ML20246D896

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Insp Rept 50-344/89-05 on 890212-0325.Violations Noted.Major Areas Inspected:Safety Verification,Maint,Surveillance,Event Followup,Design Engineering & Open Item Followup
ML20246D896
Person / Time
Site: Trojan File:Portland General Electric icon.png
Issue date: 04/19/1989
From: Rebecca Barr, Mendonca M, Obrien J, Suh G, Wagner W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML20246D887 List:
References
50-344-89-05, 50-344-89-5, NUDOCS 8905110081
Download: ML20246D896 (26)


See also: IR 05000344/1989005

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NUCLEAR REGULATORY COMMISSION

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. Report No.

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License No.

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- Licensee':

Portland General. Electric Company

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121.S.W. Salmon Street

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Portland, OR 97204.

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Facility Name: Trojan

. Inspection at: Rainier, Oregon

Inspection conducted:

February 12 - March 25, 1989

Inspectors:

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R. C. Barr

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Date Signed-

. Senior. Resident Inspector--

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Date-Signed

Resident Inspector

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J. P. O'Brien-

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Reactor Project Inspector-

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Approved By:

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M. M. Mendonca, Chief

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Reactor Projects Section 1

Summary;

Inspection on February 12 - March 25, 1989 (Report 50-344/89-05)

Areas Inspected;

Routine' inspection of operational safety verification.

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maintenance, surveillance, event follow-up, design engineering, and open item

follow-up.

Inspection procedures 30702,~30703, 37200, 37702, 38703, 61726,

62703, 71707, 90712, 92700,'92701 and 93702 were used as guidance during the

conduct of the inspection.

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Results:

This inspection identified six violations of NRC requirements.

Paragraph 3 discusses log keeping practices including the failure to log an

entry into containment while at power.

Paragraph 6 discusses inadequate work instructions of a maintenance request

for calibrating reactor plant control instruments.

Paragraph 6 also discusses

the requirements set forth in Regulatory Guide 1.33 for calibration procedures

for each instrument covered by Technical Specifications.

Paragraph 6 also discusses the need for supervisors to conduct detailed

pre-work briefing, particularly when work scope or work plans change.

Paragraph 7 discusses an instance where the reporting requirements of 10 CFR 50.73 for a 30 day Licensee Event Report was exceeded.

Paragraph 10 discusses the failure to follow procedural requirements in the

. control of top tier drawings.

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' Paragraph 11 discusses the failure to follow QA procedures for processing a

Non-Conformance Report (NCR) that allowed non-conforming weld filler material

to be used, and inadequate documentation of its use.

The subjects of these violations, quality of Maintenance work instructions,

procedural compliance and detailed supervisory and management involvement with

routine activities and off-normal events has our heightened concern.

There

appears to be a reluctance by both line and quality reviewers to challenge low

quality work instructions.

Additionally Managements' actions and follow-up

for improving the quality of work instructions, as exemplified by the steam

generator water level transient event, has been only partially effective.

As

a result of recent events, the licensee has taken action to lower the

threshold for when and how soon critiques will be held following off-normal

events.

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DETAILS

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Persons Contacted

+*D.

W. Cockfield, Vice President, Nuclear

+*C. P. Yundt, Plant General Manager

+*T. D. Walt, General Manager, Technical Functions

+ L. W.-Erickson, Manager,. Nuclear Quality Assurance

  • R. P. Schmitt, Manager, Operations and Maintenance

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+*D. W. Swan, Manager, Technical Services

  • A. N. Roller, Manager, Nuclear Plant Engineering

M. J. Singh, Manager, Plant Modifications

J. D. Reid, Manager, Plant Services

  • J. W. Lentsch, Manager, Personnel Protection
  • J. M. Anderson, Manager, Material Services

M. D. Gatlin, Warehouse Supervisor

  • A. R. Ankrum, Manager, Nuclear Security

+*M. R. Snook, Manager, Quality Support Services

R. E. Susee, Manager, Planning and Scheduling

D. F. . Levin, Supervisor, Plant Modifications

E. A. Curtis, Procurement Supervisor

  • A. M. Puzey, Office Supervisor

P. A. Morton, Branch. Manager, Plant Systems Engineering

R. L. Russell, Operations Supervisor

R. H. Budzeck, Assistant Operations Supervisor

D. L. Bennett, Maintenance Supervisor

R. A. Reinart, Instrument and Control Supervisor

T. O. Meek, Radiation Protection Supervisor

R. W. Ritschard, Security Supervisor

+ C. H. Brown, Operations Branch Manager, Quality Assurance

  • D. L. Nordstrom, Nuclear. Engineer, Nuclear Safety and Regulation

+ D. Wheeler, Quality Inspection Branch Manager

+ R. Prewitt, Quality Systems Supervisor

+ G. A. Zimmerman, Manager NSRD

+ 0. A. Desmarais, Mechanical Engineer, NPE

+ S. A. Bauer, Manager, Nuclear Regulation Branch

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+ J. Carter, Metallur0 st, NPE

+ M. Hoffman, Manager, Mechanical Branch, WPE

+ A. Ciapanno, Welding Engineer / Specialist

The inspectors also interviewed and talked with other licensee employees

during the course of the inspection.

These included shift supervisors,

reactor and auxiliary operators, maintenance personnel, plant

technicians, engineers, and quality assurance personnel.

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+ Denotes those attending the exit interview on March 9, 1989.

  • Denotes those attending the exit interview on March 23, 1989.

2.

Elant Status

The plant operated at 100% power from February 12 through February 24,

1989.

From 8:05 a.m. February 25,1989 to 5:16 a.m. February 26, 1989,

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power was reduced to 55% to repair a circulating water to main condenser

leak.

On March 4,1989, with the reactor at 100% power, a water level

transient occurred in all steam generators as a result of attempting an

instrument calibration tnat could only be performed while shutdown.

Due

to a higher than normal containment atmosphere activity, on March 9,

1989, with the reactor at 100% power, a containment entry was made to

isolate an apparent leaking valve in the pressurizer vapor space sampling

line.

On March 25, 1989, the end of the inspection period, the reactor

was at 100% power with the licensee preparing for the 1989 Refueling

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Outage that is scheduled to begin on April 6, 1989.

3.

Operational Safety Verification (71707)

During this inspection period, the inspectors observed and examined

activities to verify the operational safety of the licensee's facility.

The observations and examinations of those activities were conducted on a

daily, weekly or biweekly basis.

Daily, the inspectors observed control room activities to verify the

licensee's adherence to limiting conditions for operation as prescribed

in the facility Technical Specifications.

Logs, instrumentation,

recorder traces, and other operational records were examined to obtain

information on plant conditions, trends, and compliance with regulations.

On occasions when a shift turnover was in progress, the turnover of

information on plant status was observed to determine that pertinent

information was relayed to the oncoming shift personnel.

The inspectors identified that the containment entry of March 9,1989,

was not recorded in the control operator log.

The containment entry was

logged in the Shift Supervisors log; however, neither the time nor

duration of the entry was recorded.

Further inspection identified that

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the administrative procedure that establishes the requirements for

containment entries, A0-3-11, " Containment Access, Integrity, Evaluation,

and Inspections", Revision 21, dated January 12, 1989, was followed.

The

inspectors noted A0-3-11 did not require logging the entry of

containment; however, Administrative Procedure, A0-3-6, " Conduct of

Operations", Revision 17, dated March 3, 1988, section II.C.7. states for

control operator logs that " Log entries shall include but not be limited

to:

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Maintenance Activities that affect operations..." and " i.

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Performances of special inspections or checks (overspeed trips, oil

filters, etc.)."

