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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 571075 May 2024 08:38:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Lowering Steam Generator Water LevelThe following information was provided by the licensee via email and phone: At 0338 CDT, with the unit 1 in mode 1 at 6 percent power, the reactor automatically tripped due to lowering steam generator water level. The trip was uncomplicated with all systems responding normally post-trip. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for an actuation of the auxiliary feedwater system. Operations responded using procedure 1BwEP-0 and stabilized the plant in mode 3. Decay heat is removed by steam dumps via the main condenser. 1A and 1B auxiliary feedwater pumps were actuated manually prior to the reactor trip in an attempt to restore steam generator water level. Unit 2 is not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.Steam Generator
Reactor Protection System
Auxiliary Feedwater
Main Condenser
ENS 563526 February 2023 11:30:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Communications and Assessment CapabilitiesThe following information was provided by the licensee via email: On 02/06/2023 at 0416 EST, the Constellation Emergency Response Organization (ERO) Notification Database System uploaded data files into the Mass Notification System (Everbridge) which is used to notify ERO personnel when activated. At 0630, the individual reviewing the uploaded files discovered that the data files did not upload properly and that Everbridge may not notify all ERO individuals within the required 10 minutes of system initiation. Constellation resolved the issue by 0752. During the time period of 0416 to 0752, control room operators would have been unaware that the ERO notification was not successful. Therefore, this issue constitutes a loss of offsite communications capability and is reportable under 10 CFR 50.72(b)(3)(xiii), 'The licensee shall notify the NRC as soon as practical and in all cases within eight hours of the occurrence of any event that results in a major loss of emergency assessment capability, offsite response capability, or offsite communications capability (e.g., significant portion of control room indication, Emergency Notification System, or offsite notification system).' This loss of offsite communications capability affected all Constellation nuclear stations. There was no impact on the health and safety of the public or plant personnel. Each affected station NRC Resident Inspectors have been or will be notified.
ENS 5532524 June 2021 14:01:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Technical Support Center CapabilityThis is an eight-hour, non-emergency notification for a loss of Emergency Assessment Capability. This event is reportable in accordance with 10 CFR 50.72(b)(3)(xiii) because the Technical Support Center (TSC) supply fan belt had failed, which affects the functionality of an emergency response facility. Corrective maintenance activities will be performed to restore functionality. The work includes replacing the failed belt and restarting the TSC supply fan. The work duration is approximately 8 hours. If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing emergency planning procedures unless the TSC becomes uninhabitable due to ambient temperature, radiological, or other conditions. If relocation of the TSC becomes necessary, the Emergency Director will relocate the TSC staff to an alternate location in accordance with applicable site procedures. (The Emergency Response Organization team has been notified of the maintenance and the possible need to relocate during an emergency.) There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector and Illinois Emergency Management Agency have been notified.
ENS 5532021 June 2021 05:51:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationReactor Trip on Generator Lockout Relay TripAt 0051 CDT Braidwood Unit 1 experienced an automatic reactor trip due to a generator lockout relay trip and subsequent turbine trip and reactor trip. The cause of the generator lockout relay trip is unknown at this time and is under investigation. Numerous lightning strikes were present in the area during the time of the generator lockout relay trip. Both trains of auxiliary feedwater started automatically following the reactor trip to maintain steam generator water levels. All systems responded as expected with the exception of failure of source range nuclear instruments to automatically re-energize following the reactor trip. Both source range nuclear instruments were manually energized in accordance with station procedures. The main steam dump valves are in service to the main condenser to provide heat sink cooling. The plant is being maintained at normal operating pressure and temperature. AC power is being provided by Offsite Power with the 1B Diesel Generator in standby. 1A Diesel Generator is out of service for planned maintenance. All other safety systems are available. There is no impact to Unit 2. This report is being made per 10 CFR 50.72(b)(2)(iv)(B) for a RPS actuation, 4 hr. notification, and per 10 CFR 50.72(b)(3)(iv)(A) for an automatic actuation of the Auxiliary Feedwater system, 8 hr. notification. The NRC Resident Inspector and Illinois Emergency Management Agency have been informed.Steam Generator
Auxiliary Feedwater
Main Condenser
Main Steam
ENS 5428923 September 2019 16:06:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Lowering Steam Generator Levels

At 1106 CDT Braidwood Unit 1 experienced an automatic reactor trip due to lowering steam generator water levels following closure of the 1B steam generator feed water regulating valve.

The cause of the 1B steam generator feedwater regulating valve failing closed is unknown at this time and is under investigation.

Both trains of auxiliary feedwater started automatically following the reactor trip to maintain steam generator water levels.

All systems responded as expected with the exception of intermediate range nuclear instrument N-36 which was identified as being undercompensated following the reactor trip. Both source range nuclear instruments were manually energized in accordance with station procedures. Steam generator power operated relief valves lifted momentarily and reseated as designed in response to the secondary transient due to the reactor trip. The main steam dump valves are in service to the main condenser to provide heat sink cooling. The plant is being maintained at normal operating pressure and temperature. AC power is being provided by offsite power with the diesel generators in stand by and all safety systems available. There is no impact to Unit 2. This report is being made per 10 CFR 50.72(b)(2)(iv)(B) for a RPS actuation, 4 hour notification, and per 10 CFR 50.72(b)(3)(iv)(A) for an automatic actuation of the auxiliary feedwater system, 8 hour notification. The NRC Resident Inspector has been informed.

