SER Re Licensee 870814 & 21 Responses Re Single Failure Potential in Nuclear Svc Water Sys.Nuclear Svc Water Sys Meets Requirements of GDC 5 & 44 Re Sharing & Provisions for Suitable Redundancy in Cooling Water SysML20236D445 |
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Catawba ![Duke Energy icon.png](/w/images/7/75/Duke_Energy_icon.png) |
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Issue date: |
09/30/1987 |
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From: |
Office of Nuclear Reactor Regulation |
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To: |
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Shared Package |
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ML20236D436 |
List: |
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References |
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NUDOCS 8710280212 |
Download: ML20236D445 (4) |
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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211A9791999-08-20020 August 1999 Safety Evaluation Granting Licensee Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section Xi,For Plant,Unit 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20206P5201999-05-14014 May 1999 Safety Evaluation Accepting GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20205S5551999-04-21021 April 1999 Safety Evaluation Accepting Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20205N3651999-04-12012 April 1999 Safety Evaluation Accepting IPE of External Events Submittal ML20196J8351998-12-0808 December 1998 Safety Evaluation Granting Relief Request Re Relief Valves in Diesel Generator Fuel Oil Sys ML20196C0251998-11-27027 November 1998 SER Accepting Clarification on Calibration Tolerances on Trip Setpoints for Catawba Nuclear Station ML20196A6881998-11-25025 November 1998 Safety Evaluation Granting Relief Request 98-02 Re Limited Exam for Three Welds ML20247M0861998-05-21021 May 1998 SER Accepting 1997 Rev to Catawba UFSAR Submitted on 970925. Rev Added Analysis for Postulated Accident Involving Dropping of Sf Pool Weir Gate Onto Sf Assemblies ML20216E1771998-04-13013 April 1998 Safety Evaluation Accepting Relief Request 98-01 for Catawba Nuclear Station Units 1 & 2 from Requirements of ASME Boiler & PV Code for Second 10-year Interval Program for Inservice Testing of Pumps & Valves ML20217M4211998-04-0303 April 1998 Safety Evaluation Approving Request for Relief 97-04, non-code Repair Valves.Relief Granted Retroactively to Unit 1 & Expired Dec 1997.Relief for Unit 2 Will Expire at End of Cycle 9 Outage or Next Scheduled Outage Exceeding 30 Days ML20199A5521998-01-22022 January 1998 Safety Evaluation Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves, for Cns,Units 1 & 2 ML20199A6421998-01-22022 January 1998 Safety Evaluation Accepting Proposed EALs Changes for Plant, Units 1 & 2.Concludes That Changes Consistent W/Guidance in NUMARC/NESP-007,w/variations as Identified & Accepted in Review & Meets Requirements of 10CFR50.47(b)(4) ML20198P9641998-01-15015 January 1998 SE Granting Relief Request 97-03 for Second 10-yr Interval Inservice Insp Program ML20198R9951997-10-30030 October 1997 Safety Evaluation Authorizing Request for Approval of Alternative to Exam Requirement of Reactor Vessel Shell Weld,Per 10CFR50.55a(g)(6)(ii)(A)(5) ML20198J7651997-10-15015 October 1997 Safety Evaluation Accepting 10-yr Interval Insp Program Plan Alternatives for Listed Plants Units ML20211F8801997-09-22022 September 1997 Safety Evaluation Supporting Second ten-year Interval Inservice Inspection Program Plan & Associated Requests for Relief for Catawba Nuclear Station Unit 1 ML20149K8281997-07-29029 July 1997 SER Granting Request for Exemption from Requirements of 10CFR70.24 for Units 1 & 2 ML20141E1121997-06-16016 June 1997 Safety Evaluation Approving Licensee Position That UFSAR Table 6-77 Be Revised to Identify SA-1 & SA-4 Instead of SA-3 & SA-6 as Containment Isolation Valves ML20148H2501997-06-0505 June 1997 Safety Evaluation Accepting Proposed Restructuring of Util Through Acquisition Of,& Merger W/Panenergy Corp ML20141G6701997-05-20020 May 1997 Safety Evaluation Accepting Proposed Alternative Use of TS Requirement for Code Class Snubbers ML20135B3051997-02-27027 February 1997 Safety Evaluation Granting Second 10 Yr ISI Program Plan & Associated Requests for Relief ML20134P2421997-02-20020 February 1997 Safety Evaluation Accepting TR BAW-10199P for Ref