The entry into containment while at power to perform

maintenance and inspections clearly falls into these categories because

reactor operations are restricted so as not to change reactivity and

power, and the entry was to conduct a special inspectica and, if

necessary, corrective maintenance. The inspectors concluded that the

containment entry should have been logged in accordance with A0-3-6.

This was identified to the licensee as an apparent Severity Level V

violation (50-344/89-05-01). The inspectors also noted that frequently

the control room log continues to be maintained on scratch paper for

approximately an entire shift and then be transcribed to the legal record

near the end of the shift.

This is contrary to the industry accepted

standard that log entries should be made promptly.

This practice had

previously been discussed with licensee management.

Operations

Management acknowledged the inspector's findings and committed to provide

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additional guidance to the operating crews by clarifying A0-3-11 to

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include the requirement to log all at power containment entries.

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Additionally, the licensee conducted an evaluation of log keeping

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practices against the industry standard and is evaluating the need for

further corrective action.

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Each week the inspectors toured the accessible areas of the facility to

observe the following items:

(a) General' plant and equipment conditions.

(b) Maintenance requests and repairs.

(c) Fire hazards and fire fighting equipment.

(d) Ignition sourcesJand flammable material control.

(e) Conduct of activities in accordance with the licensee's

administrative controls and approved procedures.

(f) Interiors of electrical and control panels.

(g) Implementation of +.he licensee's physical security plun.

(h) Radiation protection controls.

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(i) Plant housekeeping and cleanliness.

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(j) Radioactive waste systems.

(k)= Proper storage of compressed gas bottles.

Weekly, the inspectors examined the licensee's equipment clearance

control with respect to removal of equipment from service to determine

that the licensee complied with technical specification limiting

conditions for operation.

Active clearances were spot-checked to ensure,

that their issuance was consistent with plant status and maintenance

evolutions.

Logs of jumpers, bypasses, caution and test tags were

examined by the irispectors.

Each week the inspectors conversed with operators in the control room,

and with other plant personnel.

The discussions centered on pertinent

topics relating to general plant conditions, procedures, security,

training and other topics related to in progress work activities.

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The inspectors examined the licensee's nonconformance reports (NCRs) to

confirm that deficiencies were identified and tracked by the system and

that these nonconformances were being tracked and followed to the

completion of corrective action.

Further details are provided in

paragraph 11.

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Routine inspections of the licensee's physical security program were

performed in the areas of access control, organization and staffing, and

detection and assessment systems.

The inspectors observed the access

control measures used at the entrance to the protected area, verified the

integrity of portions of the protected area barrier and vital area

barriers, and observed in several instances the implementation of

compensatory measures upon breach of vital area barriers.

The inspectors

noted that the licensee installed new monitors for detecting explosive

materials.

Portions of the isolation zone were verified to be free of

obstructions.

Functioning of central and secondary alarm stations

(including the use of CCTV monitors) was observed.

On a sampling basis,

the inspectors verified that the required minimum number of armed guards

and individuals authorized to direct security activities were on site.

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The inspectors conducted routine inspections of selected activities of

the. licensee's radiological protection program.

A sampling of. radiation

work permits'(RWP) was reviewed for completeness and adequacy of

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information.

During the course of inspection activities and periodic

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tours of plant areas, the inspectors verified proper use of personnel

monitoring equipment,' observed individuals leaving the radiation

controlled area and signing out on appropriate RWP's, and observed the

posting of radiation areas and contaminated areas.

Posted radiation

levels at locations within the fuel and auxiliary buildings were verified

using both NRC and licensee portable survey meters.

The involvement of

health physics supervisors and engineers and their awareness of

significant plant activities was assessed through conversations and

review of RWP sign-in records.

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The inspectors verified the' operability of selected engineered safety

features.' This was done by direct visual verification of the correct

position of valves, availability of power, cocling water supply, system

integrity and general condition of equipment, as applicable.

Portions of

the Emergency Diesel Generating System were verified operable during this

inspection period.

One apparent violation and no deviations were identified.

4.

Maintenance (62703, 92701)

The inspectors observed the performance of annual preventive maintenance

for the "C" service water booster pump motor.

The work was controlled by

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maintenance request MR 89-0587 and included physical inspection of the

electric motor, lubrication of the motor shaft bearings, and measurement

of the motor insulation resistance.

The work was performed by two

electrical maintenance personnel and was further controlled by

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radiological work permit RWP 89-21.

The inspectors reviewed the

associated clearance, verified that applicable tagouts had been made and

verified that measuring and test equipment calibrations were current.

In the lubrication of the motor shaft bearings, the maintenance personnel

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connected a grease gun to the grease fittings and delivered approximately

two pumps of the grease gun to each bearing.

The drain plug was not

removed during grease addition.

In conversations with maintenance

technicians and supervisory personnel, the inspectors understood that the

observed method may be the standard practice.

Review of the

manufacturer's technical manual showed that the manufacturer recommended

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a different annual lubrication practice which included cleaning of the

drain plug area, addition of grease until new grease is forced out the

drain, and motor operation for 30 minutes prior to replacing the drain

plug.

The lubrication survey provided by the grease manufacturer also

recommended a similar lubrication practice for electric motor bearings.

The inspectors' review of the equipment history file for the period of

1983 through 1989 of the service water booster pump motors did not reveal

bearing failures, but did indicate come history of bearing lubrication

problems.

At the exit licensee management committed to evaluate the

lubrication program.

The inspectors will follow-up on this issue during

routine inspection activity.

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No violations or deviations were identified.

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Surveillance (61726)

The inspectors observed the performance of portions of the inservice

testing of the "A" containment spray pump.

The test was conducted by

operations personnel and was controlled by Periodic Operating Test

POT-4-1, titled " Pump and Valve Inservice Testing / Eductor Performance,"

Revision 19, dated November 7, 1988.

POT-4-1 included testing of the

containment spray pumps, full stroke exercising of the eductor check

valve, and part stroke exercising of the refueling water storage tank

check valve in accordance with the licensee's topical report PGE-1048,

titled " Inservice Testing Program for Pumps and Valves Second Ten-Year

Interval." The scope of the present inspection was limited to inservice

testing of the "A" containment spray pump.

~The inspectors noted that test personnel had copies of the test procedure

and data sheets in hand during conduct of the test, and verified that an

independent verification was performed for the final position of valves

in the locked valve program.

Calibration of test equipmer.t and

instrumentation was verified to be current by review of completed

calibration sheets.

A review of completed POT-4-1 data sheets for 1988

and 1989 indicated that required test frequencies were being met, and

showed no significant changes in pump performance.

The inspectors also

reviewed the test procedure for conformance with the requirements of

technical specifications 4.0.5 and 3/4.6.2.1 and with the requirements of

Section XI of the ASME Boiler and Pressure Vessel (B&PV) Code.

In the review of the test procedure to the requirements of Section XI of

the B&PV Code, the inspectors identified the following items.

First,

paragraph IWP-3220 of Section XI required that all test data be analyzed

within 96 hours0.00111 days <br />0.0267 hours <br />1.587302e-4 weeks <br />3.6528e-5 months <br /> after completion of a test.

POT-4-1 required that the

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denoted on the data sheets within 96 hours0.00111 days <br />0.0267 hours <br />1.587302e-4 weeks <br />3.6528e-5 months <br /> but does not specify a time

limit for review of the test data by the test engineer.

POT-4-1

apparently provided the required action range for test quantities, but

did not provide the acceptable range limits or alert ranges for use by

the shift supervisor in his review.

The concern was whether the shift

supervisor review met the intent of the IWP-3220 requirement.

Second,

POT-4-1 does not provide any allowable ranges for bearing temperatures on

the applicable data sheet which was required to be checked by the shift

supervisor within 96 hours0.00111 days <br />0.0267 hours <br />1.587302e-4 weeks <br />3.6528e-5 months <br />.

