ML20214P268

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Insp Rept 50-461/86-65 on 861006-1107.Violations Noted: Failure to Follow Procedures for Condition Reporting & Failure to Follow Procedures During Initial Fuel Loading
ML20214P268
Person / Time
Site: Clinton Constellation icon.png
Issue date: 11/25/1986
From: Knop R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20214P226 List:
References
50-461-86-65, NUDOCS 8612040137
Download: ML20214P268 (34)


See also: IR 05000461/1986065

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U. S. NUCLEAR REGULATORY COMMISSION

REGION III

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Report No. 50-461/86065(DRP)

Docket No. 50-461

License No. NPF-55

Licensee:

Illinois Power Company

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500 South 27th Street

Decatur, IL 62525

Facility Name: Clinton Power Station

Inspection At: Clinton Site, Clinton, IL

Inspection Conducted: October 6 through November 7, 1986

Inspectors:

T. P. Gwynn

P. L. Hiland

J. Holmes

<fc Q

,g,s

Approved By:

R. C. Knop, Chief

Projects Section IB

Date

Inspection Summary

Inspection on October 6 through November 7, 1986 (Report No. 50-461/86065(DRP))

Areas Inspected:

Routine, unannounced safety inspection by the resident

inspectors and a region-based inspector of licensee action on previous

inspection findings; IE Circular followup; licensee action on 10 CFR 50.55(e)

report; IE Bulletin followup; licensee event report review and followup;

followup on IE Information Notices; monthly maintenance observation; monthly

surveillance observation; operational safety verification; startup test

witnessing and observation; onsite followup of events at operating reactors;

and management meeting.

Results: Of the twelve areas inspected, no violations or deviations were

identified in nine of the areas.

Six violations were identified in the

remaining areas (paragraph 10 - failure to follow procedures for condition

reporting; paragraph 11.a - eight examples of failure to follow procedures

during initial fuel loading; paragraph 12.b - two examples of performance of

safety related activities without documented instructions or procedures;

paragraphs 9. and 12.b - three examples of inadequate surveillance test

procedures; paragraph 10.b - four examples of violations of the CPS Technical

Specifications; and paragraph 12.b - two examples of personnel errors during

the performance of testing). While each of the identified violations were of

minor safety significance when taken individually, the sum of the violations

over a relatively short period of time represents a trend in performance that

must be corrected.

F612040137 861126

PDR

ADOCK 05000461

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DETAILS

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1.

Personnel Contacted

Illinois Power Company (IP)

  • @K. Baker, Supervisor - I&E Interface, Licensing and Safety (L&S)
  • R. Campbell, Manager - QA
  • W. Connell, Manager - Nuclear Planning & Support
  • @J. Cook, Assistant Manager - Clinton Power Station (CPS)
  • W. Gerstner, Executive Vice President
  1. J. Greene, Manager - Nuclear Station Engineering Department (NSED)
    1. D. Hall, Vice President, Nuclear
  • E. Kant, Assistant Manager, NSED
  1. H. Lane, Manager, Scheduling and Outage Management
  • J. Miller, Assistant Manager - Startup
  • J. Palchak, Supervisor - Plant Support Services
  • J. Peterson, Supervising Engineer - Licensing
  • J. Perry, Manager - Nuclear Program Coordination
    1. F. Spangenberg, Manager - L&S
  • @J. Weaver, Director - Licensing
    1. J. Wilson, Manager - CPS

Nuclear Regulatory Commission - Region III

  1. B. Davis, Deputy Regional Administrator
  1. C. Nore11us, Director, Division of Reactor Projects
  1. R. Knop, Chief, Projects Section 1B

@*#T. Gwynn, Senior Resident Inspector, Clinton

@*P. Hiland, Resident Inspector, Clinton

  • Denotes those attending the monthly exit meeting on November 4, 1986.

9 Denotes those attending the exit meeting on November 7, 1986.

  1. Denotes those attending the management meeting on October 22, 1986.

The inspectors also contacted and interviewed other licensee and

contractor personnel.

2.

Licensee Action On Previous Inspection Findings (92701) (92702)

a.

(Closed) Open Item (461/85005-45): As identified in the Final Safety

Analysis Report and the Safety Evaluation Report, the licensee has

installed a Class "A" Fire Detection system. The preoperational test

demonstrated that during the ground minus test, all detectors for the

zone were indicating a trouble alarm. The licensee indicated that

work has been completed on the fire alarm system and that the system

will function as a Class "A" system. On September 17, 1986, the

inspector observed a ground plus and ground minus test on the fire

alarm system with satisfactory results.

This item is considered

closed.

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b.

(Closed) Open Item (461/86016-04):

Standby' Liquid Control (SC)

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. System, operability verification. :During witnessing of a surveillance

' test conducted by-the licensee to verify SC operability, it.was

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identified that'the' surveillance ~ procedure.(CPS No. 9015.01) could

not be performed.

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This item was previously rev'iewed as documented in Inspection Report .

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50-461/86048, paragraph 2.v. 'This item remained open pending NRC~

' inspector witnessi_ng performance of the procedure.

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The inspector witnessed performance'of the SC quarterly operability

test, CPS No.'9015.01,'as documented in paragraph _7 of this report.

This item is closed.

c.

(Closed) Open. Item l(461/86028-08): The licensee provided the-

inspector with the-completed copy of the preoperational test results

'for the Emergency Lights (PTP-LL-01). The. review of the test results

found the results adequate. :This. item is considered closed.

d.

(Closed) Open Item (461/86028-12): The. reactor recirculation pumps

at the Clinton Power Station are located in a non-inerted containment

-and are not provided with an oil collection system as required by

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10 CFR 50, Appendix R.

The'11censee's response package entitled "NRC I'.E. Issue'Open Item

86-28-12" (document.not dated) stated " Illinois Power submitted a

deviation ^ request to NRR for.the oil collection system of

recirculation pump. motors required by Appendix R,Section III.0".

In a telephone call on June 13, 1986, between NRR and Region III, NRR.

agreed to ~ review previously submitted material from the licensee

regarding the lack of an oil collection system and to document these

findings in a future . safety evaluation report.

In the Clinton Safety Evaluation Report Supplement No. 6, it states,

"In the SER the staff reported that an oil collection system is not

required for the reactor coolant pumps". This' action by NRR is

sufficient to close this item.

e.

(Closed) Violation (461/86054-04):

Unauthorized modification.

installed around the body of Low Pressure. Core Spray (LPCS) injection

isolation valve IE21-F005. A steel plate used as a temporary

security barrier was installed around the LPCS injection isolation

valve without proper controls. Although the licensee identified this

condition during a management walkdown,'no action had been taken to

determine the cause of the condition and to preclude recurrence.

As documented in Inspection Report (IR) 50-461/86060, paragraph 2.t.,

the inspector reviewed the results of the licensee's investigation

into the subject violation. The item remained open pending receipt

and review of the licensee's formal response.

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LDuring..this report period, the licensee' responded to.the subject-

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iviolation in a timely manner. Additional corrective action taken by

ithe licensee to prevent furtheriviolations, not previously' documented

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'in IR 50-461/86060, included the issuance of IP letter JW-1903-86.

Thisiletter from the Manager - CPS to all IP. Plant Staff Personnel

stressed the. requirements of adhering'to CPS procedures when

' personnel identify an indeterminate or adverse condition.

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The inspector confirmed the licensee's corrective actions were

complete. -This item is closed.

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(0 pen) Openl Item (461/86028-13): . The licensee was requested to

verify the maximum depth of frost and if-necessary take corrective

action for.the underground firemain.

In'the licensee's. document entitled, " Depth Of Cover For Underground

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Firemains",

indicates that the underground firemains were installed

in 1976 in accordance with the 1973 edition of NFPA-24 which states

in part, "The depth of cover over water pipes should be determined

-by the maximum depth of frost penetration in the locality".

In the

attachment 1 of the letter from R. Parson, Sargent and Lundy to

Illinois. Power Company, dated June 25, 1986, it indicates that

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the depth of-frost at the Clinton site is 32 inches based on.

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interrelating data from Foundation Engineering by Alfred R. Jumikis,

1971.

In addition, this letter states "The design basis of 42" depth

of cover is consistent with the practices of a local municipality and

a local water company. The local municipality and water company

recommend a minimum depth of cover of 3 1/2 feet for fire protection

lines (standing water)."

The licensee has identified several areas where the underground

firemain is not provided with a depth of cover of 42 inches. The

licensee indicated that a minimum depth of cover of 42 inches will

be provided for those areas by November 30, 1986.

This item will remain open pending verification of the licensee.'s

corrective actions regarding those areas provided with less than 42

inches of cover.

No violations or deviations were identified.

3.

IE Circular Followup (92701)

(Closed) IE Circular (461/78-18): UL Fire Tests.

IE Circular 78-18 identified three concerns as follows:

a.

Flamastic 77 fire retardant coatings may absorb flammable liquid from

an inadvertent spill inside of the barrier at the bottom of vertical

trays.

Attached to the licensee's internal memorandum dated August 6, 1984

from E. Haagar to D. Kerborn (L08-84[08-06]-6) is NSED review and

response which indicated that the fire barrier sealing subcontractor

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anticipated! hat the proposed fire stops for. vertical cable. tray runs

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will be of different (other.than ceramic fiber) UL approved material.

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The: licensee indicated to the' inspector that Bisco Silicone Foam'.

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' SF-20, ~ SF-60, SF-150. NH 'is fire rated and is~ nonabsorbent.

The licensee:provided the inspector with Bisco detail No. 107 through

112 and No. 126. .The inspector noted that 9 inches.of silicone foam

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is used above 1 inch of ceramic material in Bisco detail.No. 107 and

'110.

