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Issue date | Title | |
---|---|---|
RA-23-0218, Review Request for the Aging Management Program and Inspection Plan for the Shearon Harris Nuclear Power Plant, Unit 1, Reactor Vessel Internals | 21 September 2023 | Review Request for the Aging Management Program and Inspection Plan for the Shearon Harris Nuclear Power Plant, Unit 1, Reactor Vessel Internals |
IR 05000400/2020004 | 27 January 2021 | Integrated Inspection Report 05000400/2020004 |
ML21004A236 | 4 January 2021 | 301 Exam Report Items - SRO as Given Written Exam |
ML20114E262 | 12 May 2020 | Final ASP Analysis - Shearon Harris (LER 400-02-004-09) |
RA-19-0123, License Amendment Request to Eliminate Certain Technical Specification Requirements in Alignment with Improved Standard Technical Specifications | 25 July 2019 | License Amendment Request to Eliminate Certain Technical Specification Requirements in Alignment with Improved Standard Technical Specifications |
ML20311A556 | 6 November 2017 | 2017 Q1-Q4 ROP Inspection Findings |
IR 05000400/2014005 | 27 January 2015 | IR 05000400/2014005; on October 1, 2014, Through December 31, 2014; Duke Energy Progress, Inc., Shearon Harris Nuclear Power Plant, Unit 1, Operability Determinations and Functionality Assessments |
ML15013A245 | 13 January 2015 | Initial Exam 2014-302 Draft Sim_IN-Plant JPMs |
ML15013A267 | 13 January 2015 | Initial Exam 2014-302 Final Sim_IN-Plant JPMs |
ML14338A038 | 3 December 2014 | 302 Final SRO Written Exam |
ML13295A416 | 17 October 2013 | 301 Initial Exam Final SRO Written Exam |
IR 05000400/2013002 | 30 April 2013 | IR 05000400-13-002: Carolina Power and Light Company; on January 1, 2013 - March 31, 2013; Shearon Harris Nuclear Power Plant, Unit 1; Operability Evaluations, Plant Modifications, and Event Follow-up |
HNP-12-118, Response to Recommendation 2.3 Flooding Walkdown of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident | 27 November 2012 | Response to Recommendation 2.3 Flooding Walkdown of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident |
HNP-12-119, Response to Recommendation 2.3 Seismic Walkdown of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident | 27 November 2012 | Response to Recommendation 2.3 Seismic Walkdown of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident |
ML12053A340 | 12 March 2012 | Request for Information Pursuant to Title 10 of the Code of Federal Regulations 50.54(f) Regarding Recommendations 2.1, 2.3, and 9.3, of the Near-Term Task Force Review of Insights from the Fukushima Dai-Ichi Accident |
ML12056A050 | 12 March 2012 | Enclosure 4 - Recommendation 2.3: Flooding |
ML12056A049 | 12 March 2012 | Enclosure 3 - Recommendation 2.3: Seismic |
IR 05000400/2011011 | 8 December 2011 | IR 05000400-11-011, on 08/29/2011 - 09/02/2011 & 09/19-23/2011; Shearon Harris Nuclear Plant, Unit 1; Triennial Fire Protection Inspection Report & Exercise of Enforcement Discretion |
ML112170233 | 2 August 2011 | Initial Exam 2011-301 Final RO Written Exam |
IR 05000400/2008002 | 21 April 2008 | IR 05000400-08-002 on 01/01/2008 - 03/31/2008 for Shearon Harris, Unit 1; Routine Integrated Report |
ML071500403 | 13 June 2007 | 2.206 - Final Director'S Decision Under 10 C.F.R. 2.206, Denying Petitioners' Request to Not Accept the Licensee'S Application for License Renewal at Shearon Harris Plant, Unit 1 |
ML070780537 | 2 April 2007 | G20060793 - Shearon Harris 2.206 Petition Proposed Director'S Decision |
ML062980107 | 21 September 2006 | G20060793 - 2.206 Supplement 1 Fire Protection Issues at the Shearon Harris Nuclear Power Plant |
ML062640550 | 20 September 2006 | G20060793 - John D. Runkle E-mail Re 2.206 - Recurring Fire Protection Issues at Shearon Harris Nuclear Plant |
ML053390352 | 9 January 2006 | FRN: All Nuclear Power Plants That Use Hemyc/Mt Fire Barriers Notice of Issuance of Director'S Decision Under 10 CFR 2.206 |