This created the possibility that bearing

temperature test data may not have been analyzed in a timely manner.

Third, review of completed vibration amplitude meter calibration sheets

indicated that the instrument accuracy requirements specified in Table

IWP-4110-1 of Section XI may not have been met.

The inspectors discussed

these items and other questions with test engineering personnel and

requested further information.

This is considered an unresolveu item

(50-344/89-05-02).

No violations or deviations were identified.

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Event Follow-up (62703, 92701, 93702)

Steam Generator Water Level Transient

At approximately 10:59 a.m. on March 4, 1989, while conducting

calibration of reactor plant control instrumentation, referred to by

licensee, instrument technicians as Hagan (the instrumentation

manufacturer) Cals, a steam generator (SG) level transient from a normal

operating level of 44% (narrow range-NR) to a transient level of 58% (NR)

occurred.

At the time of the event the cause of the SG water level

transient was.not obvious to the instrument technicians performitig the

calibrations or the operating crew, even though that crew had released

the instrument calibration-work to be performed. As soon as the transient

was terminated, the shift' supervisor discontinued all possible work

activity that coulu have caused the transient until the event could be

understood sufficiently to restart acintenance activities without

incident.

Subsequent operating crew and-instrument technician evaluation determined

that an instrument technician had momentarily removed a fuse while

establishing conditions necessary to check the calibration of the

lead-lag module (LY-505-E) for first stage turbine impulse pressure

signal conditioning;-and that LY-505-E should not have been attempted to

be calibrated at power since that module was required for controlling SG

water level with the reactor at power.

When the Shift Supervisor

concluded he understood the cause of the event, he contacted the Duty

Plant General Manager and informed.him of the plant transient.

The Duty

Plant General Manager concluded the event did riot require immediate

critique since to him it appeared the Shift Supervisor was taking

conservative actions.

On March 6, 1989, the Plant General Manager

decided an event report and a critique were required to expeditiously

gather the event facts.

The inspectors conducted a detailed assessrint of this event from March

6-10, 1989.

The following paragraphs describe the inspectors' findings.

On February 8, 1983, Maintenanc.e Reque;t (MR) 89-1538, a Preventive

Mair;tenance work request tc perform annual calibrations of approximately

450 reactor control instrument inodules, was processed by the acting Work '

Group Craft Supervisor.

The inspectors noted that the MR did not have a

list of the instruments to be calibrated or a clear indication of the

scope of the work to be performed.

The MR desc*ibed the work to be

conducted as " Calibrate Hagan Modules in protection racks, control racks

and associated control board inaicators." The MR work instructions were:

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Obtain permission from C0 and shift supervisor

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Remove from service using appropriate PICT

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Check calib of modules

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Return modules to service

These work instructions were insufficient to prevent the performance of

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the calibration of LY-505-E while in an operating condition that would

not support its calibration.

LY-505-E calibration is part of " Shutdown

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folder 22."

Shutdown folder 22 62 alt with the calibration of 18 modules

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including a turbine impulse pressure instrumentation circuit.

The

inspectors reviewed applicable interconnecting wiring diagrams and held

discussions with engineering and maintenance personnel.

Based on this

review, the following modules appeared to be in the safety related

portion of the instrumentation circuit:

signal summator PY-505 B (used

in computation for high steam flow), signal isolator PY-505A (used in

isolation from steam dump control), signal,comparator PB-505C (used for

rod block signal), and signal comparator PB-505 AB (used as input to low

power permissive signals).

The inspectors found that the licensee

program for calibrating instruments relies on the knowledge of the

instrument technician, and his use of electrical diagrams, vendor manuals

and calibration data cards.

Only several formal pre-written procedures

for each individual calibration have been developed to direct the

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craftsman while performing instrument calibrations.

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The MR and its work instructions were developed by the acting Work Group

Craft Supervisor.

In discussions with the individual, the inspectors

ascertained that the method used to develop the work instructions were

similar to the method used for the calibrations conducted in previous

years.

Besides not including a list of the instruments to be calibrated,

the MR also did not include a list of the procedures to be used by the

technicians performing the calibrations or special precautions to be

observed while performing the calibrations.

The calibration activity was

segmented into approximately thirty folders, referred to as shutdown

folders by the technicians, each containing from one to sixty-four

instruments for calibration.

Four of the shutdown folders, folders 8, 9,

12 and 22, contained instruments that could be calibrated while operating

or shutdown, and instruments that could only be calibrated.while

shutdown.

The other folders contained instruments that could be

calibrated either at power or shutdown.

Inspector' discussions with the Instrument and Controls Technician Work

Group Supervisor (WGS) revealed that the technicians had been provided

with an uncontrolled, marked-up, computerized copy of the instruments to

be calibrated within the scope of the MR and that the list had not been

attached to the MR when it was routed for review and approval.

The WGS

- further noted that the work was divided into groupings referred to as

" shutdown folders" and that the technicians used these in the performance

of the calibrations.

He continued by noting that the cover sheet to each

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shutdown folder listed all'the instruments in the folder and the general

maintenance procedures the technician should refer to when calibrating

those instruments.

He also noted that the tect:icians were required to

- be knowledgeable of the procedures used to caliorate the instruments on

which he was working.

However, the inspectors verified through interview

with the instrument technician that was conducting the calibrations that

he had not reviewed the general calibration procedures immediately prior

to conducting the calibrations nor did he have these procedures or the

vendor manual at the job site with him.

The inspectors also noted the

technicians had not been periodically required to recertify their

knowledge of tnese procedures and that one of the technicians performing

the calibrations had not co7 ducted these calibrations during the last

four years.

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The licensee does have Maintenance Procedures that provide general

guidance to.the technician on conducting calibrations.

In interviews

with the Maintenance Manager and the I & C Work Group Supervisor, the

inspectors concluded the licensee justification of this methodology is:

Maintenance Procedure (MP) 2-5, Revision 5, " Electrical Analog

Instrumentation", implements the standard for inspection and maintenance

of this equipment.

Additionally, this procedure references other

-maintenance procedures and vendor technical manuals with which the

technician should refer when conducting instrument maintenance and

calibrations.

However, the inspectors found that the vendor technical

manuals do not provide plant specific direction for the calibration of

all instruments.

Additionally for this specific set of instrument

calibrations, general procedure, MP-2-1, "Hagan Process Control and

Protection Equipment", Revision 6, identifies the steps necessary to

safely isolate, perform maintenance, test and return to service plant

instrumentation and control equipment.

It should be noted that during

the SG water level transient of March 4,1989, the technicians performing

the calibrations did not have nor had they reviewed this procedure

immediately prior to conducting the calibrations.

Knowledge of these

procedures has been considered by the licensee to be within the skill

level of the craftsman.

In the review of MR 89-1538 the inspectors also noted, in acco/ dance with

licensee Administrative Order (AO) 3-9, Revision 30, " Maintenance

Requests", other licensee reviews were required prior to releasing the

work to be performed.

For this MR the other reviews were conducted by

the Initiating Supervisor, a Quality Control Reviewer, the Cognizant

Supervisor (who in this case was also the initiator of the MR), and a

Shift Supervisor.

In reference to the Quality review, a portion of the

QA review requires, per Quality Support Ser/ ices 8 ranch Procedure,

" Quality Review - Work Packages / Documents," Revision 0, that the Quality

Reviewer assure " Applicable procedures are referenced".

While the review

was conducted, the reviewer failed to identify that no procedures had

been referenced.

Additionally, discussions with the reviewer indicated

to the inspectors that the review was superficial in that the reviewer

thought that the scope of the work was to have calibrated between three

and five instruments.

Since the MR did not have a list of the

instruments to be calibrated, it was understandable the QA Reviewer did

not realize the scope of the MR; however, the instructions did indicate

multiple calibrations were to be performed and should have generated

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additional questions on the part of the Quality Reviewer.