in Plants Licensing Documentation & Use in Licensing Applications ML20134L4081996-11-19019 November 1996 SER Accepting Performance of Plant Standby Nuclear Svc Water Pond ML20134G5551996-11-0707 November 1996 Safety Evaluation Accepting Proposed Application of BWU-Z CHF Correlation for Plants Mark-BW 17x17 Type Fuel ML20129E4851996-10-0101 October 1996 Safety Evaluation Recommending That Relief Request 96-02 Be Granted,Per 10CFR50.55a(g)(6)(i),per Request ML20056D9611993-07-30030 July 1993 SER Accepting Licensee 930325-0429 Submittals of Technical Info to Support Continued Operation of Facility for Remainder of Fuel Cycle 7 ML20055H9151990-07-27027 July 1990 Safety Evaluation Accepting Actions Taken to Resolve NRC Bulletin 88-002, Rapidly Propagating Fatigue Cracks in Steam Generators Tubes ML20248C0731989-08-0303 August 1989 Sser Accepting 880601,0909 & 890602 Changes to ATWS Mitigation Sys Actuation Circuitry for Plants ML20246L4221989-05-12012 May 1989 Safety Evaluation Supporting Revs 15 & 6 to Pump & Valve Inservice Testing Program & Relief Requests ML20150C2651988-06-28028 June 1988 Safety Evaluation Supporting Licensee Assessment to Fracture Toughness Requirements for Protection Against PTS Events,Per 10CFR50.61 ML20150C2611988-06-28028 June 1988 Safety Evaluation Supporting Licensee Assessment to Fracture Toughness Requirements for Protection Against PTS Events,Per 10CFR50.61 ML20154H2171988-05-18018 May 1988 Safety Evaluation Accepting Util 880414 Submittal Re Reload Startup Physics Test Program ML20148H1001988-01-22022 January 1988 Safety Evaluation Supporting Util 871113 Proposed Tech Spec Changes Reflecting Unit 2 Cycle 2 Refueling & Addition of Boron Dilution Mitigation Sys for Unit 2 ML20236M9631987-11-0606 November 1987 Safety Evaluation Accepting Util Proposed ATWS Mitigating Sys Actuation Circuitry for Facilities,Per 10CFR50.62(c)(1) & Pending Final Resolution of Tech Spec Issue ML20236D4451987-09-30030 September 1987 SER Re Licensee 870814 & 21 Responses Re Single Failure Potential in Nuclear Svc Water Sys.Nuclear Svc Water Sys Meets Requirements of GDC 5 & 44 Re Sharing & Provisions for Suitable Redundancy in Cooling Water Sys ML20236F5881987-07-29029 July 1987 Safety Evaluation Supporting Util 831104,841102,1231 & 851203 Responses to Items 3.1.1,3.1.2,3.2.1,3.2.2 & 4.5.1 of Generic Ltr 83-28 ML20215D2701987-06-11011 June 1987 SER Accepting Rev 13 to Unit 1 & Rev 4 to Unit 2 Pump & Valve Inservice Testing,Per Generic Ltr 83-28,Item 2.1 (Part 2) ML20214T4061987-06-0202 June 1987 Safety Evaluation Supporting Util 860424 Submittal Re Turbine Sys Maint Program for Early Detection of Cracking in Low Pressure Turbine Wheels ML20214M3361987-05-22022 May 1987 Safety Evaluation Supporting Util Rept Entitled, Rod Swap Methodology Rept for Startup Physics Testing ML20209B1511987-01-28028 January 1987 SER Supporting Util Responses to Generic Ltr 83-28,Item 4.5.2 Re Reactor Trip Sys on-line Testing ML20207Q5851987-01-15015 January 1987 SER Re Generic Ltr 83-28,Item 2.1 (Part 2) Concerning Vendor Interface Programs for Reactor Trip Sys Components.Util Response Acceptable.Item Closed ML20207N3011987-01-0808 January 1987 Safety Evaluation on Util 830309 & 851025 Requests for Relief from 10CFR50.55a Requirements Re Pump & Valve Inservice Testing Program.Relief Granted W/Listed Exceptions ML20207P6341986-08-31031 August 1986 Safety Evaluation Accepting Util 851120 & 860324 Proposals to Eliminate Arbitrary Intermediate Pipe Breaks in Select List of High Energy Piping Sys ML20199L3941986-07-0202 July 1986 SER Providing Final Conclusions & Recommendations from Evaluation of Tdi Owners Group Program to Validate & Update Quality of Tdi Diesel Generators ML20211E4251986-06-10010 June 1986 Draft SER Re Util 850624 Response to Generic Ltr 83-28,Items 4.1,4.2.1 & 4.2.2 Re Preventive Maint Program for Reactor Trip Breakers/Maint & Trending.Position on Item 4.1 Acceptable.Position on Items 4.2.1 & 4.2.2 Unacceptable ML20207T4241985-12-30030 December 1985 SER Re SPDS Based on Documentation & 850513-15 Audit.Spds Does Not Fully Meet Requirements of Suppl 1 to NUREG-0737. Five Listed Variables Should Be Added to Spds.Interim Implementation Acceptable ML20138M9011985-12-17017 December 1985 Draft SER on Util 850329 Response to 841003 Request for Addl Info Re Hydrogen Control Measures for Plant.Addl Info & Analyses Required Re Effect of Upper Compartment Burns on Air Return Fan ML20128F9921985-06-21021 