Based on the fact that there-is no gap between the silicone.-

foam'and the steel sleeve,-the' flammable liquid.from a potential

spill could not be absorbed by the 1 1ach of ceramic material. The

concern regarding the: absorption of flammable li_ quid into the fire

barrier is considered closed.

b.

Small fires may not actuate Sprinkler Heads.

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To reduce ~ the possibility of small fires not actuating sprinkler

heads, fast response sprinkler heads should be considered.

In the

August 6, 1984 memorandum (L08-84 [08-06]-6), the licensee indicated

that all sprinkler heads installed by the CPS sub-contractor

" Automatic Sprinkler Corporation" are UL listed and meet the

requirements of UL Standard 199. < Based on the licensee's internal

response, it is not clear that'the licensee considered in the system

layout the concern for small fires not actuating sprinkler heads.

The licensee indicated to the inspector that the sprinkler systems

have been installed to meet NFPA-13 requirements, and that in

walkdowns consideration has been given to use of fast response

sprinkler heads where required. This. item is considered closed

based on the licensee's response.

c.

Path of air movement influences the actuation of detection devices.

The tentative conclusion from the test also identified the concern

that the location of fire detection devices is of great importance.

The path of air movement in the area influences the actuation of

such devices and should be considered in the system layouts.

In the August 6, 1984 memorandum (LO8-84[08-06]-6), the licensee

states, " fire detection devices are insta11ed'as required by NFPA

72E which establishes the rules for location and spacing in high air

moving areas." This item was previously closed, however, during the

9/10-12/86 inspection the licensee provided the inspector with the

document entitled " Fire / Smoke Detector Layout For Illinois

Power Company", Pyrotronics Job #PC-4920B which indicated that

consideration was given to the placement of detectors with respect to

ceiling tiles, lighting fixtures, air diffusers, egg crate ceiling

sections, soffits, and ceiling obstructions. A field walkdown was

also conducted to-ascertain that the drawings depicted actual

conditions and also to assure that influencing factors were picked

up during the drawing review. This document indicates that a

proposed detector layout took into full account the guidelines set

forth in NFPA 72E as well as good fire protection practices and

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engineering judgment and in no case was the area coverage per

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detector greater than that recommended by either the National Fire

Protection Association or Pyrotronics.

In many areas additional

detectors were located to compensate for increased fire loading or

the physical location of the fire load. The proposed detector

layout drawings were taken back to the. field and checked against

actual site conditions, and the detector layout drawing was

finalized, which was reviewed by Sargent and Lundy.

Based on the licensee's response, this item is considered closed.

No violations or deviations were identified.

4.

Licensee Action on 10 CFR 50.55(e) Report (92700)

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(0 pen) 10 CFR 50.55(e) Report (461/84023-EE):

Ruskin Fire Dampers.

The letter dated August 28, 1985, from D. Hall, IPC, to J. G. Keppler,

NRC, indicated that " Illinois Power investigation of this matter is

complete". This letter also described the investigation results,

corrective action, and attached engineering change notices. The

corrective action taken consisted of the following:

Twenty horizontal dampers in the designated "VC" System (Control

Building) are not acceptable. Heat detectors are to be provided

within selected ducts so that administrative controls can be

implemented to manually shut the fan off to prevent transmission

of fire from one fire area to the other.

One vertical damper in the designated "VA" System (Auxiliary

Building) is acceptable per the test results with the recommended

change to larger springs. This change has been issued to the Zack

Company on Field Engineering Change Notice (FECN) 10503, dated

June 26, 1985.

Nine vertical dampers in the non-safety related ducting designated

"VF", "VJ", "V0", "VP", "VT", and "VW" Systems (Fuel Building,

Machine shop, Off gas, Drywell, Turbine, and Radwaste Building,

respectively) are not acceptable.

Heat detectors are to be provided

within the ducts to trip the fans off to prevent transmission of fire

from one fire area to the other.

The licensee provided the inspector with several documents which included

the Test Report Revision 1 NIBD23 entitled " Fire Damper Closure" and test

data sheets. The licensee identified in the August 28,4985 letter from

D. Hall to Keppler that 150 dampers (26 horizontal and 124 vertical) are

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acceptable per the test results and no modification is required. The

information provided to the inspector did not clearly indicate and compare

the test results to actual physical conditions at the site. The licensee

was requested to organize the material to facilitate review by a person

not involved with the analysis.

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In addition, the licensee agreed (during the previous inspection), to test':

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several dampers in the most severe configurations to insure that dampers:

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will close under air flow conditions.

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- The organization of material to -facilitate for review and the testing of

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dampers in their most severe configuration should be completed by the end

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of.the first refueling outage. This item is open pending licensee actions

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described above.-

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No. violations or deviations were identified.

5.

IE-Bulletin Followup '(92703)(25581)

The bulletin listed below was. reviewed to verify that the written response

was within the time period stated in the bulletin, that the written

. response included the information required to be reported, and that the:

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written. response included adequate corrective action commitments based

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(Closed) IE Bulletin (461/86001-88): Minimum Flow Logic Problems

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That Could Disable RHR Pumps.

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This bulletin was previously reviewed as documented in Inspection

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Report 50-461/86037. The bulletin remained open pending issuance of

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a NRC Temporary Instruction for inspection of this bulletin and pending

completion of the licensee's reviews.

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The inspector reviewed the completed results of the licensee's actions

on this bulletin.. The bulletin was determined to be not applicable to

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Clinton Power Station because independent logic systems were provided.

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This bulletin is closed.

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No violations.or deviations were identified.

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6.

Licensee Event Report (LER) Review and Followup (90712&92700)

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In-Office Review Of Written Reports Of Nonroutine Events At Power

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Reactor Facilities (90712)

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For the LERs listed below, the inspector performed an in-office

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review of each LER to determine that reporting requirements had

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been met; that the corrective action discussed appeared appropriate;

that the information provided satisfied the applicable reporting

requirements; to determine if appropriate actions had been taken on

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any generic issues present; and to Jetermine if any additional NRC

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inspection, notification, or other response was appropriate. Where

determined appropriate, the LER was scheduled for onsite followup

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inspection or other necessary action by cognizant NRC personnel.

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(1)

(Closed)LERNo. 86-001-00 (461/86001-LL):

Isolatior, of Reactor

Water Cleanup (RT) System Due To Spurious Trip Of RT Fump Room

3 High Differential Temperature.

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(2) (Closed) LER No. 86-002-00 (461/86002-LL): Secondary

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Containment Negative Pressure Lost Due To Personnel Defeating

Interlock Switch On Outer Airlock Doors.

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(3) (Closed) LER No. 86-003-00 (461/86003-LL): Control Room

Ventilation Chlorine Mode Initiation Due To Chlorine Detector

Failure.

(4) (Closed) LER No. 86-005-00 (461/86005-LL): Personnel Failure To

Perform Hourly Firewatch Rounds.

This LER was reported pursuant to the requirements 10 CFR 50.73-

(a)(2)(i)B which requires that the licensee report any

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operation or condition prohibited by the plant's technical

specifications.

It was not apparent to the inspector that the

event reported satisfied the referenced requirement.

This

matter was reviewed with the licensee as discussed in paragraph

6.c. of this report.

(5) (0 pen) LER No. 86-006-00 (461/86006-LL): Automatic Initiation

Of Essential Service Water Due To Transient Pressure Drop In

Nonessential Service Water.

The licensee is planning to provide a supplemental report by

December 13, 1986. This matter will be reviewed further with

the supplemental report.

No violations or deviations were identified.

b.

Onsite Followup Of Written Reports Of Nonroutine Events At Power

Reactor Facilities (92700)

(1) For the LERs listed below, the inspector performed an onsite

followup inspection of each LER to determine whether responses

to the events were adequate and met regulatory requirements,

license conditions, and commitments and to determine whether

the licensee had taken corrective actions as stated in the LER.

(0 pen) LER No. 86-004-00 (461/86004-LL): Unplanned Automatic

Initiation Of Standby Gas Treatment System Due To Inadequate

Procedures.

In-Office review of this LER raised a number of questions

concerning the adequacy of the report preparation and one

question concerning the basis for limitations on the corrective

actions taken. These matters were reviewed further by the

inspector through personnel interviews and discussion with

licensee management.

Concerning the adequacy of the report preparation, the inspector

noted that the report abstract contained information not

contained in the LER narrative description, as follows:

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-Plant conditions prior to the event.

Time of the event.

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Operator actions as a result of the Engineered Safety-

Feature (ESF) actuation.

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The results of a channel functional test.

kin addition, the narrative description did not clearly describe

the contribution made'to the event.by the-unknown status of.a

radiation monitor (IRIX-PR008C)' trip signal prior to the event -

and did not describe the ESF response'to the unplanned'

. automatic actuation signal.

Finally, .the inspector _ noted that -

"the narrative description was not sufficiently clear to' allow a

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good understanding of the. event. These matters were discussed

.with responsible licensee management.

The inspector requested

that the licensee consider providing a revision to this LER.

Concerning the corrective actions being taken by the licensee,-

the LER stated that the procedure changes made would prevent

inadvertent initiation of ESFs associated with four radiation

monitors in addition to the radiation monitor that caused the

even t . -- The inspector noted that a significant contributing

cause of the event was the unawareness of plant operators and

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test technicians of the actual' status of the radiation monitor

trip logic prior to commencement of the. surveillance test (i.e.,

the logic for radiation monitor 1R1X-PR008C was sealed in a

tripped condition prior to commencement of testing on

1R1X-PR008B with no indication that the tripped condition

existed) . The LER did not provide any information that

indicated the use of-a logic trip seal-in (without annunciation

or other status indication) was isolated to the five radiation

monitors mentioned in the report. The inspector requested that

the licensee provide the basis for limiting the scope of

corrective actions taken to the five radiation monitors

mentioned in the report.