Steam Generator
Feedwater
Auxiliary Feedwater
Main Condenser
Main Steam
ENS 5409026 May 2019 00:30:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Main Control Room Area Radiation MonitorsAt 1930 (CDT) on 5/25/2019, communications were lost with the main control room area radiation monitors. These detectors are used to determine if an emergency action level (EAL) has been reached for initiating condition RA3 (Radiation levels that impede access to equipment necessary for normal plant operations, cooldown, or shutdown). This unplanned loss of the ability to evaluate an EAL for initiating condition RA3 is considered a loss of emergency classification capability and is reportable as a Major Loss of Emergency Preparedness Capabilities per 10 CFR 50.72(b)(3)(xiii). This is an 8-hour reportable notification. Portable area radiation monitors have been established as a compensatory measure per station procedures. The NRC Resident Inspector has been notified.
ENS 534434 June 2018 14:20:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip on Lowering Steam Generator Water LevelAt 0920 CDT, Braidwood Unit 1 reactor was manually tripped due to lowering steam generator water levels following a trip of the 1C main feedwater pump. The cause of the 1C main feedwater pump trip is unknown at this time and is under investigation. Both trains of Braidwood Unit 1 auxiliary feedwater started automatically following the reactor trip to maintain steam generator water levels. All systems responded as expected. Steam generator power operated relief valves lifted momentarily and reseated as designed in response to the secondary transient due to the reactor trip. The main steam dump valves are in service to the main condenser to provide heat sink cooling. The plant is being maintained at normal operating pressure and temperature. AC power is being provided by offsite power with the diesel generators in standby and all safety systems available. There is no impact to Unit 2. This report is being made per 10CFR50.72(b)(2)(iv)(B) for a RPS actuation, 4-hr. notification, and per 10CFR50.72(b)(3)(iv)(A) for an automatic actuation of the auxiliary feedwater system, 8-hr. notification. All rods inserted into the core during the trip. Concerning the relief valves momentarily lifting and reseating, there is no known primary-to-secondary leakage. The licensee has notified the NRC Resident Inspector.Steam Generator
Feedwater
Auxiliary Feedwater
Main Condenser
Main Steam
ENS 5337130 April 2018 16:24:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Following Turbine TripAt 1124 CDT, Braidwood Unit 1 experienced an automatic Reactor Trip. The cause of the Reactor Trip was a Turbine Trip with reactor power greater than P-8. The turbine trip was actuated as a result of a Turbine Motoring Generator Trip. The cause of the generator trip is unknown at this time and is under investigation. After the Reactor Trip occurred, the 1A Auxiliary Feedwater pump was manually started to provide feedwater flow to all four steam generators. The 1A Auxiliary Feedwater pump was subsequently secured and placed in standby when the Startup Feedwater pump was placed in service. Train A Main Control Room Ventilation Filtration system shifted to Makeup Mode due to a spurious actuation signal. No secondary relief valves lifted and no secondary steam was released as a result of the Reactor Trip. The Main Steam dump valves are in service to the Main Condenser to provide heat sink cooling. The plant is being maintained at normal operating pressure and temperature. AC power is being provided by Offsite Power with the Diesel Generators in standby and all safety systems available. There is no impact to Unit 2. This report is being made per 10 CFR 50.72(b)(2)(iv)(B) for a RPS actuation, 4-hr notification, and per 10 CFR 50.72(b)(3)(iv)(A) for a manual actuation of the Auxiliary Feedwater system, 8-hr notification. The licensee notified the NRC Resident Inspector and Illinois Emergency Management Agency.Steam Generator
Feedwater
Auxiliary Feedwater
Main Condenser
Main Steam
ENS 5335822 April 2018 21:46:0010 CFR 50.72(b)(3)(iv)(A), System ActuationUndervoltage Actuation of the Engineered Safety Feature BusOn Sunday, April 22, 2018 at 1646 CDT, a valid actuation of Engineered Safety Feature (ESF) Bus 141 Undervoltage (UV) Relay occurred. At the time, Braidwood Station Unit 1 was performing a pre-planned 1A Diesel Generator (DG) Emergency Core Cooling System (ECCS) Actuation Surveillance, initiating the 1A DG to emergency start and sequence loads on a safety injection signal. Following the 1A DG solely supplying electrical power to Bus 141, the 1A DG lost voltage, resulting in an unplanned UV actuation of ESF Bus 141. The 1A DG output breaker was manually opened and local emergency stop of the 1A DG was attempted. The 1A DG continued to run at idle. Fuel supply was secured to the 1A DG and the engine stopped. Subsequently, operators restored power to ESF Bus 141 from the Unit 1 Offsite Power Source. Shutdown cooling was maintained throughout the event as the 1B Residual Heat Removal train was unaffected by the actuation. This event is reportable under 10 CFR 50.72(b)(3)(iv)(A) for 'Any event or condition that results in valid actuation of any of the systems listed...', specifically 10 CFR 50.72(b)(3)(iv)(B)(8) for the 'Emergency ac electrical power systems, including: emergency diesel generators (EDGs)...'. The licensee notified the NRC resident inspector.Emergency Diesel Generator
Shutdown Cooling
Residual Heat Removal
Emergency Core Cooling System
ENS 5334719 April 2018 16:52:0010 CFR 50.72(b)(3)(iv)(A), System ActuationUndervoltage Actuation of the Engineered Safety Feature BusOn Thursday, April 19, 2018 at 1152 CDT, a valid actuation of Engineered Safety Feature (ESF) Bus 141 Undervoltage (UV) Relay occurred. At the time, Braidwood Station Unit 1 was performing a pre-planned Bus 141 Undervoltage Actuation Surveillance, initiating the 1A Emergency Diesel Generator (EDG) to emergency start and sequence loads on the UV signal. Following the 1A EDG solely supplying electrical power to Bus 141, the EDG lost voltage resulting in an unplanned UV actuation of the ESF Bus 141. Subsequently, operators restored power to ESF Bus 141 via crosstie of the Unit 2 offsite power source. Shutdown cooling was maintained throughout the event as the 1B Residual Heat Removal train was unaffected by the actuation. This event is reportable under 10 CFR 50.72(b)(3)(iv)(A) for 'Any event or condition that results in valid actuation of any of the systems listed...', specifically 10 CFR 50.72(b)(3)(iv)(B)(8) for the 'Emergency ac electrical power systems, including: emergency diesel generators (EDGs)...'. The licensee notified the NRC Resident Inspector.Emergency Diesel Generator
Shutdown Cooling
Residual Heat Removal
ENS 5318023 January 2018 10:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Assessment Capability Due to Technical Support Center Planned Maintenance

At 0400 (CST) on 1/23/2018 the Braidwood Technical Support Center (TSC) HVAC (Heating, Ventilation and Air Conditioning) Emergency Makeup Air Filter train was taken out of service to perform a planned Makeup Air Filter charcoal replacement. The TSC HVAC Makeup Air Filter train will be rendered nonfunctional during the charcoal replacement. Subsequent charcoal and HEPA filter testing will restore functionality of the TSC HVAC Makeup Air Filter train. The expected duration of the charcoal replacement and subsequent testing is 30 hours. If an emergency is declared requiring TSC activation during the time TSC HVAC is non-functional, the TSC will be staffed and activated using existing emergency planning procedure unless the TSC becomes uninhabitable due to ambient temperature, radiological, or other conditions. If relocation of the TSC becomes necessary, the Emergency Director will relocate the TSC staff to an alternate location in accordance with applicable site procedures. This notification is being made in accordance with 10 CFR 50.72(b)(3)(xiii) due to a major loss of emergency preparedness capability. An update will be provided once the TSC HVAC Emergency Makeup Air Filter train functionality has been restored. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE AT 1645 EST ON 01/26/2018 FROM PAUL ARTUSA TO JEFF HERRERA * * *

On 1/26/18 at time 1539 EST, the TSC HVAC Emergency Makeup Air Filter train was returned to service following the planned Makeup Alr Filter charcoal replacement. Functionality was verified by charcoal and HEPA filter post maintenance testing. The licensee has notified the NRC Resident Inspector. Notified the R3DO (Cameron).

