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Category:Letter
MONTHYEARCNL-24-074, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-10-23023 October 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions IR 05000390/20243012024-10-17017 October 2024 Operator Licensing Examination Approval 05000390/2024301 and 05000391/2024301 ML24282B0412024-10-15015 October 2024 Request for Withholding Information from Public Disclosure for Sequoyah Nuclear Plant, Units 1 and 2 and Watts Bar Nuclear Plant, Units 1 and 2 ML24261C0062024-10-0404 October 2024 Correction to Amendment No. 134 to Facility Operating License No. NPF-90 and Amendment No. 38 to Facility Operating License No. NPF-96 ML24260A1682024-10-0404 October 2024 Regulatory Audit Summary Related to Request to Add and Revise Notes Related to Technical Specification Table 3.3.2-1, Function 5 ML24284A1072024-09-26026 September 2024 Affidavit for Request for Withholding Information from Public Disclosure for Sequoyah Nuclear Plant, Units 1 and 2, and Watts Bar Nuclear Plant, Units 1 and 2 CNL-24-047, Decommitment of Flood Mode Mitigation Improvement Systems2024-09-24024 September 2024 Decommitment of Flood Mode Mitigation Improvement Systems CNL-24-060, Supplement to Request for Approval of the Tennessee Valley Authority Nuclear Quality Assurance Program Description2024-09-24024 September 2024 Supplement to Request for Approval of the Tennessee Valley Authority Nuclear Quality Assurance Program Description ML24262A0602024-09-23023 September 2024 Summary of August 19, 2024, Meeting with Tennessee Valley Authority Regarding a Proposed Supplement to the Tennessee Valley Authority Nuclear Quality Assurance Plan CNL-24-065, Tennessee Valley Authority – Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-09-18018 September 2024 Tennessee Valley Authority – Central Emergency Control Center Emergency Plan Implementing Procedure Revisions 05000390/LER-2024-002, Automatic Reactor Trip Due to Main Generator Protection Relay Actuation2024-09-0505 September 2024 Automatic Reactor Trip Due to Main Generator Protection Relay Actuation IR 05000390/20240052024-08-28028 August 2024 Updated Inspection Plan and Assessment Follow-Up Letter for Watts Bar Nuclear Plant, Units 1 and 2 - Report 05000390-2024005 and 05000391-2024005 ML24218A1442024-08-27027 August 2024 Issuance of Amendment Nos. 169 and 75 Regarding Technical Specification Surveillance Requirement 3.9.5.1 to Reduce the Residual Heat Removal Flow Rate IR 05000390/20244022024-08-20020 August 2024 – Security Baseline Inspection Report 05000390-2024402 and 05000391/2024402 - Public CNL-24-061, Supplement to Application to Revise Function 5 of Technical Specification Table 3.3.2-1, ‘Engineered Safety Feature Actuation System Instrumentation,’ for the Sequoyah and Watts Bar (SQN-TS-23-02 and WBN-TS-23-08),2024-08-19019 August 2024 Supplement to Application to Revise Function 5 of Technical Specification Table 3.3.2-1, ‘Engineered Safety Feature Actuation System Instrumentation,’ for the Sequoyah and Watts Bar (SQN-TS-23-02 and WBN-TS-23-08), ML24219A0262024-08-12012 August 2024 Request for Withholding Information from Public Disclosure IR 05000390/20240022024-08-0707 August 2024 Integrated Inspection Report 05000390/2024002 and 05000391/2024002 Rev ML24204A2652024-07-25025 July 2024 Regulatory Audit Summary Related to Request to Revise Technical Specification Surveillance Requirement 3.9.5.1 to Reduce the Residual Heat Removal Flow Rate ML24199A0012024-07-22022 July 2024 Clarification and Correction to Exemption from Requirement of 10 CFR 37.11(c)(2) ML24170A8002024-07-15015 July 2024 Issuance of Amendment Nos. 168 and 74 Regarding Revision to Technical Specification Table 1.1-1 for Required Number of Fully Tensioned Reactor Pressure