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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 5704322 March 2024 01:56:0010 CFR 50.72(b)(3)(iv)(A), System ActuationAutomatic Turbine Driven Auxiliary Feedwater Pump Actuation

The following information was provided by the licensee via email: At 2056 on 3/21/24, Callaway Plant was in Mode 1 at approximately 100 percent power when an automatic start of the turbine driven auxiliary feedwater pump occurred. The event occurred while restoring inverter NN12 from maintenance. NN12 is the normal in-service inverter for the group 2 120-VAC instrument bus (NN02). The actuation occurred while swapping from the swing inverter (NN18) to the normal in-service inverter (NN12). All safety systems responded as expected. At 2334, the turbine driven auxiliary feedwater pump was secured. The plant is being maintained in a stable condition, in mode 1. The NRC Resident Inspector was notified The licensee is investigating the cause of the automatic start.

  • * * RETRACTION ON 4/25/2024 AT 1432 EDT FROM GREG CIZIN TO ERNEST WEST * * *

Event Notification (EN) 57043, made on 03/21/2024 pursuant to 10 CFR 50.72(b)(3)(iv)(A), is being retracted based upon further investigation into the cause of the turbine driven auxiliary feedwater pump (TDAFP) actuation. The TDAFP received an invalid manual initiation signal caused by a voltage transient that was generated on the NK02 125-VDC bus upon closure of downstream breaker NK0211 (while restoring inverter NN12 from maintenance). This actuation signal was due to degradation of a 48-VDC power supply (PS1) within engineered safety features actuation system (ESFAS) logic cabinet SA036C. This degradation likely prevented the power supply from sufficiently filtering the transient that occurred on the 125-VDC bus associated with the NN12 inverter. Notified R4DO (Warnick)

Auxiliary Feedwater
ENS 5696815 February 2024 08:47:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Turbine Trip/Reactor TripThe following information was provided by the licensee via email: At 0247 CST on 2/15/2024, Callaway Plant was in mode 1 at approximately 100 percent power when a turbine trip and reactor trip occurred. All safety systems responded as expected with the exception of an indication issue on the feedwater isolation valves, which were confirmed closed. A valid feedwater isolation signal and auxiliary feedwater actuation signal were also received as a result of the reactor trip. The plant is being maintained stable in mode 3. All control rods fully inserted from the reactor trip signal and decay heat is being removed via the auxiliary feedwater system and steam dumps. The NRC Resident Inspector was notified.Feedwater
Auxiliary Feedwater
Control Rod
ENS 556987 January 2022 18:23:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Turbine Trip / Reactor TripThe following information was provided by the licensee via email: At 1223 CST on January 7, 2022, Callaway Plant was in Mode 1 at approximately 100 percent power when a turbine trip / reactor trip occurred. All safety systems responded as expected with the exception of an indication issue with the 'B' Feedwater Isolation Valve, which was confirmed closed. A valid Feedwater Isolation Signal and Auxiliary Feedwater Actuation Signal were also received as a result of the reactor trip. The plant is being maintained stable in Mode 3. All control rods fully inserted from the reactor trip signal, and decay heat is being removed via the Auxiliary Feedwater and Steam Dump Systems. The NRC Senior Resident Inspector was notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The plant is in a normal shutdown electrical lineup.Feedwater
Auxiliary Feedwater
Control Rod
ENS 5504924 December 2020 18:35:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Turbine and Reactor TripAt 1235 CST on December 24, 2020, Callaway Plant was in Mode 1 at approximately 90 percent power when a turbine trip/reactor trip, from a vital main generator trip signal, occurred. All safety systems responded as expected with exception of an indication issue with the 'B' Feedwater Isolation Valve, which was confirmed closed, and one intermediate range nuclear instrumentation channel which failed off-scale low following the trip. A valid Feedwater Isolation Signal and Auxiliary Feedwater Actuation Signal were also received as a result of the plant trip. The plant is being maintained stable in Mode 3. All control rods fully inserted from the reactor trip signal, and decay heat is being removed via the Auxiliary Feedwater and Steam Dump Systems. The NRC Senior Resident Inspector was notified.Feedwater
Auxiliary Feedwater
Control Rod
ENS 5491627 September 2020 07:03:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Reactor TripAt 0203 (CDT) on September 27, 2020 the plant was in Mode 1 at 98 percent power when a turbine trip/reactor trip (from a generator trip signal) occurred. All systems responded as expected. A Feedwater Isolation signal was received due to the reactor trip with RCS average temperature less than 564 degrees Fahrenheit. The Auxiliary Feedwater system started on a valid actuation signal to restore and maintain steam generator levels. The plant is being maintained stable in Mode 3 with no complications. The NRC Resident Inspector has been notified of the reactor trip. All control rods fully inserted from the reactor trip signal, and decay heat is being removed via the Auxiliary Feedwater and Steam Dump Systems.Steam Generator
Feedwater
Auxiliary Feedwater
Control Rod
ENS 546394 April 2020 06:15:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Reactor TripAt 0114 (CDT) on April 04, 2020 the plant was in Mode 1 at 100 percent power when a Digital Feedwater Trouble alarm was received unexpectedly. Operators identified a full feedwater demand signal and lowering level in the 'C' Steam Generator. At 0115 a Reactor Trip signal for Low Steam Generator Level was received. All systems responded as expected. A Feedwater Isolation signal was received due to the reactor trip with RCS average temperature less than 564 degrees Fahrenheit. Auxiliary Feedwater started on a valid actuation signal to restore and maintain Steam Generator levels. The Plant is being maintained stable in Mode 3 with no complications. The NRC Resident Inspector has been notified of the Reactor Trip. All control rods fully inserted from the reactor trip signal, and decay heat is being removed via the Auxiliary Feedwater and Steam Dump Systems.Steam Generator
Feedwater
Auxiliary Feedwater
Control Rod
ENS 5406917 May 2019 04:03:0010 CFR 50.72(b)(3)(iv)(A), System ActuationEn Revision Imported Date 6/6/2019