June 1985 SER Based on Util 831104 Response to Generic Ltr 83-28,Item 1.1 Re post-trip Review Program Description & Procedures. Program & Procedures Acceptable 1999-08-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H0201999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Catawba Nuclear Station,Units 1 & 2 ML20216E5401999-09-0707 September 1999 Special Rept:On 990826,discovered That Meteorological Sys Upper Wind Speed Cup Set Broken,Causing Upper Wind Channel to Be Inoperable.Cup Set Replaced & Channel Restored to Operable Status on 990826 ML20212B4711999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217H0321999-08-31031 August 1999 Revised Monthly Operating Rept for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20211B1281999-08-31031 August 1999 Dynamic Rod Worth Measurement Using Casmo/Simulate ML20211A9791999-08-20020 August 1999 Safety Evaluation Granting Licensee Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section Xi,For Plant,Unit 2 ML20211F3441999-08-17017 August 1999 Updated non-proprietary Page 2-4 of TR DPC-NE-2009 ML20211C1291999-08-17017 August 1999 ISI Rept Unit 1 Catawba 1999 RFO 11 ML20210R1051999-08-0606 August 1999 Special Rept:On 990628,cathodic Protection Sys Was Declared Inoperable After Sys Did Not Pass Acceptance Criteria of Bimonthly Surveillance.Work Request 98085802 Was Initiated & Connections on Well Anode Were Cleaned or Replaced ML20210S2891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20212B4871999-07-31031 July 1999 Revised Monthly Operating Rept for July 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209E4361999-07-0909 July 1999 SER Agreeing with Licensee General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196K6631999-07-0707 July 1999 Safety Evaluation Supporting Licensee 990520 Position Re Inoperable Snubbers ML20210S2951999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2 ML20209H4561999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206T4771999-05-31031 May 1999 Rev 3 to UFSAR Chapter 15 Sys Transient Analysis Methodology ML20196L1881999-05-31031 May 1999 Non-proprietary Rev 1 to DPC-NE-3004, Mass & Energy Release & Containment Response Methodology ML20196A0001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206P5201999-05-14014 May 1999 Safety Evaluation Accepting GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20206N8391999-05-0404 May 1999 Rev 16 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr ML20206R1811999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20196A0041999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20206N8261999-04-22022 April 1999 Rev 15 to CNEI-0400-24, Catawba Unit 1 Cycle 12 Colr. Page 145 of 270 of Incoming Submittal Not Included ML20205S5551999-04-21021 April 1999 Safety Evaluation Accepting Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design Basis Accident Conditions ML20205N3651999-04-12012 April 1999 Safety Evaluation Accepting IPE of External Events Submittal ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206R1931999-03-31031 March 1999 Revised Monthly Operating Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9521999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Catawba Nuclear Station,Units 1 & 2 ML20205P9561999-02-28028 February 1999 Revised Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20204C9111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Catawba Nuclear Station,Units 1 & 2 ML20203A2581999-02-0505 February 1999 Safety Evaluation of TR DPC-NE-3002-A,Rev 2, UFSAR Chapter 15 Sys Transient Analysis Methodology. Rept Acceptable. Staff Requests Duke Energy Corp to Publish Accepted Version of TR within 3 Months of Receipt of SE ML20204C9161999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for Catawba Nuclear Station,Units 1 & 2 ML20199K8711999-01-13013 January 1999 Inservice Insp Rept for Unit 2 Catawba 1998 Refueling Outage 9 ML20199E3071998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Catawba Nuclear Station,Units 1 & 2 ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20205E9441998-12-31031 December 1998 1998 10CFR50.59 Rept for Catawba Nuclear Station,Units 1 & 2, Containing Brief Description of Changes,Tests & Experiments,Including Summary of Ses.With ML20206P2081998-12-31031 December 1998 Special Rept:On 981218,inoperability of Meteorological Monitoring Instrumentation Channels,Was Observed.Caused by Data Logger Overloading Circuit.Replaced & Repaired Temp Signal Processor