As a result of

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the reviewer not understanding the scope of the MR, the reviewer did not

schedule inspection hold points or observations of these calibrations by

the Quality Assurance organization.

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The QA department reviewed the work instructions with responsible

individuals and assured appropriate understanding.

Additionally, based

on this review a change to the QA procedure has been initiated to provide

clarification.

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As noted previously, prior to work authorization the MR was also reviewed

by an Operations representative, who is also a licensed senior reactor

operator and also a shift supervisor.

This reviewer recognized the full

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scope of the work; however, he did not challenge the quality of the work

instructions nor the absence of a list of instruments to be calibrated.

He also did not refer to Maintenance Procedure (MP) 2-1, "Hagen Process

Control and Protection Equipment", to evaluate the need for additional

precautions which in section III states: "There are a few instruments in

the control racks that maintenance cannot be performed on unless the

plant is shutdown." Therefore, no additions were made to the work

instructions to alert the shift supervisors that some calibrations within

the Hagan Process Control Racks could only be performed while shutdown.

The Operations Department determined that operators were given confidence

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by discussions with I&C which indicated work was to be conductd in

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accordance with approved procedures. Operators relied on I&C knowledge.

The licensee determined that operations personnel acted appropriately and

that the bulk of the corrective action was required in the maintenance

control and instruction area.

Based on the above, the licensee does not have appropriate, specific

procedures for each calibration of instruments called out in the

Technical Specifications as required by Regulatory Guide 1.33.

This is

an apparent violation (50-344/89-05-03).

Subsequent to the reviews the MR was authorized and released to be worked

by Operations. Each week the Planning and Scheduling organization

conducts a planning meeting with all planners present to schedule the

maintenance activities to be conducted for the next week and over the

weekend.

For the weekend of March 4, 1989, the calibration of the

instruments associated with ' shutdown folders' 16 and 23 were to be

performed. However, on Saturday March 4, 1989, when the technicians went

to the control room and requested permission from the Shift Supervisor to

conduct the scheduled calibrations, the Shift Supervisor would not

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release the MR since the plant conditions, due to previously planned and

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scheduled maintenance not being completed, were not compatible with the

calibrations to be conducted. The technicians then returned to the

instrument shop and discussed with the Work Group Supervisor the

alternative of conducting the calibrations associated with another

' shutdown folder' (folder 22). The WGS directed the technicians to

perform calibrations associated with Protection Set 1 (PICT-3-1, i.e.

' shutdown folder' 22). Licensee procedure A0-3-9, Revision 30,

' Maintenance Requests,' section 4.5.1 states in part, " The Work Group

Craft Supervisor shall:...b. Review the work instructions with the

craftsman / technician prior to the start of work and establish safety

requirements for the job." This review was conducted for the scheduled

work; however, whcn the planned work was deferred a review in accordance

with A0-3-9 was not conducted for the fill-in work.

This is an apparent

violation (50-344/89-05-05).

The technicians returned to the control room and requested permission

from the shift supervisor to conduct calibrations on the Hagan control

racks associated with Protection Set I.

The shift supervisor's review

of the work he released did not ascertain that the shutdown folder had

instruments within it that could only be calibrated when shutdown.

Although the licensee concluded that operation's response was appropriate,

the licensee needs to assure that operations personnel assume a sense of

ownership and a leadership role in assuring work activities are appropriate.

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At the time of the event the technicians were calibrating instruments contained

within ' shutdown folder' 22. The technicians, because the work instructions

were of inadequate detail, the required pre-work briefing was not conducted

per procedures and the shutdown folder's instrument list did not identify

plant conditions required to calibrate each instrument, attempted to calibrate

LY-505-E, an instrument that should only be calibrated while shutdown. When

the technician deenergized the lead-lag module for calibration by momentarily

removing a fuse, the transient occurred. The technician, because he felt

uncomfortable with what he was doing, immediately reenergized the

lead-lag module, thereby minimizing che transient.

The inspectors also

noted that the circuit diagram the technician was using when establishing

the conditions to check the calibration of LY-505-E was an uncontrolled,

out-of-date, partial print maintained within the Hagan control rack door.

In summary, without more detailed work instructions and an att:ched list

of instruments to be calibrated the MR reviewers, the technicians, and

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the operating staff could not determine the scope of the work being

conducted. Without adequate work instructions, an adequate pre-work

briefing and proper segregation of work to be performed for the

appropriate plant conditions, the technicians could not perform work

acceptably. This event represents a breakdown of work control practices

within the Maintenance Program. This event is very similar to a previous

citation (50-344/88-40-03), where a reactor trip resulted from an

instrument technician performing an instrument calibration without

adequate work instructions.

The inspectors reviewed their findings and conclusions of this event with

plant management.

Plant management acknowledged the findings and

committed to implement the following corrective actions:

- Generate a separate MR to address all Hagan modules and

instruments calibrated under an individual PICT. A separate MR will

be written each time an instrument to be calibrated requires the use

.of a different PICT to take them out of service and return them to

service.

- Generate a list of each specific instrument to be calibrated via

an MR and attached it to the applicable MR and state that only these

instruments are to be calibrated under that MR.

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- Notes will be added to the applicable I&C-4 data sheets to state

that calibration of this module is not to be performed while

operating.

I&C-4 data sheets will also be updated to include notes

to designate if they must be deenergized to perform the calibration.

- Conduct a Lessons Learned training session with the I&C shop led

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by the involved technicians.

- Move to Sundays the schedule date for Hagan cals to allow return

to the original intent which was to perform these activities when no

other maintenance is in progress.

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- An MR with appropriate instructions and prior reviews, including

the requisite pre-job briefings, will be prepared, reviewed,

approved, and scheduled for each train of the Hagan rack.

- In the long term, a review of all Hagan rack modules will be

conducted and all modules requiring the plant to be shutdown will be

separated into different folders and scheduling groups.

- MRs used to initiate preventative maintenance will insure that

adequate direction is'provided to bound all plant conditions and

will list specific equipment to be worked under that individual MR.

Two apparent violations and no deviations were identified.

7.

Follow-up of Licensee Event Reports (92700, 90712)-

a.

The following LER is closed based on in-office review, inspector

verification of the implementation of selected corrective actions

and licensee commitment to perform future corrective actions:

LER 88-26, Revision 0 and Revision 1, (Closed), " Reactor Trip on Low

Reactor Coolant Loop Flow Signal Due to a Technician's Procedural

Error".

This LER and its revision discussed a reactor trip that

resulted from technician error, inadequate work instructions and

ineffective supervisory involvement and oversight.

A detailed

discussion of the event was included in inspection report

50-344/88-40.

All NRC open items associated with this event have

been previously closed.

b.

The following LERs are closed based on inspector. follow-up that

included discussions with licensee representatives, detailed event

evaluation, verification of appropriateness and implementation of

corrective actions and licensee commitment to perform future

corrective action:

LER 88-05, Revision 1, (Closed), " Surveillance Interval for Valves

Exceeded Due to Personnel Procedural Error." This LER discussed two

separate instances where surveillance associated with in-service

testing were missed.

The first event, identified by NRC inspectors

and reported in Inspection Report 50-344/88-13, discussed exceeding

the surveillance interval for testing Chilled Water return valves

CV-10015 and CV-10016.

Additionally during licensee assessment of

the event, five other cases were identified where valves had not

been tested within'the required surveillance interval.

The licensee

attributed personnel error to be the cause of the missed

surveillance for these cases, since an engineer incorrectly logged

dates of testing performance and an inadequate procedure, PET 9-4,

provided insufficient detail for performing equipment testing at-

increased frequency.