The inspector reviewed CPS No. 9911.20, Safety Related PRM

Surveillance - Monthly Channel Functional Test, revision 23

dated October 17, 1986, to verify that procedure changes

identified in the licensee's report had been incorporated.

The inspector also reviewed Plant Managers Standing Order

(PMS0)-30, SS/ ASST. SS Notification During Surveillance Testing,

revision 3 dated October 20, 1986, and discussed its use with

several licensed senior reactor operators.

PMS0-30 appeared to

be an effective tool in assuring that the impact of initial

performance of mode 1, 2, or 3 surveillance tests was known to

shift operators prior to test performance. However, the

description of corrective action provided in the LER (i.e., "A

standing order was generated to evaluate all plant surveillances

prior to performance to ensure conditions will support the

test") did not appear to be consistent with the PMSO which

appeared to limit the evaluation to mode 1, 2, and 3 initial

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performance surveillance tests that required lifting leads,

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installing jumpers, or installing test equipment that could

affect the circuit. This matter was also discussed with the

. licensee concerning the need for a revised LER as documented'

above.

This LER will be reviewed further during a subsequent

inspection.

No violations or deviations were identified.

c.

Event Reporting (92700)

Several questions regarding event reporting were discussed with the

licensee during the report period. Those questions resulted from

NRC review of LERs and followup on events that occurred during the

inspection. Those questions involved the following:

(1) LER No. 86-005-LL was reported pursuant to 10 CFR 50.73(a)(2)(1)B which usually applies to violations of Technical

Specification (TS) Action statements. The subject of LER No.

86-005-LL did not involve a violation of a TS action statement.

The licensee was requested to confirm the applicable reporting

requirements.

(2) The licensee did not report two matters involving actuations of

engineered safety features (ESFs) based on their determination

that the actuation was part of the " preplanned sequence during

testing or reactor operation" and that, in accordance with 10 CFR 50.72(b)(2)(11), the actuations were not reportable. The

actuations resulted from operator actions that were performed

without documented instructions or procedures. The licensee was

requested to confirm the applicable reporting requirements and

to provide clarification concerning their definition of a

" preplanned sequence during testing or reactor operation".

(3) The licensee reported a change to their operating organization

which was in conflict with the organization chart provided in

Section 6.1 of the CPS TS via the Emergency Notification System

(ENS).

This matter was clearly not ENS reportable. The basis

for their report was the CPS operating license paragraph 2.F.

The licensee was requested to clarify the applicability of

license paragraph 2.F for reporting violations of the TS and the

Environmental Protection Plan.

At the conclusion of the inspection period, the licensee was

developing interpretations for the information and use of their

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operating organization concerning the above matters.

Items 1, 2,

and 3 above are considered to be unresolved pending issuance of the

interpretations, training of applicable personnel, and inspector

review (461/86065-01).

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7.

Followup on IE Information Notices (92701)

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For each of the IE Information Notices listed below, the inspector

verified that the licensee had received the Information Notice, had

distributed the Notice to appropriate personnel, had reviewed the Notice

for applicability, and, if applicable, had scheduled or completed

appropriate corrective actions.

Information Notice

Number

Subject

85-53

Performance Of NRC-Licensed

Individuals While On Duty.

85-59

Valve Stem Corrosion Failures.

85-62

Backup Telephone Numbers To The NRC

Operations Center.

85-77

Possible Loss of Emergency

Notification System Due To Loss Of AC

Power.

85-89

Potential Loss Of Solid State

Instrumentation Following Failure Of

Control Room Cooling.

85-91

Load Sequences For Emergency Diesel

Generators.85-101

Applicability Of 10 CFR 21 To

Consulting Firms Providing Training.

86-18

NRC On-Scene Response During A Major

Emergency.

86-27

Access Control At Nuclear Facilities.

86-30

Design Limitations Of Gaseous

Effluent Monitoring Systems.

86-37

Degradation Of Station Batteries.

86-39

Failures Of RHR Pump Motors And Pump

Internals.

86-44

Failure To Follow Procedures When

Working In High Radiation Areas.

86-48

Inadequate Testing Of Boron Solution

Concentration In The Standby Liquid

Control System.

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'86-65

Malfunctions Of ITT Barton Model 580

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Series Switches During Requalification

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86-72'

Failure 17-7 PH' Stainless Steel

Springs In Valcor Valves Due To

Hydrogen Embrittlement.

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Failures Of. Scram Discharge Volume

Vent And Drain-Valves.

Concerning Information Notice 86-72, the' inspector determined that'Valcor

Engineering Inc. had notified the licensee of the potential deficiency by

letter dated April 25, 1986. _The licensee performed an initial evaluation

for appitcability/reportability under 10 CFR 21 referral No. 21PE36-from

Baldwin Associates (the plant constructor) dated May 5,1986. The results

of their evaluation, documented in memorandum Y-80932 dated June 4,~

1986,

indicated that the condition identified by Valcor did not apply to-Clinton

Power Station due to different chemistry. Subsequent correspondence,.

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memorandum Y-81702 dated August 15, 1986, indicated that the Nuclear

Station Engineering Department was evaluating the desirability of

modifying plant chemistry controls to include hydrogen addition to the

reactor coolant system. The correspondence indicated that a part of

the modification approval process (if applicable) would include

reconsideration of the applicability of this problem. Information Notice 86-72 was still under review by the licensee at the time of this

inspection.

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The inspector noted that, of the 17 information notices reviewed, only one

(Information Notice 85-91) had been completed with records transmitted to

the CPS Central Files for retention. The inspector observed that the

original records of IN 85-91 had been retained in the Licensing & Safety

(L&S) Department while copies had been transmitted to the CPS Central

Files. This practice appeared to deviate from the recommended practice

in CPS Records Management Standard (RMS) No. 2.01, Standard For the

Collection and Review of Records, which specifies that the original

documents should be transmitted for retention. Discussion with L&S

personnel indicated that the originals would be transmitted to the CPS

Central Files for Information Notice 85-91 and that future records

transmittals would be made in accordance with the RMS.

For the other 16 information notices reviewed, the inspector noted that

a number had exceeded their scheduled completion dates with no forecast

for completion and that the others were pending closure action by L&S

personnel. Discussion with the Manager - L&S indicated that management

was aware of the current program status and had implemented actions based

on recommendations of a management consultant to improve the program.

The results of actions taken by L&S to improve their industry experience

program will be reviewed during a future inspection. This is an open

inspection item (461/86065-02).

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No violations or deviations were identified.

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8.

Monthly Maintenance Observation (62703)

i

Station maintenance activities of safety related systems and components

listed below were observed / reviewed to ascertain that they were conducted

in accordance with approved procedures, regulatory guides and industry-

codes or standards and in conformance with Technical Specifications.

The following items were considered during this review:

limiting

conditions for operation were met while components or systems were removed

,

from service; approvals were obtained prior to initiating the work;

l

activities were accomplished using approved procedures and were inspected

as applicable; quality control records were maintained; activities were

accomplished by qualified personnel; parts and materials used were

properly certified; radiological controls were implemented; and fire

prevention controls were implemented.

The following maintenance activities were observed / reviewed:

a.

Maintenance Work Request (MWR) C-27926 was observed by the inspector

during its performance. This MWR was initiated to perform motor

operated valve testing (M0 VATS) on Reactor Core Isolation Cooling

system valve IE51-F078. Valve IE51-F078 had failed a local leak rate

test (LLRT) and the performance of M0 VATS testing was to verify

proper valve operation. During the testing sequence, maintenance

personnel identified that the stem follower (position indicator) was

interfering with a brass stem nut.

This interference was apparently

preventing the valve disc from seating properly. The Quality Control

(QC) inspector monitoring the maintenance activity requested an

evaluation from the Nuclear Station Engineering Department (NSED)

which was provided at the job site. Condition Report (CR)

1-86-10-252 was initiated to document the identified deficiency

and to provide for corrective action.

Review of the work package present at the job site indicated that

authorization to commence the maintenance activity had been obtained

from the Shift Supervisor; testing equipment was within calibration

,

and verified prior to commencement of the work; approved procedures

l

were present at the work location; and QC hold and witness points

were adhered to.

b.

MWR C-15430 was observed by the inspector during its performance.

This MWR was initiated to perform plant modification IS-7 on the

Main Steam Isolation Valve Leakage Control (IS) system.

The

inspector observed the electrical termination work activities in

progress at local panel 1PL100J. The inspector noted that the

applicable portions of the work package were present at the work

I

site; parts and materials used were properly certified; QC was

performing the inspections required by the MWR and applicable

procedures; the calibration of tools was current and verified by

QC.

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No violations or deviations were identified.

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9.

Monthly Surveillance Observation (61726)

The inspector observed Technical Specifications (TS) required surveillance-

testing on the Standby Liquid Control (SC) System and verified that

testing was performed in accordance with approved procedures in the time

frame required by the TS surveillance schedule; that test instrumentation

was calibrated; that limiting conditions for operation were met; that

removal from and restoration to service of the affected components was

properly accomplished; that documented test results were consistent with

inspector observations and conformed with Technical Specifications and

procedure requirements; that test results were reviewed and approved in

accordance with the licensee's procedures; and that any deficiencies

identified during the testing were properly reviewed and resolved by

appropriate management / supervision.

On October 9, 1986, the performance of surveillance test procedure CPS No.

9015.01, Standby Liquid Control System Operability, revision 22, step

8.2.6 resulted in closure of the reactor water cleanup (RT) system pump

suction isolation valve due to a logic interlock function. The licensee

determined that the surveillance test procedure was missing information

necessary to preclude operation of the interlock. A temporary procedure

change was written to complete test performance and a critique of the test

was held with the test crew and the shift supervisor at the completion of

the test.