EN Revision Text: REACTOR TRIP DUE TO SOURCE RANGE HI FLUX SIGNAL This is an 8-hour, non-emergency notification for a valid reactor trip signal with the reactor not critical, and a valid auxiliary feedwater system actuation in accordance with 10 CFR 50.72(b)(3)(iv)(A) - Valid System Actuation.

At 2303 (CDT) on May 16, 2019, the plant was administratively in mode 2 due to withdrawing control rods for startup following refuel. The reactor had not been declared critical. The P-6 permissive at 10E-10 Amps was met for one of two Intermediate Range detectors allowing for block of the Source Range high flux trip (1E5CPS). Prior to performing the block, the Source Range high flux trip setpoint was exceeded and a reactor trip received. All systems responded as expected. A feedwater isolation signal was received due to the reactor trip with feedwater temperature less than 564 degrees Fahrenheit. Auxiliary feedwater was started to maintain steam generator levels. The plant is being maintained stable in mode 3 with no complications. The NRC Resident Inspector was present during the startup and was notified of the reactor trip.

  • * * UPDATE FROM JONATHAN LAUF TO HOWIE CROUCH AT 1454 EDT ON 6/5/19 * * *

A correction is being made for the sixth sentence in the second paragraph above, which states, 'A Feedwater Isolation signal was received due to the reactor trip with feedwater temperature less than 564 degrees Fahrenheit.' Within this sentence, 'feedwater temperature' is to be replaced with 'reactor coolant system temperature.' The licensee has notified the NRC Senior Resident Inspector.

Steam Generator
Reactor Coolant System
Feedwater
Auxiliary Feedwater
Control Rod
ENS 5400517 April 2019 06:37:0010 CFR 50.72(b)(3)(iv)(A), System ActuationUndervoltage to a Safety Related Bus Resulting in Valid System ActuationAt approximately 0137 CDT, with the Plant (Callaway) in No Mode (Defueled) the "B" Switchyard Bus cleared resulting in a loss of normal power to "A" Train Safety Related Transformer XNB01. This resulted in an under voltage condition on Safety Related Bus NB01. The "A" Emergency Diesel started per design and re-energized Bus NB01. This actuated the shutdown sequencer which first sheds loads including the "A" Spent Fuel Pool Cooling Pump and started "A" Essential Service Water Pump, "A" Component Cooling Water Pump, "A" Control Room A/C and other design loads. No complications were identified. The "A" Switchyard Bus remained energized at all times. The "A" Spent Fuel Pool Cooling Pump was restarted per off normal procedure response at 0149 CDT. Spent Fuel Pool water temperature started at 102 F and rose to 103 F prior to restart. There was no movement of irradiated fuel in progress in the Fuel Building during this time. The plant remains stable in No Mode (Defueled). At the time of the loss of "B" Switchyard Bus, the plant was closing Generator Output breaker MDV53 to establish a backfeed alignment. Further investigation is in progress. This event is reportable per 10 CFR 50.72(b)(3)(iv)(A). The NRC Senior Resident has been notified.Service water
ENS 518463 April 2016 04:02:0010 CFR 50.72(b)(3)(iv)(A), System ActuationReactor Protection System Actuation While Reactor Shutdown

At 2302 (CDT) on April 2, 2016, with the plant shutdown, (with) all control rods inserted in the reactor and while attempting to reset the reactor trip breakers to support outage activities (reset of the main turbine), the reactor trip breakers reopened. This was identified to be due to having both trains of Solid State Protection System (SSPS) out of service while in Mode 5. With both trains of SSPS out of service, a condition was met that would cause a reactor trip signal due to having a general warning condition on both trains. Per procedure, the control rods were incapable of withdrawal and fully inserted. Reactor Coolant System boron was 2280 ppm. There were no actuations as a result of the reactor trip breakers opening due to SSPS being removed from service. The licensee will be notifying the NRC Resident Inspector.

