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Category:Letter
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TS 3.7/3.14 AOT for SW Piping Maintenance IR 05000280/20240112024-08-13013 August 2024 Comprehensive Engineering Team Inspection Report 05000280/2024011 and 05000281/2024011 ML24164A0012024-08-12012 August 2024 Proposed Alternative Relief Request V-1 Inservice Testing of Pressure Isolation Valves (EPID l-2023-LLR-0060) IR 05000280/20240022024-08-0101 August 2024 Integrated Inspection Report 05000280/2024002 and 05000281/2024002 05000280/LER-2024-001, Troubleshooting Initiated Unknown Turbine Trip Feature in Control System2024-07-30030 July 2024 Troubleshooting Initiated Unknown Turbine Trip Feature in Control System ML24165A2782024-07-17017 July 2024 Issuance of Amendment Nos. 318 and 318, Reclassification of Regulatory Guide 1.97 Variable for Low Head Safety Injection ML24165A1232024-07-17017 July 2024 Proposed Alternative Relief Request P-1, P-2 Inservice Testing of Residual Heat and Containment Spray Pumps (EPID l-2023-LLR-0058) ML24190A4192024-07-0808 July 2024 Inservice Testing (IST) Program for Pumps and Valves Revised Sixth IST Interval Start Date and Updated Technical Specifications References for Alternative Request V-1 ML24179A2932024-07-0101 July 2024 Notification of Inspection and Request for Information for NRC Problem Identification and Resolution Inspection ML24178A2422024-06-25025 June 2024 2023 Annual Report of Emergency Core Cooling System (ECCS) Model, Changes Pursuant to the Requirements of 10 CFR 50.46 ML24177A2792024-06-20020 June 2024 Preparation and Scheduling of Operator Licensing Examinations ML24166A0622024-06-18018 June 2024 – Proposed Alternative Relief Request P-3, P-4 Inservice Testing of Boric Acid, Component Cooling Water Pumps ML24157A0542024-06-13013 June 2024 Audit Summary in Support of License Amendment Request for Proposed Reclassification of Low Head Safety Injection Flow Instrumentation Related to Regulatory Guide 1.97 ML24143A1622024-06-12012 June 2024 – Correction to Issuance of Amendment Nos. 297 and 280 and Surry Units 1 and 2, Correction to Issuance of Amendment Nos. 317 and 317, to Change Emergency Plan Staff Augmentation Times ML24170B0532024-06-10010 June 2024 DOM-NAF-2-P/NP-A, Revision 0.5, Reactor Core Thermal-Hydraulics Using the VIPRE-D Computer Code ML24141A2862024-05-22022 May 2024 Information Request for the Cyber Security Baseline Inspection, Notification to Perform Inspection 05000280/2024403 and 05000281- 2024403 ML24141A2512024-05-20020 May 2024 Proposed License Amendment Request - 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[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000280/LER-2024-001, Troubleshooting Initiated Unknown Turbine Trip Feature in Control System2024-07-30030 July 2024 Troubleshooting Initiated Unknown Turbine Trip Feature in Control System 05000281/LER-2020-001, Cancellation of LER 2020-001-00 for Surry Power Station Unit 2 Re Loss of Containment Cooling Affecting Containment Partial Pressure Indication2020-11-0606 November 2020 Cancellation of LER 2020-001-00 for Surry Power Station Unit 2 Re Loss of Containment Cooling Affecting Containment Partial Pressure Indication 05000280/LER-2019-0022020-02-0404 February 2020 LER 2019-002-00 for Surry Power Station Unit 1, Items Non-Conforming