10 CFR 50, Appendix B, Criterion V states, in part:

" Activities affecting

quality shall be prescribed by documented instructions, procedures, or

drawings, of a type appropriate to the circumstances and shall be

accomplished in accordance with these instructions, procedures, or

drawings...".

The failure to provide adequate instructions to prevent

actuation of the RT pump suction isolation interlock during performance

of surveillance test procedure CPS No. 9015.01 is a violation of

10 CFR 50, Appendix B, Criterion V (461/86065-04A(DRP)).

One violation was identified.

10. Operational Safety Verification (71707)

The inspectors observed control room operations, attended selected

pre-shift briefings, reviewed applicable logs, and conducted discussions

with control room operators during the inspection period.

The inspectors

verified the operability of selected emergency systems and verified

tracking of LCOs.

Routine tours of the auxiliary, fuel, containment,

control, diesel generator and turbine buildings and the screenhouse were

conducted to observe plant equipment conditions including potential for

fire hazards, fluid leaks, and operating conditions (i.e., vibration,

process parameters, operating temperatures, etc). The inspectors verified

that maintenance requests had been initiated for discrepant conditions

observed. The inspectors verified by direct observation and discussion

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with plant personnel that security procedures and radiation protection.

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(RP) controls were being proper.ly implemented.

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.The inspectors' observed plant housekeeping / cleanliness conditions. No

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discrepancies were noted.

The'above ' reviews and observations were accomplished to verify that

facility operations'were conducted in conformance with the CPS technical

specifications and the conditions of the operating license.

The inspector reviewed the status and implementation of the licensee's

condition reporting (CR) program as defined in CPS No. 1016.01, CPS

Condition Reports, revision 11 dated September 18, 1986. About 300 CRs

were initiated during the month of October with a total of about 562 CRs

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open at the end of the month. Three.CRs were reviewed in some detail

-(in process) and 17 CRs were reviewed for procedural compliance

(completed and in the CPS central files), as follows:

'CR STATUS

REVIEW TYPE

CR No.

C-COMPLETE I-INPROCESS

D-DETAILED N-NONDETAILED

1-86-08-075

C

N'

1-86-08-076

C

N

1-86-08-077

C

N

1-86-08-078

C

N

1-86-08-079

C

N

1-86-08-104

C

N

1-86-08-134

C

N

1-86-08-171

C

N

1-86-08-172

C

N

1-86-09-008

C

N

1-86-09-021

C

N

1-86-09-075

C

N

1-86-09-078

C

N

1-86-09-082

C

N

1-86-09-092

C

N

1-86-10-054

I

D

1-86-10-056

I

D

1-86-10-065

I

D

This review resulted in identification of the following violation of

CPS No. 1016.01:

CPS No. 1016.01, paragraph 2.2.9 requires a resolution for each

condition report as follows:

Resolution - An approved plan of corrective action (remedial and

generic) which includes a schedule with accountability assignments

for performing scheduled tasks, and a tracking and reporting system

to ensure adequate progress is being made. Resolution of remedial

and generic corrective action may occur simultaneously or separately.

For the purpose of this definition, an " approved" plan is one that

has been signed by the applicable Department Head.

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CPS No. 1016.01, paragraph 8.6 requires the following:

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Investigation and Resolution

The department / organization assigned investigation responsibility

shall complete the resolution and investigation and shall sign and

date BLOCK 9, unless a NCMR was initiated, except as noted in section

8.4.5.2.

Investigation responsibility may be reassigned per section

8.7 of this procedure.

CPS No. 1016.01, paragraph 8.2.1.2 identifies the requirements for

filling out block 2 of the CR form, as follows:

BLOCK 2 - Requirements Reference

Enter the references against which the CR is written.

Enter the

document title, number, revision, date, and applicable section, as

appropriate.

If there is no referencing document indicate "NONE".

CPS No. 1016.01, paragraph 8.4.3 states the requirements for the

Compliance Department to review the completed CR form, as follows:

Review

Compliance shall review the CR to ensure that it conforms to the

requirements of this procedure.

Nor,e of the 18 CRs reviewed had a documented corrective action plan that

had been reviewed and approved by the applicable department head prior to

corrective action implementation.

In each case, the information

documented in block 9 of the CR represented a historical summary of

actions taken and results achieved rather than a plan for corrective

action based on the results of an investigation.

In addition, several CRs

reviewed (e.g., CR Nos. 1-86-10-054,1-86-10-065), both in process and in

the CPS Central File, had no requirements referenced in block 2 of the CR.

These violations of CPS No. 1016.10 apparently were not identified during

reviews by the Compliance Department, the QA Department, and the Facility

Review Group. The above represent examples of failure to follow CPS No.

1016.01 in the processing of CRs. This is a violation of 10 CFR 50,

Appendix B, Criterion V and the IP Operational Quality Assurance Manual,

Chapter 5 (461/86065-03).

Several of the CRs reviewed were written during performance of activities

which had subsequently been completed with no plan of corrective action

prepared.

Failure to provide a documented corrective action plan based on

the results of an investigation represented a potentially serious lack of

management control of the licensee's corrective action program and

represented a violation of procedure that was either not recognized or

was recognized and accepted by plant management.

One violation was identified.

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11. Startup Test Witnessing And Observation (72302/72524)

The inspectors witnessed the conduct of portions of the following startup

"

test procedures to ascertain through direct observation and record review

,

that startup testing was performed in accordance with approved procedures-

and the requirements of the CPS operating license.

a.

STP-03, Initial Fuel Loading Witnessing (72524)

(1) Purpose

The inspectors witnessed initial fuel loading. activities being

performed by the licensee in accordance with test procedure

STP-03-0, Fuel Load.

For the portions of the test and fael load

activities witnessed, the inspectors verified that Clinton Power

Station (CPS) Technical Specification requirements and license

conditions were met; that nuclear instrumentation was calibrated

and operating with a measurable count rate; that prerequisites

and initial conditions were met; that staffing requirements and

communications were in accordance with Technical Specifications;

that proper procedures were in use and being followed; that

1/M plots were maintained in accordance with the procedure;

that shutdown margin and control blade operability were

verified at required frequencies; that shift turnovers were

conducted; that control of personnel access to refuel floors

was adequate; that refuel status boards were maintained; that

personnel at each refuel station understood responsibilities;

that overtime limits were observed; that the " master" copy of

procedure STP-03-0 was maintained; that changes to fuel load

procedures were technically adequate and in accordance with

approved CPS procedures; that corrective actions for

deficiencies or problems were adequate; that data sheet entries

were legible, traceable and permanent; and that problems or

deviations from the fuel load procedure were adequately

documented in the control room log.

(2) Discussion

During this report period, the licensee completed loading the

initial core of 624 fuel bundles. The inspectors monitored fuel

loading activities on a continuous basis during the first

one-third core load and on a daily basis thereafter until fuel

loading was completed on October 21, 1986.

Inspectior. results

for the first one-third core load were documented in Inspection

Report 50-461/86060.

The results documented below complete the

inspection activities for the initial fuel load.

(3) Results

Except as discussed below, fuel loading activities were

controlled in accordance with the plant Technical Specifications

and the governing procedures; CPS No. 3007.02, Preparation For

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and Recovery From Refueling Operations For Initial Fuel Load;

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CPS No. 1898.00, Special Nuclear Materials Program; and startup

phase test procedure STP-03-0, Fuel Load. As documented in

paragraph 12 and in the paragraphs below, the licensee violated

the plant Technical Specifications for conducting core

'

alterations (fuel loading) on two occasions and made several

procedural errors during the conduct of initial fuel load.

Procedural errors made were as follows:

(a), On October 3, 1986, an incorrect fuel bundle was

transferred from the 755' elevation of the Fuel Building

to the 828' elevation of Containment. The Special Nuclear

Material (SNM) Transfer Checklist in use (86-106)

designated movement of fuel bundle No. LY3502 from 755'

Fuel Building to 828' Containment.

Fuel bundle No. LY3216

was leaded into the Inclined Fuel Transfer carriage and

moved from 755' Fuel Building to 828' Containment. The fuel

movement error was identified by the Senior Reactor

Operator (SRO) in charge of Fuel Handling. The incorrect

fuel bundle (LY3216) was returned to the 755' Fuel

Building and the correct fuel bundle (LY3502) was moved to

the 828' Containment in accordance with the approved SNM

transfer checklist. The licensee initiated Condition

Report (CR) 1-86-10-056 to document the procedural error

and to provide corrective action.

10 CFR 50, Appendix B,

Criterion V states in part:

" Activities affecting quality

shall be prescribed by documented instructions, procedures,

or drawings, of a type appropriate to the circumstances

and shall be accomplished in accordance with these

instructions, procedures, or drawings...".

The failure

to follow the SNM checklist for movement of fuel bundles

between the 755' Fuel Building and the 828' Containment

as required by CPS No. 1898.00, paragraph 8.4.5, is a

violation of 10 CFR 50, Appendix B, Criterion V

(461/86065-05A(DRP)).

(b) On October 4, 1986, two fuel bundles of the wrong

enrichment were placed into the reactor.

Fuel bundles LY3213 and LY3246 of medium enrichment

(1.54%) were placed into reactor locations requiring high

enrichment (2.00%) type fuel . The licensee initiated

Condition Report (CR) 1-86-10-054 to docuraent the error

and provide corrective action. The licensee identified

the root cause of this event to be an error by the onshift

,

Nuclear Engineer who changed the SNM transfer checklist.

CPS No. 1898.00, paragraph 8.4.6.2, allowed changes to

an approved SNM transfer checklist if made by a member

of the Technicai Department Nuclear Group and approved

by an SRO. While making a change to the approved SNM

Transfer Checklist, the onshift Nuclear Engineer selected

the wrong enrichment type fuel resulting in its subsequent

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placement into the reactor. This error was noted during

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the previous report period and documented in Inspection

Report 50-461/86060, paragraph 6.e.