  • * * RETRACTION AT 1635 EDT ON 4/4/16 FROM TIM HOLLAND TO JEFF HERRERA * * *

At 0713 EDT on April 3, 2016, EN #51846 provided notification of a Reactor Protection System actuation as revealed by the reactor trip breakers opening. Upon further investigation, it has been determined that the system actuated during maintenance activities due to a reactor trip signal caused by both trains of the Solid State Protection System (SSPS) being in test. This signal was not in response to actual plant conditions or parameters satisfying the requirements for initiation of the system and was therefore invalid. As such, the notification made by EN #51846 for a valid actuation of a specified system is hereby retracted. In addition, an editorial change to the first sentence of the original notification description is hereby made. The first sentence is revised to read as follows: At 2303 EDT on April 2, 2016, with the plant shut down and all control rods inserted into the reactor, while attempting to reset the reactor trip breakers to support outage activities (reset of the main turbine), the reactor trip breakers reopened. The NRC Resident Inspector will be notified. Notified the R4DO (Kellar).

Reactor Coolant System
Reactor Protection System
Main Turbine
Control Rod
ENS 5130811 August 2015 06:39:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip After an Offsite Electrical FaultReactor trip caused by turbine trip. Turbine tripped immediately following the trip of one of four 345KV offsite lines. The reason for protective relaying not preventing the grid disturbance from tripping the turbine generator is not known at this time. All normal offsite and onsite power sources are available. Auxiliary Feedwater actuated as expected on low steam generator level following the trip from 100% power. All systems functioned as expected in response to the trip. The NRC Senior Resident Inspector has been notified. An electrical fault on a 345 kV line 2 miles from the site caused the bus to strip and reclose, which cleared the fault. All control rods fully inserted and the plant is in its normal shutdown electrical lineup.Steam Generator
Auxiliary Feedwater
Control Rod
05000483/LER-2015-004
Auxiliary Feedwater Control Valve Inoperable Due To Faulty Electronic Positioner Card
ENS 5125723 July 2015 18:57:0010 CFR 50.72(b)(3)(iv)(A), System ActuationAuxiliary Feedwater Manual Start Due to Loss of Main Feedwater Pump During Plant CooldownDuring plant cooldown in response to conditions reported to the NRC in Event Notification 51253, Callaway was in Mode 3 (Hot Standby) and on the way to Mode 5 (Cold Shutdown). In accordance with cooldown procedures, Callaway was operating with one Main Feedwater Pump when the pump speed unexpectedly lowered to 0 RPM. The pump was manually tripped in response to the condition. This led to a decrease in water level in the steam generators. In response, operators manually activated the Auxiliary Feedwater System. All systems and components functioned normally in response to the event, and plant operators are currently continuing the controlled shutdown from Mode 3 to Mode 5. Safety related buses are receiving normal off-site power and the grid is currently stable. The NRC Resident Inspector was notified.Steam Generator
Feedwater
Auxiliary Feedwater
ENS 506503 December 2014 06:22:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Turbine TripAn unexpected main turbine trip causing a reactor trip occurred on 12/03/2014 (at 0022 CST) with the plant operating in Mode 1 at 100 percent power. As part of the plant design, an expected, valid actuation of the Auxiliary Feedwater System occurred in response to the reactor trip. As part of the Auxiliary Feedwater actuation, the 'B' Motor Driven Auxiliary Feedwater Pump to 'D' Steam Generator throttle valve did not throttle as expected and was manually isolated. All other systems functioned normally in response to the plant conditions. The plant is currently stable in Mode 3 at 0 percent power. Safety related buses are receiving normal off-site power and the grid is currently stable. The NRC Resident Inspector was notified. All control rods fully inserted on the reactor trip. Steam generator levels are being maintained by the AFW system and decay heat is being removed by the main condenser. No primary or secondary safety relief valves lifted during the transient.Steam Generator
Auxiliary Feedwater
Safety Relief Valve
Main Condenser
Control Rod
ENS 4921927 July 2013 04:49:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Unusual Event Declared Due to a Fire in the Turbine Building Lasting Greater than 15 Minutes

On July 26, 2013, at 2349 CDT, the Callaway nuclear power plant declared an Unusual Event due to a fire not extinguished within 15 minutes of control room notification, EAL HU 2.1. The fire was located in the turbine building near the main generator. Concurrent with the fire, the reactor tripped due to a turbine trip. All control rods fully inserted and all reactor coolant pumps (RCPs) tripped. The fire has been extinguished and the licensee is in progress of restoring RCPs. The licensee notified the NRC Resident Inspector, State Emergency Management Agency and Local Authorities. Notified DHS SWO, FEMA, and DHS NICC.

  • * * UPDATE ON 7/27/13 AT 0201 EDT FROM MARK COVEY TO BILL HUFFMAN * * *

The licensee terminated the Unusual Event at 0101 CDT. Decay heat is being removed via aux feed water from the steam generators to the condenser. Visual inspection determined the location of the fire to be in the phase B generator bus duct. Notified R4DO (Allen), NRR EO (Monninger), IRD (Marshall), DHS SWO, FEMA, and DHS NICC.

