05000333/LER-2022-001, Exhaust Drain Pot Line Filled with Water Up to HPCI Turbine Due to Relay Failure
| ML22179A366 | |
| Person / Time | |
|---|---|
| Site: | FitzPatrick |
| Issue date: | 06/28/2022 |
| From: | Timothy Peter Constellation Energy Generation |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| JAFP-22-0034 LER 2022-001-00 | |
| Download: ML22179A366 (1) | |
| Event date: | |
|---|---|
| Report date: | |
| Reporting criterion: | 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
| 3332022001R00 - NRC Website | |
text
Constellation JAFP-22-0034 June 28, 2022 United States Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C. 20555-0001 James A. FitzPatrick NPP PO Box 110 Lycoming. NY 13093 Timothy C. Peter Site Vice President-JAF James A. FitzPatrick Nuclear Power Plant Renewed Facility Operating License No. DPR-059 NRC Docket No. 50-333
Subject:
Dear Sir or Madam:
LER: 2022-001, Exhaust Drain Pot Line Filled with Water up to HPCI Turbine due to Relay Failure This report is being submitted pursuant to 10 CFR 50. 73(a)(2)(v)(D).
There are no new regulatory commitments contained in this report.
Questions concerning this report may be addressed to Mr. Richard Sullivan, Regulatory Assurance Manager, at (315) 349-6562.
TCP/RS
Enclosure:
LER: 2022-001, Exhaust Drain Pot Line Filled with Water up to HPCI Turbine due to Relay Failure cc:
USNRC, Region I Administrator USNRC, Project Manager USNRC, Resident Inspector INPO Records Center (IRIS)
NRC FORM 366 (08-2020)
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (08-2020)
APPROVED BY OMB: NO. 3150-0104 EXPIRES: 08/31/2023
- 1. Facility Name James A. FitzPatrick Nuclear Power Plant
- 2. Docket Number 05000333
- 3. Page 1 OF 3
- 4. Title LER: 2022-001, Exhaust Drain Pot Line Filled with Water up to HPCI Turbine due to Relay Failure
- 5. Event Date
- 6. LER Number
- 7. Report Date
- 8. Other Facilities Involved
Month
Day
Year
Year Sequential Number Revision No.
Month Day Year Facility Name N/A Docket Number N/A 04 29 2022 2022 - 001 - 00 06 28 2022 Facility Name N/A Docket Number N/A
- 9. Operating Mode 1
- 10. Power Level 100 Month Day Year No Yes (If yes, complete 15. Expected Submission date)
Abstract (Limit to 1560 spaces, i.e., approximately 15 single-spaced typewritten lines)
At 1251 EDT on April 29, 2022, while troubleshooting the failure of the High Pressure Coolant Injection (HPCI)
Exhaust Drain Pot High Level Alarm to clear, it was discovered that the High Pressure Coolant Injection exhaust line condensate drain system was not functioning as designed to support removal of condensate from the turbine exhaust. Troubleshooting determined that a logic relay failed to start the HPCI Gland Seal Condensate pump. This resulted in some water accumulation in the turbine casing.
Subsequently, the High Pressure Coolant Injection System was declared inoperable. The turbine casing was manually drained and the failed relay was replaced. The system was restored to Operable.
As a result, this condition is being reported under 10 CFR 50.72(b)(3)(v)(D) as a condition that could have prevented fulfillment of the safety function at the time of discovery.
(See NUREG-1022, R.3 for instruction and guidance for completing this form http://www.nrc.gov/reading-rm/doc-collections/nuregs/staff/sr1022/r3/)
(See Page 3 for required number of digits/characters for each block)
LICENSEE EVENT REPORT (LER)
=
Background===
The High Pressure Coolant Injection (HPCI) System [EIIS Identifier: BJ] at James A. FitzPatrick Nuclear Power Plant (JAF) is a part of the Emergency Core Cooling System (ECCS); HPCI provides and maintains an adequate coolant inventory inside the Reactor Pressure Vessel [RPV] to prevent damage to the reactor core under postulated accident scenarios. The system is comprised of various components which include pumps, valves, piping, and instrumentation. The HPCI system is powered by a steam turbine using steam from the reactor. Steam is pressurized up to the admission valve 23MOV-14 which will open to admit steam to the HPCI turbine on a system initiation signal.