Vessel Head Closure Bolts ML24172A1342024-07-15015 July 2024 Exemptions from 10 CFR 37.11(C)(2) (EPID L-2023-LLE-0024) - Letter IR 05000390/20244402024-07-12012 July 2024 95001 Supplemental Inspection Supplemental Report 05000390-2024440 and 05000391-2024440 and Follow-Up Assessment Letter 05000391/LER-2024-003, Inoperability of Both Trains of Unit 2 Low Head Safety Injection2024-07-11011 July 2024 Inoperability of Both Trains of Unit 2 Low Head Safety Injection ML24131A0012024-07-0202 July 2024 Issuance of Amendment Nos. 167 and 73 Regarding Adoption of Technical Specification Task Force Traveler TSTF-427-A, Revision 2 CNL-24-052, Response to Request for Additional Information Regarding Application to Modify the Technical Specification Surveillance Requirement 3.9.5.1 (WBN-TS-21-14)2024-06-27027 June 2024 Response to Request for Additional Information Regarding Application to Modify the Technical Specification Surveillance Requirement 3.9.5.1 (WBN-TS-21-14) CNL-24-018, License Amendment Request for Adoption of Technical Specification Task Force Traveler TSTF-276-A, Revision 2, Regarding TS 3.8.1 AC Sources – Operating to Clarify Requirements for Diesel Generator Testing (WBN-TS2024-06-25025 June 2024 License Amendment Request for Adoption of Technical Specification Task Force Traveler TSTF-276-A, Revision 2, Regarding TS 3.8.1 AC Sources – Operating to Clarify Requirements for Diesel Generator Testing (WBN-TS ML24089A1152024-06-21021 June 2024 Transmittal Letter, Environmental Assessments and Findings of No Significant Impact Related to Exemption Requests from 10 CFR 37.11(c)(2) ML24141A0482024-05-17017 May 2024 EN 56958_1 Ametek Solidstate Controls, Inc ML24100A7642024-05-16016 May 2024 Issuance of Amendment No. 166 Regarding Revision to Technical Specification 3.8.2, AC Sources-Shutdown, to Remove Reference to C-S Diesel Generator (CNL-23-062) IR 05000390/20240012024-05-14014 May 2024 Integrated Inspection Report 05000390/2024001 and 05000391/2024001 CNL-24-040, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-05-0808 May 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions 05000391/LER-2024-002, Re Automatic Reactor Trip Due to Steam Generator 3 Level LO-LO2024-05-0606 May 2024 Re Automatic Reactor Trip Due to Steam Generator 3 Level LO-LO IR 05000391/20240072024-04-30030 April 2024 Assessment Follow-up Letter for Watts Bar Nuclear Plant, Unit 2 – Report 05000391/2024007 ML24120A1182024-04-29029 April 2024 – Notification of NRC Supplemental Inspection (95001) and Request for Information CNL-24-037, Clinch River, Sequoyah, Units 1 and 2, Watts Bar, Unit 1 and 2, Nuclear Quality Assurance Plan, TVA-NQA-PLN89-A, Revision 422024-04-22022 April 2024 Clinch River, Sequoyah, Units 1 and 2, Watts Bar, Unit 1 and 2, Nuclear Quality Assurance Plan, TVA-NQA-PLN89-A, Revision 42 ML24087A1912024-04-18018 April 2024 Exemption from Select Requirements of 10 CFR Part 73, Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting CNL-24-024, Hydrologic Engineering Center River Analysis System Project Milestone Status Update2024-04-17017 April 2024 Hydrologic Engineering Center River Analysis System Project Milestone Status Update CNL-24-033, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-04-17017 April 2024 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions CNL-24-010, License Amendment Request to Recapture Low-Power Testing Time (WBN-TS-23-19)2024-04-17017 April 2024 License Amendment Request to Recapture Low-Power Testing Time (WBN-TS-23-19) ML24072A0052024-04-15015 April 2024 Issuance of Amendment Nos. 165 and 72 Regarding Increase in the Maximum Number of Tritium Producing Burnable Absorber Rods and Supporting Changes, and Revision to the Updated Final Safety Analysis Report CNL-24-004, Application to Modify