As corrective actions, the licensee confirmed

that testing had been done in the six cases and revised PET 9-4 to

clarify testing at an increased frequency.

Subsequent to the submittal of Revision 0 of this LER, the licensee

identified another instance of a missed surveillance in the area of

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in-service testing.

POT-2-3-DD, ' Safety Injection System, ECCS

Valve Quarterly In-Service Test' was missed as a result of errors on

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the part of two operations staff members.

First, the operations

clerk provided the wrong surveillance, POT-2-3-DB, ' Safety Injection

System, ECCS Valve Monthly In-Service Test' instead of POT-2-3-DD,

' Safety Injection System, ECCS Valve Quarterly In-Service Test' to

the control operator for performance.

Second, the shift supervisor,

who had the responsibility for ensuring the correct surveillance,

were performed and recorded, failed to recognize that the incorrect

surveillance was performed.

The inspectors noted the shift

supervisor reviewed POT-2-3-DB and incorrectly annotated that

POT-2-3-DD had been performed.

As corrective actions, the licensee counseled the personnel involved

and performed P0T-2-3-DD.

The licensee Project Review Board (PRB) on May 4, 1988, determined

this most recent identified missed surveillance was reportable.

Because the event was similar in subject to LER 88-05, Revision 0,

the PRB incorrectly ' decided to revise LER 88-05 vice submit a new'

Licensee Event Report.

The practice of adding additional events to

an already submitted LER is appropriate only when a continuing

review of a previous event identifies additional instances of the

same event with the same root cause.

In those cases, to comply with

10 CFR 50.73, the licensee is required to submit the revised LER

within thirty (30) days.

Therefore, the licensee should have

submitted a new LER vice LER 88-05 Revision 1, and in any event the

revised LER should have been submitted within thirty days from

discovery.

This was identified to the licensee as an apparent

Severity Level V violation (50-344/89-05-06).

At the exit the

licensee stated that the PRB is now assigning each event its own

separate event report number and as such amending previously

reported events has been discontinued.

LER 88-45, Revision 0, (Closed), " Reactor Coolant System Check Valve

Leak Rate Not Measured Due to Construction Error".

This LER

discussed the invalid performance of leek rate testing for the "C"

reactor coolant loop first-off pressure isolation check valve

(894]C) due to not drilling an orifice in a fitting of a section of

the safety injection test line associated with check valve 8948C.

Therefore with the test line blocked, the leak rate tests performed

from 1977-1982 and from 1984-1988 were invalid.

In July 1983, a

valid leak rate test was conducted yielding a leak rate of 2.9 gpm.

In November of 1988, another valid leak rate was performed yielding

a leak rate of 4.1 gpm.

From this data the licensee concluded from

1977-1988 that the leak rate had not exceeded the technical

specification limit of 5.0 gpm.

On three occasions the licensee had the opportunity to identify that

a blockage existed in the test line.

In 1983 the licensee suspected

the test line was blocked and conducted an alternate test.

No

attempt was made at that time to identify the cause of the blockage.

In 1984 an attempt, blowing air tnrough the test line, was made to

clear the blockage.

Plant personnel concluded the blockage was

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cleared, but no test was performed to verify the blockage had been

cleared.

In July 1988, the method of performing the leak rate

testing was changed and the test results indicated a blockage;

however, neither the operator nor the engineer that reviewed the

test recognized the test indicated a blockage existed.

As a corrective action when the licensee recognized the orifice had

not been drilled, the licensee performed valid leak rate testing.

Additionally, the_ licensee considered drilling an orifice in the

test line fitting.

The licensee concluded for radiological and

mechanical consideration not to drill the orifice, but to continue

testing by an alternate method.

LER 88-25, Revision 0, (Closed), " Construction Activity

Inadvertently Disturbs Archeological Site"

This event occurred as

a result of the licensee not conducting a timely safety evaluation,

as required by 10 CFR 50.59.

In November 1987, NRC conducted a

management meeting with the licensee to clarify when safety

evaluations should be conducted.

During this meeting examples were

presented that were similar to the activity that resulted in this

event.

However, the licensee believed that an effective safety

evaluation program had been implemented and, therefore, did not

review the safety evaluation program for weaknesses. As a result of

this event, the licensee conducted a review of the safety evaluation

associated with facility modifications not directly related to the:

reactor plant cnd implemented improvements stated in the LER.

One apparent violation-and no deviations were identified.

8.

Follow-up on Notices of Violations and Deviations (91700, 92701)

The following open items are closed based on a review of licensee

response to Notices of Violation and/or Deviation, the licensee's

in-depth root cause analysis, and inspector follow-up and verification of

licensee committed actions.

Open Item 87-18-02, (Closed), Violation of Procedural Compliance While

Sluicing Between Safety Injection (SI) Cold Leg Accumulators. This

violation described a procedural noncompliance during the transfer of

water between SI cold leg accumulators.

Since the event the licensee has

emphasized coroliance with procedures by conducting both formal and

informal meeting. with all levels of management and supervision.

Additionally, the licensee has initiated the Quality Operations Rover

program.

Weekly, a member of the Quality Assurance Organization

evaluates various aspects of nuclear plant operation, including

procedural compliance, to assess the plant staffs' compliance with

procedures.

The Rovers' evaluations indicate improved compliance with

procedures.

The inspectors' evaluations have also indicated improved

compliance with procedures by plant operators.

The inspectors will

continue to evaluate procedural compliance by all plant personnel during

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routine inspection.

Open Item 87-18-05, (Closed), Violation of procedural Compliance to Post

Quality Control (QC) Hold Tags for Defective Equipment. This violation

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describes a procedural noncompliance in that QC Hold Tags were not posted

on equipment damaged as the result of transferring water between SI

accumulators prior to understanding and correcting the cause of the

damage.

Since this event, the inspectors verified the licensee had

strengthened Nuclear Division Procedure 600-1 " Control of Nonconforming

Materials, Parts, and Components".

The inspectors verified the licensee

has extensively used QC Hold Tags to control significant equipment and

component non onformances.

A recent example was the hanging of QC Hold

Tags on safety * elated nonconforming circuit breakers to alert operators

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of the potentiai for certain plant circuit breakers not to be able to be

remotely shut after a seismic event.

Open Item 67-31-01, (Closed), Deviation for Instrument Air System

Deviations from UFSAR.

The licensee determined that when the Su11 air

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Compressor (C116) was installed, the subsequent FSAR revision did not

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clarify that the "oilless compressor cylinder" referred only to the

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reciprocating compressors (C 102 A, B and C).

As part of an action plan

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in response to NRC Generic Letter 88-14, the licensee has completed a

detailed review of the as-built Instrument Air system as compared to

descriptions in UFSAR, design bases document and PPID's.

This review was

completed 3/3/89, and appropriate UFSAR revisions are in progress.

Open Item 88-30-01, (Closed), Violation for Failure to Include Service

Water Pump Bearing Water Flow Indicators in the Preventive Maintenance

Program.

The licensee concluded personnel error was the cause of the violation.

Because the gages could not be physically calibrated, they were not

included in the calibration program; however, by oversight the vendor

requirement to periodically inspect and clean the instrument to maintain

instrument accuracy was omitted.

As corrective action, the licensee

committed to include the subject flow instruments in the Preventive

Maintenance Program by May 1, 1989.

The instrument had been included in

the PM program by the end of the reporting period.

Additionally, one of

the three instruments had been cleaned and inspected.

These instruments

will be cleaned prior to the end of the 1989 Refueling Outage.

The

licensee also committed to evaluate the need for sending the instruments

to the vendor for calibration by' July 1, 1989.

A search for other

instruments of this type was made and none were identified.

Open Item 88-30-02, (Closed), Violation for Inadequate Administrative

Controls to Control Overtime of Maintenance Personnel.