HVAC
ENS 5210318 July 2016 20:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Offsite Communications CapabilityLoss of the Offsite Emergency Response Organization (ERO) notification system (Everbridge) identified the system cannot notify all ERO individuals. This constitutes a loss of offsite communications capability. The Offsite ERO notification system (Everbridge) capability loss of Braidwood was identified at approximately 1500 CDT on July 18, 2016, due to an undetermined loss of system communications, which is currently being investigated. The Offsite ERO notification system (Everbridge) capability loss for the common Emergency Response Facility (ERF) (Emergency Offsite Facility (EOF) at Cantera) was identified at approximately 1500 CDT on July 18, 2016. The issue has subsequently been reported resolved by the vendor at 1912 CDT and site testing has verified resolution at 2108 CDT. The onsite communication system was not affected. This event is reportable under 10 CFR 50.72(b)(3)(xiii) as a loss of communications capability. The NRC Resident Inspector has been notified.
ENS 514505 October 2015 06:05:0010 CFR 50.72(b)(3)(iv)(A), System ActuationSpecified System ActuationsBraidwood Unit 2 was performing a planned plant shutdown for refueling outage A2R18. In accordance with plant shutdown procedures while in Mode 1 (Power Operations) at approximately 15% power, operators attempted to start the Start Up Feedwater (SFWP) pump and the pump immediately tripped on Phase A Overcurrent. The 2A Motor Driven Feedwater pump (MDFWP) was manually started to maintain Steam Generator Water Level during the shutdown and subsequent plant cooldown. While in Mode 3 (Hot Standby) at (550 Degree-F), the 2A MDFWP was manually secured due to pump inboard journal bearing temperature exceeding its (200 Degree-F) operating limit. At 0105 (CDT) an anticipated automatic Auxiliary Feedwater actuation signal was generated on low Steam Generator level (36.3%) and both the 2A and 2B Auxiliary Feedwater pumps (AFP) auto-started. Also at 0105 (CDT) a Reactor Protection System (RPS) Reactor trip signal was received due to low Steam Generator level (36.3%) with the reactor not critical. Both Auxiliary Feedwater trains operated as designed with the Main Steam Dumps in service and the Main Condenser providing the heat sink. All systems operated as designed with the exception of the SFWP and the MDFWP described above. The plant is currently stable in Mode 5 with both AFPs secured. This report is being made per 10 CFR 50.72(b)(3)(iv)(A) for automatic actuation of the (1) RPS Reactor Trip with the reactor not critical and (6) Auxiliary Feedwater System, 8 hour notification. The licensee notified the NRC Resident Inspector.Steam Generator
Feedwater
Reactor Protection System
Auxiliary Feedwater
Main Condenser
Main Steam
05000457/LER-2015-002
ENS 5115415 June 2015 12:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTsc Ventilation to Be Removed from Service for Planned Maintenance

On 6/16/2015, planned preventive maintenance activities (will be) performed on the Braidwood Generating Station Technical Support Center (TSC), Ventilation System. The work will be completed within approximately 48 hours. This activity includes preventative maintenance that requires the TSC ventilation system to be out of service which will render the TSC ventilation system non-functional. If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing emergency planning procedures unless the TSC becomes uninhabitable due to ambient temperature or other conditions. If relocation of the TSC becomes necessary, the Emergency Director will relocate the TSC staff as necessary. This event is reportable per 10 CFR 50.72(b)(3)(xiii) for 'any event that results in a major loss of emergency assessment capability.' The planned maintenance will not be able to restore the TSC condensing unit or ventilation system to service within the facility activation time specified in the emergency plan (1 hour) in the event of an accident. The Emergency Response Organization team has been notified of the maintenance and the possible need to relocate during an emergency. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE AT 1102 EDT ON 6/18/15 FROM DAVID KORTGE TO JEFF HERRERA * * *

Braidwood Generating Station TSC ventilation was restored to available status at 0700 CDT on June 18, 2015. The previously reported system preventative maintenance has been completed. The licensee notified the NRC Resident Inspector. Notified the R3DO (Pelke).

ENS 5109227 May 2015 14:45:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTechnical Support Center Out of Service for Planned Maintenance

On 5/27/15, planned preventive maintenance activities are being performed on the Braidwood Generating Station Technical Support Center (TSC), Ventilation System. The work will be completed within approximately 10 hours. This activity includes preventative maintenance that requires the TSC ventilation system to be out of service which will render the TSC ventilation system non-functional. If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing emergency planning procedures unless the TSC becomes uninhabitable due to ambient temperature or other conditions. If relocation of the TSC becomes necessary, the Emergency Director will relocate the TSC staff as necessary. This event is reportable per 10CFR50.72(b)(3)(xiii) for 'any event that results in a major loss of emergency assessment capability.' The planned maintenance will not be able to restore the TSC condensing unit or ventilation system to service within the facility activation time specified in the emergency plan (1 hour) in the event of an accident. The Emergency Response Organization team has been notified of the maintenance and the possible need to relocate during an emergency. The licensee informed the NRC Resident Inspector.

  • * * UPDATE FROM PETER MOODIE TO VINCE KLCO ON 5/27/2015 AT 2153 EDT * * *

Planned work is complete and the Technical Support Center was restored to service on May 27, 2015 at 1808 CDT. The licensee will notify the NRC Resident Inspector. Notified the R3DO (Lipa).

ENS 509576 April 2015 13:09:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTechnical Support Center Out of Service for Planned Maintenance

On 04/06/2015, planned preventive maintenance activities are being performed on the Braidwood Generating Station Technical Support Center (TSC) Ventilation System. The work will be completed within approximately 42 hours. This activity includes preventive maintenance on the TSC condensing unit which affects the TSC ventilation. During the planned maintenance, the TSC condensing unit will be rendered non-functional. If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing emergency planning procedures unless the TSC becomes uninhabitable due to ambient temperature or other conditions. If relocation of the TSC becomes necessary, the Emergency Director will relocate the TSC staff as necessary. This planned maintenance will not impact the emergency filtration capability of the TSC. This event is reportable per 10CFR50.72(b)(3)(xiii) for 'any event that results in a major loss of emergency assessment capability.' The planned maintenance will not be able to restore the TSC condensing unit to service within the facility activation time specified in the emergency plan (1 hour) in the event of an accident. The Emergency Response Organization team has been notified of the maintenance and the possible need to relocate during an emergency. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE FROM GREG HARNOIS TO JOHN SHOEMAKER AT 1013 EDT ON 4/8/15 * * *

The TSC ventilation system has been restored to normal operation as of 0600 CDT on April 8, 2015. The NRC Resident Inspector has been notified. Notified R3DO (Skokowski).