the Watts Bar Nuclear Plant, Unit 1 and Unit 2 Technical Specifications for Main Control Room Chiller Completion Time Extension (WBN-TS-23-13)2024-04-0404 April 2024 Application to Modify the Watts Bar Nuclear Plant, Unit 1 and Unit 2 Technical Specifications for Main Control Room Chiller Completion Time Extension (WBN-TS-23-13) IR 05000390/20244012024-04-0202 April 2024 – Security Baseline Inspection Report 05000390/2024401 and 05000391/2024401 - (Public) CNL-24-020, Clinch River, Sequoyah, Units 1 and 2, Watts Bar, Units 1 and 2, Request for Approval of Quality Assurance Program Description and Application to Revise the Technical Specifications Associated with QAPD Requirements2024-04-0101 April 2024 Clinch River, Sequoyah, Units 1 and 2, Watts Bar, Units 1 and 2, Request for Approval of Quality Assurance Program Description and Application to Revise the Technical Specifications Associated with QAPD Requirements CNL-24-008, Guarantee of Payment of Deferred Premiums - 2023 Annual Report2024-03-27027 March 2024 Guarantee of Payment of Deferred Premiums - 2023 Annual Report CNL-24-007, Annual Insurance Status Report2024-03-27027 March 2024 Annual Insurance Status Report CNL-24-025, Notice of Intent to Pursue License Renewal for Watts Bar Nuclear Plant, Unit 1 - Submittal Schedule2024-03-25025 March 2024 Notice of Intent to Pursue License Renewal for Watts Bar Nuclear Plant, Unit 1 - Submittal Schedule ML24081A0262024-03-21021 March 2024 Emergency Plan Implementing Procedure Revisions ML24079A0312024-03-19019 March 2024 Wb 2024-301, Corporate Notification Letter (210-day Ltr) CNL-24-031, Supplement to Request for Exemption from Various Part 72 Regulations Resulting from Fuel Basket Design Control Compliance2024-03-18018 March 2024 Supplement to Request for Exemption from Various Part 72 Regulations Resulting from Fuel Basket Design Control Compliance CNL-24-029, Response to Request for Additional Information Regarding Tennessee Valley Authority - Request for Exemption from Specific Requirements of 10 CFR Part 372024-03-14014 March 2024 Response to Request for Additional Information Regarding Tennessee Valley Authority - Request for Exemption from Specific Requirements of 10 CFR Part 37 2024-09-05
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000390/LER-2024-002, Automatic Reactor Trip Due to Main Generator Protection Relay Actuation2024-09-0505 September 2024 Automatic Reactor Trip Due to Main Generator Protection Relay Actuation 05000391/LER-2024-003, Inoperability of Both Trains of Unit 2 Low Head Safety Injection2024-07-11011 July 2024 Inoperability of Both Trains of Unit 2 Low Head Safety Injection 05000391/LER-2024-002, Re Automatic Reactor Trip Due to Steam Generator 3 Level LO-LO2024-05-0606 May 2024 Re Automatic Reactor Trip Due to Steam Generator 3 Level LO-LO WBL-24-013, Automatic Reactor Trip Due to Main Generator Protection Relay Actuation2024-03-27027 March 2024 Automatic Reactor Trip Due to Main Generator Protection Relay Actuation WBL-24-006, Automatic Reactor Trip Due to Loss of Main Feedwater Regulating Valve Control2024-02-29029 February 2024 Automatic Reactor Trip Due to Loss of Main Feedwater Regulating Valve Control 05000391/LER-2017-0052018-01-25025 January 2018 Unplanned Emergency Core Cooling System Injection into the Reactor Coolant System due to Personnel Error, LER 17-005-00 for Watts Bar, Unit 2, Regarding Unplanned Emergency Core Cooling System Injection into the Reactor Coolant System due to Personnel Error 05000390/LER-2017-0152018-01-0808 January 2018 Failure to Enter Limiting Condition of Operation Action Statement Results in a Condition Prohibited by Technical Specifications, LER 17-015-00 for Watts Bar, Units 1 and 2, Regarding Failure to Enter Limiting Condition of Operation Action