A notice of violation

was not issued at that time based on the licensee's self

identification and immediate corrective action. However,

during this report period, the inspectors were unable to

verify the adequacy of corrective action implementation

due to the violation discussed in paragraph 10 above, and

a similar error (see subparagraph (e) below) which

occurred during this report period. This indicated the

licensee's corrective actions to this procedural violation

were.either inadequate or inadequately implemented.

10 CFR 50, Appendix B, Criterion V states, in part:

" Activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings, of a type

appropriate to the circumstances and shall be accomplished

in accordance with these instructions, procedures, or

drawings...". The failure of the Nuclear Engineer to

prescribe the correct enrichment type fuel on the SNM

Transfer Checklist, is a violation of 10 CFR 50, Appendix

B, Criterion V (461/86065-05B(DRP)).

(c) On Octcber 5, 1986, after loading fuel into control cell

20-29, a subcriticality check of the just loaded cell

(20-29) was not performed.

Procedure STP-03-0, " Fuel

Load", paragraph 7.3.8 required the performance of a

subcriticality check for the just-loaded cell.

Paragraph 7.3.8 of STP-03-0 directed that the control rod

in the new fully loaded cell be fully withdrawn and

inserted. This action would perform a control rod

functional check; would perform a subcriticality check for

the just loaded cell; and would perform a subcriticality

check for the next cell to be loaded. Since the just

loaded control cell (20-29) was located in two quadrants,

the licensee determined that Source Range Monitors (SRM) A

and B were required to be on scale (above .7 counts) for

control cell 20-29. At that point in the fuel load process

SRM-B was not on scale; therefore, the licensee determined

that instead control rod 24-33 would be withdrawn (this

control-cell was located in only one quadrant) for the

subcriticality check required for the next control cell

(20-33) to be loaded.

The control rod functional check performed by paragraph

7.3.8 of STP-03-0 was a parallel test being conducted per

STP-05-0, " Control Rod Drive System". The conduct of the

control rod functional test (STP-05-0) was controlled by

its own procedure and its performance in parallel with the

subcriticality checks was not a requirement as defined in

STP-05-0, paragraph 7.1.

The licensee performed a subcriticality check for the next

control cell to be loaded (20-33) by withdrawing control

.

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rod 24-33. A subcriticality check on the just loaded cell

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(20-29) was not performed in accordance with STP-03-0,

paragraph 7.3.8 nor was a revision made to STP-03-0 that

allowed omission of this requirement. On October 8, 1986,

the licensee initiated Condition Report (CR) 1-86-10-096 to

document this procedural error and provide corrective

action.

10 CFR 50, Appendix B, Criterion V states in part:

" Activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings, of a type

appropriate to the circumstances and shall be accomplished

in accordance with these instructions, procedures, or

drawings...".

The failure to perform a subcriticality

check on the just loaded cell 20-29 in accordance with

procedure STP-03-0, paragraph 7.3.8 is a violation of 10 CFR 50, Appendix B, Criterion V (461/86065-05C(DRP)).

(d) On October 7, 1986, two fuel bundles were loaded into

control cell 20-41 without performing a subcriticality

check before loading the cell.

Procedure STP-03-0,

" Fuel Load", paragraph 7.3.8.2 required performance of a

subcriticality check for the next cell to be loaded. The

itcensee initiated Condition Report (CR) 1-86-10-063 to

document the procedural error and provide corrective

action. The licensee's iraediate action upon identifying

this error was to suspend core alterations, remove the two

bundles that were loaded, and the required subcriticality

check was performed. The licensee determined the root

cause of this event was personnel error by the Shift Test

Director responsible for the performance of STP-03-0. 10 CFR 50, Appendix B, Criterion V states, in part:

" Activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings, of a type

appropriate to the circumstances and shall be accomplished

in accordance with these instructions, procedures, or

drawings...".

The failure to perform a subcriticality

check prior to loading fuel into control cell 20-41 as

required by STP-03-0, paragraph 7.3 is a violation of 10 CFR 50, Appendix B, Criterion V (461/86065-05D(DRP)).

(e) On October 8, 1986, two fuel bundles of the wrong

enrichment were designated on SNM Transfer Checklist 86-24

for placement into the reactor.

The inspector was present

in the control room when the error was identified by the

Shift Test Director during the positioning of fuel bundle

LY3213 over the reactor for insertion into the core. The

Shift Test Director advised the Shift Supervisor of the

fuel enrichment error and core alterations were suspended.

A review of approved SNM Transfer Checklist 86-24 in use

identified that two fuel bundles of medium enrichment had

been designated in steps 16 and 17 for placement into

reactor locat. ions requiring high enrichment type fuel. The

licensee initiated Condition Report (CR) 1-86-10-065 to

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document this procedural error and provide corrective

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action. The licensee determined the cause of this event

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was multiple personnel errors on the part of the

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individuals who had initiated, checked, and approved SNM

3

Transfer Checklist 86-24 in accordance with CPS No.

I

1898.00, paragraph 8.4.

10 CFR 50, Appendix B, Criterion

,p

V states, in part:

" Activities affecting quality shell

M

be prescribed by documented instructions, procedures, or

A,

drawings, of a type appropriate to the circumstances and

M

shall be accomplished in accordance with these

'l-

instructions, procedures, or drawings...".

The failure

@

of personnel who had initiated, checked, and approved SNM

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Transfer Checklist 86-24 to prescribe the correct fuel

A

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bundle enrichment type is a violation of 10 CFR 50,

@

Appendix B, Criterion V (461/86065-05E(DRP)).

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(f) On October 11, 1986, two fuel bundles were loaded into the

ji:

reactor without verification by the control room SRO, Shift

+

Test Engineer, and Shift Test Director that the fuel loaded

was the proper enrichment type. As part of the licensee's

corrective action for previous fuel loading errors.

memorandum DLH-86-312, dated October 8, 1986, was

2-

incorporated into STP-03-0 (Fuel Load Procedure).

This

%1

memorandum directed that the control room SRO, Shi*t Test

R_

Engineer, and Shift Test Director verify and approve that

y

the fuel to be moved was the proper enrichment type prior

'"

to movement of fuel into each centrol cell.

Fuel bundles

Sg

LY3596 and LY3711 were loaded into the reactor before

igit

verification of fuel enrichment was performed in accordance

f

with memorandum DLH-86-312. The licensee initiated

==

Condition Report (CR) 1-86-10-095 to document this

Q

procedural error and provide corrective action.

Fuel

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bundles LY3596 and LY3711 were verified to be of the

E2

correct enrichment in accordance with the DLH-86-312

1.

memorandum before the licensee proceeded to load the next

e

fuel cell.

10 CFR 50, Appendix B, Criterion V states, in

Z

part:

" Activities affecting quality shall be prescribed by

p

documented instructions, procedures, or drawings, of a type

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appropriate to the circumstances and shall be accomplished

7

in accordance with these instructions, procedures, or

1.

drawings...".

The failure of the control room SRO, the

=

Shift Test Engineer, and the Shift Test Director to verify

$

proper fuel bundle enrichments, in accordance with

4-

memorandum DLH-86-312, prior to placement of fuel bundles

2

LY3596 and LY3711 into the reactor is a violation of

'f

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10 CFR 50, Appendix B, Criterion V (461/86065-05F(DRP)).

gr

(g) On October 14, 1986, two fuel bundles were again loaded

into the reactor without prior verification by the control

d

room SRO, Shift Test Engineer, and Shift Test Director.

A

The two bundles were verified to be of the correct

E

enrichment type after the licensee identified the failure

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-to-follow the directions of memorandum DLH-86-312

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(described'in' item f. above) and before continuing fuel-

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. loading of the next' control cell. . The licensee' initiated

i

LCondition Report.(CR) 1-86-10-135_to document the

~: procedural error' and provide corrective action.

10-CFR 50, Appendix _B, Criterion.V states, in part:

" Activities affecting -quality shall .be prescribed by

documented instructions, procedures, or drawings, of a

type appropriate to the circumstances and shall be

accompitshed in accordance with these instructions,

procedures, or drawings...".

The failure of the control

room SRO, the Shift Test Engineer, and the Shift Test

Director to verify proper enrichments, in accordance

with memorandum DLH-86-312, prior to placement of fuel

bundles LY3189 and LY3320'into the Lreactor is a violation

of 10CFR50, Appendix B, Criterion V (461/86065-05G(DRP)).

The inspector noted that the Shift Test Director's'(STD)

log entries for this procedural error did not properly

reflect the sequence of events. Specifically, the log.

entries on page 103 of _the STD log for-STP-03-0 for time

0231,.0232, and 0235 indicated that all procedural-

'

-requirements nad been met prior to insertion of fuel

bundles LY3189 and LY3320 into the reactor. The inspector

did note that the Shift Test Engineer's log entries for

the procedural error accurately reflected the sequence'of

'

events.

In addition, the licensee had initiated Condition

Report (CR) 1-86-10-135 when the procedural error was

initially identified. The inspector _ discussed the need for

i

accurate records with cognizant licensee personnel. A

subsequent log entry to the STD log for STP-03-0 was made

to accurately detail the sequence of events.

In addition,

memorandum DLH-86-316, dated October 20, 1986, was

,

distributed to all Startup Test Directors emphasizing the

need for accurate log keeping. Based on the review of the

Shift Test Engineers log entries for October 14, 1986, the

i

licensee's initiation of Condition Report (CR) 1-86-10-135,

subsequent log entries made into the STD log on October 14,

1986, and memorandum DLH 86-316, the inspector concluded-

that the licensee had taken. appropriate' action to resolve

the inspector's concerns.