ML20203A4101998-12-22022 December 1998 Rev 16 to CNEI-0400-25, Catawba Unit 2 Cycle 10 Colr ML20203A4041998-12-22022 December 1998 Rev 14 to CNEI-0400-24, Catawba Unit 1 Cycle 11 Colr ML20198B1341998-12-14014 December 1998 Revised Special Rept:On 980505,discovered That Certain Fire Barriers Appeared to Be Degraded.Caused by Removal of Firestop Damming Boards.Hourly Fire Watches Established in Affected Areas ML20196J8351998-12-0808 December 1998 Safety Evaluation Granting Relief Request Re Relief Valves in Diesel Generator Fuel Oil Sys ML20199E3221998-11-30030 November 1998 Revised MOR for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 Re Personnel Exposure ML20198E3151998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Catawba Nuclear Station,Units 1 & 2 ML20196C0251998-11-27027 November 1998 SER Accepting Clarification on Calibration Tolerances on Trip Setpoints for Catawba Nuclear Station ML20196A6881998-11-25025 November 1998 Safety Evaluation Granting Relief Request 98-02 Re Limited Exam for Three Welds ML20196D4041998-11-19019 November 1998 Rev 1 to Special Rept:On 980618,determined That Method Used to Calibrate Wind Speed Instrumentation Loops of Meteorological Monitoring Instrumentation Sys Does Not Meet TS Definition for Channel Calibration.Procedure Revised ML20195E5521998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20198E3261998-10-31031 October 1998 Revised Monthly Operating Repts for Oct 1998 for Catawba Nuclear Station,Units 1 & 2 ML20154M7661998-10-12012 October 1998 LER 98-S01-00:on 980913,terminated Vendor Employee Entered Protected Area.Caused by Computer Interface Malfunction. Security Retained Vendor Employee Badge to Prevent Further Access & Computer Malfunction Was Repaired.With 1999-09-07
[Table view] |
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I j PLANT SYSTEMS BRANCH l SAFETY EVALUATION REPORT RESPONSE TO 50.54(f) REGARDING SINGLE FAILURE POTENTIAL IN NUCLEAR SERVICE WATER SYSTEM CATAWBA NUCLEAR STATION, UNITS 1 & 2 DOCKET NOS. 50-413/414 INTRODUCTION-
-During a Quality Validation Inspection Audit, the staff reviewed the Catawba 1 nuclear service water (RN) system design and identified concerns regarding whether the shared system satisfied the requirements of General Design Criteria (GDCs)
- 5. " Sharing of Structures, Systems, and Components", and 44, " Cooling Water."
Specifically, the concern is related to at least one scenario in which one unit is shut down (i.e., in Modes 5 or 6) with one of two diesel generators in
! that unit out of service, and the remaining unit has a postulated loss-of-coolant accident (LOCA). Because there is no Technical Specification (TS) l limiting condition for operation (LCO) with one diesel generator out of service l in Modes 5 or 6, this condition could continue indefinitely. In this condition. l a single failure to open of a particular opposite train motor operated RN valve in the suction suppl ultimate heat sink (y transfer from the normal heat sink (Lake Wylie) to theUHS),thesta leave one RM pump to serve both units. This results in a condition which exceeds the design basis for Catawba. The licensing basis as described in the Final Safety Analysis Report (FSAR) states that two out of four RN pumps are necessary to remove LOCA heat loads in one unit and shutdown and cooldown heat loads in the other unit (i.e., the requirements of GDC 5). i As a result of this concern, the staff transmitted a letter to the 'iicensee, Duke Power Company, dated August 7,1987, which requested the licensee, pursuanttotheprovisionsof10CFR50.54(f),toprovide,(1)ananalysis justifying the adequacy of the single RN pump to serve both units, or (2) a description of actions implemented or planned to be implemented that justify continued plant operation. In the interim, the staff notified the licensee by phone, that it should notify the NRC within one hour whenever a diesel generator was taken out of service, and that consideration should be given to switchover to the SNSWP in a time frame less than the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> action statement currently
% being used by the licensee's interpretation of the existing Technical Specifications. The licensee consnitted to comply with these actions and proposed to switchover to the NSWP if the diesel generator is unavailable for 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> s in lieu of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.