ENS 5093327 March 2015 14:41:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessSeismic Monitor Not Available for Emergency Plan Assessment

Braidwood Generating Station has completed a review of seismic monitor performance. The emergency preparedness plan requires seismic monitoring instruments to diagnose an earthquake for emergency action levels (EAL) HA4 (natural and destructive phenomena affecting vital areas) or HU4 (natural and destructive phenomena affecting the protected area). Contrary to that requirement, this review identified 5 times in the past 3 years that the seismic monitor was non-functional such that emergency classification at the ALERT or UNUSUAL EVENT level could not be obtained with site instrumentation. The seismic monitor is currently functional; however, the seismic monitor was determined to be non-functional on the following dates:

1. April 24, 2012
2. December 5, 2012
3. December 20, 2012
4. June 17, 2013
5. October 8, 2014

These non-functional conditions of the seismic monitor have been corrected and were entered into the Braidwood Corrective Action Program. While Exelon procedural direction allowed the use of offsite sources to obtain seismic data when the seismic monitor is incapable of assessing emergency plan Emergency Action Levels (EALs), this was not explicitly referenced in the Braidwood approved EALs. The loss of assessment capability is reportable to the NRC within 8 hours of discovery in accordance with 10 CFR 50.72(b)(3)(xiii). This report is required per 10 CFR 50.72(a)(1)(ii) as an event that occurred within 3 years of the date of discovery. Corrective actions are in progress. The licensee has notified the NRC Resident Inspector.

ENS 504316 September 2014 11:13:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTechnical Support Center Air Conditioning Condensing Units Out of ServiceAt 0613 (CDT) on 9/6/2014, Technical Support Center roof mounted condensing units were found tripped by operations personnel. An attempt was made to restart both condensing units, neither condensing unit would restart. This caused a loss of Technical Support Center cooling capability. Technical Support Center Air Handling system is in service and required filtration remains available. Wet bulb temperature of the TSC, taken at 0950 (CDT) is 78.0 degrees F. Corrective action process has been initiated. This event is reportable under 10 CFR 50.72(b)(3)(xiii) as described in NUREG-1022, Rev. 3, since this condition affects an emergency response facility. The NRC Resident Inspector has been notified.
ENS 5039725 August 2014 10:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTechnical Support Center Planned Maintenance

On 8/25/2014, planned preventive maintenance activities are being performed on the Braidwood Generating Station Technical Support Center (TSC) Ventilation System. The work will be completed within approximately 42 hours. This activity includes preventive maintenance on the TSC condensing unit which affects the TSC ventilation. During the planned maintenance, the TSC condensing unit will be rendered non-functional. If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing emergency planning procedures unless the TSC becomes uninhabitable due to ambient temperature or other conditions. If relocation of the TSC becomes necessary, the Emergency Director will relocate the TSC staff as necessary. This planned maintenance will not impact the emergency filtration capability of the TSC. This event is reportable per 10CFR50.72(b)(3)(xiii) for 'any event that results in a major loss of emergency assessment capability.' The planned maintenance will not be able to restore the TSC condensing unit to service within the facility activation time specified in the emergency plan (1 hour) in the event of an accident. The Emergency Response Organization team has been notified of the maintenance and the possible need to relocate during an emergency. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE AT 1526 EDT ON 08/29/14 FROM ANNE MATHEWS TO S. SANDIN * * *

Braidwood Generating Station TSC ventilation was restored to available status at 1200 CDT on August 29th, 2014. The previously reported system preventative maintenance has been completed. The licensee informed the NRC Resident Inspector. Notified R3DO (Stone).

ENS 502471 July 2014 12:15:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessOffsite Alert and Notification System Failure

At approximately 0715 (CDT) on 7/1/2014, during the daily morning test, Braidwood Generating Station experienced Offsite Alert and Notification System (ANS) failure of sirens BD10 and BD13 due to a loss of power to the sirens. Loss of power to the sirens was due to the adverse weather conditions experienced on the evening of 6/30/2014. Siren BD10 provides coverage for 20% of Braidwood's Emergency Planning Zone (EPZ) population and siren BD13 provides coverage for 14.1% of the Braidwood EPZ population. This event is being reported in accordance with 10CFR50.72(b)(3)(viii) for 'any event that results in a major loss of emergency assessment capability, offsite response capability, or offsite communications capability (e.g., significant portion of control room indication, Emergency Notification System, or offsite notification system).' The failure of the sirens resulted in the loss of the capability to alert a large segment of the population in the EPZ (~34%) for more than 1 hour. Per NEI 13-01, Rev 0, a large segment of the population in the EPZ should be taken to mean approximately 25% of the total EPZ population. Immediate actions taken included placing a portable generator online to restore siren BD10 at 1015 CDT on 7/1/2014. ComEd is currently in the area attempting to restore normal power. Proposed long term corrective actions including an upgrade to the sirens to contain a battery backup are being evaluated. The licensee has notified the NRC Resident Inspector. The county emergency managers (for Will County - (for siren) BD10 and Grundy County - (for siren) BD13) are aware of the siren outage and the requirements to initiate mobile route alerting (FEMA approved backup) if required.

  • * * UPDATE FROM MURTAZA ABBAS TO DANIEL MILLS AT 1756 EDT ON 07/02/2014 * * *

Siren BD10 was restored to functional on 7/1/2014 at 1130 CDT. Siren BD13 was restored to functional on 7/2/2014 at 1145 CDT. The NRC Resident Inspector has been notified of this ENS update. Notified R3DO (McCraw)