  • * * UPDATE ON 7/27/13 AT 0430 EDT FROM MARK COVEY TO DONG PARK * * *

The licensee made notifications under 10CFR50.72(b)(2)(iv)(B) (RPS Actuation), 10CFR50.72(b)(2)(xi) (Offsite Notification) and 10CFR50.72(b)(3)(iv)(A) (ESF Actuation - AFW). The licensee will be making a press release and notifying the NRC Resident Inspector. Notified R4DO (Allen).

  • * * UPDATE ON 7/27/13 AT 0826 EDT FROM MARK COVEY TO BILL HUFFMAN * * *

Upon further review, the licensee believes that the initially reported EAL for the UE notification, HU 2.1, was not applicable. Although indications of a fire were present for greater than 15 minutes, the criteria at Callaway apply to a fire within 50 feet of safety related equipment. There was no safety related equipment within 50 feet of where the fire occurred. The proper EAL classification should have been HU 3.1 due to release of potentially toxic gas or asphyxiant or flammable gas that could impact plant operation. This EAL is applicable due to the heavy smoke release from burning electrical insulation and melted bus and ductwork which prevented access to the turbine building area where the fire took place. The licensee will notify the NRC Resident Inspector of this update. Notified R4DO (Allen).

Steam Generator
Control Rod
05000483/LER-2013-008
ENS 4571520 February 2010 03:45:0010 CFR 50.72(b)(3)(iv)(A), System ActuationSpecified System Actuations Due to Loss of the 'A' Safeguards TransformerAt 2145 CST on 2/19/2010, the Callaway Plant experienced a loss of switchyard bus 'A'. This resulted in a loss of off site power to 'B' train vital 4160 volt bus NB02. Technical specification LCO 3.8.1 was entered. The 'B' train emergency diesel generator started and the shutdown sequencer actuated for bus NB02. 'B' motor driven auxiliary feed water pump, 'B' centrifugal charging pump, and both 'A' and 'B' essential service water pumps started. The turbine driven auxiliary feed water pump actuated, and steam generator blowdown and sample isolation occurred. 'A' train offsite vital power and emergency diesel generator were available. The actuations that occurred were consistent with the loss of one vital AC train. All emergency systems responded as expected with the exception of steam generator blowdown valve BMHV0002 which was manually isolated when it failed to fully close. The loss of switchyard bus 'A' was due to a fault on the 'A' safeguards transformer. The faulted transformer has been isolated, and switchyard bus 'A' was reenergized at 0132 on 2/20/2010. The 'B' train vital 4160 volt bus NB02 was tied to offsite power at 0222 on 2/20/2010, and the 'B' emergency diesel generator was secured at 0233 on 2/20/2010. Technical specification LCO 3.8.1 was exited. Currently the plant is at 100% power. The licensee has notified the NRC Resident Inspector.Steam Generator
Service water
Emergency Diesel Generator
Auxiliary Feedwater
ENS 4471914 December 2008 23:14:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Electrical Fault on an Operating Condensate PumpCallaway Plant was at 98% power with two condensate pumps in service. At 1714 on 12-14-08, the reactor was manually tripped due to a motor ground fault on the 'B' condensate pump. The 'C' condensate pump was not available for service (See EN #44714). This left only one condensate pump available so the reactor was manually tripped. The plant is in mode 3 and stable. Reactor trip procedures have been implemented and exited and normal operating procedures are in progress at this time. All safety systems actuated as designed. All control rods inserted during the trip. Offsite power is available and powering safety loads. There is no primary to secondary leakage. Decay heat is being removed via steam dumps to the condenser with makeup provided by Auxiliary Feedwater to the steam generators. The standby diesel generators and safety systems are available. The NRC Senior Resident Inspector has been notified.Steam Generator
Auxiliary Feedwater
Control Rod
ENS 4471712 December 2008 16:42:0010 CFR 50.72(b)(3)(iv)(A), System ActuationInadvertent Valid Reactor Trip and Feedwater Isolation Signals Due to MaintenanceValid Reactor Trip and Manual Initiation of Auxiliary Feedwater While in MODE 3 At 1042 on 12/12/2008, while in Mode 3, a valid reactor trip signal was generated during I&C maintenance activities on intermediate range nuclear instrument SENI0036. This resulted in a feedwater isolation signal. Reactor Operators manually started both motor driven auxiliary feedwater pumps to maintain steam generator levels. These pumps were started prior to receiving an Auxiliary Feedwater Actuation. Plant is stable in Mode 3. Normal feedwater supply has been restored. The cause of the reactor trip is understood. All systems functioned normally in response to plant conditions. The NRC Resident Inspector has been notified.Steam Generator
Feedwater
Auxiliary Feedwater
ENS 4471412 December 2008 05:01:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to a Feedwater TransientThe 'C' condensate pump tripped due to an electrical problem which caused a feedwater transient. The unit (automatically) tripped on high steam generator level at approximately 2301 CST. The unit is in mode 3 and stable. The reactor trip procedures are in progress at this time. All control rods fully inserted into the core during the reactor trip. Offsite power is available and powering safety loads. The steam generator atmospheric steam dumps lifted momentarily during the transient and reseated. There is no known primary to secondary leakage. Decay heat is being removed via steam dumps to the condenser with makeup provided by auxiliary feedwater to the steam generator. The standby diesel generators and safety systems are available. The licensee notified the NRC Resident Inspector.Steam Generator
Feedwater
Auxiliary Feedwater
Control Rod
ENS 4465212 November 2008 00:46:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to a Feedpump TripAt 1846 the reactor was manually tripped due to 'B' Main Feed Pump (MFP) trip on low lube oil pressure. The plant was operating at 97 percent (power) when annunciation was received that 'B' MFP was experiencing low lube oil pressure. Subsequently the 'B' MFP tripped on low lube oil pressure. The operating crew manually tripped the reactor per procedure OTO-AE-00001. The Auxiliary Feedwater System automatically actuated. All control rods fully inserted during the event and all safety systems responded as designed. The unit is removing decay heat using steam dumps to the Main Condenser. No primary relief valves or Main Steam relief valves lifted during the event. (The licensee is) currently investigating low lube oil pressure on 'B' MFP. Aux Feed is supplying make up to the steam generators. The plant is in normal electrical shutdown line-ups. The licensee notified the NRC Resident Inspector.Steam Generator
Auxiliary Feedwater
Main Condenser
Control Rod
Main Steam
ENS 4456111 October 2008 10:08:0010 CFR 50.72(b)(3)(iv)(A), System ActuationSteam Generator Water Level Trip Actuation Initiated Reactor Trip System