By letter dated August 14, 1987, the licensee responded to the staff's 10 CFR 50.54(f) request. In addition, by letter dated August 21, 1987, the licensee
- ' provided minor corrections to the figures provided in the August.14.' 1987 letter.
'4h jw pm cw 8710280212 870930
, PDR ADOCK 0S000413 P PDR
.4 BRIEF DESCRIPTION OF THE CATAWBA NUCLEAR SERVICE WATER SYSTEM (RN)
.The RN system consists of two redundant trains (A and B) of essential equip-ment per unit. TheAtrainissuppliedbytwoARNpumps(oneperunit)and
- l. the B. train by the two B RN pumps. Two pumps-(A and B) are designated for l
each unit and are. powered from separate emergency power sources associated ,
with that unit. The A and B pumps are interconnected by a comon discharge '
header such that operation of any two pumps is sufficient to supply all cooling l water requirements for the two units for all plant conditions including a LOCA in one unit end shutdown and cooldown of the other unit. During normal power operation, only one pump is needed to remove operating plant heat loads from both units. The crossover connections between train A and train B are automatically isolated on a high-high containment pressure or low RN pump pit level signal to ensure train integrity. Refer to the FSAR Section 9.2.1 for a more complete description. Thus, with all trains operable including power supplies, no single failure will reduce the capability of the RN system to less than two pumps.
DISCUSSION AND EVALUATION l
The licensee's response to the 50.54(f) letter discussed conformance to GDCs 5 and-44, single pump operation, actions justifying continued operation and L planned actions to improve safety. Further clarification regarding the system design and the licensee's interpretation of the current Technical Specifications
- were provided by the licensee at a meeting with the staff on August 27, 1987.
Further, the licensee stated in its response that as previously concluded in Section 9.2.1 of the Catawba Safety Evaluation Report (NUREG-0954), the RN system design meets GDCs 5 and 44 and that the staff's previous conclusions remain valid. While the staff's previous conclusions regarding the design of the RN system and GDCs 5 and 44 remain valid as discussed below, it should be noted that the staff's basis for meeting GDC 5 as identified in NUREG-0954 is incorrect. 'In NUREG-0954 Section 9.2.1, the staff stated that its basis for concluding the design meets GDC 5 was the automatic separation capability of the RN system between Units 1 and 2. However, such isolation capability only exists between trains not between units. As a result of this reevaluation the staff concludes that the design as described above meets the requirements of GDC 5. Specifically the design of the RN system is such that no single failure can keep the system from performing its safety function, namely two pumps will be available to handle a LOCA in one unit and bring the other unit to a safe
)
a cold shutdown. The RN system is continuously shared by each unit. .Therefore, l the Technical Specifications (TS) should be revised to adequately address sharing the RN system between units in order to ensure adequate heat removal capability. The current TS for the emergency diesel generators require that two separate and independent diesel generators be operable in Modes.1, 2, 3 and 4. With one diesel generator out of service, operation may continue for up to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. The nuclear service water system TS requires at Isast two in-dependent service water " loops" to be operable in Modes 1, 2, 3, and 4. With l
1
= = - -
w..--
1 L - !
only one loop operable, operation may continue for up to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. Neither of these specifications indicate that the action statement is applicable to both
' units despite the shared nature of the RN system. TS 3.0.5.a specifies that "whenever the Limiting Condition for Operation refers to systems or components which are shared by both units, the ACTION requirements will apply to both
. units simultaneoung. This will be indicated in the ACTION statement". As ar example,.the SNSWP specification, TS 3.7.5, identifies that the ACTION statement applies.to Units 1 and 2.