ENS 501621 June 2014 18:14:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Technical Support Center Cooling CapabilityAt 1314 (CDT) on 6/01/2014, Technical Support Center ventilation alarm was received in the main control room. The Equipment Operator reported that the trouble alarm for the roof mounted condensing units was in alarm and the condensing units were tripped. Upon resetting the alarms the condensing units ran for three to five minutes and tripped again. This caused a loss of Technical Support Center cooling capability. Technical Support Center Air Handling system and filtration remain in operation. The room temperature is being monitored locally. Wet bulb temperature at 1500 (CDT) was reported to be 78.5 deg F. Corrective action process has been initiated. This event is reportable under 10CFR50.72(b)(3)(xiii) as described in NUREG-1022, Rev. 3 since this condition affects an emergency response facility. The licensee has notified the NRC Resident Inspector.
ENS 4972316 October 2013 19:20:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTechnical Support Center Out of ServiceOn 10/16/2013 at 14:20 (CDT), the Technical Support Center (TSC) Emergency Makeup Filter Flow Control Damper (OVV145Y) was discovered degraded and non functional during planned maintenance activities. The degraded damper adversely impacted the TSC ventilation system function. On 10/16/2013 at approximately 15:00 (CDT), administrative actions were developed and briefed to isolate instrument air to the degraded nonfunctional damper OVV 145Y providing the capability to restore TSC Emergency Makeup Filter functionality. Isolating instrument air to the degraded damper places the damper in the failed open position, thereby restoring TSC Emergency Makeup Filter functionality. On 10/16/2013 at 20:25 (CDT), instrument air was isolated to the degraded damper OVV 145Y under administrative controls restoring TSC Emergency Makeup Filter functionality. This action was taken after determining no adverse affects on system operation. On 10/30/2013, degraded damper OVV145Y was repaired, instrument air restored and post maintenance testing completed, thereby restoring the degraded TSC emergency Makeup Filter Unit flow control damper functionality. This event is reportable per 10CFR50.72(b)(3)(xiii) for a major loss of emergency assessment capability because the emergent degraded TSC flow control damper OVV145Y adversely impacted the function of TSC Emergency Makeup Filter and was not restored within the TSC activation time (60 minutes). This event was originally determined not reportable because the capability to restore within the TSC activation time (60 minutes) existed from the time of discovery. Upon further review it was determined to be reportable because the degraded damper 0VV145Y was not restored to service within the TSC activation time (60 minutes). The licensee has notified the NRC Resident Inspector.
ENS 4832821 September 2012 01:35:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTechnical Support Center Ventilation InoperableAt 2035 CDT on 9/20/2012 power was removed from the Technical Support Center ventilation for planned maintenance on the supply breaker and the supply breaker cubicle. At 2109 CDTduring restoration, it was discovered that the breaker for the Technical Support Center ventilation could not be closed. The cause for not being able to close the supply breaker is unknown. Troubleshooting is currently in progress and the Technical Support Center ventilation is expected to be returned to service on 09/21/2012. This event is reportable under 10 CFR 50.72(b)(3)(xiii) as described in NUREG-1022, Rev.2 since this work activity affects an emergency response facility. The licensee has notified the NRC Resident Inspector.
ENS 4784518 April 2012 02:30:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessPlant Process Computer Removed from Service for Planned Replacement

At 2130 (CDT) on April 17, 2012, the Unit 1 Plant Process Computer (PPC) was removed from service for a planned replacement in the current Unit 1 Refueling Outage. The Unit 1 PPC feeds the Safety Parameter Display System (SPDS) used in the Main Control Room (MCR) and the Technical Support Center (TSC). The Unit 1 PPC also feeds the Emergency Response Data System (ERDS). The Unit 1 and Unit 2 PPCs also feed the Plant Parameter Display System (PPDS) used in the MCR, TSC and Emergency Operations Facility (EOF). Meteorological data will remain available in the MCR but not through ERDS for either Unit 1 or Unit 2. The dose assessment program will remain functional as the Unit 2 Plant Process computer will be capable of providing the necessary data through PPDS to run the program. The dose assessment program is not affected by the Unit 1 PPC being out of service. As compensatory measures, a proceduralized backup method to fax or communicate via a phone circuit applicable data to the NRC, TSC, and EOF exists. There is no impact to the Emergency Notification System (ENS) or Health Physics Network (HPN) communication systems. The new Unit 1 PPC is scheduled to be functional on April 21, 2012. However, based on the mode Unit 1 will be in, this will limit the number of points that would provide usable data. The Unit 1 PPC will be tested as mode changes occur. The Unit 1 PPC is planned to be declared functional by Mode 2. A follow-up ENS call will be made once the Unit 1 PPC is declared functional. The loss of SPDS and ERDS is a 'major loss of assessment capability' and is reportable under 10CFR50.72(b)(3)(xiii). The NRC Senior Resident Inspector and the State of Illinois (through the Illinois Emergency Management Agency Resident Inspector) have been notified of this ENS call.

  • * * UPDATE FROM JOE KLEVORN TO JOHN KNOKE AT 1035 EDT ON 05/15/12 * * *

As of 1035 EDT on May 15, 2012, the Unit 1 PPC is considered operational with respect to the Safety Parameter Display System (SPDS), Plant Parameter Display System (PPDS) and Emergency Response Data System (ERDS). Therefore, a Major Loss of Assessment Capability no longer exists on Unit 1. The EP Manager will contact the NRC Computer Center for Unit 1 to ensure the ERDS data is being satisfactorily sent to the NRC. The NRC Resident Inspector and the State of Illinois (through the Illinois Emergency Management Agency Resident Inspector) have been notified of this ENS update. The R3DO (Patty Pelke) has been notified.

Emergency Response Data System
Safety Parameter Display System
ENS 4762226 January 2012 03:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTechnical Support Center Out of Service Due to Planned Maintenance

Planned preventive maintenance activities are being performed on the Braidwood Nuclear Station Technical Support Center (TSC) Ventilation System. These work activities are planned to be performed and completed expeditiously within 8 hours. This maintenance activity includes the performance of preventive maintenance on the TSC outside air supply fan unit which affects the TSC emergency filter train and air handling unit. During a portion of the time these activities are being performed, this equipment will not be available for operation. As such, the TSC Ventilation will be rendered non-functional during the performance of portions of the work activity. If an emergency condition occurs that requires activation of the Technical Support Center, during the time this work activity is being performed, it will take no more than 4 hours to return the equipment back to functional status, dependent on the stage of the work activity at the time an emergency occurs. Plans are to utilize the TSC for any declared emergency during the time this work activity is being performed as long as radiological conditions allow. This event is reportable per 10CFR50.72(b)(3)(xiii) as described in NUREG-1022, Rev. 2 since this work activity affects an emergency response facility for the duration of the maintenance. The licensee notified the NRC Resident Inspector.

  • * * UPDATE AT 1107 EST ON 01/26/12 FROM RICHARD ROWE TO S. SANDIN * * *

Braidwood Nuclear Station TSC ventilation was restored to available status at 0635 CST on January 26, 2012. The previously reported system preventative maintenance has been completed. The licensee notified the NRC Resident Inspector. Notified R3DO (L. Kozak).

