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NRC Pere 308 U 8. NUCLE AR C.ELULATOAV C048Ma&S10s.
1 % 31 APPRIVED OMS NO 2180 010e UCENSEE EVENT REPORT (LER)
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F ACILITY NARIE (11 DOCKET NUGASER (2p PAGE 33i SURRY POWER STATION, UNIT 1 0 l5 l 0 l0 l 0 l2 lg l 0 1 l0Fl013 TITLt (4)
Pressurizer PORVs Declared Inoperable Due to Excessive Stroke Time SVENT DATE Ill LER NueseER (el REPORT DATE (7)
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no A T A ACT n-, e.oo e.oo e...~.,,-.,0 us,,,0.e.=o,.e., p oi On December 23, 1986, both Unit 1 and Unit 2 were at cold shut-down with their reactor coolant systems depressurized to atmos-pheric.
Unit 2 Pressurizer PORVs, PCV-2455C and PCV-2456 f ailed to open within the maximum allowabic stroke time when using the backup air supply in accordance with a Periodic Test.
On Janu-ary 2, 1987, with both Units still at cold shutdown and depressu-rized, the Unit 1 Pressurizer PORV, PCV-1455C failed to open i
within the maximum allowable stroke time similar to the Unit 2 l
valves. These valves were declared inoperable when the cycessive stroke times were discovered, and they were lef t in the open position in accordance with Technical Specification 3.1.G.
This was the first time these valves had been tested by this Periodic Test, which was written to test the backup air supply in response to IEIN 86-50.
The excessive stroke times were caused by insuf-ficient air flow due to air line size. The air lines and associ-ated components will he replaced with larger tubing and components.
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NRCteem aneA U $ NUCLEKA 1EIULATORY COMuisseON LICEN!EE EVENT REPORT (LER) TEXT CONTINUATION
EXPIRES: S/31/W FACIL8TV NAME tu DOCKli NUMetR (26 LtR NUMSER (61 PAGE (3)
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vtan SURRY POWER STATION, UNIT 1 0 l5 l0 l0 l0 l 2l8 l 0 8l7 0 l 0l 1 0l0 0l2 OF 0l3 textinm N w wo-wmicr.=assrsmn 1.0 Description of the Event On December 23, 1986, both Unit I and Unit 2 were at cold shutdown (CSD) and the reactor coolant systems depressurized to atmospheric pressure. Unit 2 Pressurizer PORVs, PCV-2455C and PCV-2456 (EIIS-PCV) failed to open within the maximum allowable stroke time when using the backup high pressure air supply bottles in accordance with a Periodic Test.
On January 2, 1987, with Unit I and Unit 2 at CSD and depressurized, the Unit 1 Pressurizer PORV PCV-1455C failed to open within the maximum allowable stroke time similar to the Unit 2 valves. PORV PCV-1456 was inoperable at the time of the test on PCV-1455C. These valves were declared inoperable at the time the excessive stroke times were discovered and they were left open in accordance with Technical Specification (T.S.)
3.1.C.
These PORVs provide Overpressure Mitigation Protection for the Reactor Coolant System (RCS) when the RCS is less than 350 degrees Fahrenheit. The backup air supply for these PORVs is the safety related air supply and consists of high pressure air bottles, air pressure regulators, SOVs and instrument air tubing. The Periodic Test that found these PORVs to have excessive stroke time, is a new Periodic Test that was written in response to ICIN 86-50 to specifically test the backup air supply. This was the first time this Periodic Test was performed on either Unit. These events are being reported in accordance with the requirements of 10CFR 50.73(a) (2) (vii).
2.0
Safety Consequences and Implications
When the reactor coolant average temperature is less than 350 degrees Fahrenheit and the Reactor Vessel head is bolted, the oper-ability of two PORVs, or the RCS vented through an open PORV, en-sure that the Reactor Vessel will be protected from pressure transients which could exceed the limits of Appendix G to 10CFR 50.
When the Reactor Coolant average temperature is greater than 350 degrees Fahrenheit, overpressure protection is provided by a bubble in the pressurizer and/or pressurizer safety valves.