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(h) On October 16, 1986,- an incorrect fuel bundle was

transferred from the 755' elevation of the Fuel Building

to the 828' elevation of Containment. The Special Nuclear

~

Material (SNM) Transfer Checklist in use (86-82) designated

movement of fuel bundle No. LY3409 from 755' Fuel Building

to 828' Containment.

Fuel bundle No. LY3445 was loaded

into the Inclined Fuel Transfer carriage in error and moved

from 755' Fuel Building to 828' Containment. The fuel

movement error was identified by the Senior Reactor

Operator (SRO) in charge of Fuel Handling. The incorrect

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fuel bundle (LY3445) was placed in storage at an 828'.

Containment storage location and the correct fuel bundle

+

(LY3409) was subsequently moved from the 755' Fuel Building

to 828' Containment in accordance.with approved SNM

Transfer Checklist 86-82. The licensee initiated Condition-

Report-(CR) 1-86-10-142.to document the procedural error

and to provide corrective action. 10CFR50,' Appendix B,

Criterion V states, in part: " Activities affecting quality-

shall be_ prescribed by documented instructions, and shall

be accomplished in accordance with these instructions,

procedures, or drawings...". The failure to follow the

SNM transfer checklist for movement of fuel bundles between

the 755' Fuel Building and the 828' Containment as required

by CPS No. 1898.00, paragraph'8.4.7, is a violation of

10 CFR 50, Appendix B, Criterion V-(461/86065-05H(DRP)).

The above. identified procedural violations that occurred during

initial fuel loading were generally minor in nature when

considered individually. However, the repetitive nature of-

several of the violations and the number of violations that

occurred over a relatively short period of time,. represent a

trend in performance that must be corrected. This matter was

.

discussed between NRC management and the licensee in a meeting

documented in paragraph 13 of this report.

Following completion of fuel loading, the inspector reviewed

the fully loaded core geometry and fuel bundle locations and

-

verified that the initial fuel core had been properly loaded.

This review was performed by comparing completed checklists

CPS No. 2209.01C001, " Orientation / Location Verification

Checklist" to completed checklist CPS 2209.01C002,"QA

Verification Checklist".

In addition, these checklists were

compared to video tapes No. 1, 4, 5, and 9 which recorded the

.

fuel bundle orientation, location in the core, and the serial

!

number of each fuel bundle. The inspector also reviewed proper

fuel enrichment location by comparison of NRC Form 741 reports

.

to the licensee's Plant Staff Nuclear Record Core Map. No

!

discrepancies were noted during this review.

b.

STP-05-0, Control Rod Drive System Test Witnessing (72302)

L

The inspectors witnessed portions of procedure step 7.1, Individual

CRD Functional Tests, performed in conjunction with STP-03. For

the portion of the test witnessed, the inspector verified that the

'

procedure in use was the most recent revision; that the test crew

was adequate, knowledgeable of the test requirements, and observed

the requirements of the procedure; that test data was recorded as

'

required using calibrated test equipment; and that preliminary test

results were evaluated against appropriate acceptance standards. The

inspector observed that coordination between the two tests (STP-03

and STP-05-0) was good and that the interface with the control room

operators was well established and properly controlled.

4

23

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One violation with eight examples was identified.

-

-

12 .- Onsite Followup of Events at Operating Reactors (93702)

a.

General

The inspector performed onsite followup activities for events which

occurred during the inspection period.

Followup inspection included

reviews of operating logs, procedures, condition reports, direct

observation of licensee actions, and interviews of licensee

personnel.

For each event, the inspector reviewed one or more of

the following:

the sequence of actions; the functioning of safety

systems required by plant conditions; licensee actions to verify

consistency.with plant procedures and license conditions; and

attempted to verify the nature of the event. Additionally, in some

cases, the inspector verified that licensee investigation had

identified root causes of equipment malfunctions and/or personnel

errors and were taking or had taken appropriate corrective actions.

Details of the events and licensee corrective actions noted during

the inspector's followup are provided in paragraph b. below.

b.

Details

(1) Reactor Water Cleanup Isolation (ENS 06695).

At approximately 3:30 a.m. on October 9, 1986, the reactor

water cleanup (RT) system automatically isolated due-to a high

differential flow signal in the Leak Detection system. At the

time of the isolation, the_ plant operators were restoring the

RT system to service after an interlock between the standby

liquid control (SC) system and the RT pump suction isolation

valve caused the suction valve to shut during performance of

an SC surveillance test.

Plant operators apparently did not

recognize that the RT system piping had partially drained to

the main condenser while the pump suction was isolated. When

the operators restored the RT pump to service, the leak

detection system saw a high flow rate into the RT system with

a low flow rate out of the system while the system piping was

refilling. This condition resulted in the isolation.

The licensee notified the NRC Operations Center of the above

event via the Emergency Notification System (ENS) at 6:45 a.m.

the same day. Condition report 1-86-10-085 and a licensee

event report (LER) were initiated to provide for appropriate

corrective action and reporting of this event.

Initial

investigation by the licensee indicated that the RT system

operating procedure was the primary cause of the event. The

LER will be reviewed upon receipt.

(2) Reactor Trip Due to High Main Steam Line Radiation Signal

(ENS Nos. 06567 an.d 06574).

24

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,

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.

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.

4

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.

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At approximately 12:30 a.m. and again at approximately 1:00 p.m.

on October 15. 1986, while operating in mode 5 (initial fuel

'

load), a reactor trip signal was received from the main steam

line (MSL) radiation monitors. At the time of each occurrence,

MSL radiation monitor channel D was inoperable and in a tripped

condition when a spurious trip signal was received on MSL

radiation monitor channel B.

This satisfied the 2 out of 4

coincident logic and resulted in a reactor trip signal.

The licensee notified the NRC Operations Center of the above

events via the Emergency Notification System (ENS) at

approximately 2:00 a.m. and 5:00 p.m. respectively. Condition

Reports (CRs) No. 1-86-10-126 and No. 1-86-10-137 and a

Licensee Event Report (LER) were initiated to provide

appropriate corrective action and reporting of the event.

The LER will be reviewed when it is issued.

Following the second reactor trip due to the MSL radiation

monitors, the licensee noted that Intermediate Range Monitors

(IRM) Channels A and G were tripped upscale.

In evaluating

the cause for the IRM' upscale trips, the licensee decided to

perform a manual reactor trip in mode 5 with all control rods

fully inserted as part of their troubleshooting effort for the

IRM readings. On October 15, 1986, at approximately 6:00 p.m.,

a manual reactor trip was performed. The performance of this

reactor trip was noted in the Shift Supervisor's Log as a

" Pre-Planned Manual Scram".

However, the Shift Supervisor

was unable to provide the inspector with either the procedure

that was followed to perform the manual trip or an approved

troubleshooting plan. The inspector identified through

discussions with the licensee that the manual trip was conducted

for testing under the verbal direction of the Manager - CPS.

The performance of a manual trip for testing without an approved

procedure or troubleshooting plan is a violation of CPS

No. 1011.01, Test Programs and Control, paragraph 2.1 which

requires that performance tests, modification tests, and

special tests be conducted using approved procedures and is a

violation of 10 CFR 50, Appendix B, Criterion V (461/86065-06A).

This is more significant due to the direct involvement of the

Manager - CPS.

(3) Containment Isolation Valve Closure (ENS Nos. 06568 and 06552).

At approximately 5:15 a.m. on October 14, 1986, while operating

in mode 5 (initial fuel loading), two isolation valves were

inadvertently actuated during the performance of a surveillance

test. Containment and Drywell isolation valves IIA 005 and

IIA 008 actuated closed when surveillance procedure CPS No.

9056.01, " Automatic Actuation of ADS (DIV 1), revision 20,

dated May 3, 1986, was attempted to be performed.

.

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The purpose of surveillance CPS No. 9056.01 was to simulate

- -

automatic actuation and logic system functional test for-

" "

. Division 1.of the Aut'omatic Depressurization System (ADS).

~

. Satisfactory completion of this surveillance was to satisfy

CPS Technical Specifications 4.5.1.e.2 and 4.3.3.2 for

Division 1 of ADS. This surveillance had a frequency

requirement of at least once per 18 months.

,

Performance of surveillance procedure CPS No. . 9056.01.was'

1

authorized by the Shift Supervisor at about 1:30 a.m. on

October 14, 1986. .During the installation of transmitter

simulators per paragraph 8.1.39 at about 5:15 a.m., containment

isolation valve IIA 005 and drywell isolation valve IIA 008

actuated closed. The prior performance of paragraph.8.1.15

l.

was supposed:to have prevented both of these valves-from

actuating. Paragraph 8.1.15 directed the lifting of a wire

at terminal PPP69 in panel H13-P862 to prevent closure of

valves IIA 005, IIA 008, ICC072,'1CC073, and opening of valves

ISM 001A and ISM 002A. The wire at terminal PPP69 was lifted

-

in accordance with paragraph 8.1.15; however, this action

prevented only four of the six valves identified from actuating.

,;

10 CFR 50, Appendix B, Criterion V states, in part:

" Activities affecting quality shall be' prescribed by

documented instructions, procedures, or drawings, of a type

appropriate to the circumstances and shall be accomplished

in accordance with these. instructions, procedures, or

.

' drawings...". The failure to prescribe the proper wiro(s)

to be lifted during the performance of surveillance CPS

i .

No. 9056.01, paragraph 8.1.15 is a violation of 10 CFR 50,

Appendix B, Criterion V (461/86065-04B(DRP)).