Statement Results in a Condition Prohibited by Technical Specifications 05000390/LER-2017-0142017-12-20020 December 2017 Main Control Room Boundary Door Left Open Leading to a Loss of Safety Function, LER 17-014-00 for Watts Bar, Unit 1, Regarding Main Control Room Boundary Door Left Open Leading to a Loss of Safety Function 05000390/LER-2017-0122017-10-23023 October 2017 Error in Plant Emergency Procedures Leads to a Condition Prohibited by the Technical Specifications, LER 17-012-00 for Watts Bar, Unit 1, Regarding Error in Plant Emergency Procedures Leads to a Condition Prohibited by the Technical Specifications 05000390/LER-2017-0112017-10-23023 October 2017 Failure to Enter Technical Specification 3.6.3 for Containment Isolation Valve, LER 17-011-00 for Watts Bar, Unit 1, Regarding Failure to Enter Technical Specification 3.6.3 for Containment lsolation Valve 05000390/LER-2017-0102017-10-10010 October 2017 Actuation of Turbine Driven Auxiliary Feedwater Pump Due to Loss of 6.9kV Shutdown Board, LER 17-010-00 for Watts Bar Nuclear Plant, Unit 1 Regarding Actuation of Turbine Driven Auxiliary Feedwater Pump Due to Loss of 6.9kV Shutdown Board 05000391/LER-2017-0042017-09-25025 September 2017 Manual Reactor Trip Due to Inoperable Rod Position Indication, LER 17-004-00 for Watts Bar Nuclear Plant, Unit 2 Regarding Manual Reactor Trip Due to Inoperable Rod Position Indication 05000390/LER-2017-0042017-08-31031 August 2017 Manual Reactor Trips Due to Failed Reactor Coolant Pump Power Transfer During Plant Startup, LER 17-004-01 for Watts Bar, Unit 1, Regarding Manual Reactor Trips Due to Failed Reactor Coolant Pump Power Transfer During Plant Startup 05000390/LER-2017-0082017-08-14014 August 2017 Shield Building Inoperability and Potential Loss of Safety Function Resulting from Spurious Equipment Operation, LER 17-008-00 for Watts Bar, Unit 1, Regarding Shield Building Inoperability and Potential Loss of Safety Function Resulting from Spurious Equipment Operation 05000390/LER-2017-0072017-08-0808 August 2017 Multiple Unreported Potential Loss of Safety Function Events Associated with Inoperable Single Train Systems Due to Misinterpretation of Reporting Guidance, LER 17-007-00 for Watts Bar, Unit 1, Regarding Multiple Unreported Potential Loss of Safety Function Events Associated with Inoperable Single Train Systems Due to Misinterpretation of Reporting Guidance 05000390/LER-2017-0062017-07-31031 July 2017 Structural Degradation of 161 kV Line Pole Leads to a Condition Prohibited by Technical Specifications, LER 17-006-00 for Watts Bar, Unit 1, Regarding Structural Degradation of 161 kV Line Pole Leads to a Condition Prohibited by Technical Specifications 05000390/LER-2017-0052017-07-10010 July 2017 Isolation of the 1 B-B Safety Injection Pump Leads to Condition Prohibited by Technical Specifications, LER 17-005-00 for Watts Bar re Isolation of the 1B-B Safety Injection Pump Leads to a Condition Prohibited by Technical Specifications 05000391/LER-2017-0032017-05-22022 May 2017 Automatic Start of Auxiliary Feedwater System Due to Main Condenser Failure, LER 17-003-00 for Watts Bar, Unit 2, Regarding Automatic Start of Auxiliary Feedwater System Due to Main Condenser Failure 05000391/LER-2017-0022017-05-12012 May 2017 Manual Reactor Trip as a Result of a Secondary Plant Transient, LER 17-002-00 for Watts Bar, Unit 2, Regarding Manual Reactor Trip as a Result of a Secondary Plant Transient 05000391/LER-2017-0012017-05-0303 May 2017 Containment Airlock Function Lost Due to Equalizing Valve Not Closing, LER 17-001-00 for Watts Bar, Unit 2, Regarding Containment Airlock Function Lost Due to Equalizing Valve Not Closing 05000390/LER-2017-0032017-03-0303 March 2017 Inadequate Operability Determination Leads to a Condition Prohibited by