When the PORVs were determined to have excessive stroke time, they were placed in the open position to provide a vent path for the RCS in accordance with Technical Specification 3.1.C.
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LICENSEE EVENT REPORT (LER) TEXT CENTINUATION Arec.ovio ous s o. mo4io4 EXPtRES: 8/31/08
- ACILITY psAME ili COCKET NUMOR R (2)
LtR 98UhAGER (S)
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SURRY POWER STATION, UNIT 1 0l0 0l3 OF gl3 0 l5 l 0 l 0 l 0 l 2 l8 l 0 8l7 0l 0 l1 TEXT (# snare assce a soeveest use sewoonst Nec perm Jese'st (17)
The PORVs that were declared inoperable did cycle, although the time to cycle exceeded the required time by a maximum of 5.81 seconds. There were no RCS pressure transients that these valves would have had to responded to during the existing Unit outages.
Therefore, these events did not constitute an unreviewed safety question and the health and safety of the public were not affected.
3.0 Cause
The air supply lines to the valve operators from the backup high pressure air bottles are undersized. This has restricted the air flow to the valve to less than the minimum air flow required to open the valves within the specified stroke time.
4.0
Immediate Corrective Actions
When the PORVs were determined to be inoperable, they were placed in the open position to provide a RCS vent path in compliance with Technical Specification 3.1.G.
5.0
Additional Corrective Actions
The air line and component sizes will be increased to provide suf-ficient flow to cycle open the PORVs within the required time period prior to the units returning to service.
6.0 Actions Taken to Prevent Recurrence No further action is considered necessary.
7.0
Similar Events
None.
8.0 Manuf acturer/!!odel Number N/A g,o.. u..
s PCO VIRGINIA ELECTRIC AND POWER COMPANY Surry Power Station P. O. Box 315 Surry, Virginia 23883 January 23, 1987 U.S. Fuclear Regulatory Commission Serial No:
86-061 Document Control Desk Docket No.:
50-280 016 Phillips Building License No: DPR-32 Washington, D.C.
20555 Gentlemen:
Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report for Surry Unit 1.
REPORT NUMBER 87-001-00 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be reviewed by Safety Evaluation and Control.
Very truly yours, S
R. F. Saunders Station Manager Enclosure cc:
Dr. J. Nelson Grace Regional Administrator Suite 2900 101 Marietta Street, NW Atlanta, Georgia 30323
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| 05000280/LER-1987-001, :on 861223,pressurizer PORVs Declared Inoperable Due to Excessive Stroke Time.Caused by Insufficient Air Flow Due to Air Line Size.Air Lines Will Be Replaced W/Larger Tubing |
- on 861223,pressurizer PORVs Declared Inoperable Due to Excessive Stroke Time.Caused by Insufficient Air Flow Due to Air Line Size.Air Lines Will Be Replaced W/Larger Tubing
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000281/LER-1987-001-03, :on 870312,loss of Reactor Coolant Loop Occurred Due to Loss of Charging Pumps & Seal Injection Flow to Reactor Cooling Pumps.Caused by Personnel Error.Personnel Reinstructed Re Listed Procedures |
- on 870312,loss of Reactor Coolant Loop Occurred Due to Loss of Charging Pumps & Seal Injection Flow to Reactor Cooling Pumps.Caused by Personnel Error.Personnel Reinstructed Re Listed Procedures
| | | 05000280/LER-1987-002-02, :on 870104,three Control/Relay Room Chillers Tripped on High Condenser Discharge Pressure.Caused by Insufficient Svc Water Flow to Condenser of Chiller Unit. Valve Lineup to & from Chiller Checked |