During plant shutdown to begin a scheduled refueling outage, with the plant at 0% power in Mode 3, an actuation of the reactor trip system (RTS) occurred when a steam generator (S/G) Low-Low water level trip inadvertently occurred during recovery from a feedwater isolation actuation that had previously occurred in response to a steam generator high water level trip condition. At approximately 0500 hours, plant operators were closing the main steam isolation valves (MSIVs) for plant shutdown. Once the MSIVs were closed, the reactor coolant system (RCS) cooldown rate decreased significantly. The 'A' atmosphere steam dump valve (ASD) was then opened. Shortly after the ASD was opened, the MSIV was also opened. With both the MSIV and ASD open, however, the 'A' S/G water level swelled until the P-14 S/G Hi Level protective interlock setpoint was reached, resulting in a feedwater isolation (FWIS) actuation at 0505 hours. Subsequent to the FWIS actuation, plant operators took action to recover from the FWIS in accordance with off-normal operating procedure OTO-SA-00001, 'Engineered Safety Feature Actuation Verification and Restoration.' The motor-driven auxiliary feedwater pumps were started to restore S/G water level. However, S/G water level lowered rapidly in response to the cold auxiliary feedwater flow to the S/G. A S/G Low-Low water level trip signal was then reached on the 'A' S/G, thus resulting in a reactor trip system actuation at 0508 hours. All systems functioned normally in response to plant conditions. The NRC Senior Resident Inspector has been informed.

  • * * UPDATE AT 0239 EDT ON 10/12/08 FROM FRED BIANCO TO VINCE KLCO * * *

This report is an update to information reported under ENS notification 44561. The original notification reported a valid reactor trip system actuation as a 4-hour notification under 10CFR50.72(b)(2)(iv)(B). The correct reporting requirement is 10CFR50.72(b)(3)(iv)(A), an 8-hour notification, as the plant was in Mode 4 with the reactor subcritical at the time of the event. The (NRC) Resident Inspector will be notified. Notified R4DO (Powers).

Steam Generator
Reactor Coolant System
Feedwater
Main Steam Isolation Valve
Auxiliary Feedwater
ENS 432279 March 2007 16:43:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip at Reduced Power Due to Inadequate Feedwater Control

At approximately 0803 Central Standard Time (CST) on 3/9/2007, Callaway Plant received indications of a condenser tube leak. At approximately 0826 CST, a power reduction from 100 percent to less than 5 percent was initiated in accordance with the Secondary Water Chemistry Program. At 1043 CST, with the reactor at approximately 30 percent power, a manual reactor trip was initiated due to inadequate feedwater control to the C steam generator. There was indication of feedwater flow to and increasing level in the C steam generator with both the main feedwater reg valve and its bypass valve closed. Cause of the inadequate feedwater control is under investigation. All safety systems functioned as designed with the exception of the digital rod position indication for control rod K10 which failed during the trip due to an existing problem. Control rod K10 is believed to be fully inserted, but is being treated as indeterminate at this time. Main feedwater isolation and motor-driven auxiliary feedwater actuations occurred as expected. Both trains of the emergency diesel generators and the offsite power supplies are available.

Callaway plant is currently stable in Mode 3 at normal reactor coolant system parameters.

