ML20207C058

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Weekly Info Rept for Wk Ending 861219
ML20207C058
Person / Time
Issue date: 12/23/1986
From: Rehm T
NRC OFFICE OF THE EXECUTIVE DIRECTOR FOR OPERATIONS (EDO)
To:
References
WIR-861219, NUDOCS 8612300037
Download: ML20207C058 (28)


Text

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F I

l December 23, 1986' For:

The Commissioners From:

T. A. Rehm, Assistant for Operations, Office of the EDO

Subject:

WEEKLY INFORMATION REPORT - WEEK ENDING DECEMBER 19, 1986 A summary of key events is included as a convenience to those Commissioners who may prefer a condensed version of this report.

Contents Enclosure Administ' ration,

A E

Nuclear Reactor Regulation B

'i Nuclear Material Safe u and Safeguards C

Inspection and Enfcrcement D

Nuclear Regulatory Research E

General Counsel F*

International Programs G

State Programs H*

Resource Management I*

Analysis and Evaluation of Operational Data J

Small & Disadvantaged Business Utilization & Civil Rights T.

  • Regional Offices L*

CRGR Monthly, Reports M*

Executive Director for Operations N*

Items Addressed by the Commission 0*

Meeting Notices P

Proprietary or Other Sensitive Information (Not for 0

external distribution)

  • No input this week.

[

/

/

T.' A Rhm,M t for Operations Office of the Executive Director for Operations

Contact:

B612300037 861223 42 7 PDR COMMS retCC WEEKLYINFOREPT PDR

HIGHLIGHTS OF WEEKLY INFORMATION REPORT WEEK ENDING DECEMBER 19, 1986 State of Ohio and Toledo Coalition for Safe Enercy Sue NRC On Tuesday morning, December 9, 1986, the State of Ohio filed a petition with the 6th Circuit Court. The Petition requested a review of the NRC's denial of the State's 2.206 petition and sought to stay the restart of Davis-Besse.

A Petition seeking similar review and stay filed on Wednesday, December 10, 1986, by the Toledo Coalition for Safe Energy.

12, 1986, the Sixth Circuit Court denied both the On Friday morning, December State of Ohio's petition (to stay the restart of Davis-Besse) and the similar petition for a stay by the Toledo Coalition for Safe Energy.

Marble Hill _

16, 1986 the staff By Order Terminating Construction Pennits dated Decemberte No. 1 and No. 2.

Public Service Company of Indiana stopped construction on th L

I December 1983.

approximately 55% and 35% complete.

Meetina With DOE on High Level Defense Waste NRC and DOE held a public technical exchange in On December 9-10, 1986 Washington, DC on the activities at the Defense Waste Processing Facility (DWPF) at Savannah River, South Carolina and the West Valley Demonstration Project at West Valley,.New York as they relate to the Waste Acceptance Process DOE reviewed for radioactive waste to be disposed of in a geologic repository.

the overall status of the waste glass projects, description of the process, Agreements were product description, quality control programs and schedules. r production glass and basic elements of the process control program the quality of the waste glass.

meetings to resolve outstanding major open items such as the Waste Complianc Plan and quality a:surance for DWPF.

Sequoyah Fuels Update Sequoyah Fuels (SFC) has had difficulties maintaining UFs production during

However, the week of December 12 because of residual moisture in the system.

they now feel that all moisture has been removed and anticipate continuedSF operation of the fluorination system.

into a cylinder.

This opera-December 12, 1986, by draining 80 pounds of UF6 SFC began tion was successful and fluorination continued over the weekend. When filling the first cylinder (14-ton cylinder) on Monday December 15th.All other operations completed, the cylinder contained 27,310 pounds of UF.

6 are progressing without incident.

December 19, 1986

OFFICE OF ADMINISTRATION Week Ending December 19, 1986 ADMINISTRATION OF THE FREEDOM 0F INFORMATION ACT STATUS OF REQUESTS Initial Appeal of Request Initial Decision Carryovers, 1985 181 15 Received, 1986 869 237 Granted 661 101 Denied 221 91 Pending 168 60 ACTIONS THIS WEEK E

Received Steven Aron, Requests copies of reports by the NRC and the University The Cleveland of Wisconsin regarding an incident at the University Clinic Foundation where sealed sources of IR-192 were lost after implementation (86-852) in pigs.

Charles Paulson, Requests copies of three categories of records related to Attorney-At-Law operation Doomsday, atomics testing in Nevada in the 1950's.