- on 870104,three Control/Relay Room Chillers Tripped on High Condenser Discharge Pressure.Caused by Insufficient Svc Water Flow to Condenser of Chiller Unit. Valve Lineup to & from Chiller Checked
| | | 05000281/LER-1987-002-01, :on 870316,reactor Trip by Turbine Trip Occurred,Resulting in Insertion of Shutdown Banks.Caused by Personnel Error.Reactor Trip Breakers Reset & Shutdown Banks Withdrawn |
- on 870316,reactor Trip by Turbine Trip Occurred,Resulting in Insertion of Shutdown Banks.Caused by Personnel Error.Reactor Trip Breakers Reset & Shutdown Banks Withdrawn
| | | 05000280/LER-1987-003, :on 870213 & 16,one of Three Control/Relay Room Chillers Operable.Second Chiller Out for Maint & Third Chiller Inoperable.Caused by Inadequate Heat Sinks.One Chiller Replaced,Two New Chillers Ordered |
- on 870213 & 16,one of Three Control/Relay Room Chillers Operable.Second Chiller Out for Maint & Third Chiller Inoperable.Caused by Inadequate Heat Sinks.One Chiller Replaced,Two New Chillers Ordered
| | | 05000281/LER-1987-003-01, :on 870404,reactor Tripped by Generator anti- Motoring Turbine Trip.Caused by Leaking Turbine Governor Valves.Valves Will Be Inspected & Repaired During Next Outage of Sufficient Duration |
- on 870404,reactor Tripped by Generator anti- Motoring Turbine Trip.Caused by Leaking Turbine Governor Valves.Valves Will Be Inspected & Repaired During Next Outage of Sufficient Duration
| | | 05000280/LER-1987-004, :on 870213,discovered Potential for Control Room Ventilation Fans to Admit More Unfiltered Air than Allowed.Caused by Inadequate Sealing of Fan Shaft.Temporary Seal Installed Until Fans Repaired |
- on 870213,discovered Potential for Control Room Ventilation Fans to Admit More Unfiltered Air than Allowed.Caused by Inadequate Sealing of Fan Shaft.Temporary Seal Installed Until Fans Repaired
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000281/LER-1987-004-03, :on 870831,while Performing Surveillance Procedure,Containment Cooling Water Outlet Header Isolation Trip Valve Found Inoperable.Caused by Ruptured Diaphragm in Air Pilot Relay.Relay Replaced |
- on 870831,while Performing Surveillance Procedure,Containment Cooling Water Outlet Header Isolation Trip Valve Found Inoperable.Caused by Ruptured Diaphragm in Air Pilot Relay.Relay Replaced
| | | 05000280/LER-1987-005, :on 870221,control/relay Room Chillers 1-VS-E-4B & 4C Tripped Due to Insufficient Svc Water Flow to Condensers.Caused by Clogged Y-type Suction Strainers. Maint Procedures Re Strainer Cleaning Revised |
- on 870221,control/relay Room Chillers 1-VS-E-4B & 4C Tripped Due to Insufficient Svc Water Flow to Condensers.Caused by Clogged Y-type Suction Strainers. Maint Procedures Re Strainer Cleaning Revised
| | | 05000281/LER-1987-005-03, :on 871014 Electrician Inadvertently Completed Flood Protection Circuit Causing Two of Four Condenser Circulating Water Inlet Valves to Close.Caused by Personnel Error.Procedure Written for Maint Personnel |
- on 871014 Electrician Inadvertently Completed Flood Protection Circuit Causing Two of Four Condenser Circulating Water Inlet Valves to Close.Caused by Personnel Error.Procedure Written for Maint Personnel
| | | 05000280/LER-1987-006, :on 870310,control/relay Chiller Observed Inoperable Due to Chiller Svc Water Pump Trip.Cause of Pump Trip Not Determined.Thermal Trip Device Reset |
- on 870310,control/relay Chiller Observed Inoperable Due to Chiller Svc Water Pump Trip.Cause of Pump Trip Not Determined.Thermal Trip Device Reset