ML053390311 | 9 January 2006 | G20050379 - Mr. Paul Gunter Ltr. Re. 2.206 - Inoperable Hemyc/Mt Fire Protection Systems |
ML052630411 | 20 October 2005 | G20050379 - Paul Gunter Ltr 2.206 Inoperable Hemyc/Mt Fire Protection Systems, Proposed Directors Decision |
ML051740562 | 27 June 2005 | G20050379 - Paul Gunter Ltr. 2.206 Inoperable Hemyc/Mt Fire Protection System |
ML051520445 | 27 May 2005 | Significant Adverse Condition Investigation Report |
ML051440209 | 12 May 2005 | G20050379 - Paul Gunter Ltr Re 2.206 - Inoperable Hemyc/Mt Fire Protection Systems |
IR 05000400/2003007 | 29 April 2005 | Draft Letter to Carolina Power and Light from Ogle, Shearon Harris Nuclear Power Plant - NRC Fire Protection Inspection Report No. 05000400-2003-007 |
ML050380443 | 3 February 2005 | Undated Draft, Revision 4, NRC Fire Protection Inspection Report No. 05000400/2003007 |
ML040850494 | 19 March 2004 | Comment (1) of Tony Groblewski Regarding Notice of Clarification of Steam Generator Tube Integrity Event Reporting Guideline in NUREG-1022 |
ML042360559 | 23 February 2004 | E-mail, C. Ogle to Eng Branch, Fwd: Peer Review of Inspection Reports |
ML042380284 | 16 January 2004 | E-mail, C. Ogle to Eng Branch, Peer Review of Inspection Reports |
ML050380368 | 16 January 2004 | E-mail from C. Ogle to Eng. Branch - Peer Review of Inspection Reports |
ML033380523 | 18 November 2003 | IR 05000400-03-007, Shearon Harris, on 02/01/03 - 10/21/03, Significance Determination of Fire Protection Findings |
ML051520410 | 23 October 2003 | Action Request 000997103 |
ML022670157 | 22 March 2002 | August 2002 Exam 50-400/2002-301 Final Written SRO Exam |
ML18016A794 | 29 January 1999 | LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor |
Information Notice 1997-48, Inadequate or Inappropriate Interim Fire Protection Compensatory Measures | 9 July 1997 | Inadequate or Inappropriate Interim Fire Protection Compensatory Measures |
ML18011A805 | 2 March 1995 | LER 95-002-00:on 950207,unanalyzed Condition Existed Re Potential of Loss of Automatic ESF Actuations & Subsequent TS 3.0.3 Entry.Caused by Both Trains of Ssps Declared Inoperable.Plant Evolutions avoided.W/950303 Ltr |
ML18010B104 | 3 June 1993 | Responds to NRC 930506 Ltr Re Violation & Deviation Noted in Insp Rept 50-400/93-08.Corrective Actions:Fuel Pool Cooling Pump QA-SA Placed on Increased Testing Frequency & Maint Procedure MMM-012 Revised |
NRC Generic Letter 1992-02 | 6 March 1992 | NRC Generic Letter 1992-002: Resolution of Generic Issue 79, Unanalyzed Reactor Vessel (PWR) Thermal Stress During Natural Convection Cooldown. |
ML031140549 | 7 November 1991 | Withdrawn NRC Generic Letter 1991-018: Information to Licensees Regarding Two NRC Inspection Manual Sections on Resolution of Degraded and Nonconforming Conditions and on Operability |
Information Notice 1991-38, Thermal Stratification in Feedwater System Piping | 13 June 1991 | Thermal Stratification in Feedwater System Piping |
ML18009A440 | 9 April 1990 | LER 90-006-00:on 900309,discovered That Evolution Violated Requirements of FSAR to Keep Individual Tanks Isolated from Another Tank.Caused by Failure to Address Evolution in Operating Procedure.Procedure revised.W/900409 Ltr |
ML18022A778 | 1 March 1990 | Rept of 10CFR50.59 Chnages to Procedures &/Or Plant Mods for 1989 |
ML18009A339 | 22 January 1990 | LER 89-020-00:on 891031,jumper Wires in Limitorque Operator for Pressurizer PORV Block Valve 1RC-117 Found Contaminated W/Grease Leaking from Gear Box.Caused by Overfilling Gear Box.Wires repaired/replaced.W/900122 Ltr |
ML18005B073 | 26 September 1989 | LER 89-015-00:on 890827,discovered That Fuel Handling Bldg Operating Floor Equipment Hatch in Storage Location on Operating Deck Not Installed as Required.Caused by Inadequate Procedure.Procedure revised.W/890926 Ltr |