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 Issue dateFromTitleProject stage
ML20080R76710 February 1984Southern Nuclear
Beckham J
Responds to IE Bulletin 84-01 Re Insp for Cracks in Mark I Containment Torus Vent Header.No Apparent Cracking or Relevant Indications Found on Unit 1.No Addl Cracking Found Beyond Original Cracking on Unit 2Other
ML20080N56610 February 1984FirstEnergy
Fiedler P
Forwards Drywell Coating Evaluation, Technical Data Rept, Per SEP Topic VI-1, Organic Matls & Post-Accident ChemistryRequest
ML20087H14813 March 1984Southern Nuclear
Gucwa L
Forwards GE Repts on Metallographic Exam of Metal Samples Taken from Cracked Vent Header,Per NRC 840206 Meeting W/ Util,Bwr Regulatory Response Group & Ge.Vent Header Cracking Brittle Fracture Caused by Injection of Cold NitrogenMeeting
ML20083L65530 March 1984Exelon
Daltroff S
(FORMERLY PHILADELPHIA ELECTRIC
Submits Info on IE Bulletin 84-01, Entitled Cracks in BWR Mark I Containment Vent Headers. Primary Containment Drywell to Torus Bypass Tests Performed.Status of GE SIL 402 Recommended Actions ListedOther
ML20084L44431 March 1984Marisa Herrera
GENERAL ELECTRIC CO.
Ranganath S
Obermiller K
Analysis of Vent Header Cracking at Hatch 2Other
ML20084R1705 April 1984Southern Nuclear
Gucwa L
Comments on Status of Recommendations of GE Svc Info Ltr 402 Re Wetwell/Drywell Inerting.Evaluation of Nitrogen Inerting Sys Design Performed & Redundant Low Temp Shutoff Valve AddedOther
ML20083R73918 April 1984Exelon
Rybak B
Forwards Response to GE SIL 402 Generated Due to Large Crack in Torus Vent Header at Another Operating Plant Attributed to Brittle Fracture Identified During Insp of Cold Nitrogen Into Torus During InertingOther
ML20084L4257 May 1984Southern Nuclear
Gucwa L
Forwards Analysis of Vent Header Cracking at Hatch 2. Analysis Shows That Observed Cracking Can Be Explained by Injection of Cold Nitrogen Into Containment & Any Cracking Expected to Be through-wall,detectable by Visual InspOther
ML20091B78723 May 1984Southern Nuclear
Gucwa L
Provides Status of GE Svc Info Ltr 402 Re Vent Header Cracking Incident.Recommended Ultrasonic Testing Not Planned Due to Lack of Baseline Test Data.Cracking from Injection of Cold Nitrogen Detectable by Surface ExamOther
NLS8400242, Submits List of Actions Taken on Recommendations from GE 840214 Svc Info Ltr 402, Wetwell/Drywell Inerting. Evaluation of Inerting Sys Design Determined That Failure of Cold Temp Shutdown Switch Cause of Problem12 September 1984Nebraska Public Power District
Pilant J
Submits List of Actions Taken on Recommendations from GE 840214 Svc Info Ltr 402, Wetwell/Drywell Inerting. Evaluation of Inerting Sys Design Determined That Failure of Cold Temp Shutdown Switch Cause of ProblemOther
FVY-84-110, Forwards Response to NRC Request Re Actions Taken in Response to GE Significant Info Ltr 420 Concerning Hatch-2 Vent Header Crack14 September 1984VERMONT YANKEE NUCLEAR POWER CORP.
Capstick R
Forwards Response to NRC Request Re Actions Taken in Response to GE Significant Info Ltr 420 Concerning Hatch-2 Vent Header CrackOther
BECO-84-150, Responds to IE Bulletin 84-01, Cracks in BWR Mark I Containment Vent Headers. Util Endorses GE Svc Info Ltr 402 Recommendations.Equipment Damage Has Not Occurred & Inerting Sys Operation Suitable14 September 1984Harrington W
Eversource Energy
Responds to IE Bulletin 84-01, Cracks in BWR Mark I Containment Vent Headers. Util Endorses GE Svc Info Ltr 402 Recommendations.Equipment Damage Has Not Occurred & Inerting Sys Operation SuitableOther
ML20097E00314 September 1984Niagara Mohawk
Hooten B
Forwards Response to IE Bulletin 84-01 Re Potential for Cracking in BWR Vent Headers Using Nitrogen Inerting Sys. Nitrogen Inerting Sys Not Used at Facility.Recommendations Identified in GE Svc Info Ltr 402 AddressedOther
ML20098G55714 September 1984FirstEnergy
Fiedler P
Submits Supplemental Info in Response to IE Bulletin 84-01, Cracks in BWR Mark I Containment Vent Headers. Program Initiated to Address Concerns of GE SIL 402 & Implementation ScheduleSupplement
ML20098A02617 September 1984Mangan C
Niagara Mohawk
Forwards Responses to Recommendations Contained in IE Bulletin 84-01, Cracks in BWR Mark I Containment Vent Headers & GE Svc Info Ltr 402, Wetwell/Drywell Inerting. No Anomalies Indicated in Drywell/Wetwell PressuresOther
ML20097H26917 September 1984Exelon
John Marshall
Forwards Response to GE Significant Info Ltr 402 & IE Info Notice 84-17 Re Nitrogen Inerting SysOther
SNRC-1082, Submits Status of Evaluation Re IE Info Notice 84-17, Problems W/Liquid Nitrogen Cooling Components Below Nil Ductility Temp & GE Svc Info Ltr SIL-402, Wetwell/Drywell Inerting18 September 1984John Leonard
Long Island Lighting Company
Submits Status of Evaluation Re IE Info Notice 84-17, Problems W/Liquid Nitrogen Cooling Components Below Nil Ductility Temp & GE Svc Info Ltr SIL-402, Wetwell/Drywell InertingOther
ML20098F15926 September 1984Exelon
(FORMERLY PHILADELPHIA ELECTRIC
Kemper J
Submits Mods Identified for Completion Prior to Liquid Nitrogen Inerting of Containment.Low Temp Switch Will Be Replaced & Relocated to Improve Response Time & Eliminate Adverse Impact of Cold Outdoor Ambient TempsOther
ML20098F07127 September 1984DTE Energy
Jens W
Responds to GE Svc Info Ltr 402 Re Wetwell/Drywell Temp. Design & Operation of Nitrogen Sys Provides Adequate Assurance That Impingement of Liquid or Extremely Cold Nitrogen Against Vital Plant Components Will Not OccurOther
ML20098G6741 October 1984Power Authority of the State of New York
J. P. Bayne
Responds to IE Bulletin 84-01, Cracks in BWR Mark I Containment Vent Headers. No Evidence of Outside or Inside Vent Header & Nitrogen Penetration Cracking Found.Addl Insps & Evaluations Will Be PerformedOther
ML20098G6821 October 1984Carolina Power & Light Co.
Zimmerman S
Responds to Verbal Questions Concerning Recommendations of GE Svc Info Ltr 402 Re IE Bulletin 84-01, Cracks in BWR Mark I Containment Vent Headers. Steps Taken to Evaluate & Implement Containment Inerting RecommendationsOther
ML20138A22529 November 1985NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Walker R
Summarizes 851108 Mgt Meeting at Region II Ofc Re Util Response to Recommendations of Svc Info Ltr 402 in Handling Unit 1 Nitrogen Inerting & Purge Line Crack Discovered on 841215.Summary of Topics & List of Attendees EnclMeeting