| | | 05000280/LER-1987-007, :on 870323,one (1-VS-E-4A) of Three Control/ Relay Room Chillers (EIIS-CHU) Tripped.Caused by Insufficient Svc Water Flow Due to Seal Leak on Supply Pump.Svc Water Flow Increased & Pump Repaired |
- on 870323,one (1-VS-E-4A) of Three Control/ Relay Room Chillers (EIIS-CHU) Tripped.Caused by Insufficient Svc Water Flow Due to Seal Leak on Supply Pump.Svc Water Flow Increased & Pump Repaired
| | | 05000280/LER-1987-008, :on 870326,one of Three Control/Relay Room Chillers Tripped Due to High Condenser Discharge Pressure. Caused by Operator Error.Addl Valve Handles Will Be Installed on Each Chiller |
- on 870326,one of Three Control/Relay Room Chillers Tripped Due to High Condenser Discharge Pressure. Caused by Operator Error.Addl Valve Handles Will Be Installed on Each Chiller
| | | 05000280/LER-1987-009-02, :on 870330,discovered That Inside Containment Isolation Valve for Containment Sump Pumps Would Not Close. Caused by Corrosion Product Buildup in Valve Operator.New Valve Operator Installed |
- on 870330,discovered That Inside Containment Isolation Valve for Containment Sump Pumps Would Not Close. Caused by Corrosion Product Buildup in Valve Operator.New Valve Operator Installed
| | | 05000280/LER-1987-010, :on 870313,improper Routing of App B Related Cables Discovered.Caused by Relocation of Cables Through Cable Vault & Tunnel.Fire Watch of Area at Least Once Per Shift Established & Design Changes Reviewed |
- on 870313,improper Routing of App B Related Cables Discovered.Caused by Relocation of Cables Through Cable Vault & Tunnel.Fire Watch of Area at Least Once Per Shift Established & Design Changes Reviewed
| | | 05000280/LER-1987-011, :on 870516,low Flow RCS (EIIS-AB) Flow Reduced to 47%,following Reactor Trip.Caused by Failure of RCS a Hot Leg Loop Stop Valve.Samples of Loop Stop Valve Stems Will Undergo Ultrasonic Testing |
- on 870516,low Flow RCS (EIIS-AB) Flow Reduced to 47%,following Reactor Trip.Caused by Failure of RCS a Hot Leg Loop Stop Valve.Samples of Loop Stop Valve Stems Will Undergo Ultrasonic Testing
| | | 05000280/LER-1987-011-01, :on 870516,low Flow Reactor Trip Occurred. Caused by Hot Leg Loop Stop Valve Stem Failure Permitting Disc to Drop,Blocking Loop Flow.Procedure Revised to Reduce Stress on Valve Stem |
- on 870516,low Flow Reactor Trip Occurred. Caused by Hot Leg Loop Stop Valve Stem Failure Permitting Disc to Drop,Blocking Loop Flow.Procedure Revised to Reduce Stress on Valve Stem
| | | 05000280/LER-1987-012-01, :on 870607,recirculation Spray Pump Declared Inoperable Due to High Vibrations.Caused by Threaded Nut & Bolt Detached & Located in Impeller Region of Pump.Loose Nut & Bolt Removed & Pump Realigned |
- on 870607,recirculation Spray Pump Declared Inoperable Due to High Vibrations.Caused by Threaded Nut & Bolt Detached & Located in Impeller Region of Pump.Loose Nut & Bolt Removed & Pump Realigned
| | | 05000280/LER-1987-013-01, :on 870623,unit Shutdown Commenced Due to High RCS Leak Rate.Caused by Failed Packing on Loop Stop Valve MOV-1593.Loop Stop Valves Repacked & Diaphragm on Drain Header Isolation Valve Replaced |
- on 870623,unit Shutdown Commenced Due to High RCS Leak Rate.Caused by Failed Packing on Loop Stop Valve MOV-1593.Loop Stop Valves Repacked & Diaphragm on Drain Header Isolation Valve Replaced
| | | 05000280/LER-1987-014, :on 870630,discovered That Auxiliary Feedwater (AFW) Could Be Lost to Operating Unit in Event of High Energy Line Break in Main Steam Valve House.Caused by Poor Review of AFW Supply.Review Continuing |
- on 870630,discovered That Auxiliary Feedwater (AFW) Could Be Lost to Operating Unit in Event of High Energy Line Break in Main Steam Valve House.Caused by Poor Review of AFW Supply.Review Continuing