ENS 4676619 April 2011 04:09:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessPlant Process Computer Removed from Service for Planned Replacement

At 2309 (CDT) on April 18, 2011, the Unit 2 Plant Process Computer (PPC) was removed from service for planned replacement in the current Unit 2 refueling outage. The Unit 2 PPC feeds the Safety Parameter Display System (SPDS) used in the Main Control Room (MCR) and the Technical Support Center (TSC). The Unit 2 PPC also feeds the Emergency Response Data System (ERDS). The Unit 1 and Unit 2 PPCs also feed the Plant Parameter Display System (PPDS) used in the MCR, TSC and Emergency Operations Facility (EOF). Meteorological data will remain available. The dose assessment program will remain functional as the Unit 1 Plant Process computer will be capable of providing the necessary data through PPDS to run the program. The dose assessment program is not affected by the Unit 2 PPC being out of service. As compensatory measures, the backup method to fax or communicate via a phone circuit applicable data to the NRC, TSC and EOF exists. There is no impact to the Emergency Notification System (ENS) or Health Physics Network (HPN) communications systems. The new Unit 2 PPC is scheduled to be functional on April 23, 2011. However, based on the mode Unit 2 will be in, this will limit the number of points that would provide usable data. The Unit 2 PPC will be tested as mode changes occur. The Unit 2 PPC is planned to be declared functional by Mode 2. A follow-up ENS call will be made once the Unit 2 PPC is declared functional. The loss of SPDS and ERDS is a 'major loss of assessment capability' and is reportable under 10CFR50.72(b)(3)(xiii). The NRC Senior Resident Inspector and the State of Illinois (through the Illinois Emergency Management Agency Resident Inspector) have been notified of this ENS call.

  • * * UPDATE FROM SCOTT BUTLER TO JOE O'HARA AT 0932 ON 5/10/11 * * *

As of 0815 CT on May 10, 2011, the Unit PPC is considered operational with respect to the Safety Parameter Display System (SPDS), Plant Parameter Display System (PPDS) and Emergency Response Data System (ERDS). Therefore, a Major Loss of Assessment Capability no longer exists on Unit 2. The EP Manager will contact the NRC Computer Center today to conduct an ERDS test for Unit 2 to ensure the data is being satisfactorily sent to the NRC. The NRC Resident Inspector and the State of Illinois (through the Illinois Emergency Management Agency Resident Inspector) have been notified of this ENS update. Notified R3DO(Passehl)

Emergency Response Data System
Safety Parameter Display System
ENS 4626220 September 2010 22:04:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripAt 1704 CDT, Braidwood Unit 1 experienced an automatic reactor trip. The reactor trip red first out was Over Temperature Delta Temperature (OTDT). At the time of the reactor trip, the Instrument Maintenance Department was performing a calibration of Power Range Channel N-43 and a calibration of the 1C S/G Narrow Range Level Channel 1L-0538. The cause of the trip is unknown at this time. After the reactor trip occurred, all four Steam Generators reached their Low-2 reactor trip setpoint and Pressurizer pressure reached its low pressure reactor trip setpoint which is an expected response on a trip from full power. Steam Generator levels and Pressurizer pressure have been restored. Both the 1A and 1B Auxiliary Feedwater pumps auto started on the Low-2 Steam Generator levels as expected. All control rods fully inserted into the core. Train B Main Control Room Filtration system shifted to makeup mode and the Train B Fuel Handling Building ventilation shifted to Emergency Mode due to a spurious actuation signal. No secondary relief valves lifted and no secondary steam (was) released as a result of the reactor trip. The Main Steam Dumps are in service to the Main Condenser to provide heat sink cooling. The plant is being maintained at normal operating pressure and temperature. This report is being made per 10CFR50.72(b)(2)(iv)(B) for RPS actuation, 4-hr. notification, and per 10CFR50.72(b)(3)(iv)(A) for automatic actuation of the Auxiliary Feedwater system, 8-hr. notification. AC power is being provided by offsite power with the Diesel Generators in standby and all safety systems available. There is no Unit 2 impact. The licensee notified the NRC Resident Inspector. The licensee also anticipates that there will be a press release issued regarding this event.Steam Generator
Auxiliary Feedwater
Main Condenser
Control Rod
Main Steam
ENS 4617816 August 2010 07:06:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trips at Both UnitsBraidwood Unit 2 automatically tripped at 0206 (CST) due to a turbine generator trip due to generator lockout relay actuation. All systems responded as expected, with the auxiliary feed water pumps starting on Low-2 Steam Generator level. The Unit is stable in Mode 3, all primary systems are stable with the secondary heat sink being maintained via aux feed water and the steam dumps. Offsite power is supplying Unit 2, and both emergency diesel generators are available. Cause of generator lockout is under investigation. Braidwood Unit 1 automatically tripped at 0219 (CST) on a turbine trip caused by a loss of condenser vacuum. All systems responded as expected, with the auxiliary feed water pumps supplying steam generator levels. Secondary heat sink is steam generator PORVs. One steam generator safety valve is not fully seated. No steam generator tube leakage. Cause of the loss of vacuum is under investigation. For both Units all control rods fully inserted. There were no complications during the trip and all systems functioned as required. Offsite power remained available throughout the transient. The licensee notified the NRC resident inspector. Braidwood Unit 1's loss of condenser vacuum was caused by the loss of an electrical bus supplying the circ water pumps. At the time of this report, both plants were in a normal shutdown electrical lineup with the exception of the deenergized bus supplying power to the circ water pumps on Unit 1. The steam generator safety valve that has not fully seated was characterized as weeping a small amount of steam. The licensee is uncertain if the Unit 1 trip is related to the Unit 2 trip.Steam Generator
Emergency Diesel Generator
Auxiliary Feedwater
Control Rod
ENS 4523831 July 2009 02:08:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Unusual Event Declared Due to a Loss of Offsite Power for Greater than 15 Minutes

Unit 2 automatically tripped from 100% reactor power as a result of the over-current trip of the 2C Reactor Coolant Pump. Both station auxiliary transformers on Unit 2 subsequently tripped offline. All control rods fully inserted on the trip. Auxiliary feedwater auto-started and maintained Steam Generator water level. The unit is stable in Mode 3. The Emergency Diesel Generators auto started and loaded supplying both emergency busses with power. All systems functioned as required. There was no affect on Unit 1. The licensee notified the NRC Resident Inspector.

  • * * UPDATE AT 0218 ON 8/2/2009 FROM DEAN YARBROUGH TO MARK ABRAMOVITZ * * *

At 2059 on July 30, 2009, a reactor trip of Unit 2 at Braidwood occurred. A loss of offsite power occurred and an Unusual Event was declared at 2108. NRC Headquarter Operations was notified at 2155 (ENS call # 45238). Power from System Auxiliary Transformer (SAT) (credited offsite power supply) 242-2 was restored to buses 241 and 242 (safety related buses) at 0036 on August 2, 2009. The Unusual Event was terminated at 0036 on August 2, 2009. This call is being made due to the termination of the Unusual Event declared on July 30, 2009. An Event Summary Report is required by Exelon procedures within 24 hours of termination of the Unusual Event and will be communicated to the Headquarter Operations later today. The initial event was the result of the actuation of the SAT sudden pressure relay. When the transformer tripped, a slow automatic bus transfer resulted. When the RCPs (Reactor Coolant Pump) and condensate pumps were reenergized, they tripped on overcurrent causing the reactor trip. The sudden pressure relay has subsequently tripped during testing and may have caused the initial event. The licensee reported no damage to the plant. The licensee notified the NRC Resident Inspector. Notified the R3DO (Daley), IRD (McDermott), NRR (Howe), DHS (An), and FEMA (Biscoe).

