ENS 54069
ENS Event | |
---|---|
04:03 May 17, 2019 | |
Title | En Revision Imported Date 6/6/2019 |
Event Description | EN Revision Text: REACTOR TRIP DUE TO SOURCE RANGE HI FLUX SIGNAL
This is an 8-hour, non-emergency notification for a valid reactor trip signal with the reactor not critical, and a valid auxiliary feedwater system actuation in accordance with 10 CFR 50.72(b)(3)(iv)(A) - Valid System Actuation. At 2303 [CDT] on May 16, 2019, the plant was administratively in mode 2 due to withdrawing control rods for startup following refuel. The reactor had not been declared critical. The P-6 permissive at 10E-10 Amps was met for one of two Intermediate Range detectors allowing for block of the Source Range high flux trip (1E5CPS). Prior to performing the block, the Source Range high flux trip setpoint was exceeded and a reactor trip received. All systems responded as expected. A feedwater isolation signal was received due to the reactor trip with feedwater temperature less than 564 degrees Fahrenheit. Auxiliary feedwater was started to maintain steam generator levels. The plant is being maintained stable in mode 3 with no complications. The NRC Resident Inspector was present during the startup and was notified of the reactor trip.
A correction is being made for the sixth sentence in the second paragraph above, which states, 'A Feedwater Isolation signal was received due to the reactor trip with feedwater temperature less than 564 degrees Fahrenheit.' Within this sentence, 'feedwater temperature' is to be replaced with 'reactor coolant system temperature.' The licensee has notified the NRC Senior Resident Inspector. |
Where | |
---|---|
Callaway ![]() Missouri (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-0.47 h-0.0196 days <br />-0.0028 weeks <br />-6.43806e-4 months <br />) | |
Opened: | Jeff Gulick 03:35 May 17, 2019 |
NRC Officer: | Joanna Bridge |
Last Updated: | Jun 5, 2019 |
54069 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 54069\u003C/a\u003E - \u003Ca href=\"/Callaway\" title=\"Callaway\"\u003ECallaway\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EEn Revision Imported Date 6/6/2019\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 54069 - Callaway\n","link":"","lat":38.76076111111111,"lon":-91.78175833333333,"icon":"/w/images/0/06/Ameren_icon.png"}],"imageoverlays":null} | |
Unit 1 | |
---|---|
Reactor critical | Not Critical |
Scram | A/R |
Before | Startup (0 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 570432024-03-22T01:56:00022 March 2024 01:56:00
[Table view]10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Turbine Driven Auxiliary Feedwater Pump Actuation ENS 569682024-02-15T08:47:00015 February 2024 08:47:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Turbine Trip/Reactor Trip ENS 556982022-01-07T18:23:0007 January 2022 18:23:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Turbine Trip / Reactor Trip ENS 540692019-05-17T04:03:00017 May 2019 04:03:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation En Revision Imported Date 6/6/2019 ENS 540052019-04-17T06:37:00017 April 2019 06:37:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Undervoltage to a Safety Related Bus Resulting in Valid System Actuation ENS 518462016-04-03T04:02:0003 April 2016 04:02:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Protection System Actuation While Reactor Shutdown ENS 513082015-08-11T06:39:00011 August 2015 06:39:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip After an Offsite Electrical Fault ENS 512572015-07-23T18:57:00023 July 2015 18:57:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Auxiliary Feedwater Manual Start Due to Loss of Main Feedwater Pump During Plant Cooldown ENS 506502014-12-03T06:22:0003 December 2014 06:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip ENS 492192013-07-27T04:49:00027 July 2013 04:49:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to a Fire in the Turbine Building Lasting Greater than 15 Minutes ENS 457152010-02-20T03:45:00020 February 2010 03:45:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Specified System Actuations Due to Loss of the 'A' Safeguards Transformer ENS 447192008-12-14T23:14:00014 December 2008 23:14:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Electrical Fault on an Operating Condensate Pump ENS 447172008-12-12T16:42:00012 December 2008 16:42:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Inadvertent Valid Reactor Trip and Feedwater Isolation Signals Due to Maintenance ENS 447142008-12-12T05:01:00012 December 2008 05:01:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a Feedwater Transient ENS 446522008-11-12T00:46:00012 November 2008 00:46:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to a Feedpump Trip ENS 445612008-10-11T10:08:00011 October 2008 10:08:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Steam Generator Water Level Trip Actuation Initiated Reactor Trip System ENS 432272007-03-09T16:43:0009 March 2007 16:43:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip at Reduced Power Due to Inadequate Feedwater Control ENS 426212006-06-06T18:39:0006 June 2006 18:39:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of "a" Train of Offsite Vital Power Due to Relay Testing ENS 425712006-05-12T05:53:00012 May 2006 05:53:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip on High Steam Generator Level ENS 415462005-03-29T16:57:00029 March 2005 16:57:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuation of the Reactor Protection System and Auxiliary Feedwater System While Establishing Initial Conditions for Leak Test in Mode 3. ENS 413472005-01-19T18:51:00019 January 2005 18:51:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Callaway Automatic Reactor Trip on Low Steam Generator Level ENS 405222004-02-15T21:19:00015 February 2004 21:19:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip with Auxiliary Feedwater Actuation ENS 405152004-02-12T04:58:00012 February 2004 04:58:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Eccs Actuation During Rcs Heatup ENS 405002004-02-03T10:39:0003 February 2004 10:39:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Main Genrator Output Breakers Opening. ENS 403172003-11-12T20:21:00012 November 2003 20:21:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Inadvertent Actuation of Essential Service Water System 2024-03-22T01:56:00 | |