| | | 05000280/LER-1987-015-01, :on 870717,individual Rod Position Indicators for Shutdown Banks a & B & Control Banks A,B,C & D Declared Inoperable.Caused by Banks Indicating Below Demand Counter Position Due to Dirty Dc Power Contacts |
- on 870717,individual Rod Position Indicators for Shutdown Banks a & B & Control Banks A,B,C & D Declared Inoperable.Caused by Banks Indicating Below Demand Counter Position Due to Dirty Dc Power Contacts
| | | 05000280/LER-1987-016, :on 870722,main Control Ventilation Isolation Occurred.Caused by High Sensor Voltage on Chlorine Gas Detector.Chlorine Gas Treatment Sys & Sewage Treatment Plant Replaced by Ultraviolet Sys |
- on 870722,main Control Ventilation Isolation Occurred.Caused by High Sensor Voltage on Chlorine Gas Detector.Chlorine Gas Treatment Sys & Sewage Treatment Plant Replaced by Ultraviolet Sys
| | | 05000280/LER-1987-017-01, :on 870727,containment Vacuum Flow Paths for Units 1 & 2 Became Inoperable When Discharge Valves Closed. Caused by Electrical Spiking Due to Failed Central Processing Unit Card.Failed Card Replaced |
- on 870727,containment Vacuum Flow Paths for Units 1 & 2 Became Inoperable When Discharge Valves Closed. Caused by Electrical Spiking Due to Failed Central Processing Unit Card.Failed Card Replaced
| | | 05000280/LER-1987-018, :on 870729,control/relay Room Chiller a Freon Relief Valve Lifted.Chillers B & C Tripped on Listed Dates. Caused by Low Svc Water (SW) Flow Due to Buildup of Seaweed in Upstream SW Strainers.Strainers Cleared |
- on 870729,control/relay Room Chiller a Freon Relief Valve Lifted.Chillers B & C Tripped on Listed Dates. Caused by Low Svc Water (SW) Flow Due to Buildup of Seaweed in Upstream SW Strainers.Strainers Cleared
| | | 05000280/LER-1987-019, :on 870807,manual Reactor Trip Initiated Following Short Rampdown Due to Loss of Cooling & Oil Flow for Main Transformer B.Caused by Failed Undervoltage Relay. Relay & Local Annunciator Panel Replaced |
- on 870807,manual Reactor Trip Initiated Following Short Rampdown Due to Loss of Cooling & Oil Flow for Main Transformer B.Caused by Failed Undervoltage Relay. Relay & Local Annunciator Panel Replaced
| | | 05000280/LER-1987-020, :on 870813 & 21,main Control Room Ventilation Isolated.Caused by High Voltage Output on Chlorine Gas Detector CLA-VS-100A.Ventilation Sys Realigned & Verified No Chlorine Gas in Room |
- on 870813 & 21,main Control Room Ventilation Isolated.Caused by High Voltage Output on Chlorine Gas Detector CLA-VS-100A.Ventilation Sys Realigned & Verified No Chlorine Gas in Room
| | | 05000280/LER-1987-021, :on 870818,control/relay Room Chiller 1-VS-E-4B Tripped on High Condenser Discharge Pressure.Caused by Inadequate Svc Water Flow Due to Buildup of Seaweed in Y-type Suction Strainers.Strainers Cleaned |
- on 870818,control/relay Room Chiller 1-VS-E-4B Tripped on High Condenser Discharge Pressure.Caused by Inadequate Svc Water Flow Due to Buildup of Seaweed in Y-type Suction Strainers.Strainers Cleaned
| | | 05000280/LER-1987-022, :on 870830 & 0903,main Control Room Ventilation Isolation Occurred.Caused by High Voltage Output on Chlorine Gas Detector.Chemistry Dept Verified That No Chlorine in Main Control Room.Ventilation Sys Realigned |
- on 870830 & 0903,main Control Room Ventilation Isolation Occurred.Caused by High Voltage Output on Chlorine Gas Detector.Chemistry Dept Verified That No Chlorine in Main Control Room.Ventilation Sys Realigned