to Design for Tornado Missile Protection 05000280/LER-2017-0012017-10-0606 October 2017 1 OF 3, LER 17-001-00 for Surry, Unit 1, Regarding Shutdown due to an Unisolable Leak in Reactor Coolant Pressure Boundary 05000281/LER-2016-0012016-12-0202 December 2016 Unit 2 Reactor Trip due to Generator Differential Lockout, LER 16-001-00 for Surry Power Station, Unit 2, Regarding Reactor Trip Due to Generator Differential Lockout 05000280/LER-2016-0012016-07-11011 July 2016 1 OF 4, LER 16-001-00 for Surry Power Station, Unit 1 and 2, Regarding Emergency Service Water Pump Inoperable Due to Corrosion of Valve Support ML1015505662009-03-0404 March 2009 Event Notification for Surry on Relief Valve Failure Results in Tritium and Cesium Spill ML0702501902007-01-17017 January 2007 Special Report on Qpt Not Less than Two Percent for Twenty Four Hours ML19105B1281979-08-21021 August 1979 LER 1979-011-03X for Surry Units 1 & 2 Loss of Power with Both Units at Cold Shutdown, Observed Radiation Monitors Without Power ML19093B4141978-09-26026 September 1978 Reporting Condenser Cooling Water Outlet Temperature to James River Decreased by 3.5oF as Measured at Station Discharge Structure ML19105A3001978-09-0808 September 1978 LER 78-013-03X-1, LER 78-029-03L-0, & LER 78-031-03L-0 for Surry 2 Re Critical Below Minimum Insertion Limit on D Control Bank ML19105A3011978-09-0101 September 1978 LER 1978-028-03L-0 for Surry 2 Re Containment Pressure Exceeded Allowable Limit ML19095A4971978-08-25025 August 1978 Submit Licensee Event Report No. LER 78-024/03L-0 Re No Alarm During a Planned Release of Liquid Radioactive Waste ML19095A4981978-08-22022 August 1978 Submit Licensee Event Report Nos. LER 1978-019/03L-0, LER 1978-021/03L-0, LER 1978-022/03L-0, LER 1978-023/03L-0, LER 1978-025/03L-0, LER 1978-026/03L-0 for Surry Unit No. 1 ML19105A0771978-08-16016 August 1978 Submit LER 78-027/03L-0 Re Seven Snubbers Not Meeting Inspection Criteria ML19105A0781978-08-16016 August 1978 Submit LER 78-027/03L-0 Re Seven Snubbers Not Meeting Inspection Criteria ML19105A0791978-08-11011 August 1978 LER 78-026/03L-0. Follow-up Inspection for Valve Cleanliness, Discovered That Containment Spray Isolation Valves (MOV-CS-201C and D) Contained No More That Five Milliliters. Technical Specification TS 6.6.2.b.(3) ML19095A4991978-08-0404 August 1978 Sutmit Licensee Event Report No. LER 78-018/03L-0 Re Two Main Steam Safety Valves Were Not within Plus or Minus 3% of Setpoint as Required ML19105A0801978-07-28028 July 1978 LER 1978-022-03L-0 Re Axial Power Distribution Monitoring Was Exceeded,& Three LERs 1978-021-03L-0, LER 1978-023-03L-0, & LER 1978-024-03L-0 Re Inlet Circulating Water Temperature Exceeded ML19095A5001978-07-28028 July 1978 Submit Licensee Event Report Nos. LER 78-017/03L-0 Re Not Documenting Four Electric Maintenance Procedures & Two Periodic Tests, & 78-020/03L-0 Re Suspended Air Bubbles in Reservoir Fluid ML19095A2281978-07-27027 July 1978 Reporting & Providing Additional Information on Incidence of Missing Two Steam Generator Tube Plugs Found During Inspection ML19095A2291978-07-26026 July 1978 Reporting of Cooling Water Discharge Temperature Change Rate on 7/9/1978 & Found No Evidence of Any Detrimental Effects in River or Its Inhabitants ML19095A5011978-07-21021 July 1978 Submit Licensee Event Report No. LER 78-016/03L-0 