the Technical Specifications, LER 17-003-00 for Watts Bar, Unit 1, Regarding Inadequate Operability Determination Leads to a Condition Prohibited by the Technical Specifications 05000390/LER-2017-0022017-02-22022 February 2017 Incorrectly Hung Clearance Leads to a Condition Prohibited by the Technical Specifications, LER 17-002-00 for Watts Bar Nuclear Plant, Unit 1, Regarding: Incorrectly Hung Clearance Leads to a Condition Prohibited by the Technical Specifications 05000390/LER-2016-0112016-12-0909 December 2016 Loss of Centrifugal Charging Pump Due to Repeat Failure of Associated Room Cooler, LER 16-011-01 for Watts Bar Nuclear Plant, Unit 1 Regarding Loss of Centrifugal Charging Pump Due to Repeat Failure of Associated Room Cooler 05000391/LER-2016-0082016-10-28028 October 2016 Reactor Trip Resulting from Failure of 2B Main Bank Transformer, LER 16-008-00 for Watts Bar, Unit 2, Regarding Reactor Trip Resulting from Failure of 2B Main Bank Transformer 05000391/LER-2016-0052016-08-19019 August 2016 Main Feedwater Pump Trip on Loss of Condenser Vacuum Leads to Turbine Trip and Reactor Trip, LER 16-005-00 for Watts Bar, Unit 2, Regarding Main Feedwater Pump Trip on Loss of Condenser Vacuum Leads to Turbine Trip and Reactor Trip 05000390/LER-2016-0102016-08-0808 August 2016 Emergency Diesel Generator Crankcase Pressure Switches Not Analyzed to Withstand the Effects of a Tornado, LER-16-010-00 for Watts Bar Nuclear Plant, Units 1 and 2 Regarding Emergency Diesel Generator Crankcase Pressure Switches Not Analyzed to Withstand the Effects of a Tornado 05000391/LER-2016-0042016-08-0404 August 2016 Reactor Trip and Safety Injection Actuation Caused by Turbine Governor Valve Failure, LER 16-004-00 for Watts Bar, Unit 2, Regarding Reactor Trip and Safety Injection Actuation Caused by Turbine Governor Valve Failure 05000391/LER-2016-0032016-07-27027 July 2016 Turbine Driven Auxiliary Feedwater Pump Inoperable for Longer than Allowable Outage Time due to Governor Valve Spring Over-Tensioning, LER 16-003-00 for Watts Bar, Unit 2, Regarding Turbine Driven Auxiliary Feedwater Pump lnoperable for Longer Than Allowable Outage Time Due to Governor Valve Spring Over-Tensioning 05000390/LER-2016-0082016-07-15015 July 2016 Emergency Diesel Generator Manual Start Due to Loss of Voltage on the 6.9kV Shutdown Board 1B-B, LER 16-008-00 for Watts Bar, Unit 1, Regarding Emergency Diesel Generator Manual Start Due to Loss of Voltage on the 6.9kV Shutdown Board 1B-B 05000390/LER-2016-0092016-07-15015 July 2016 Failure to Complete Surveillance Requirements Causes a Condition Prohibited by the Technical Specifications, LER 16-009-00 for Watts Bar, Unit 1, Regarding Failure to Complete Surveillance Requirements Causes Conditions Prohibited by the Technical Specifications 05000391/LER-2016-0022016-07-11011 July 2016 Turbine Driven Auxiliary Feedwater Pump Inoperable for Longer than Allowable Outage Time due to Turbine Speed Control Failure, LER 16-002-00 for Watts Bar, Unit 2, Regarding Turbine Driven Auxiliary Feedwater Pump Inoperable for Longer Than Allowable Outage Time Due to Turbine Speed Control Failure 05000390/LER-2016-0062016-06-30030 June 2016 Undersized Room Cooler Fan Shaft Results in Loss of Centrifugal Charging Pump, LER 16-006-00 for Watts Bar, Unit 1, Regarding Undersized Room Cooler Fan Shaft Results in Loss of Centrifugal Charging Pump 05000390/LER-2016-0072016-06-20020 June 2016 Technical Specification Action Not Met for Rod Position Indication, LER 16-007-00 for Watts Bar Nuclear Plant, Unit 1 Regarding Technical Specification Action Not Met for Rod Position Indication 05000391/LER-2016-0012016-06-13013 June 2016 Loss of Automatic Containment Isolation for the Steam Generator Blowdown Sampling Lines, LER 16-001-00 for Watts Bar, Unit 