HPCI has a Gland Exhaust System to collect steam leakage from the turbine shaft seals, turbine control & stop valve stems, and turbine exhaust casing drains. The system works with the HPCI exhaust Drain Pot to collect condensation from the bonnets of several valves and the HPCI turbine casing. The condensation is collected in the Gland Seal Condenser, and then pumped to Radwaste while in a standby lineup.
23LS-98 senses level in the Exhaust Drain Pot, causes Annunciator ARP-09-3-3-18 (HPCI Exhaust Drain Pot Level High) and opens a valve to allow the Drain Pot to drain to the Gland Seal Condenser.
23LS-100 senses level in the Gland Seal Condenser, energizes 23A-K31, and auto starts the 23P-141 (HPCI Gland Seal Condensate Pump) to pump the Gland Seal Condenser to Radwaste.
Event Description
On April 28, 2022, at 2245, control room annunciator ARP-09-3-3-18, HPCI drain pot water level alarm was received. Troubleshooting determined that HPCI logic relay 23A K31 failed to activate the HPCI Gland Seal Condensate pump to remove condensate from the turbine exhaust. As a result, water from 23MOV-14 steam leakby had accumulated in the HPCI turbine casing.
The crew placed the HPCI auxiliary oil pump in Pull to Lock to mitigate any potential impact to personnel while draining the HPCI exhaust. The Pull to Lock switch position prevents the HPCI turbine from starting. The HPCI Exhaust Drain Pot was manually drained by Operations. Following draining, the HPCI system was declared operable.
The condition was reported as a condition which could have prevented fulfillment of a safety function to mitigate the consequences of an accident per 10 CFR 50.72(b)(3)(v)(D), as submitted by ENS 55871.
Event Analysis
Level switch 23LS-100 senses water level in the HPCI gland seal condenser. On a high level, the level switch actuates relay 23A-K31 which alarms in the control room and starts the HPCI gland seal condenser pump (23P-141). The pump removes the condensate by pumping the water to the radwaste system. Troubleshooting determined that 23A-K31 had failed, preventing the auto start of 23P-141. This caused the HPCI exhaust drain pot to fill with condensate and subsequently a volume of condensate also accumulated in the HPCI turbine casing.
The potential effects of water in the HPCI turbine casing is that a slug of water could cause a HPCI exhaust rupture disk diaphragm to be damaged upon HPCI initiation. Another potential effect of water in the turbine U.S. NUCLEAR REGULATORY COMMISSION (08-2020)
LICENSEE EVENT REPORT (LER)
CONTINUATION SHEET APPROVED BY OMB: NO. 3150-0104 EXPIRES: 08/31/2023
- 3. LER NUMBER James A. FitzPatrick Nuclear Power Plant 05000 - 333 YEAR SEQUENTIAL NUMBER REV N0.
2022
- - 001
- - 00 Page 3 of 3 (See NUREG-1022, R.3 for instruction and guidance for completing this form http://www.nrc.gov/reading-rm/doc-collections/nuregs/staff/sr1022/r3/)
exhaust line is that it could cause abnormal turbine operation due to high exhaust pressure. The backup of water into the HPCI turbine is a condition that could have prevented the operation of HPCI and is reportable per 10 CFR 50.73(a)(2)(v)(D).
Cause
The direct cause of this event was a failure of 23A-K31 from actuating 23P-141 to pump down the condensate water before it filled the HPCI exhaust drain pot.
Similar Events
Condition Report: AR 04381156,Suspected leakage past 23MOV-14, dated October 31, 2020 FAILED COMPONENT IDENTIFICATION:
Manufacturer:
General Electric Manufacturer Model Number:
CR2820B SERIES A Manufacturer Code:
G080 Component Code:
RLY FitzPatrick Component ID:
Corrective Actions
Completed Actions Operators manually drained the HPCI Drain Pot The HPCI Logic Relay 23A-K31 was replaced Planned Actions Evaluate PM strategy for affected relay and condensate drain system.
Perform further analysis on impacts of water in HPCI turbine casing.
Operations refresher training on Abnormal Condition Monitoring Plans.
Safety Significance
Nuclear safety - There were no actual consequences caused by this condition. The potential consequence during a postulated accident scenario is when HPCI actuates, the water present in the turbine could damage or prevent the system operation. While HPCI is operating, the ability to drain water through the drain pot is not required for continued system operation since excess water accumulation is pushed out with steam exhaust.
The risk for this event is restricted to the period when the relay failed to automatically actuate the pump to remove water which was determined to be less than 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br />.
References Issue Report - IR 04496616, HPCI Exhaust Drain Pot Level Hi Troubleshooting, dated April 29, 2022