Re Valve MOV-RH-100 Was Not Opening ML19105A0821978-07-17017 July 1978 LER 1978-025-03L for Surry Unit 2 Excessive Gap Around Battery Room Ventilation Duct ML19105A0811978-07-17017 July 1978 LER 1978-025-03L for Surry Unit 2 Excessive Gap Around Battery Room Ventilation Duct ML19095A5021978-07-0707 July 1978 Submit Licensee Event Report Nos. LER 78-013/03L-0 Re Six Snubbers Not Meeting Test Criteria, & 78-014/03L-0 Re Mount Plate Was Warped, & 3 of 8 Bolts Were Insufficiently Embedded ML19095A5031978-06-27027 June 1978 Submit Licensee Event Report No. LER-78-015/03L-0 Re Valve Cleanliness Inspection Found Foreign Material on Valve Seating Surfaces ML19095A5041978-06-27027 June 1978 Submit Licensee Event Report No. LER-78-015/03L-0 Re Valve Cleanliness Inspection Found Foreign Material on Valve Seating Surfaces ML19105A0831978-06-23023 June 1978 LER 1978-017-03L, LER 1978-018-03L, LER 1978-019-03L, & LER 1978-020-03L for Surry Unit 2 Related to Snubbers ML19095A2481978-06-19019 June 1978 06/19/1978 Letter Reporting Increase of Condenser Cooling Water Discharge ML19095A5051978-06-0707 June 1978 Submit Licensee Event Report No. LER-78-012/03L-0 Re Inside Recirculation Spray Pump 1-RS-P-1A, Failure to Rotate by Hand ML19105A0851978-05-23023 May 1978 LER 1978-015-03L for Surry Unit 2 Finding of Air Leak on Header of Control Room Emergency Air Supply Bank ML19095A5061978-05-23023 May 1978 Submit Licensee Event Report Nos. LER-78-008/03L-0, LER-78-009/03L-0, LER-78-010/03L-0, LER-78-011/03L-0 for Surry Unit No. 1 ML19105A0861978-05-12012 May 1978 LER 1978-013-03L for Surry Unit 2 Reactor Brought Critical Below Minimum Insertion Limit on D Control Bank ML19105A0871978-05-0505 May 1978 LER 1978-014-03L for Surry Unit 2 Charging Pump Service Water Pump a Tripped on High Current ML19095A5071978-05-0505 May 1978 Submit Licensee Event Report No. LER-78-007/03L-0 Re Leak on Body to Bonnet Joint Diaphragm Valve 1-CH-98 ML19105A0881978-04-19019 April 1978 LER 1978-006-01T for Surry Unit 2 Review of Fire Protection Yard Piping Revealed That Two Pipe Extensions May Not Have Been Seismically Qualified ML19095A5081978-04-19019 April 1978 Submit Licensee Event Report No. LER-78-006/01T-0 Re Seismically Disqualified Two Pipe Extensions on Fire Protection Yard Piping ML19095A5091978-04-0707 April 1978 Forwarding Licensee Event Report No. LER-78-005/01T-0 Re Westinghouse'S Error in LOCA-ECCS Evaluation Model, Which Will Result in Higher Calculated Peak Clad Temperature ML19105A0901978-04-0606 April 1978 LER 1978-012-01T for Surry Unit 2 Failure to Meet Containment Integrity ML19105A0921978-04-0404 April 1978 LER 1978-011-03L for Surry Unit 1 Loss of Service Water Flow Through Charging Pump Intermediate Seal Cooler ML19095A5101978-04-0404 April 1978 Submit Licensee Event Report No. LER-78-004/03L-0 Re Loss of Service Water Flow Through Charging Pump Intermediate Seal Cooler ML19105A0931978-03-30030 March 1978 LER 1978-008-03L Re Snubber Body in Contact with Structure; LER 1978-009-03L Re Trip of Boric Acid Transfer Pump; & LER 1978-010-03L Re Failure of Pressurizer Channel ML19095A5111978-03-28028 March 1978 Submit Licensee Event Report No. LER-78-003/03L-0 Re Failed Heat Tracing, Panel 8 Circuit 24 ML19095A5121978-03-21021 March 1978 Submit Licensee Event Report No. LER-78-002/01T-0 Re Additional Radial Peaking