(86-853)

Cindee Virostek, Requests copies of all notifications to Region I regarding Kiski Valley incidents at NUMEC that caused or threatened to cause Coalition exposures, radioactive releases, loss of facility operation, (86-854) or damage to property at levels defined at 10 CFR 20.403(a) and (b).

Steven Sholly, Requests three categories of records regarding " discretionary MHB Technical enforcement" discussed in a September 9,1986 meeting Associates with NRC staff and utility representatives.

(86-855)

Katherine Senter, Requests a copy of 01A's report on Region IV.

Sierra Club (86-856)

Charles Ashbaugh, Requests copies of five categories of records related Nuclear Theory to a November 21, 1986 staff meeting to discuss neutron-

.& Technologies irradiated gemstones.

(86-857)

CONTACT:

Donnie H. Grimsley 492-7211 DECEMBER 19, 1986 ENCLOSURE A

2 Received, Cont'd Ellyn Weiss, Requests a copy of Technical Report A-3825-R prepared by Union of Concerned Brookhaven for the NRC, Scientists (86-858)

Ophelia Williams, Requests a copy of NRC's response to Yankee Rowe's J/R/A Associates October 15, 1985 request for exemption from 10 CFR (86-859) 50.62 requirements.

Steve Culpepper, Requests a copy of the OIA report regarding Region IV.

Capital City Press (86-860)

Ophelia Williams, Requests a copy of Volume 8 of BMI-2104, "Radionuclide J/R/A Associates Release Under Specific LWR Accident Conditions."

(86-861)

Ophelia Williams, Requests copies of (1) October 20, 1986 memo from Denton t

J/R/A Associates to Stello regarding Phase 2 maintenance surveillance, and (86-862)

(2) July 7, 1986 memo from Denton to Stello, " Review and Assessments of Water Hammer Occurrences, 1981."

Ophelia Williams, Requests a copy of a January 11, 1986 ACRS letter regarding J/R/A Associates control of heavy loads.

(86-863)

Ophelia Williams, Requests copies of SECY papers86-162, 86-184,86-228, J/R/A Associates86-234, 86-164,86-316, and 86-258.

(86-864)

Ophelia Williams, Requests a copy of an August 1286 document by an IDCOR J/R/A Associates Group to the BWR Owners Group.

(86-865)

Michael O'Brien, Requests copies of the investigatory records and report Clark, McGreevy &

pertaining to allegations by QC inspectors' regarding the Johnson, P.C.

Byron nuclear power plant.

(86-866)

Andrew Schlesinger, Requests copies of records concerning the Hanford "N" ABC News reactor and the Savannah River reactors which were reviewed (86-867) by NRR and referenced in NRR's June 23, 1986 memo to V. Stello and V. Stello's June 30, 1986 memo to the Commissioners.

Per Ramfjord, Requests copies of any contracts NRC has entered with Sidley & Austin Quantex Corporation, Rockville, Maryland.

(86-868)

(Anindividual Requests a copy of a report submitted in 1983 from Dr. Wald requesting of the University of Pittsburg to Region I regarding information)

Nuclear Metals, Inc. of Massachusetts.

(86-869)

DECE"BER 19, 1986 ENCLOSURE A

3 Received, Cont'd Gregory Holmes, APPEAL the lack of response to a request for the chron MHB Technical and reading files of Mr. Hans Schierling from September 1, Associates 1981 through December 31, 1983, concerning the Diablo (86-A-235-86-151) Canyon nuclear power plant.

Gregory Holmes, APPEAL the lack of response to a request for the chron MHB Technical and reading files of Mr. Hans Schierling from January 1, Associates 1981 through March 20, 1986, concerning the Diablo Canyon (86-A-236-86-197) nuclear power plant.

(NRCemployee)

APPEAL TO THE COMMISSION NRC's response to a request (86-A-237-84-61) for records concerning himself.

Granted Kristine Albrecht, In response to a request for inspection reports and Food Irradiation other records regarding the low-level contamination of

Response

the Status 4 Atlantic Richfield Company irradiator, made (86-752) available six records.

In response to a request for records identifying four Vincent Kiernan, The Herald categories of information concerning current projects at (86-785) the Lawrence Livermore or Sandia-Livermore Labs for the NRC, made available four records.

David White, In response to a request for copies of minutes or other The Ohio State records of special meetings between the NRC and Toledo University Edison Company staff regarding the loss-of-feedwater (86-787) event on June 9, 1985, at the Davis-Besse nuclear power plant, made available six records.

Informed the requester that 50 additional records subject to this request are already available at the PDR.