  • * * UPDATE AT 1617 ON 8/2/2009 FROM SCOTT BUTLER TO VINCE KLCO * * *

The Event Summary Report was received and documented the following technical conclusions: The Unusual Event declaration was caused by a sudden pressure relay on SAT 242-1 causing a lockout of both SATs followed by a trip of Unit 2 due to the 2C RCP tripping during the automatic bus transfer for bus 258. This led to a loss of offsite power to Unit 2. It is currently unknown why the sudden pressure relay on SAT 242-1 actuated. Troubleshooting on the sudden pressure relay is in progress. The licensee will notify the NRC Resident Inspector. Notified the R3DO (Daley). Notified the IRD (McDermott) and NRR (Howe) via e-mail.

Steam Generator
Emergency Diesel Generator
Auxiliary Feedwater
Control Rod
ENS 4501724 April 2009 16:41:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip During Instrument CalibrationAt 1141 CT, Braidwood Unit 2 experienced an automatic Reactor Trip. The Reactor Trip red first out annunciator was Over Temperature Delta Temperature (OTDT). At the time of the Reactor Trip the Instrument Maintenance Department was performing a scheduled calibration of a Pressurizer Pressure channel (2PT-456) which is in the B loop of reactor protection. During the calibration a spike occurred on the D loop of reactor protection. Specifically, the RCS (Reactor Coolant System) temperature for the D loop. This caused a Reactor Trip on a 2 of 4 coincidence. After the reactor trip occurred, all four steam generators reached their low-2 Reactor Trip setpoints and pressurizer pressure reached its low pressure Reactor Trip setpoint all of which is an expected response on a trip from full power. Steam Generator levels and Pressurizer pressure have been restored. Both the 2A and 2B Auxiliary Feedwater pumps auto started on the low-2 steam generator levels as expected. All control rods fully inserted into the core. No secondary relief valves lifted and no secondary steam released as a result of the Reactor Trip. Steam Generators are now being filled by the 2A Main Feedwater pump and the Auxiliary Feedwater pumps have been placed in standby. The main steam dumps are in service to the main condenser to provide heat sink cooling. The plant is being maintained at normal operating pressure and temperature. This report is being made per 10 CFR 50.72(b)(2)(iv)(B) for RPS actuation, 4 hour notification, and per 10 CFR 50.72(b)(3)(iv)(A) for automatic actuation of the Auxiliary Feedwater System, 8 hour notification. The electrical line up transferred to the normal shutdown configuration with the standby diesel generators and safety systems available. There is no Unit 1 impact. The licensee plans on issuing a press release and has notified the NRC Resident Inspector.Steam Generator
Feedwater
Auxiliary Feedwater
Main Condenser
Control Rod
Main Steam
ENS 4474327 December 2008 20:18:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip as a Result of a Generator TripAt 1418 on 12-27-08 Braidwood Unit 2 experienced an automatic Reactor Trip. The Reactor Trip red first out annunciator was Turb(ine) Trip above P8 Rx Trip. At the time of the trip the Unit Aux Transformer (UAT) 241-1 sudden pressure relay actuated causing a main generator trip which resulted in a main turbine trip which resulted in a Reactor Trip. Also at the same time as the Reactor Trip, the 2C Heater Drain Pump tripped on phase A over current. Damage was subsequently noted on the pump motor terminal box. No fire or smoke was observed at UAT 241-1 or the 2C Heater Drain Pump. After the Reactor Trip occurred, all four steam generators reached their low-2 Reactor Trip setpoints and the pressurizer reached its low pressure Reactor Trip setpoint all of which is an expected response on a trip from full power. Steam generator levels and pressurizer pressure have been restored. Both the 2A and the 2B Auxiliary Feedwater Pumps auto started on the low-2 steam generator levels as expected. All control rods fully inserted into the core. No secondary relief valves lifted and no secondary steam was released as a result of the Reactor Trip. Steam generators are now being filled by the Startup Feedwater Pump and the Auxiliary Feedwater Pumps have been placed in standby. The main steam dumps are in service to the main condenser to provide heat sink cooling. The plant is being maintained at normal operating pressure and temperature. This report is being made per 10CFR 50.72(b)(2)(iv)(B) for RPS actuation, 4 hr (notification), and per 10CFR 50.72(b)(3)(iv)(A) for automatic actuation of the Auxiliary Feedwater System, 8 hr (notification). The electrical line up transferred to the normal shutdown configuration with standby diesel generators and safety systems available. There was no impact on Unit 1. The licensee plans on issuing a press release and has notified the NRC Resident Inspector.Steam Generator
Feedwater
Auxiliary Feedwater
Main Condenser
Control Rod
Main Steam
ENS 4359023 August 2007 20:30:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness
Manual Reactor Trip Because of Lowering Condenser VacuumAt 1530 hours on 8/23/07, Braidwood Station Unit 2 was manually tripped due to lowering condenser vacuum. The lowering condenser vacuum resulted from the trip of two circulating water pumps. The cause of the two circulating water pump tripping is under investigation. All control rods inserted and there were no complications during the trip and all systems functions as required. Following the unit trip, the Auxiliary Feedwater System actuated as expected to maintain steam generator level. At the time of the unit trip, the Braidwood Station area was experiencing severe thunderstorms. Additionally, at 1604 hours, 19 of 70 emergency sirens for the Braidwood Station were declared inoperable due to a loss of power from storms in the area. As of 1704 hours, 19 sirens (greater than 25%) remain inoperable. This event is considered a major loss of offsite response capability and applies to both Braidwood Station Unit 1 and Unit 2. These events are is being reported under: (1) 10 CFR 50.72(b)(2)(iv)(B) as an event that results in the actuation of the reactor protection system (RPS) when the reactor is critical, (2) 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the PWR auxiliary feedwater system. (3) 10 CFR 50.72(b)(3)(xiii) as a major loss of offsite response capability. All safety buses remained powered by offsite power throughout this event. Emergency diesel generators are available if needed. No steam generator PORV's lifted as a result of the trip. Decay heat is being discharged to the condenser via the steam dumps. The licensee informed the NRC Resident Inspector.Steam Generator
Reactor Protection System
Emergency Diesel Generator
Auxiliary Feedwater
Control Rod
ENS 4344927 June 2007 14:21:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Trip Due to Off-Site Power Fluctuation

Switchyard line 2001 tripped and re-energized during a thunderstorm. This caused main generator output breaker, ACB 3-4, to trip open. At this time '1D' reactor coolant pump (RCP) tripped and caused a reactor trip. Cause for the '1D' RCP trip is under investigation. The heat sink is being provided by Aux Feedwater and the use of Steam Dumps. Electrical power is being provided by offsite power. All rods inserted. There were no complications during the trip and all systems functioned as required. Offsite power remained available throughout the transient. The electrical transient had no impact on Unit 2. The licensee notified the NRC Resident Inspector.