2, Regarding Loss of Automatic Containment Isolation for the Steam Generator Blowdown Sampling Lines 05000390/LER-2016-0042016-05-23023 May 2016 Automatic Reactor Trip Due to Actuation of Over Temperature Delta Temperature Bistables, LER 16-004-00 for Watts Bar, Unit 1, Regarding Automatic Reactor Trip Due to Actuation of Over Temperature Delta Temperature Bistables 05000390/LER-2016-0052016-05-13013 May 2016 Both Trains of Unit 1 Emergency Gas Treatment System Inoperable During Unit 2 Testing, LER 16-005-00 for Watts Bar, Unit 1, Regarding Both Trains of Unit 1, Emergency Gas Treatment System Inoperable During Unit 2, Testing 05000390/LER-2016-0032016-05-10010 May 2016 Technical Specification Surveillance Requirement Not Met During Emergency Core Cooling System Venting, LER 16-003-00 for Watts Bar, Unit 1, Regarding Technical Specification Surveillance Requirement Not Met During Emergency Core Cooling System Venting 05000390/LER-2016-0022016-05-0404 May 2016 Technical Specification Action Not Met for Inoperable Containment Isolation Valve, LER 16-002-00 for Watts Bar, Unit 1, Regarding Technical Specification Action Not Met for Inoperable Containment Isolation Valve 05000390/LER-2016-0012016-03-0909 March 2016 Channel Mode Switch in Incorrect Position Renders Lower Containment Atmosphere Particulate Radiation Monitor Inoperable, LER 16-001-00 for Watts Bar, Unit 1, Regarding Channel Mode Switch in Incorrect Position Renders Lower Containment Atmosphere Particulate Radiation Monitor Inoperable ML1134703432011-12-13013 December 2011 Withdrawal of License Event Report 390/2011-003, Mode Change Without Meeting Limiting Condition for Operation (LCO) 3.7.5 2024-09-05
[Table view] |
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text
TENNESSEE VALLEY 1\\'4 AUTHORITY
Te n n essee V alley A ut ho rity, Post Office Bo x 2000, Spring City, Tennessee 37381
WBL-24-017
May 06, 2024
10 CFR 50.73
ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555-0001
Watts Bar Nuclear Plant, Unit 2 Facility Operating License No. NPF-96 NRC Docket No. 50-391
Subject: Licensee Event Report 391 / 2024 - 002-00, Automatic Reactor Trip Due to Steam Generator #3 Level LO-LO
Pursuant to the reporting requirements of 10 CFR 50.73, attached is the subject Licensee Event Report concerning the Automatic Reactor Trip and Reactor Protection System Actuation for Watts Bar Nuc lear Plant, Unit 2, which occurred on March 05, 2024.
There are no new regulatory commitments contained in this letter. Please direct any questions concerning this matter to Jonathan Johnson, WBN Licensing Manager, at jtjohnsonO@tva.gov.
~ ~ ~-
Anthony L. Williams IV Site Vice President Watts Bar Nuclear Plant U.S. Nuclear Regulatory Commission WBL-24-017 Page 2 May 06, 2024
Enclosure : LER 391/2024-002-00, "Automatic Reactor Trip Due to Steam Generator #3 Level LO - LO "
cc (w/Enclosure) :
NRC Regional Administrator - Region 11 NRC Senior Resident Inspector - Watts Bar Nuclear Plant NRC Project Manager - Region II ENCLOSURE Tennessee Valley Authority Watts Bar Nuclear Plant Unit 2
LER 391/2024 -002-00, " Automatic Reactor Trip Due to Steam Generator #3 Level LO -LO "
WBL-24-017 E1 of 1 NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB : NO. 3150-0104 EXPIRES : 04/30/2027 (04-02-2024) Estimated
- 1. Facility Name rzl 050 2. Docket Number 3. Page Watts Bar Nuclea r Plant, Unit 2 052 1 OF 6 00391
4. Title Automatic Reactor Trip Due to Steam Generator #3 Level LO-LO
- 5. Event Date 6. LER Number 7. Report Date 8. Other Facilities Involved Month Day Year Number No. N/A 050
03 05 2024 2024 - 002 - 00 05 06 2024 Fac iN/A 052 lity Nam e Do c ket Numb er
- 9. Operating Mode 10. Power Level 1 100 11. This Report is Submitted Pursuant to the Requirements of 10 CFR § : (Check all that apply )