This violation

describes an instance where overtime hours for maintenance personnel were

not sufficiently controlled to prevent exceeding work hour limitations.

The licensee concluded that oersonnel error was the cause of the

violation, in that the Maintenance Department supervisors did not

adequately monitor the overtime of personnel.

Also, Plant Management

failed to implement lessons learned from a similar event during the 1989

refueling outage.

The inspector verified that the corrective actions the

ifcensee ccmmitted to in the LER, review what controls exist and to set

up a system to assist Maintenance supervisors in maintaining control of

work hours, had been implemented.

Maintenance workers will report

overtime daily to a clerk, who will check to determine if a risk of

exceeding work-hour limits exists.

When an individual approaches-the

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limits, the supervisor will be alerted.

Also, the Plant General Manager

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issued a memoranuum directing all branch managers to review their

controls on work-hour limitations, and to establish measures appropriate

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for their work functions to ensure limits are not; exceeded.

The

inspectors also reviewed a recent QA audit, that covered the last forced

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outage, that concluded adequate controls exist concerning control of work

hours.

The NRC inspectors found that no formal written guidance existed for the

established measures" for the' Maintenance Department on the control of

work hours, that is,'no Maintenance Department procedure, no policy

statement nor change to the job descriptions of the clerk or craft

supervisors has been made.

Also, the new " Conduct of Maintenance Manual"

does not address the requirements for the individual worker to report

their time daily, nor the Supervisors' responsibilities to monitor

overtime.

Without these formal documented measures the potential to.

again exceed work hour limitations appears likely.

Additionally, the

absence of formal guidance on controlling work hour limitation appears to

conflict with recent Management policy on clear definition of

responsibility =and accountability.

The inspectors will continue to

closely assess licensee control of work hours during routine inspection.

Open Item ~ 88-30-05, (Closed), Violation for Failure to Initiate and

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' Document Required Investigation for Recorder LR-5521 Out-of-Calibration.

The licensee concluded the cause.of this violation was personnel error on

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the part of the I & C Supervisor, in that he failed to use an instrument'

list for a quality related test.

As a result of this error, an

out-of-calibration' form was not generated, and therefore, did not prompt

the required investigation.

A review of recent surveillance test data was performed, and the review

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indicated that since the last out-of-calibration occured in Febraury

1988, Periodic Operating Test (POT)-7-1 had since been performed with

satisfactory results and with the LR-5521 in-calibration.

The Systems Engineering Group performed the required out of-calibration

evaluation..for this occurrence, and recommended the use of the 1986

instrument list be discontinued.

This instrument list was compiled by

Plant Engineering in.1986, and is not formally controlled or maintained

current.

Use of the list has been terminated, and the I & C Supervisor

will prepare an out-of-calibration form for all quality related

instruments that are out-of-calibration.

The Systems engineering group

will-perform the evaluations as appropriate.

Open Item 88-30-07, (Closed), Violation for Lack of Adequate Management

Oversight to Ensure Maintenance Problems and Discrepancies Are Resolved

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Before Proceeding.

The licensee determined that the root causes of the

event were inadequate management oversight and the lack of a trending

program for maintenance history.

Contributing to this issue was an

inadequate system for monitoring and tracking open MRs.

An engineering

evaluation by the licensee was conducted to address the~ low flow

condition, and appropriate revisions to the Operating Instructions were

implemented.

An improved system for tracking and monitoring the status

of open'MRs was developed and implemented on February 15, 1989.

A long

term program to improve maintenance f.istory, and to trend equipment

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problems and maintenance request problems was implemented in March 1989.

The effectiveness of these later two items will be addressed in future

NRC inspections.

Open Item 88-30-08, (Closed), Violation for Failure to Perform

Preventive Maintenance (PMs) on Equipment in Storage.

The license

determined that the root cause of the violation was personnel error by

warehouse employees.

Contributing to the procedural compliance

deficiency were two factors:

a.

Lower-tier procedures established in 1987 were cumbersome and

difficult to understand.

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b.

No formal support program was developed to ensure compliance

(ie. QA audit, nor preventive maintenance scheduling system).

The inspector verified that the following interim corrective steps had

been taken:

a.

All materials requiring desiccants had been inspected and where

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necessary, desiccants were replaced.

This was completed on

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October 6, 1988.

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b.

Shaft rotation maintenance had been performed on all equipment

and material requiring such preventive maintenance.

This

action was completed on October 6, 1988.

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c.

Electrical energization of materials requiring such preventive

maintenance was completed November 8, 1988.

d.

Meggering of electrical motors requiring such preventiva

maintenance was completed October 18, 1988.

e.

Examination of inventory items for shelf-life was completed by

December 31, 1988.

f.

A review of the Trojan Materials Management Department

improvement action plan was performed to identify any other

programs which were not receiving the correct priorities.

No

other problems were identified.

g.

Procedures for a comprehensive preventive maintenance program

were developed and fully implemented by January 16, 1989.

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These included lower-tier procedures which will provide clear

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direction for warehouse personnel.

Training was provided for

warehouse personnel prior to implementing the procedures.

The inspector also reviewed packages submitted to plant engineering for

all storage items identified to require PMs.

Engineering review is

expected to include a review of applicable technical manuals and vendor

recommendations for any additional required PMs (e.g. maintenance needed

to extend shelf-life).

The inspector also reviewed documents concerning

a computerized system to track required PM actions.

This program will

provide a formalized notification process to alert maintenance crews and

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warehouse management when action is required.

Follow-up of the revisions

to the PM program, as a result of the engineering review, and

effectiveness of the computerized tracking system will be addressed in

future NRC inspections.

Open Item 88-30-09, (Closed), Violation for Failure to Perform and

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Document Leak Test per ASME Criteria for Service Water Strainer Gasket

Replacement.

The licensee's root cause analysis concluded the cause of

the violation was personnel error due to the craftsman's failure to

document that he performed the inspection.

Licensee questioning of the

craftsman determined that the craftsman did inspect the system for

leakage.

Additionally, the licensee identified that the practice of

revising a work request to include additional work, which has been since

discontinued, prevented the reviewers from recognizing the inspection had

not been documented.

Also, the licensee identified that in the process

of generating the maintenance request (MR) the work group planner had not

recognized the repair as an ASME code repair, and therefore,.did not

require an inspection to be performed.

The licensee reviewed the MR and

the subject of code repairs with the planning staff to prevent

recurrence.

The NRC inspectors reviewed recent MRs to verify the

practice of appending work requests with additional repairs had been

discontinued.

Additionally, a recent maintenance request associated with

the service water system was assessed to verify the requirement to

inspect for leakage had been included.

Open Item 88-30-10, (Closed), Unresolved Item Concerning Inablity to

Retrieve Maintenance Request Packages.

This concern was raised due to

the inability of the work planning group to find seven of the eighty

Maintenance Request packages asked for by the team.

The licensee has

since identified the problems in locating these packages.

A review of

the work planning procedures and issues raised in response to violation

50-344/88-30-07 has resulted in the licensee developing an improved

system for tracking and monitoring the status of open MRs.

This system

was implemented on February 15, 1989.

The effectiveness of this program

will be observed during the 1989 refueling outage, and evaluated in

future NRC inspections.

Open Item 88-43-03, (Closed), Violation for Quality Control (QC)

Inspector's Failure to Report a Nonconforming Activity (NCAR).

This violation resulted from the QC inspector's misconception that

nonconformances were not required to be formally documented if a " circle

Q",

required observation, was not annotated on the work document; and

Quality Assurance supervision discouraging the inspectors from initiating

NCARs on inspector perceived " insignificant" procedure violations.