Factor Surveillance ML19105A0941978-02-27027 February 1978 LER 1978-006-03L Re Failure of Sola Transformer, & LER 1978-007-03L Re Trip of Boric Acid Transfer Pump on Thermal Overload ML19095A5131978-02-24024 February 1978 Submit Licensee Event Report No. LER-78-001/03L-0 Re Hydraulic Shock Suppressor Found Inverted with Empty Reservoir ML19105A0951978-02-16016 February 1978 LER 1978-003-03L Re Erroneous Readings of Loop a Hot Leg Temperature Protection Channel; LER 1978-004-03L Re Unqualified Welding of Two Diaphragm Welds on Heat Exchanger; & LER 1978-005-03L Re Low Current Condition from Heat Tracing ML19105A0971978-02-0202 February 1978 LER 1978-001-03L for Surry Unit 2 Inoperability of Condenser Circulating Water Outlet Valve ML19095A5141978-01-0909 January 1978 Submit Licensee Event Report Nos. LER-77-021/03L-0 & LER-77-022/03L-0 2024-07-30
[Table view] |
LER-2024-001, Troubleshooting Initiated Unknown Turbine Trip Feature in Control System |
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2802024001R00 - NRC Website |
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10CFR50.73
Virginia Electric and Power Company Surry Power Station 5570 Hog Island Road Surry, Virginia 23883
July 30, 2024
U.S. Nuclear Regulatory Commission Serial No.: 24-230 Attention: Document Control Desk SPS: MMT Washington, D. C. 20555-0001 Docket No.: 50-280 License No.: DPR-32
Dear Sir or Madam:
Pursuant to 1 0CFR50. 73, Virginia Electric and Power Company hereby submits the following Licensee Event Report applicable to Surry Power Station Unit 1.
Report No. 50-280 I 2024-001-00
This report has been reviewed by the Station Facility Safety Review Committee and will be forwarded to the Management Safety Review Committee.
David H. Wilson Site Vice President Surry Power Station
Enclosure Commitment contained in this letter: None
cc: U.S. Nuclear Regulatory Commission, Region II Marquis One Tower, Suite 1200 245 Peachtree Center Ave., NE Atlanta, GA 30303-1257
NRC Senior Resident Inspector Surry Power Station
Abstract
On June 2, 2024, at 1708 hours0.0198 days <br />0.474 hours <br />0.00282 weeks <br />6.49894e-4 months <br /> with Unit 1 at 13% power, Unit 1 experienced an automatic reactor trip due to a turbine trip.
Upon synchronizing Unit 1 turbine generator to the grid, the Turbine Control System (TCS) did not transition to load control as expected. TCS troubleshooting identified that the Breaker Cycling Test mode was active, inhibiting the control system response to breakers being closed. While disabling Breaker Cycling Test mode, the breaker status points were taken off scan. This action initiated an unexpected turbine trip and automatic reactor trip. The turbine trip initiation was caused by a flawed TCS trip logic design. The flawed trip logic rendered a Remote IO failure indication on the TCS Remote IO Failure Trip where no failure existed.
The TCS was returned to a normal configuration for turbine startup, an extent of condition review of the Ovation System for additional unrecognized trips was performed, and TCS indicators and controls were updated in station operating procedures. The health and safety of the public were not affected by this event.
This report is being submitted pursuant to 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in the automatic actuation of the Reactor Protection System.