10 CFR Part 20 20. 2203(a)(2)(vi) 10 CFR Part 50 50. 73(a)(2)(ii)(A) 50. 73(a)(2)(viii)(A) 73.1200(a) 2O. 2201(b) 20. 2203(a)(3)(i) 50. 36(c)(1 )(i)(A) 50. 73(a)(2)(ii)(B) 50. 73(a)(2)(viii)(B) 73.1200(b) 20. 2201(d) 20.2203(a)(3)(ii) 50. 36(c)(1 )(ii)(A) 50. 73(a)(2)(iii) 50. 73(a)(2)(ix)(A) 73.1200(c) 20. 2203(a)(1) 20. 2203(a)(4) 50.36(c)(2) rzl 50. 73(a)(2)(iv)(A) 50.73( a)(2)(x) 73.1200(d) 20. 2203(a)(2)( i) 10 CFR Part 21 50.46(a)(3)(ii) 50.73(a)(2)(v)(A ) 10 CFR Part 73 73.1 200(e) 20.2203(a)(2)(ii) D 21.2(c) 50.69(9) 50.73(a)(2)(v)(B) 73. 77(a)(1) 73.1200(f) 20.2203(a)(2)(iii) 50.73(a)(2)(i)(A) 50. 73(a)(2)(v)(C) 73.77(a)(2)(i) 73.1 200(9) 20.2203(a)(2)(iv) 50.7 3(a)(2)(i)(B) 50.73(a)(2)(v)(D) 73.77(a)(2)(ii) 73.1200(h) 20.2203(a)(2)(v) 50.73(a)(2)(i)(C) 50.73(a)(2)(vii)
OTHER (Specify here, in abstract, or NRC 366A).
- 12. Licensee Contact for this LER Licensee Contact Phone Number (Include area code)
K. R. Skubisz, licens ing program manager 423-365 -1771
- 13. Complete One Line for each Component Failure Described in this Report
Cause System Component Manufacturer Reportable to IRIS Cause System Component Manufacturer Reportable to IRIS A JB HS N/A y N/A N/A N/A N/A N/A
- 14. Supplemental Report Expected Month Day Year
- 15. Expected Submission Date N/A N/A N/A rzl No ID Yes ( If yes, complete 15. Ex pected S u bm ission Date
16. Abstrac t (Limit to 1326 spaces, i.e., approximately 13 single-spaced typewritten lines)
On March 03, 2024, at 0132 Eastern Standard Time (EST), with Unit 2 in Mode 1 at 100 percent power, the reacto r automat ically tripped due to a main feedwater isolation signal which resulted in a steam generator (SG) LO-LO-level reactor trip.
An aux iliary operator inadvertently manipulated 2-HS-3-945-A (Hand Switch For Control Building Isolation). This manipulation caused feedwater to be lost to all steam generators, Unit 2 tripped on LO-LO steam generator water level. A bump guard was placed over this hand-switch.
This event is being reported to the Nuclear Regulatory Commission ( NRC ) under 10 CFR 50.73(a)(2)(iv)(A) as a safety system actuation of the reactor protection system and the auxiliary feedwater (AFW) system.
I. Plant Operating Conditions before the Event
Watts Bar Unit 2 was at 100 percent Rated Thermal Power (RTP).
II. Description of Event
A. Event Summary
On Ma rch 05, 2024, at 0132 EST, with Unit 2 in Mode 1 at 100 percent power, the reactor automatically tripped due to a main feedwater isolation signal which resulted in a steam generator (S G) {EIIS :SG} LO-LO-level reactor trip.
All control rods fully inserted and all automatically actuated safety related equipment operated as designed. At 0144 EST, operations personnel exited the emergency operating in structions after the plant was stabilized.
Unit 1 was not affected.
This event is being reported to the Nu clear Regulatory Commission (NRC) under 10 CFR 50.7 3(a)(2)(iv)(A) as a safety system actuation of the reactor protection system {EIIS :JC} and the auxiliary feedwater (AFW) {EIIS :BA} system.
B. Status of structures, components, or systems that were inoper able at the start of the event and that contributed to the event
There were no safety related inoperable structures, components, or systems that contributed to this event.
C. Dates and a 1proximate times of occurrences Dates and Approximate Occurrence Times An auxiliary operator inadvertently manipulates 2-HS 03/05/2024 0131 EST 945 -A. This manipulation causes feedwater to be isolated from all steam generators. Steam generator water level rapidly lowers.
Unit 2 Reactor trips on LO-LO steam generator water level.
03/05/2024 0132 EST Unit 2 enters Mode 3. Auxiliary feedwater functions r-------------+---- - --~ normally and begins to restore steam generator water level.