To

prevent recurrence, the licensee took the following corrective actions:

initiated an NCAR, issued a memorandum outlining expectations on

documentation of procedural non-compliances for Nuclear Quality Assurance

Department (NQAD) personnel, and revised Quality Inspection Procedures to

clarify the requirements for reporting and documenting procedural

noncompliance.

The inspectors verified Administrative Order (AO) 13-1,

" Inspection Control" had been revised (February 1, 1989) and that

supplemental training had been provided to Quality Inspections personnel.

Additionally, NRC inspectors have inspected maintenance that had been

observed by the licensee Quality Control inspectors.

An additional

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instance of a QC inspector failing to document a procedural noncompliance

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was identified in NRC inspection report 50-344/89-01.

It appears

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additional licensee corrective action is required to ensure all

inspectors are knowledgeable of documentation requirements.

The

licensee's corrective action to the Notice of Violation associated with

inspection report 50-344/89-01 is being drafted and will be evaluated

upon receipt.

No violations or deviations were identified.

9.

Follow-up on 10 CFR Part 21 Reports (92700, 92701)

10 CFR Part 21 Report on ASEA Brown Boveri K-Line Circuit Breakers

(0 pen Item 89-08-P Closed):

A Part 21 report was submitted which dealt

with the need to install slow close lever rebound springs on various

K-line circuit breakers to ensure proper operation after a seismic event.

The inspectors reviewed the licensee's actions in response to the

information provided in the Part 21 report.

Licensee review of drawings

and technical manuals revealed that there were approximately ninety

applicable K-Line circuit breakers installed in the plant.

Of these,

seven breakers had been purchased after July 1974.

According to the Part

21 report, breakers manufactured after July of 1974 were equipped with

the rebound spring.

Licensee inspection of breakers manufactured before

and after July 1974 confirmed the need to install rebound springs on the

older breakers.

A nonconformance report, NCR 89-033, was initiated which concluded that

continued use was acceptable.

This was based upon the finding that the

only safety-related equipment affected by the potential failure of the

circuit breaker to close after a postulated seismic event and a loss of

off-site power were the containment air coolers.

Licensee calculations

concluded that the plant could be maintained in Mode 3, Hot Standby, for

about eight hours without adversely affecting the environmental

qualification of equipment inside containment assuming no containment air

coolers were functioning.

Rebound springs were being ordered at the time

of inspection with plans to install them on safety related breakers in

the 1989 refueling outage and on non-safety related breakers as

preventive maintenance became due on each per the maintenance schedule.

The inspectors performed a sampling inspection to verify the licensee

tabulation of applicable breakers, reviewed the nonconformance report,

and discussed the supporting analysis with licensee engineering and

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licensing personnel.

A review of operating procedures verified that

operators were instructed to start containment air coolers in response to

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a loss of offsite power event.

In addition, the inspectors observed a

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demonstration that was attended by operations personnel of the necessary

actions to reset the slow close lever.

Discussions with maintenance

management indicated that electrical maintenance personnel would normally

reset the slow close lever, if needed.

The inspectors concluded licensee

actions addressed the concerns raised in the Part 21 report.

No violations or deviations were identified.

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10.

Review of Design Change Program (37702, 92701)

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The inspectors conducted a review of the' licensee's design change

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program.

The program as described in the following procedures was

reviewed for consistency with regulatory requirements set forth in the

administrative control section of the technical specifications and with

guidelines outlined in industry standards:

Nuclear Division Procedure NDP 200-1, Revision 8, titled

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" Design Change Control"

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Nuclear Plant Engineering Procedure NPEP 200-14, Revision 7,

titled " Detailed Construction Package Preparation and Control"

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Nuclear Plant Engineering Procedure NPEP 200-11, Revision 1,

titled " Verification of Design"

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Nuclear Plant Engineering Procedure NPEP 200-15, Revision 7,

titled " Processing of As-Built Packages"

Nuclear Plant Engineering Procedure NPEP 200-6, Revision 3,

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titled " Preparation of Engineering Drawings"

The above procedures discussed the licensee's request for design change

(RDC) process which included preparation of a preliminary design,

performance of independent design verifications, review and approval of

the design change by engineering management and the Plant Review Board,

preparation of a detailed construction package (DCP), implementation of

the design change by the construction work group, and turnover to the

plant operations department.

The procedures also addressed the process

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by which the implemented design change is reflected on engineering

drawings and documents.

The inspectors reviewed two recently completed safety-related as-built

design packages and discussed the design changes with engineering and

plant modifications personnel.

The design packages were RDC 85-052/DCP

13, which dealt with modifications to the remote shutdown station room

and equipment base frame supports, and RDC 83-061/DCP 1, which controlled

the replacement of 18 packless globe valves in various emergency core

cooling systems and the reactor coolant system.

RDC 85-052/DCP 13

involved a revision of the detailed construction package.

In the review

of the RDC's and DCP's, the inspectors verified that required independent

design verifications were performed, that the need for system change

descriptions which initiated changes to procedures and personnel training

was addressed, and that appropriate reviews and approvals were obtained

for DCP revisions.

The inspectors also verified the review and approvals

obtained for field changes to the detailed construction packages.

No

significant discrepancies were identified in the review.

In the control of engineering drawings, the use of drawing change notices

(DCN) was one method to show as-built changes to an existing nuclear

plant design drawing.

Per NPEP 200-6, DCNs were required to be

incorporated in new or revised drawings within 90 days of issuance or

whenever the number of DCNs against a particular drawing exceeds five in

number.

The inspectors reviewed a sample of control room drawings and

noted that DCNs for piping and instrument diagrams appeared to meet the

above requirement.

Various electrical drawings, however, either had more

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than five associated DCNs or had recent DCNs which were not closed within

90 days of issuance.

Examples of findings are described below.

Three of the electrical drawings were designated by the licensee as top

documents which were defined in NPEP 200-15 as those design documents

which are of prime interest to plant operations personnel.

Drawing E-45

which dealt with 120 VAC safety relatec instrument bus panels had DCN 69

and 70 issued for revision 37 which were not closed within 90 days of

issuance.

Drawing E-46 which dealt with other 120 VAC instrument bus

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panels had DCN 113, 114, and 115 for revision 63 which were not closed

within 90 days of issuance.

Drawing E-22, the electrical fuse schedule,

had DCN 80, 81, 82, and 84 for Revision 8 which were not closed within 90

days of issuance.

Drawing change notices 80 and 84 dealt with safety

related components of the auxiliary fet dwater system and chemical and

volume control system, respectively.

L-45, E-46, and E-22 were

designated us top documents per NPEP 200-15.

In addition, E-22 had 15

associated DCNs for Revision 8 before llevision 9 was issued.

At the time of inspection, the following electrical drawings had more

than five associated DCNs:

E-29, Revinion 58, the pull and terminal box

schedule with 17 DCN's; E-191, Revision 37, electrical raceway schedule

with 37 DCNs; and E-192, Revision 36, the electrical circuit schedule

with 53 DCNs.

A number of these DCNs had also been issued in excess of

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90 days.

.These findings indicata the need for increased attention to assure

compliance with procedtral requirements for drawing revisions.

The

inspectors consider the above findings to be an apparent violation

(50-344/89-05-07).

One apparent violation and no deviations were identified.

11.

Commercial Grade Procurement (38703)

In response to a Region V request, the licensee, on February 21, 1989,

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submitted additional information regarding commercial grade material use

in the Main Feedwater system.

This included a list of pressure-bearing

materials, the approximate quantity installed, identification or heat

number, manufacturer, supplier, and the physical and chemical test

results to date.

This list also identified all weld filler material used

in the MFW piping replacement.

In addition, the submittal documented the

licensee's evaluation that the feedwater piping was acceptable for

continued use until the 1989 refueling outage.

