Controller Would Not Control in Automatic.Caused by Open Electrical Resistor R26.Resistor Replaced.Controller Dynamically Tuned + (ML20214K591)
- 05000440/LER-1986-036, :on 860718,during Performance of Channel Functional Surveillance Test on Scram Discharge Vol Channel D Level Instrument,Unexpected Full Scram Occurred.Caused by Faulty Auxiliary Contact Mechanism.Mechanism Replaced + (ML20214K592)
- ST-HL-AE-2185, Forwards Comparison of Facility SPDS Design Requirements W/ Requirements of Suppl 1 to NUREG-0737 for Closure of Section 3.1 in SPDS Audit Rept,Per NRC Requests + (ML20214K593)
- 05000440/LER-1986-037, :on 860719,while in Shutdown Cooling Mode,Rhr Sys Automatically Isolated.Caused by Faulty Leak Detection Switch Modules.Info Tags Hung on Subj Panels Clarified & Faulty Leak Detection Switch Repaired + (ML20214K595)
- 05000440/LER-1986-038, :on 860719 & 20,standby Train of Annulus Exhaust Gas Treatment Sys Automatically Started.Caused by Instrument Inaccuracy & Technician Error.Setpoints Recalculated & Adjusted & Technician Counseled + (ML20214K597)