03/05/2024 0133 EST The operating crew entered the emergency network procedure E-0, "Reactor Trip or Safety Injection."
The operating crew exited the emergency network and 03/05/2024 0144 EST transitioned to the general operating procedure, 2-GO-5 "Unit Shutdown From 30% Reactor Power To Hot Standby."
03/05/2024 0158 EST 2-HS-3-945-A is restored to its normal pos ition.
03/05/2024 0414 EST The station notified the NRC of the event. Event number 57006 is assigned to this not ification.
D. Manufacturer and model number of each component that failed during the event
Not applicable
E. Other systems or secondary functions affected
None
F. Method of discovery of each component or system failure or procedural error
The effects resulting from the manipulation of 2-HS 945-A were immediately evident to the main control room operat ing crew. Feedwater was lost to all steam generators and 30 seconds after the switch manipulation, Unit 2 tripped on LO-LO steam generator water level.
G. The failure mode, mechanism, and effect of each failed component
Not applicable
H. Operator actions
Operations personnel promptly stabilized the plant following the reactor trip.
I. Automatically and manually initiated safety system responses
The automatic reactor trip was followed by an automatic subsequent turbine trip. Safety systems responded as expected.
Ill. Cause of the event
A. Cause of each component or system failure or personnel error
An auxiliary operator inadvertently manipulated 2-HS-3-945-A. This manipulation caused feedwater to be lost to all steam generators and 30 seconds after the switch manipulation,
Un it 2 tripped on LO - LO steam generator water level.
B. Cause(s) and circumstances for each human performance related root cause
The Human performance error reduction tool "2 minute rule" was inappropriately reduced in scope to where ingress and egress paths were not checked for hazards.
IV. Analysis of the event
While operating at approximately 100 percent power dur ing steady state operation, the Watts Bar Unit 2 reactor experienced an automatic reactor trip at approx imately 01 :32 EST on March 05,
2024, in response to a LO-LO steam generator water level. The LO-LO steam generator water level resulted from a complete loss of normal feedwater flow. Normal feedwater was lost after an auxiliary operator inadvertently manipulated 2-HS-3-945 -A. This event was compared with previous WBN plant trips and was also compared with applicable Final Safety Analys is Report (UFSAR) transients/accidents. The sequence of events associated with the trip were bounded by the FSAR Safety Analysis assumptions. The parameter response for the reactor trip is bounded by the FSAR analyses in UFSAR Section 15.2.8, " Loss of Normal Feedwater." The plant response post-trip was uncomplicated and the plant responded as designed. Operations entered E-0,
"Reactor Trip or Safety Injection," and subsequently transitioned to ES-0.1, "Reactor Trip Response," and 2-GO -5, "Unit Shutdown from 30 percent Reactor Power to Hot Standby ".
B. Corrective Actions to Prevent Recurrence or to reduce the probability of similar events occurring in the future
Master Equipment List (MEL ) changes were submitted to update the nomenclature associated with both 1-HS-3-945-A and 2-HS-3-945-A The new nomenclature states that these Hand Switches (HS) are "Fire Safe Shutdown lsol 1-FCV-3-236, 239, 242, 246 " and "Fire Safe Shutdown lsol 2-FCV-3-236, 239, 242, 246 ".
The plant label for 2-HS-3-945-A was updated with the nomenclature of "Fire Safe Shutdown lsol 2-FCV-3-236, 239, 242, 246 ".
2-HS-3-945-A was identified in the plant as a reactor trip hazard.
VII. Previous Similar Events at the Same Site
A plant trip due to a secondary plant transient which led to a loss of main feedwater was reported to the NRC in LER 391/2017-002-00 dated May 12,2017. This event was attributed to non operations personnel inadvertently depressing the local trip button for the 2A hotwell pump. The event described in this LER is different in that it involved an inadvertent equipment contact by operations personnel.
A plant trip due to a Reactor Coolant System loop low flow was reported to the NRC in LER 391 /2018-001-00 dated June 11,2018. This event was attributed to a failure to recognize the aggregate risk of minor maintenance being performed on the common drain line for the RCS Loop 1 flow transmitters. The maintenance on the common drain line was not identified as work involving trip sensitive equipment during the planning process.
VIII. Additional Information
None.
IX. Commitments
None.