| | | 05000280/LER-1987-023, :on 870901,standby Charging Pump Automatically Started on Low Charging Pump Discharge Pressure Signal. Caused by Personnel Error.Pressure Transmitter Drain Valve Closed & Isolation Valve Opened |
- on 870901,standby Charging Pump Automatically Started on Low Charging Pump Discharge Pressure Signal. Caused by Personnel Error.Pressure Transmitter Drain Valve Closed & Isolation Valve Opened
| 10 CFR 50.73(o)(2) | | 05000280/LER-1987-024, :on 870920,RCS Flow Reactor Trip Occurred When Reactor Coolant Pump B Tripped.Caused by Complete Separation of Phase Main Load Connection Bus Bar A.Failed Bus Bar Replaced & Other Bus Bars Inspected |
- on 870920,RCS Flow Reactor Trip Occurred When Reactor Coolant Pump B Tripped.Caused by Complete Separation of Phase Main Load Connection Bus Bar A.Failed Bus Bar Replaced & Other Bus Bars Inspected
| | | 05000280/LER-1987-025, :on 871008,RCS Leakage Rate Test Results of 4.06 Gpm Found in Excess of Tech Specs 3.1.C.2 & 3.1.C.5. Caused by Inadequate Procedure & HX Bypass Valve Leakage. Valve Tightened & Procedure PT-10 Revised |
- on 871008,RCS Leakage Rate Test Results of 4.06 Gpm Found in Excess of Tech Specs 3.1.C.2 & 3.1.C.5. Caused by Inadequate Procedure & HX Bypass Valve Leakage. Valve Tightened & Procedure PT-10 Revised
| | | 05000280/LER-1987-026, :on 871018,main Control Room (MCR) Ventilation Isolated Due to High Voltage Output on Chlorine Gas Detector.Chemistry Verified No Chlorine Gas in MCR & Ventilation Sys Realigned |
- on 871018,main Control Room (MCR) Ventilation Isolated Due to High Voltage Output on Chlorine Gas Detector.Chemistry Verified No Chlorine Gas in MCR & Ventilation Sys Realigned
| | | 05000280/LER-1987-027, :on 871027,electrical Short in Train a Turbine Bldg Flood Control Panel Caused Spurious Completion of Flood Protection Circuit.Caused by Leak on Access Manway of Moisture Separator Reheater 1-MS-E-1B |
- on 871027,electrical Short in Train a Turbine Bldg Flood Control Panel Caused Spurious Completion of Flood Protection Circuit.Caused by Leak on Access Manway of Moisture Separator Reheater 1-MS-E-1B
| | | 05000280/LER-1987-028, :on 871021,reported That Emergency Diesel Generators Output Breaker Protection Circuits Contained Instantaneous Overcurrent Tripping Relays.Caused by Design Deficiency.Trip Relay Settings Increased |
- on 871021,reported That Emergency Diesel Generators Output Breaker Protection Circuits Contained Instantaneous Overcurrent Tripping Relays.Caused by Design Deficiency.Trip Relay Settings Increased
| | | 05000280/LER-1987-029, :on 871108,main Control Room Ventilation Isolated Due to High Voltage Output on Chlorine Detector. Caused by Increased Voltage Output Inducing Spurious Signal.Ventilation Sys Realigned |
- on 871108,main Control Room Ventilation Isolated Due to High Voltage Output on Chlorine Detector. Caused by Increased Voltage Output Inducing Spurious Signal.Ventilation Sys Realigned
| | | 05000280/LER-1987-031, :on 871112,containment Isolation Valve Observed to Be Inoperable.Caused by Mechanical Binding of Valve Operator.Valve Operator Freed.Insp Performed on Similar Valves.Engineering Work Request Initiated |
- on 871112,containment Isolation Valve Observed to Be Inoperable.Caused by Mechanical Binding of Valve Operator.Valve Operator Freed.Insp Performed on Similar Valves.Engineering Work Request Initiated
| | | 05000280/LER-1987-032, :on 871111,RCS (EIIS AB) Loop B Average Temp Protection Channel Failed High.Caused by Power Supply Failure of Summator in Signal Conditioning Circuitry. Summator Hagan/4111084-003 Replaced |