,

As described above, the signal that closed isolation valves

IIA 005 and IIA 008 occurred during the installation of

transmitter simulators in accordance with paragraph 8.1.39 of

CPS No. 9056.01. More specifically, the transmitter simulators

installed to Analogue Trip Modules (ATM) 821-N691A and ATM

B21-691E generated the closure signal. These two ATMs are the

<

two channels capable of providing a signal to the trip system

" Reactor Vessel Water Level - Level 1" (Division 1). When

paragraph 8.1.39 was performed at about 5:15 a.m. on October 14,

,

1986, both channelslof the Reactor Vessel Water Level - Level 1

(Division 1) trip system were made inoperable.

CPS Technical Spacification Table 3.3.2-1, Instrument 1.j.,

" Reactor Vessel Water Level - Level 1" requires a minimum

operable channels per trip system of 2.

The performance of

paragraph 8.l.39 as written was a violation of Technical

,

Specification Table 3.3.2-1, Instrument 1.3. minimum operable

i

channel requirement (461/86065-07A(DRP)).

3

Following the isolation valve closure of 5:15 a.m., the

licensee's immediate action was to stop the performance of

26

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surveillance: CPS No. 9056.01; placed ATM_1821-N691E-in-a

- -

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pretest mode and reset-the trip-logic; and rcopened valves-

,

,

.

~1IA005 and IIA 008. The inspector was informed of the isolation

. valve closures and the licensee's intent.to inform.the'NRC

-

Operations-Center of the event-via the ENS at about.7:00 a.m.

,

on October'14. 'The licensee notified the NRC Operations Center

of the above event via the ENS at approximately 8:00 a.m. on

'

!

October 14, 1986.

Condition Report (CR) 1-86-10-117 and an

.LER were initiated _to provide appropriate corrective action

and reporting of the event. The LER will be reviewed when it

is issued.

At-8:11 a.m. on October 14, 1986, the-licensee suspended

specified condition CORE ALTER /" IONS to meet Action Statement-

No. 29 of; Technical Specification 'able 3.3.2-1, Instrument 1.~j.

.

This action was taken by the.. licensee-when it was recognized

'

that channel IB21-N691E was not meeting Table 3.3.2-1, note

"k" which7al10wed a channel to be placed in an inoperable.

i

status for up to_2 hours for required surveillance. At this

i

,'

time in the event, the following misapplication of the

'

Technical Specification occurred.

.

.

(a) Recognition by the licensee that channel 1821-N691E had

I

,

been inoperable for greater than two hours was based-on the

'

isolation valve closure time of 5:15 a.m.

The. inspector

,

noted that paragraph 8.1.15 of surveillance-CPS No. 9056.01

directed the lifting of electrical leads to prevent

actuation of six isolation valves.

Hence, the-correct

'

performance of this paragraph. effectively makes the trip

channels inoperable. .The licensee authorized. performance

of surveillance CPS No. 9056.01 at about 1:30 a.m.

1

'

i

Sometime between the authorized start time (1:30 a.m.) and

'

the time when the isolation valves went closed (5:15 a.m.),

paragraph 8.1.15 -(lifting of leads) was performed.

,

Technical Specification Table 3.3.2-1, Note "k"

required

that a channel may be placed in an inoperable status for

up to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for-required surveillance. 'The licensee

performed CORE ALTERATIONS with both channels (1821-N691A

and 1B21-N691E) for Reactor Vesse1~ Water Level - Low (Table

3.3.2-1, Instrument 1.J.) in an inoperable status

between 1:30 a.m. and 8:11 a.m. on October 14, 1986. This

is a violation of Technical Specification Table 3.3.2-1,

Note "k" (461/86065-07B(DRP)).

(b) As described in Condition Report (CR) 1-86-10-118, the

<

licensee had recognized that channel 1821-N691E was not

'

restored to an operable condition within the required two

hours. The licensee performed the action required by

. Action Statement 29 of Technical Specification Table

3.3.2-1.

The correct Action Statement indicated in Table

3.3.2-1 for instrument 1.j. in specified condition CORE

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ALTERATIONS was Action Statement No. _25.

The performance-

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of Action Statement 29 (suspend CORE ALTERATIONS) was

.

considered _ appropriate by the licensee based on the

instructions contained within _ the action statement. When-

'

. core alterations'were suspended, Action Statement:25

(establish 1 SECONDARY CONTAINMENT. INTEGRITY with the standby

.gasLtreatment system operating within-1 hour) was no longer

requi red.'

The-inspector noted-through discussions with

cognizant licensee personnel that a technical specification

revision was_being requested to clarify the applicability

of Action Statement No. 29 in.-Technical. Specification Table

3.3.2-1.

This will1 remain an Open. Item pending the-

inspector's_ review of the licensee's revised technical

specifications (461/86065-08(DRP)).

The licensee revised surveillance procedure CPS No. 9056.01 by

- use of Temporary Procedure Deviation (TPD) 86-1261. . This TPD

,

provided the necessary steps to restore channel B21-N691E to

licensee to identify that the other channel-(1821-691A)

still had a transmitter simulator installed. With the

transmitter simulator still installed on ATM 1821-691A, the

licensee reentered specified condition CORE ALTERATIONS _at ,

11:55 a.m. on October. 14, 1986. Technical Specification 3.0.4

states in part: ." Entry . into an Operational Condition or other -

specified condition shall not be made unless the conditions for

the . Limiting Condition for Operation are met without reliance

on provisions contained in the Action requirements." Entry

into specified condition CORE ALTERATIONS while not meeting

Technical Specification Table 3.3.2-1, Instrument 1.J., minimum

operable channel requirement of 2 is a violation of~ Technical Specification 3.0.4 (461/86065-07C(DRP)).

The licensee identified that the transmitter simulator was still

installed on ATM IB21-N691A at about 11:00 p.m. on October 14,

,

1986, and suspended core alterations. When the licensee removed

'

the transmitter simulator from ATM 1821-N691A at 11:35 p.m. on

October 14, 1986, isolation valves IIA 005 and IIA 008

-

automatically actuated shut. This was an unnecessary ESF

actuation since a temporary Procedure Deviation could have been

used similar to that used for channel B21-N691E. The-inspector

noted that a control room log entry, which may have been made

after the transmitter simulator was removed, identifiec; the

" anticipated" closure of isolation valves IIA 005 and IIA 008.

The licensee removed the transmitter simulator fron ATM

1821-N691A under the verbal direction of the Shift Supervisor.

When the transmitter simulator had been removed from ATM

IB21-N691E earlier that day, the licensee had prepared a

temporary procedure deviation (TPD 86-1261) to preclude the

unnecessary actuation of isolation valves IIA 005 and IIA 008,

10 CFR 50, Appendix B, Criterion V states, in part: " Activities

affecting quality shall be prescribed by documented instructions,

procedures, or drawings, of a type appropriate to the

i-

28

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circumstances and shall be accomplished in accordance with

-

-

these instructions, procedures, or drawings...".

The failure

'

of the licensee to implement written instructions to remove

the transmitter simulator from ATM 1821-N691A when returning

the ATM to service on October 14, 1986, is a violation of

-10 CFR 50, Appendix B, Criterion V (461/86065-06B(DRP)).

The' licensee notified the NRC Operation Center of the violation

of Technical Specification Table 3.3.2-1 via the ENS at about

2:00 a.m. on October 15, 1986.

Condition Reports (CRs)

1-86-10-118, CR 1-86-10-125, and an LER were initiated to

provide appropriate corrective action and reporting of the

event. The LER will be reviewed when it is' issued.

The inspector noted that the-licensee reported the violation of

Technical Specification Table 3.3.2-1 via the ENS as a 24-hour

report required by paragraph 2.F. of Facility Operating License

NPF-55. -The required reporting requirements for Technical

Specification violations were discussed with the licensee as

documented in paragraph 6.c of this report.

(4) Shutdown Service Water Pump Auto Start (ENS. No. 06588).

At approximately 10:00 p.m. on October 16, 1980, Division 1

Shutdown Service Water Pump started unexpectedly during the

performance of a routine surveillance.

Surveillance procedure

CPS No. 9463.02. " Suppress. ion Pool Water Level LT"CM030(31),

LT-SM013(DG) Channel Calibration", revision 21, dated July.14,

1986, directed in Appendix A the lifting of leads from

Termination Module (TCM) 107. When this step was performed the

Division 1 Shutdown Service Water pump sensed a low pressure

signal from its associated strainer output pressure transmitter

(IPT-SX028). The automatic start was initiated due to this low

pressure signal.

The licensee notified the NRC Operations Center of the above

events via the ENS at approximately 11:30 p.m. on October 16,

1986. Condition Report (CR) 1-86-10-150 and an LER were

initiated to provide appropriate corrective action and reporting

of the event.

The LER will be reviewed when it is issued.

The licensee determined the cause for the event was the

procedure in use (CPS No. 9463.02) was in error. Appendix A to

the procedure incorrectly identified Termination Module 107 for

the lifting of leads. The leads that were to be lifted for

correct performance of this surveillance were located on

4

Tercination Module 104. The root cause for the procedural error

was the incorrect use of electrical drawing E02-1SM013, revision

A in the preparation of the procedure (procedural reference

No. 11.20).

10 CFR 50, Appendix B, Criterion V states in part:

" Activities affect.ing quality shall be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to

29

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the circumstances and'shall be accomplished.in accordance with?

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'these instructions, procedures, or drawings...".

The failure-

-

,

to-prescribe the' correct Termination Module in-surveillance

1

procedure CPS No. 9463.02, revision 21, is a violation of

10 CFR 50, Appendix B, Criterion _V (461/86065-04C(DRP)).

_

- (5) Reactor Trip Due To Personnel ' Error ~ (ENS =No. 06615).

b

At approximately 2:30 a.m. on October 19, 1986, while in mode 5

and performing core alterations (initial fuel;1oad), a reactor-

trip signal was initiated by personnel performing surveillanc'e

procedure CPS No. 9031.14, "IRM Channel-Functional", revision.