This notification is being made in accordance with 10CFR50.72(b)(2)(iv)(B) for manual reactor trip (RPS actuation), 10CFR50.72(b)(2)(xi) for offsite notification and 10CFR50.72(b)(3)(iv)(A) Specified System Actuation. The licensee informed the resident inspector of the event and will be making State notifications. A press release is expected.

  • * * UPDATE ON 03/12/07 AT 2116 EDT FROM S. GANZ TO MACKINNON * * *

Repairs were made to the Digital Rod Position Indication (DRPI) for control rod K10. The cause was determined to be a bent pin on a cable connector. When DRPI was restored, control rod K10 was verified to be fully inserted. Post maintenance testing was completed satisfactorily. The cause of the inadequate feedwater control for the C steam generator was a failure of the positioner for the C main feedwater reg valve. The positioner was replaced and tested satisfactory. The plant is currently in Mode 2 (Startup) The resident inspector was informed of the update. R4DO (Mike Shannon) notified.

Steam Generator
Reactor Coolant System
Feedwater
Emergency Diesel Generator
Auxiliary Feedwater
Control Rod
ENS 426216 June 2006 18:39:0010 CFR 50.72(b)(3)(iv)(A), System ActuationLoss of "a" Train of Offsite Vital Power Due to Relay TestingCallaway plant was in mode 1 at 100 percent power. Work was in progress on calibrating lockout devices on the B switchyard buss. At approximately 1339 CDT during performance of this work, Callaway plant experienced a loss of switchyard buss B. This resulted in loss of A train offsite power, load shed on A train vital 4160 volt buss (NB01), shutdown sequencer actuation for buss NBO1, start on the A train emergency diesel generator, turbine driven auxiliary feedwater pump actuations, (and) steam generator blowdown and sample isolations. B train offsite vital power and both emergency diesel generators were available. These actuations were consistent with loss of 1 vital AC train. Emergency systems responded as expected. As of 1630 CDT, the plant is at 100 percent power. Power has been restored to the B switchyard buss. The normal offsite supply to bus NBO1 has been restored and the diesel generator secured. Determination of the cause of the lockout device actuation is in progress. The licensee notified the NRC Resident Inspector.Steam Generator
Emergency Diesel Generator
Auxiliary Feedwater
ENS 4257112 May 2006 05:53:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip on High Steam Generator LevelWhile lowering turbine load to 45% for planned maintenance to replace an RCS Loop flow transmitter, Callaway Plant experienced high vibration on two main turbine bearings. The main turbine was manually tripped at 0047 in accordance with off-normal procedures. At 0052, received a Steam Generator High-High Level (P-14) on the "A" S/G resulting in a Feed Water Isolation Signal (FWIS) and Auxiliary Feed Water Actuation (AFAS). The reactor was manually tripped at 0053. Emergency Operating Procedures were completed and exited at 0115. After receiving the main turbine high vibration alarm, the plant reduced power to below the reactor trip/turbine trip setpoint and manually tripped the main turbine. Steam generator level rose to the P-14 feedwater isolation setpoint at which time, the reactor was manually tripped. All rods fully inserted on the trip. Decay heat is being removed by condenser steam dumps. Steam generator level is being maintained with the startup feed pump. The electrical grid is stable. No relief valves or safety valves lifted. The cause of the high vibration is being investigated. The licensee notified the NRC Resident Inspector.Steam Generator
Feedwater
Auxiliary Feedwater
Main Turbine
ENS 4154629 March 2005 16:57:0010 CFR 50.72(b)(3)(iv)(A), System ActuationActuation of the Reactor Protection System and Auxiliary Feedwater System While Establishing Initial Conditions for Leak Test in Mode 3.The licensee faxed the following information: On 3/29/05, with the Callaway plant at 0 % power in Mode 3, Steam Generator (S/G) levels were being maintained using 'B' Condensate Pump. Reactor Coolant System (RCS) temperature was being controlled using Condenser Steam Dumps. Preparation was in progress for performance of a leak test on Main Feedwater Isolation Valve AEFV0041. As part of the leak test, condensate flow was temporarily isolated to 'C' S/G and the Auxiliary Feedwater System was aligned to provide water to the 'C' S/G. When low was initiated to 'C' S/G using auxiliary Feedwater, level initially increased due to the injection of a small volume of warm water contained within the Feedwater piping at the S/G, then proceeded to rapidly decrease due to S/G shrink caused by the injection of Auxiliary Feedwater with a temperature of approximately 70 degree F. Level in 'C' S/G decreased until S/G Lo Lo Level reactor trip and Auxiliary Feedwater Actuation signals were generated. Performance of the leak test was terminated and RCS temperature and S/G levels were stabilized at normal parameters for Mode 3. The licensee informed the NRC Resident Inspector.Steam Generator
Reactor Coolant System
Feedwater
Reactor Protection System
Auxiliary Feedwater
ENS 4134719 January 2005 18:51:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Callaway Automatic Reactor Trip on Low Steam Generator LevelUnit experienced an automatic reactor trip following a momentary loss of power to a process control system power supply that resulted in a low Steam Generator water level. This event is being reported in accordance with 10CFR50.72(b)(2)(iv)(B) due to an automatic Reactor Trip and subsequent Aux Feedwater actuation and Feedwater isolation. On 1/19/2005 at 12:51 CST with Callaway plant at 100% reactor power, a Reactor Trip occurred on low Steam Generator 'A' level due to an apparent momentary loss of power in Control Cabinet (Relay Panel) RP043. A failed Primary Power Supply to RP043 replacement was in progress at the time of the trip. A momentary power spike on the in-service backup power supply caused the Main Feedwater Regulating valve (MFRV) 'A' to shut and both Main Feedwater Pumps (MFPs) went to their low speed stops. Attempts by the Reactor Operator to take manual control of 'A' MFRV and the MFPs were unsuccessful resulting in the Reactor Trip. Following the reactor trip all systems responded as designed with no abnormal responses. The plant is currently stable in Mode 3 with RCS pressure at 2237 psig and RCS temperature at 557.8 F. The Auxiliary Feedwater is currently supplying the Steam Generators with steam flow to the Main Condenser for decay heat removal. All control rods fully inserted. Both NRC Resident Inspectors were contacted and responded to the Control Room. Corporate Communications will be providing public information on the plant trip to the media.Steam Generator
Feedwater
Auxiliary Feedwater
Decay Heat Removal
Main Condenser
Control Rod
05000483/LER-2005-001
ENS 4052215 February 2004 21:19:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip with Auxiliary Feedwater Actuation