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Martin Hill, In response to a request for records pertaining to the j

San Diego Magazine Nuclear Fuel Fabrication facility operated by GA l

(86-797)

Technologies located on Flintkote Avenue in La Jolla, California, informed the requester that records subject to this request are already available at the PDR.

Paul George In response to a request for copies of all accident or (86-811) safety reports to the NRC by the University of California or any other interested party relating to the research reactors located in Etcheverry Hall, Berkeley, California, made available 42 records.

Informed the requester that one record subject to this request is already available at the PDR.

Steven Aftergood, In response to a request for four categories of records

.l Committee to related to the rule to limit the use of HEU in research Bridge the Gap and test reactors, made available three records.

Informed (86-812) the requester that nine additional records subject to this request are already available at the PDR.

DECEMBER 19, 1986 ENCLOSURE A i

O 4

Granted, Cont'd Paul Bowman, In response to a request for copies of all correspondence Syncor since April 1985 concerning license amendment requests International and supporting records for the Washington Hospital Center, Corporation made available 12 records.

(86-820)

Lyle Graber, In response to a request for copies of enclosures to NUS Corporation the following records: (1) La Crosse letter dated (86-827)

August 27, 1986, transmitting the Semi-annual Effluent Report;(2)BigRockPointletterdatedAugust 28, 1986, transmitting the Semi-annual Effluent Release Report; and (3) Turkey Point and St. Lucie SALP report dated August 21, 1986, made available one record. Informed the requester that the remaining requested records are already available at the PDR.

L (NRC employee)

In response to a request for records regarding any actual (86-828) or requested change in her job series, grade, or position, made available four records.

Sara Powell, In response to a request for lists of NRC's publications Interactive with the offices that sponsor or publish the publications, Features, Inc.

made available five records.

(86-830)

Scott MacDonald In response to a request for lists of (1) 1985 and 1986 (86-839)

LERs with contact names and phone numbers and (2) R0 and l

SR0's, made available a copy of item 2.

In response to I

item 1, made available printouts of LERs sorted by docket number, year and LER number.

Taformed the requester that the NRC does not have lists with contact names and phone numbers, however, this infomation is already available at the PDR in each LER.

Ellyn Weiss, In response to a request for a copy of the Performance Union of Concerned Appraisal Team report on the review of TMI-l from Scientists August 25 to September 5, 1986, informed the requester (86-847) that this report is already available at the PDR.

Denied Jeff Fowler, In response to a request for inspection reports and/or KTVY violation reports for the last five years on the Kerr-(86-576)

McGee Cimarron plant in Oklahoma, made available three

(

records.

Informed the requester that 19 additional records subject to this request are already available at the PDR. Denied portions of six records containing unclassified safeguards information.

DECEMBER 19, 1986 ENCLOSURE A

5 Denied, Cont'd David Perkey, In response to a request for copies of SECY-86-173 and NUS Corporation SECY-86-258, denied portions of these papers, disclosure (86-799) of which would tend to inhibit the open and frank exchange of ideas essential to the deliberative process.

Billie Garde, In response to an APPEAL TO THE EDO for the release of Government two denied records regarding a request for records Accountability concerning Enforcement Action 86-09 dated May 3, 1986, Project on the Comanche Peak nuclear power plant, denied one (86-A-197-86-386) record in its entirety and portions of one record containing the advice, opinions, and recommendations of the staff in the deliberative process of determining proper enforcement actions regarding the Comanche Peak nuclear power plant.

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DECEMBER 19, 1986 EflCLOSURE A

4 I

WEEKLY INFORMATION REPORT

=

DIVISION OF CONTRACTS WEEK ENDING DECEMBER 19, 1986 PROPOSAL UNDER EVALUATION RFP No.: RS-NRR-86-051

Title:

" Technical. Assistance ~ in Support of NRC Reactor Licensing Activities"

==

Description:==

Performance of technical evaluations in support of licensing actions and other support work on licensing activities including: generic and plant-specific safety assessments, Near Term Operating Licenses (NT0Ls), generic issue resolution, i

risk assessments, and analyses of operating reactor experience.

Period of Performance: Three years plus option for two years Sponsor: Office of Nuclear Reactor Regulation Status: Negotiations have been completed. 'Best and Final offers are due on January 8,1937.

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H'i CONTRACTS AWARDED IFB No.: RS-ADM-87-174

Title:

" Text Processing Services" i

==

Description:==

Furnish all plant, equipments, materials and labor to perform i

text processing services for NRC's Electronic Text Processing Branch.

m Period of Performance: Two years Sponsor: Office of Administration Status: A fixed price requirements type Contract No. NRC-10-87-174 was awarded to Keyboard Telecommunications in the amount of

$448,630 effective February 1,1987.