20, dated May 17, 1986. Procedural-Step 8.1.1 directed the

placement of Intermediate Range Monitor (IRM)-C drawer function

switch to " Standby".

Personnel performing the surveillance

mistakenly placed the Source Range Monitor (SRM)-C drawer .

function switch to " Standby".

Since-the RPS shorting links had

been removed for initial fuel loading, placement of SRM-C drawer

function switch to " Standby" satisfied the noncoincident

circuitry resulting in a reactor trip. At the time of

occurrence, all control rods were already fully inserted; no

control rod motion resulted from the reactor trip. The licensee-

returned the SRM-C drawer function switch to operate and' reset

the reactor trip.

,

The licensee notified the NRC Operations Center of the above-

event via the ENS at approximately 5:00 a.m. on October 19,

1986. Condition Report (CR) 1-86-10-171 and an LER were

initiated.to provide appropriate corrective action and reporting

of the event. The LER will be reviewed when it is issued.

.

10 CFR 50,' Appendix B,- Criterion V~ states, in parts

" Activities

affecting quality shall be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to-

the circumstances and shall be accomplished-in accordance with-

these instructions, procedures, or drawings...".

The failure of

personnel performing surveillance procedure CPS No. 9031.14 to

operate the IRM-C drawer function switch in accordance with

procedural step 8.1.1 is a violation of 10 CFR 50, Appendix B,

Criterion V (461/86065-09A).

The inspector noted that the

licensee's immediate respons- to this event adequately

identified the cause (persennel error); the licensee documented

the event-(CR No. 1-86-10-171); and the licensee made

appropriate NRC notifications. No response from the licensee

to this violation is required.

(6) Standby Gas Treatment System Exhaust Fan Start (ENS V-

06640).

At approximately 11:30 p.m. on Octobe-

1, 1986, the licensee

identified that the Division 2 Standby Gas Treatment System (VG)

'

Exhaust Fan had started. The licensee determined that the cause

i

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of_the fan start was the installation of a jumper and start

-

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signal onto the Division 2 VG fan start relay. Preoperational

,

Test Procedure (PTP)-VQ-01, step 7.6.96 directed installation

of a jumper and signal onto relay IVAY-VG515D (VR/VQ LOCA relay).

Personnel performing this procedural step mistakenly placed a

jumper and signal onto relay 10AY-VG511F (VG Division 2 fan

start relay). When the expected actions of the PTP did not

occur, the licensee identified the running exhaust fan and the

improperly connected jumpers. _The licensee removed the jumpers

from the Division 2 VG exhaust fan relay (IUAY-VG511F) and

restored the Division 2 Standby Gas Treatment train to a standby

status. At the time of occurrence, the plant was in mode 5.

The licensee notified the NRC Operations Center of the above

event via the ENS at approximately 2:00 a.m. on October 22,

1986. Condition Report (CR) 1-86-10-201 and an LER were

initiated to provide appropriate corrective action and reporting

of the event. The LER will be reviewed when it is issued.

10 CFR 50, Appendix B, Criterion V states, in part: " Activities

affecting quality shall be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to

the_ circumstances and shall be accomplished in accordance with

these instructions, procedures, or drawings...".

The failure _of

personnel performing Preoperational Test Procedure (PTP)-VQ-01

to install a jumper and signal in accordance with procedural

step 7.6.96 is a violatier, of 10 CFR 50, Appendix B, Criterion V

-(461/86065-09B).

The inspector noted that the licensee's

immediate response to this event adequately identified the cause

(personnel error); the licensee documented the event (CR No.

1-86-10-201 and PTP-VQ-01 log entry); and the licensee made

appropriate NRC notifications. No response from the licensee

to this violation is required.

(7) Loss of ENS Due to Power Supply Breaker Accidental Opening

(ENS 06634).

At about 10:30 a.m. on October 21, 1986, an electrician

accidentally tripped 18 circuit breakers while performing

maintenance on Auxiliary Building Motor Control Center 1A1 120

volt AC distribution panel. While removing the 120 volt AC

distribution panel cover, the electrician accidentally tripped

18 circuit breakers interrupting the 120 volt power supplies to

various plant equipment. The licensee determined that one of

the breakers tripped interrupted power to the emergency

notification system (ENS).

In addition, the licensee identified

that two containment isolation valves (1RE022 and 1RF022) had

actuated in the " failed closed" position due to a loss of power

to their associated air solenoids.

The inspector obse.rved the licensee's critique and noted that

the sequence of events were accurately reconstructed. The

31

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.

licensee notified the NRC Operations Center via the ENS at

-

approximately 12:00 p.m. on October 21 of the loss of ENS.

,

An additional notification was made at approximately 1:00 p.m.

on October 21, 1986, on the closure of the two containment

isolation valves. Condition Report 1-86-10-182 and an LER were

initiated to provide appropriate corrective action and reporting

of the event. The LER will be reviewed when it is issued.

(8) Entry Into Specified Condition CORE ALTERATIONS While Relying

On TS Action Statement [ ENS No. 06652]

At approximately 4:00 p.m. on October 22, 1986, the licensee

identified that a violation of the CPS TS had occurred the

previous day. On October 21, 1986, the licensee was operating

in specified condition CORE ALTERATIONS while one train of the

Standby Gas Treatment (VG). System was inoperable.

[TS 3.6.6.3

requires that two independent standby gas treatment subsystems

be OPERABLE during CORE ALTERATIONS. With one train of VG

inoperable, TS action statement 3.6.6.3.a.2 (which requires that

the inoperable train be restored to OPERABLE status within 7

days or suspend CORE ALTERATIONS) applies.] The plant operators

were tracking the inoperable VG train as limiting condition for

operation (LCO) No. 86-10-22. At about 4:10 p.m. on October 21,

the plant operators reentered specified condition CORE

ALTERATIONS while relying on the action statement of the LC0

for the VG system. TS 3.0.4 states, in part, that entry into

an OPERATIONAL CONDITION or other specified condition shall not

be made unless the conditions for the Limiting Conditions for

Operation are met without reliance on the action requirements.

No exception to this TS was stated in the TS for the VG system.

The licensee's reentry into operational condition CORE

ALTERATIONS on October 21 at about 4:10 p.m. was in violation

of TS 3.0.4 (461/86065-07D(DRP)).

The licensee notified the NRC Operations Center of the above

event via the ENS at 3:55 p.m. on October 22. Condition Report

1-86-10-197 and an LER were initiated to provide appropriate

corrective action and reporting of this matter. The LER will

be reviewed when it is issued.

Four violations were identified.

13. Management Meeting (30702)

On October 22, 1986, NRC management met with IP management at the

Region III Office in Glen Ellyn, IL to discuss NRC concerns related to

Clinton fuel loading procedure violations and other events occurring since

issuance of the low power license. Key personnel attending the meetings

are identified by (#) in paragraph 1 of this report.

NRC concerns included the re.latively high number of reportable events that

occurred during the initial fuel loading process; the number of procedural

32

F

'

-

~ . .

.

-

-

-

violations that had occurred duringEthe. fuel loading. process; and the

-~

-

adequacy of implementation of the . licensee's condition reporting system

,

,

to provide'for good root cause determinations and clear corrective

actions to preclude recurrence of the condition.

.The licensee presented information concerning each of the fuel loading

procedure violations and several of the events reported during the

-

initial fuel' loading process. The information' discussed by-the li_censee

' involved personnel errors, equipment malfunctions, design deficiencies,

,

and procedure; inadequacies that contributed to each event, as applicable.

<

Much of .the information discussed by the licensee was preliminary

information. Corrective actions identified by the licensee during the

meeting included.the following:

a.

A Plant Manager's Standing Order was initiated to provide a detailed

evaluation of the impact of performance of certain surveillance tests

prior to their implementation.

b.

. Expanded and improved pre-shift briefings.

c.

Improved vertical communications.

d.

Review and revision.of the CPS Condition Reporting system by the

onsite- safety review committee (Facility Review. Group).

e.

_ Reduced reliance on personnel overtime.

f.

Management change in the'0perations Department.

g.

Improved QA interface with the operating and maintenance

organizations.

h.

Established a plant goal of zero personnel errors.

During the course of the meeting, there was an apparent difference in the

sequence, timing, and numbers of procedure violations as discussed by the

licensee as opposed to information available to the Region III staff.

Those differences were resolved during subsequent discussions between the

NRC resident inspector and licensee management.

At the conclusion of the meeting, Region III management reiterated the

need for timely identification of root causes and completion of corrective

action to prevent recurrence. The licensee acknowledged this.

14. Open Items

Open items are matters which have been discussed with the licensee, which

will be reviewed further by the inspector, and which will involve some

action on the part of the NRC or licensee or both. Two open items

disclosed during the inspection were discussed in paragraphs 7 and

12.b.(3)(b).

-

,

33

,

-

..

.

15. Unresolved Items

-

-

'

Unresolved items are matters about which more information is required in

order to ascertain whether they are acceptable items, violations, or

deviations. One unresolved item disclosed during this inspection was

discussed in paragraph 6.c.

16. . Exit Meetings (30703)

The inspector met with licensee representatives (denoted in paragraph 1)

throughout the inspection and at the conclusion of the inspectio1 on

November 4 and 7, 1986. The inspector stemmarized the scope and findings

of the inspection activities. The licensee acknowledged the inspection

findings. The licensee stated that a detailed analysis which included

many of the findings of this inspection had been performed and that a plan

of corrective action was being developed.

The inspectors also discussed the likely informational content of the

inspection report with regard to documents or processes reviewed by the

inspectors during the inspection.

The licensee did not identify any such

documents / processes as proprietary.

The resident irspectors attended exit meetings held between Region III

based inspectors and the licensee as follows:

Inspector (s)

Date

Falevits

10/30/86

Maura

11/4/86

34