The following information was received from the licensee via facsimile: At 1519 (CDT) on 2-15-04, the plant was at 20 power, increasing load. During the transfer from the bypass feedwater regulating valves to the main feedwater regulating valves, the main turbine tripped due to a P-14 S/G Hi-Hi level signal. The P-14 signal also caused a Feedwater Isolation Signal (FWIS), which resulted in a Motor Driven Aux Feedwater Actuation (MDAFAS), and Steam Generator Blowdown Isolation Signal. Steam Generator levels subsequently shrunk to low levels causing a Steam Generator low level reactor trip at 1524 (hrs). Sometime after the turbine trip, the turbine driven aux feed pump ((TDAFP)) was manually started to help restore S/G levels. The pump was later manually secured, but then received a subsequent auto-start signal and tripped on overspeed. The TDAFP was declared inoperable at 1535 (hrs). With the exception of the TDAFP, all safety systems operated properly. The plant is currently stable in Mode 3, with the primary plant at 557 deg F and 2235 psig, and pressurizer level at 25%. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE AT 0031 EST ON 2/16/04 HOPE BRADLEY TO GOTT * * *

The following information was received from the licensee via facsimile as a "rewrite of above paragraph 2. Sometime after the turbine trip, the Turbine Driven Aux Feedwater Pump (TDAFP) was manually started to help restore S/G levels. Due to decreasing reactor coolant system (RCS) temperature, it was decided to stop the TDAFP since it is a steam load. The steam supply valves were remote manually closed from the control room. At the same time the steam supply valves were closing, the steam generator levels shrunk to low levels causing a Steam Generator low level reactor trip and Turbine Driven Aux Feedwater Actuation (TDAFAS) at 1524. The steam supply valves immediately reopened due to the TDAFAS. It is postulated that this transient in the steam supply caused the pump to overspeed trip. The TDAFP was declared inoperable at 1535. With the exception of the TDAFP, all safety systems operated properly. The licensee notified the NRC Resident Inspector. Notified R4DO (Cain).

Steam Generator
Reactor Coolant System
Feedwater
Auxiliary Feedwater
Main Turbine
ENS 4051512 February 2004 04:58:0010 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Eccs Actuation During Rcs HeatupAt 2258 (CST) on 02/11/04, Callaway Plant was performing a heat up of the Reactor Coolant System in Mode 3 using plant procedure, OTG-ZZ-00001. When performing Section 6.4 of OTG-ZZ-00001, a Steam Line Pressure Safety Injection was initiated due to the automatic resetting of permissive P-11 at 1970 psig Reactor Coolant System pressure with steam line press less than 615 psig. Actual steam pressure was approximately 600 psig, 15 psig below the Steam Line Pressure Safety Injection set point. As a result of the Safety Injection (signal), the following safety related systems actuated: Safety Injection, Residual Heat Removal, Auxiliary Feedwater, Essential Service Water, and both of the Emergency Diesel Generators. During the injection phase, Pressurizer water level increased to approximately 98 percent and pressurizer pressure increased above the Pressurizer Power Operated Relief Valve (PORV) set point causing the PORVs to operate. During the operation of the PORVs, an open alarm for a Pressurizer Safety Relief Valve actuated, however, there are no indications that this valve actually opened. Initial indications are that a valve position limit switch has malfunctioned. All systems responded as expected during the event with the exception of the above mention Pressurizer Safety valve position indication problem and one Steam Generator Atmospheric Safety Valve that would not operate properly in Manual. At present, the plant is being stabilized using plant procedures. Both Emergency Diesel Generators are in standby and the primary system is at 500 degrees F and 1900 psig with Pressurizer level at 25%. The licensee notified the NRC Resident Inspector.Steam Generator
Reactor Coolant System
Service water
Emergency Diesel Generator
Auxiliary Feedwater
Residual Heat Removal
Safety Relief Valve
05000483/LER-2004-004
ENS 405003 February 2004 10:39:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Main Genrator Output Breakers Opening.