1.0 Description of the Event On June 2, 2024, at 1708 hours0.0198 days <br />0.474 hours <br />0.00282 weeks <br />6.49894e-4 months <br />, during Unit 1 startup following the completion of a scheduled refueling outage, Unit 1 automatically tripped from 13% power due to a Turbine trip greater than P-7 (10% power). Upon synchronizing Unit 1 turbine generator to the grid, the Turbine Control System (TCS) (EIIS System JJ, Component DCC) did not transition to load control as expected. MWs slowly increased to 50 MWe with no other actions taken. TCS troubleshooting identified that the Breaker Cycling Test mode was active, inhibiting the control system response to breakers being closed. The operating crew remained diligent in monitoring the unit. All critical parameters such as reactor power, steam generator levels, pressurizer pressure, and pressurizer level remained relatively stable during this time. The operating crew was not challenged by the slow increase in load. Manually tripping the reactor was considered and determined to result in a more severe transient compared to the slow increase in electrical load. A value was established for manually tripping the reactor if the load increase continued. The unit stabilized at a level below this threshold.
A troubleshooting sheet was developed and tested on the simulator. The troubleshooting sheet would allow disabling Breaker Cycling Test mode and the TCS to be swapped to load control. While disabling the Breaker Cycling Test mode, the breaker status points were taken off scan. This action initiated an unexpected turbine trip and automatic reactor trip.
The turbine trip initiation was caused by a flawed TCS trip logic design. The flawed trip logic rendered a Remote IO failure indication on the TCS Remote IO Failure Trip where no actual failure existed. The automatic reactor trip was uncomplicated and all control rods fully inserted into the core. There was no emergency core cooling system (ECCS) or auxiliary feedwater system actuation, and the operating crew responded as expected. There were no inoperable structures, systems or components that contributed to the event.
The TCS was returned to a normal configuration for turbine startup, an extent of condition review of the Ovation System for additional unrecognized trips was performed, and station operating procedures were updated. This report is being submitted pursuant to 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in the automatic actuation of the Reactor Protection System.
2.0 Significant Safety Consequences and Implications
No significant safety consequences resulted from this event. The health and safety of the public were not affected by this event.
3.0 Cause of the Event
The cause of the event was a flawed TCS trip logic design resulting in a TCS Remote IO Failure Trip. The trip logic was flawed in that a Remote IO failure was indicated on the TCS Remote IO Failure Trip where no failure existed. The trip logic was made up with the flawed Remote IO failure indicated concurrent with 2/2 Output Circuit Breakers (OCBs) indicating Bad quality.
4.0 Immediate Corrective Action
The TCS was returned to a normal configuration for turbine startup including returning the OCB points to scan, turning off the Breaker Cycling Test Mode, and forcing input to the Primary Control Module to clear input to impacted AND gate.
The Vendor and Dominion Engineering performed a review for additional unrecognized trips associated with the Ovation System and found no additional unrecognized trips. Procedures for Turbine-Generator Startup to 20%-25% Turbine Power were revised to include steps to perform TCS Alarm Screen and TCS Forced or Off Scan Point review in accordance with the procedure for TCS Ovation Operation, and added steps to check that the Bypass Sync Check Relay and the Breaker Cycling Test buttons are inactive. Additionally, the TCS Ovation Operation procedure was revised to enhance reviews of the TCS Alarm Screen and review TCS Forced or Off Scan Points.
5.0 Additional Corrective Actions
Corrective Actions to Address Contributing Causes (CACC) were developed to address procedural review requirements (electronic and non-electronic), specific guidance requirements when developing digital design changes (to include software functionality), training analysis for troubleshooting procedure, revise guidance for Owners Review tracking of open items to resolution, and adding supervisory review requirements for Owners Review in guidance document.
6.0 Actions to Prevent Recurrence Correct flawed identified TCS trip logic for both Unit 1 and Unit 2 Turbine Control Systems.
7.0 Similar Events
No similar events have been noted at Surry.
8.0 Additional Information
The health and safety of the public were not affected by this event. There was no impact to Unit 2.