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This 4 and 8 hour notification is being ma … This 4 and 8 hour notification is being made to report that Salem Unit 2 suffered an unplanned automatic reactor trip and subsequent automatic auxiliary feedwater system actuation. The trip was initiated due to a Main Turbine Trip above P-9 (49% power). The Main Turbine trip was caused by a Main Generator Protection signal.</br>Salem unit 2 is currently stable in Mode 3. Reactor coolant system pressure is 2235 psig and Reactor Coolant System temperature is 547 F with decay heat removal via the main steam dump and auxiliary feedwater systems. Unit 2 has no active shutdown tech spec action statements in effect. All control rods (fully) inserted on the reactor trip. All ECCS (Emergency Core Cooling System) and ESF (Emergency Safety Features) systems functioned as expected.</br>No safety related equipment or major secondary equipment was tagged for maintenance prior to this event. No personnel were injured during this event.</br>The main generator protection signal was either a ground fault or a differential current trip. The plant is in its normal shutdown electrical lineup. No safeties or relief valves lifted during this event.</br>Unit 1 is defueled and was not affected by this event.</br>The licensee notified the NRC Resident Inspector and will notify the Lower Alloways Creek Township. notify the Lower Alloways Creek Township. +
08:23:00, 28 June 2016 +
52,048 +
06:58:00, 28 June 2016 +
08:23:00, 28 June 2016 +
This 4 and 8 hour notification is being ma … This 4 and 8 hour notification is being made to report that Salem Unit 2 suffered an unplanned automatic reactor trip and subsequent automatic auxiliary feedwater system actuation. The trip was initiated due to a Main Turbine Trip above P-9 (49% power). The Main Turbine trip was caused by a Main Generator Protection signal.</br>Salem unit 2 is currently stable in Mode 3. Reactor coolant system pressure is 2235 psig and Reactor Coolant System temperature is 547 F with decay heat removal via the main steam dump and auxiliary feedwater systems. Unit 2 has no active shutdown tech spec action statements in effect. All control rods (fully) inserted on the reactor trip. All ECCS (Emergency Core Cooling System) and ESF (Emergency Safety Features) systems functioned as expected.</br>No safety related equipment or major secondary equipment was tagged for maintenance prior to this event. No personnel were injured during this event.</br>The main generator protection signal was either a ground fault or a differential current trip. The plant is in its normal shutdown electrical lineup. No safeties or relief valves lifted during this event.</br>Unit 1 is defueled and was not affected by this event.</br>The licensee notified the NRC Resident Inspector and will notify the Lower Alloways Creek Township. notify the Lower Alloways Creek Township. +
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Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
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