  • * * UPDATE AT 2217 EDT ON 6/28/07 FROM B. SHEAR TO W. HUFFMAN * * *

This is a revision to a previously transmitted ENS call on 6/27/07 EN# 43449. Braidwood Unit 1 Reactor automatically tripped on a loss of '1D' RCP greater than P-8 setpoint. The cause of the RCP trip was an electrical disturbance during a thunderstorm. The reactor trip automatically caused a main turbine and generator trip. Auxiliary feedwater system automatically started on the low-2 S/G water level that is expected from a full power reactor trip. Auxiliary feedwater and main steam dumps are providing a heat sink. A switchyard line also tripped during this electrical transient causing multiple switchyard breakers to open. Electrical power is being provided by offsite power. All control rods fully inserted. There were no complications during the trip and all systems functioned as required. Offsite power remained available throughout the transient. The electrical disturbance had no impact on Unit 2. The licensee notified the NRC resident inspector." R3DO (Louden) notified.

Feedwater
Auxiliary Feedwater
Main Turbine
Control Rod
Main Steam
ENS 431371 February 2007 15:25:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Offsite Phone Connections

At approximately 0925 CST, Braidwood lost approximately 85% of phone functionality. The loss of phones has been determined to be an off site issue and the local phone company is investigating the situation. The Emergency Response Organization (ERO) can still activate ERO pagers using cell phones. The Shift Manager has a dedicated cell phone. The licensee notified the NRC Resident Inspector.

  • * * UPDATE BY KLEVORN TO HUFFMAN AT 2239 EST ON 2/1/07 * * *

The licensee declared the ENS and commercial lines operable based on testing and information from the telephone company. The R3DO (Hills) has been notified.

ENS 4185821 July 2005 00:17:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessEmergency Sirens Failed for One HourAt 2017 CDST on July 20, 2005, it was determined that greater than 25% of Braidwood Station Emergency Sirens, which are maintained by others, had been failed for one hour. The initial failure occurred at 1917 CDST on July 20, 2005, and was apparently caused by storm activity in the area. At 2041 CDST on July 20, 2005, Braidwood Station was notified by the Corporate Emergency Planning organization that the number of failed Emergency sirens was less than 25% of the total number of sirens, and that sirens were in the process of being restored at that time. This notification is required by 10CFR 50.72(b)(3)(xiii) The licensee notified the NRC Resident Inspector.
ENS 4153528 March 2005 18:46:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Trip Due to Generator Protection CircuitryThe licensee faxed the following: Unit 2 reactor trip due to generator protection circuitry. Auxiliary feedwater actuated as expected. There were no additional malfunctions or unexpected plant response. The cause of the generator protection circuitry induced trip is still under investigation. This is a 4 hour notification of an RPS actuation per 10CFR 50.72(b)(2)(iv)(B). The 8 hour notification of an auxiliary feedwater system actuation per 10CFR 50.72(b)(3)(iv)(A) is being made under the same telephone call. See Event 41534. The licensee notified the NRC Resident Inspector.Auxiliary Feedwater
ENS 4128022 December 2004 19:07:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Rps Actuation Due to Steam Generator Low Level Signal

Unit 2 reactor trip due to 2C steam generator LO-2 reactor protection signal. Auxiliary Feed Water actuated as expected. No additional malfunctions or unexpected plant response. Cause of LO-2 steam generator reactor protection signal under investigation. This is a 4 hour notification of an RPS actuation per 10 CFR 50.72(b)(2)(iv)(B). The 8 hour notification of Auxiliary Feed Water system actuation per 10 CFR 50.72 (b)(3)(iv)(B) is being made under this same telephone call. The licensee notified the NRC Resident Inspector. All control rods fully inserted. Decay heat is being removed to the main condenser via the turbine by-pass valves. The electrical grid is stable.

  • * * UPDATE FROM F. EHRHARDT TO M. RIPLEY 15:55 ET 12/22/04 * * *

The licensee has determined that the RPS and Auxiliary Feed Water actuations were the result of an actual low level in the 2C steam generator. The cause of the low level is under investigation. The NRC Resident Inspector was informed. Notified R3 DO (L. Kozak).

Steam Generator
Auxiliary Feedwater
Main Condenser
Control Rod
ENS 409224 August 2004 12:15:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Emergency Notification Due to Inoperable SirensAt 0715 on August 4, 2004, Exelon was notified by Fulton Contracting that Braidwood Station had >(greater than) 25% of its emergency notification sirens inoperable. The cause of the inoperability (at 0626) for the sirens was due to a loss of power due to severe weather. As of 0708 on August 4, 2004, the number of inoperable sirens was less than 25%. Due to a major loss of emergency preparedness capabilities, this event is reportable per 10 CFR 50.72(b)(3)(xiii). The licensee notified the NRC Resident Inspector.
ENS 403703 December 2003 09:36:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Plant Had an Auto Reactor Trip from 100% Power Due to Steam Generator Low LevelThe "2 D" steam generator Lo-2 level was caused by the loss of the "2C" feedwater pump while performing the "2 BWOS" feedwater weekly surveillance of the HP stop valve. Both trains of the aux feed actuated as expected on the "2D" Lo-2 s/g level signal. The plant is currently in mode 3 with all rods fully inserted. No ECCS or safety relief valves actuated. Licensee notified the NRC Resident InspectorSteam Generator
Feedwater
Safety Relief Valve
ENS 402985 November 2003 03:32:0010 CFR 50.72(b)(3)(iv)(A), System ActuationBraidwood 2 Afw Support System Actuation During OutageUnit 2 auxiliary feedwater support systems actuated during scheduled ATWS testing when an unrelated clearance order placement de-energized two 6.9 kv busses (256 and 258). The 2 of 4 6.9 kv bus undervoltage coincidence initiated a valid auto-start signal causing lube oil pumps 2AF01PA-A, 2AF01PB-A and 2AF01PB-C to start. Auxiliary Feedwater Pump AOV discharge valves 2AF004A and 2AF004B auto opened. 2AF01PA 4kv breaker, which was in the equipment test position. Neither auxiliary feedwater pump started and no water transferred to the steam generators. The licensee notified the NRC resident inspector.Steam Generator
Auxiliary Feedwater