The inspector's technical evaluation of the licensee's submittal involved

matching ASTM chemical and physical requirements to that specified on the

Certified Material Test Reports and the licensee's laboratory test

results.

The MFW piping replacement was procured to standard

specification ASTM A 106, Grade B or ASTM A 333 Grade 6.

The laboratory

test provided independent mechanical and chemical test data as supporting

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evidence that the critical characteristics of the installed piping

materials conform to code requirements.

The ASTM material

specifications, the CMTRs and the results of the licensee's independent

testing were found to be within tolerance.

The licensee's hardness

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testing of materials supports the acceptability of materials where

physical testing had not been conducted.

In general, the licensee's

review of the various manufacturers and suppliers found that they had QA

programs of varied degrees with several having ASME Quality Systems

Certificates (QSC).

Most had been audited by organizations other than

PGE.

The below discussed items summarize the material that was

relat-ively weakly addressed.

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. Flow Bend 14-inch elbows, heats 8278 and A403

No independent chemical, physical, or hardness testing had been

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performed by the licensee to verify the associated CMTRs due to

the unavailability of material samples.

No known manufacturer QA program.

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The inspector considered the material to be acceptable for the

following reasons:

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Three other heats of Flow Bend elbews were independently tested by

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the licensee and found to be satisfactory, indicating the validity

of Flow Bend CMTRs.

Bechtel audited Flow Bend in 1983, 1984, 1985, and 1989.

Flow

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Bend is considered by Bechtel to be a good commercial supplier.

Flow Bend is not known by the NRC to be an unacceptable

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supplier.

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In process construction inspections and tests of the subject

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material indicate that it is acceptable material.

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Additional testing will be performed during the 1989 outage.

Mills Iron 14 x 16 reducers (2), heat 80A

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No independent chemical, physical or hardness testing done had-

been performed by the licensee to verify the validity of the

associated CMTRs.

The inspector considered the material acceptable for the following

reasons:

The raw steel was procured by Mills Iron from U.S. Steel.

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Two other Mills Iron fittings of a different heat in the

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warehouse tested satisfactory.

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Mills Iron has a QA program.

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The QA program has been favotably audited by Bechtel to

NCA3800.

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Various small pieces' including:

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2 ft. of 4-inchipipe'from Nippon.

.(4) 1-inch half. couplings.from Fuji.

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. The'.. ins'pector considered the material acceptable f or the following -

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reasons:

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All of the material has been in ' service since 1987.

All of the material was subject to weld inspections and

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hydrostatic testing.

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Nippon has a QSC.

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The small quantity and size involved minimize the potential of

problems.

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' Weld rod

Generally no independent chemical or physical testing had been

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done.

Information. supporting the quality of the materials includes:

[All.boughtfrommanufacturerswithanASMEQualitySystems

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Certificate (QSC).

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E-7018 bought in sealed containers, thereby minimizing the

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possibility of supplier problems.

The inspector's independent evaluation of the information provided by the

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licensee, regarding the MFW piping and fittings, is that sufficient

-evidence of quality in the subject material exists to conclude that this

material was acceptable for continued use until the 1989 refueling

outage. "The licensee has scheduled additional testing to restive any

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remaining material concerns prior to completion of the 1989 refueling

. outage.

The quality of the weld filler materials were evaluated

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separately.

In order to evaluate the acceptability of the weld material used in

welding the MFW replacement piping, the inspector reviewed the

radiographs associated with welds made on the feedwater pipe.

The welds

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were :randcaly selected from design drawing numbers EBB-3-1 (Revision 13)

and EBB-3-2 (Revision 11).

These drawings identify the weld numbers and

' locations within the applicable Steam Generator Loops (A, B, C and D).

.The radiographs reviewed were for the following welds: Weld No. P25923

from Loop A, Weld Nos. P25876 aGd P25972R4 from Loop B, Weld Nos.

P25991R1 and P25889 from Loop C, and Weld No. P25881R4 from Loop D.

Intermittent radiographs were included in'the inspector's review; these

are "information only" shots taken at various stages of the welding

process to identify any deficiencies that would cause weld rejection.

Rejected welds that required repair are identified by placing an R after.

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the weld number.

For example, P25972R4 indicates that 4 repairs were

made before the weld joint was determined to be acceptable in accordance

with ASME Section XI requirements.

For the radiographs of the weld

joints reviewed, the inspector observed that.the weld repairs were always

made to the weld root and, in each case, involved the use of 1/8" E705-2

' Heat No. 065502.

Discussions with licensee personnel revealed an

exp.assed concern, by the welding ar.d QC departments, on the use of this

particular weld rod.

High levels of porosity were identified with the

use of this weld rod which resulted in one MFW pipe weld root being cut

.out,.and the failure'of previously qualified welders to qualify based on-

radiographic rejection of the welders test coupons.

When questioned why

this problem wasn't addressed on a Nonconformance Report (NCR), the

inspector.was informed that on July 30, 1987 an NCR was initiated.

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copy was~provided for the inspector's review.

This NCR described the

nonconforming condition as '/ Filler metal (Linde or L-Tec) E705-21/8" to

3/32" G.T.A,W. wire do not produce x-ray quality welds, for welder

qualification and in plant requirements of piping components that.have to

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meet such criteria." This NCR, however, was not validated and assigned

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an NCR number.

The Plant Modifications Manager, when informed, had the

1/8" E70S-2 weld rod placed on hold in the warehouse;.but no NCR was

generated to formally address the problem.

Although this nonconforming

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weld rod was not dispositioned through the NCR process, the inspector is

satisfied that the MFW pipe welds selected for review were satisfetory.

This conclusion is based on the inspector's review of the intermittent

- radiographs and the final radiographs taken of the repaired welds for

code acceptability.

The failure to process the NCR in accordance with.the established QA

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program procedures to assure that the nonconforming weld rod is promptly

identified, the root cause of the condition is determined and corrective

action taken to preclude repetition is an apparent violation of

10 CFR 50, Appendix B, Criterion V (50-344/89-05-08).

.At the inspector's request, the Materials Manager had the warehouse

searched to identify if any of this weld rod was located onsite.

All of

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the 1/8" E705-2 Heat No. 065502-was removed from the warehouse and sent

to local schools.

However, the 3/32" E705-2 Heat No. 065472 was in

stock;'this rod produced weld porosity although to a lesser extent than

the 1/8" rod.

The licensee stated they would try to determine if any of

the 1/8" rod is still available and, if so, obtain some for testing.

In

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the interim, the licensee committed to perform some tests on the existing

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supply of the 3/32" E70S-2 rod.

The inspector will review the results of

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this, effort during a future inspection when evalurting licensee actions

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taken'to address the nonprocessed NCR.

12.

Unresolved Item

.An unresolved item is a matter about which more information is required

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to ascertain whether it is an acceptable item, a deviation, or a

violation.

An unresolved item is discussed in paragraph 5.

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13.

Severity Level V Violations

As stated in Section V.A of 10 CFR Part 2, Appendix C, " General Statement

of Policy and Procedure for NRC Enforcement Actions," 53 Fed. Reg. 40019

(October 13, 1988), a Notice of Violation will not normally be issued for

isolated Severity Level V violations provided that the licensee has

initiated appropriate corrective actions before the inspection ends.

Two

apparent Severity Level V violations for which a Notice of Violation was

not issued are discussed in paragraphs 3 and 7 of this report.

14.

Exit Interview (30703)

The inspectors met with the licensee representatives denoted in paragraph

1 on March 9,1989.

The inspectors summarized the scope and findings

associated with the Commercial Grade Procurement follow-up inspection

conducted March 8-9, 1989.

The inspectors met with the licensee representatives denoted in paragraph

1 on March 23, 1989, and with licensee management throughout the

inspection period.

In these meetings the inspectors summarized the scope

and findings of the inspection activities.

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