- on 871111,RCS (EIIS AB) Loop B Average Temp Protection Channel Failed High.Caused by Power Supply Failure of Summator in Signal Conditioning Circuitry. Summator Hagan/4111084-003 Replaced
| 10 CFR 50.73(a)(2) | | 05000280/LER-1987-033, .On 871124,charging Pump Component Cooling Water Sys (EIIS-CC) Became Inoperable.Caused by Inadequate Hydrostatic Test Procedure.Procedure Enhancement to Include Sys Depressurizing Instructions Planned | .On 871124,charging Pump Component Cooling Water Sys (EIIS-CC) Became Inoperable.Caused by Inadequate Hydrostatic Test Procedure.Procedure Enhancement to Include Sys Depressurizing Instructions Planned | | | 05000280/LER-1987-034, :on 871126,specific Activity Sample of Reactor Coolant Showed Dose Equivalent I-131 of 1.19 Uci/Cc.Caused by Fuel Element Defect in Reactor Core.Required Tech Spec 4.1.2B Implemented |
- on 871126,specific Activity Sample of Reactor Coolant Showed Dose Equivalent I-131 of 1.19 Uci/Cc.Caused by Fuel Element Defect in Reactor Core.Required Tech Spec 4.1.2B Implemented
| 10 CFR 50.73(a)(2) 10 CFR 50.73(o)(2)(vii) | | 05000280/LER-1987-035, :on 870717,emergency Diesel Generator Degraded/ Undervoltage Protection Surveillance Not Performed.Caused by Failure to Incorporate Tech Spec Amend Into Test Program. Special Tests of Interlocks Performed |
- on 870717,emergency Diesel Generator Degraded/ Undervoltage Protection Surveillance Not Performed.Caused by Failure to Incorporate Tech Spec Amend Into Test Program. Special Tests of Interlocks Performed
| | | 05000280/LER-1987-036, :on 871202,during Hot Shutdown Inner Door of Containment Personnel Air Lock Exceeded Leakage Criteria for Periodic Test 16.7.Caused by Inadequate Seal.Shim Welded to Actuator Mechanism to Allow Proper Sealing |
- on 871202,during Hot Shutdown Inner Door of Containment Personnel Air Lock Exceeded Leakage Criteria for Periodic Test 16.7.Caused by Inadequate Seal.Shim Welded to Actuator Mechanism to Allow Proper Sealing
| | | 05000280/LER-1987-037, :on 871203,emergency Diesel Generator 3 Automatically Started.Caused by Blown Fuse & Failed Relay. Undervoltage Relay 59 ABC-1J1 & Dc Control Fuse Replaced.W/ |
- on 871203,emergency Diesel Generator 3 Automatically Started.Caused by Blown Fuse & Failed Relay. Undervoltage Relay 59 ABC-1J1 & Dc Control Fuse Replaced.W/
| | | 05000280/LER-1987-038, :on 871208,calculated Offsite Thyroid Dose from Steam Generator Tube Rupture Increased Due to Potential post-trip Steam Generator Tube Bundle Uncovery.Caused by Reanalysis Using Updated FSAR Assumptions |
- on 871208,calculated Offsite Thyroid Dose from Steam Generator Tube Rupture Increased Due to Potential post-trip Steam Generator Tube Bundle Uncovery.Caused by Reanalysis Using Updated FSAR Assumptions
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000280/LER-1987-039, :on 871215,protection Sys Channel Inoperable Due to Failed Summator in Signal Conditioning Circuit.Caused by Loss of Power to Summator.Affected Protection Channels & Summator Replaced & Returned to Normal |
- on 871215,protection Sys Channel Inoperable Due to Failed Summator in Signal Conditioning Circuit.Caused by Loss of Power to Summator.Affected Protection Channels & Summator Replaced & Returned to Normal
| | | 05000280/LER-1987-040, :on 871231,discovered That Containment Hog Particulate Filters Unintentionally Discarded.Caused by Failure to Perform Sr-89 & Sr-90 Analyses.Personnel Reinstructed in Procedures |
- on 871231,discovered That Containment Hog Particulate Filters Unintentionally Discarded.Caused by Failure to Perform Sr-89 & Sr-90 Analyses.Personnel Reinstructed in Procedures
| 10 CFR 50.73(a)(2)(i) |
|