AT 0439, 02/03/04, Callaway Plant experienced a reactor trip while operating transmission breakers located in the plant switchyard. Auxiliary feedwater actuated as expected to stabilize steam generator water levels. All other plant systems responded as expected. At present, the cause of the reactor trip is undetermined. Initial indications are that there were no voltage or frequency perturbations on the electrical grid. Plant staff is investigating potential areas in an effort to identify the cause of the trip. The main generator output breakers opened when one of the transmission breakers in the switchyard was opened per the scheduled maintenance test. When the incoming Transmission line breaker was opened it should not have caused the main generator output breakers to open. All rods fully inserted into the core. Both Motor Driven Auxiliary Feedwater pumps automatically started on a loss of both main feedwater pumps and the Turbine Driven Auxiliary Feedwater pump started on low low steam generator water level. The "C" Steam Generator atmospheric steam dump valve opened for about 17 seconds before it closed (no leaking steam generator tubes in the "C" Steam Generator). All Emergency Core Cooling systems are fully operable except for the "A" Safety Injection System. It was declared inoperable when it failed a valve test last night at 0205 CST. All Emergency Diesel Generators are fully operable.

  Turbine Driven Auxiliary Feedwater Pump discharge valves were closed after it had operator for about two hours.  Approximately one hour after the valves were closed the Turbine Driven Auxiliary Feedwater pump tripped. This incident is being investigated.  

The NRC Resident Inspector was notified of this event by the licensee.

Steam Generator
Feedwater
Emergency Diesel Generator
Auxiliary Feedwater
Emergency Core Cooling System
ENS 4048427 January 2004 23:30:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Reactor Trip

At 1730, 1/27/04, Callaway Plant experienced a reactor trip. Auxiliary feedwater actuated as expected to stabilize steam generator levels. All other plant systems responded as expected. At present the cause of the reactor trip is undetermined. Initial indications are that there were no voltage or frequency perturbations on the electrical grid and that the trip signal originated from Callaway's switchyard breaker circuitry. Plant staff is currently engaged in a review of all indications that occurred at the time of the trip and systematically investigating potential problem areas in an effort to identify the cause of the trip. The licensee also reported that all control rods inserted on the reactor trip, no primary or secondary system relief valves operated, and that reactor temperature is being maintained using steam dump to the condenser. Steam generator water levels are being maintained using auxiliary feedwater. The station electrical system is available and in a normal configuration. The licensee notified the NRC Resident Inspector.

  • * * UPDATE 0250 EST ON 1/28/04 FROM EURMAN HENSON TO S. SANDIN * * *

The licensee provided the following information as an update to their initial report: The cause of the reactor trip has been identified as a failed electrical relay in the main generator protection circuitry. The relay is designed to sense a fault in the main electrical generator and trip the generator output breakers. The failed relay was designated as a 321/G relay and provides phase fault backup protection to prevent exceeding thermal limits of the stator windings. After determining the cause of the reactor trip, preparations for a reactor startup are in progress. The licensee will inform the NRC Resident Inspector. Notified R4DO(Johnson).

Steam Generator
Auxiliary Feedwater
Control Rod
ENS 4031712 November 2003 20:21:0010 CFR 50.72(b)(3)(iv)(A), System ActuationInadvertent Actuation of Essential Service Water SystemOn 11/12/03, Callaway Plant was restoring normal electrical power to electrical bus PB122 in the Circulating and Service Water Pumphouse. While attempting to restore the normal electrical power source to bus PB122, a Reactor Operator operated an incorrect switch. As a result of the incorrect switch operation, two other electrical feeder breakers opened and de-energized electrical busses PB121 and PB122. This resulted in a loss of the normal service water system which supplies cooling water to both safety related and non-safety related loads during normal operation. At 1421, operators manually initiated operation of the Essential Service Water system to restore cooling water to safety related loads. As a result of the loss of normal cooling water to non-safety related loads, a turbine runback occurred and power was stabilized at 68% reactor power. Initial plans are to perform inspections of affected electrical breakers plus circulating water and service water pumps. These inspections will not prevent a return to normal power. Essential Service Water is an alternate source of emergency feedwater but in this instance, it was actuated to supply cooling water to safety related loads, not to supply emergency feedwater. This event is voluntarily being reported as an 8-hour ENS call for a valid actuation of an emergency feedwater system. The licensee notified the NRC Resident Inspector.Feedwater
Service water