In the August 14,'1987 response, the licensee stated that plant procedures were revised in 1986 to require both units to enter a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> action statement anytime.a diesel . generator _ on either unit' was removed from service. It was also stated that prior to an emergency diesel generator being or expected to be out of service for 72 haurs or more, plant procedures require that the un-laced in a non-degraded condition by (1)
.affected unaffected unit train be p(A or B) for SNSWP recirculation, isolating andor(2) pre-aligning other- th wise restricting flow to the degraded train of the degraded unit in a manner which insures adequate post-accident flows to components of this (affected) train of the other (operating) unit. Pre-aligning the unaffected train trans-fers the suction and discharge of the RN system train from Lake Wylie to the SNSWP. Following this realignment, the licensee would remove the unaffected unit from the action statement, because the licensee concluded that following the realignment and the shutdown of the affected unit, adequate flow would be-available to supply post-accident heat loads in the operating unit given any single active failure i.e., two complete OPERABLE loops were restored to the operating unit as required by TS. At the August 27, 1987 meeting, the licensee stated that since both units have become operational, the RN Technical Specification has been interpreted to apply to both units.
The staff concludes that the Technical Specifications should be revised to reflect the fact that with a diesel generator or a shared RN component out of service, the action statement should address both units, and should also ad-dress.the alternate actions associated with pre-alignment of the unaffected train from Lake Wylie to the ultimate heat sink including isolation and/or restricted flow to the degraded train of the degraded unit to ensure two pumps are operable and the requirements of GDCs 5 and 44 are met. The bases section of the specification should also identify or define what is to be considered a
" loop" and/or " train". Based upon discussion with the licensee, the staff con-
'cludes that the definition of an RN loo) is not clear. Specifically, the RN system description in the FSAR and it s1ared operation are in terms of " units" and " trains" while the TS discusses " loops".
In the August 14, 1987 letter, the licensee also stated that the transfer from Lake Wylie to the SNSWP as a source of water for the RN system.in)the absense of a loss of-suction from Lake Wylie as originally designed (inipated whenever a high containment pressure was sensed) represents an unnecessary ghallenge to the associated RN suction valves from the SNSWP. To improve the evere11 reliability of the RN system, the licensee is implementing two modifications to reduce the potential for unnecessary challenges. The first modification would remove the containment pressure signal that realigns the RN pumps suction from Lake Wylie
c ~, ,
L. ...*;
i
{
to the SNSWP. This signal .is not necessary since realignment to the SNSWP will. .
occur on loss of suction from Lake Wylie as sensed by low RN pump pit level. !
The second modification will reduce the possibility of spurious transfer signals l by installing additional transmitters to upgrade the logic of the low RN pump l pit level . signal'from a 1 out of 2, to a 2 out of 3 system. The staff finds j the proposed modifications acceptable as they do not degrade the original design basis for' provision of an assured post-accident water source and improve the overall reliability of the RN system.
The licensee also performed an analysis to demonstrate the adequacy of a single.
RN pump to remove LOCA heat loads in one unit and the shutdown heat loads of the other unit. Review of this. analysis is beyond the scope of this SER. The original I and, current licensing design basis requires two pumps as described above and i in the FSAR. It should also be noted that this evaluation did not include a !
review of the affects of the pre-alignment of the RN system for SNSWP recircu- !
1ation on the ultimate heat sink. The staff assumed that the initial FSAR review .I consisidered such effects as overflow capability and temperature changes (in-cluding instrumentation capability) while in the SNSWP recirculation mode.
CONCLUSION Based on'its review as described above, the staff has reached the following conclusions:
- 1. 'he T nuclear service water system design meets the requirements !
of General Design Criteria 5 and 44 as they relate to sharing T and provisions for suitable redundancy in cooling water systems.
The procedures implemented by the licensee and revisions of the Technical _ Specifications which the licensee has committed to submit will ensure that at least two RN pumps will be available for removal of design basis accident (LOCA) heat loads in one
. unit and shutdown and cooldown heat loads of the other unit in the event of a sinole active failure.
1
- 2. Prompt notification (within one hour as previously committed to by the licensee) of the NRC anytime a diesel generator is taken out of service is no longer necessary, similarily switchover to the pond within a 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> period with a diesel generator out of service is no longer necessary.
- 3. The modifications to elim uate the high containment pressure sional from the SNSWP transfer logic and the upgrade of the RN pump pit level logic are acceptable. l
- 4. The licensee shall propose revised Technical Specifications and associated bases to specifically address the fact that the j
' nuclear serv :e water system action statement applies to both j units anytime a diesel generator or shared RN component is taken i out of service, and is applicable during all Modes of operation.
The licensee has comitted to provide the above TS changes. The ;
staff considers a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> LCO on the RN pumps to be appropriate. :
The staff, therefore, concludes that continued operation of Catawba is acceptable, i
I