RFP No.: RS-ADM-87-208 i

Title:

" Human Skill Building Training Courses"

==

Description:==

Presentation of four courses entitled, " Conflict Resolution,"

"Small Group Dynamics," " Interviewing Techniques," and

" Conducting and Participating in Meetings."

Period of Performance: Two years i

Sponsor: Office of Adminstration Status: A fixed price indefinite quantity type Contract No. NRC-10-87-208 was awarded to SBA/ Space Qualified Systems Corporation in the i

amount of $208,294 effective December 10, 1986. This firm has been certified by the Small Business Administration as a socially and economically disadvantaged firm eligible for noncompetitive t

awards under that agency's 8(a) program.

1

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DECEMBER 19, 1986 ENCLOSURE A

0FFICE OF NUCLEAR REACTOR REGULATION ITEMS OF INTEREST Week Ending December 19, 1986 Oconee 1, 2. 3 A small seismic tremor was experienced at'the Oconee site about 9:00 A.M.

on December 11, 1986. The Oconee site is located on the Keowee River in western South Carolina near the Tennessee / Georgia border. The tremor was not felt by site personnel but-measured about 2.5 on the Richter scale as reported by a nearby university. Preliminary indications are that no seismic instruments at the Oconee site were triggered.

The licensee is performing a structural inspection of the Keowee and Jocasse dams.

E This was the fourth tremor of this magnitude at the Oconee site in 1986.

State of Ohio and Toledo Coalition for Safe Energy Sue NRC On Tuesday morning, December 9,1986, the State of Ohio filed a petition with the 6th Circuit Court. The Petition requested a review of the NRC's denial of the State's 2.206 petition and sought to stay the restart of. Davis-Besse.

A Petition seeking similar review and stay filed on Wednesday, December 10, 1986, by the Toledo Coalition for Safe Energy.

On Friday morning, December 12, 1986, the Sixth Circuit Court denied both the State of Ohio's petition (to stay the restart of Davis-Besse) and the similar petition for a stay by the Toledo Coalition for Safe Energy.

Callaway Thermal hydraulic anomalies have been detected at Callaway. They were dis-covered recently, but it has been determined that they existed since Feb.1986.

Callaway was shut down in April 1986 for a refueling outage.

The anomalies include coincident deviations in reactor coolant flow (decrease of about.3%), temperature (increase of about l'F) and r.eutron flux (decrease i

ofabout.7%). The anomalies are of about 20 seconds in duration and have an average frequency of 3 minutes. There is no evidence of any loose part flow blockage, or obvious internals abnormality.

Union Electric Company (UE) has hired two independent consultants to investi-gate the anomalies. Preliminary evaluation showed no indication of core barrel vibration or fuel movement.

Further evaluations are expected by December 16, 1986.

The staff plans to meet with the licensee to discuss the safety implications of the observed anomalies as soon as the latest consultant evaluations are comple+ed.

DECE!!BER 19, 1986 ENCLOSURE B

Marble Hill By Order Terminating Construction Pennits dated December 16, 1986 the staff terminated construction permits CPPR-170 and CPPR-171 for Marble Hill, Units No. I and No. 2.

Public Service Company of Indiana stopped construction on these units in December 1983. At the point of cessation of construction Units 1 and 2 were approximately 55% and 35% complete.

Limerick The Philadelphia Electric Company's management announced on December 17, 1986 b

that Limerick, Unit I had recently set a record for continuous first cycle operation for.BWR's greater than 830 MWE. Limerick, Unit i recently passed the 158 day mark (154.5 effective full power days) for continuous operation i

in fuel cycle 1.

Plant shutdown is not expected prior to February-March, r

1987. The next closest were Leibstadt, a BWR6/1220 MWE, for 134 days,

~2 Susquehanna 2 for 122 days and WNP-2 for 101 days. The data for these 3 plants are for days of continuous operation and do not reflect whatever capacity the plant operated at.

Millstone 1 Return to Power Millstone Unit I returned to power on December 15, 1986 after.15-day unplanned outage to replace the main 24/345 kV transfonner that was. damaged on November 30, 1986. The plant was synchronized to the electric grid at 8:30pm on December 15, 1986 and is, as of 9:00am on December 16, 1986, at 70% of rated power. During the outage:

the damaged main transformer was replaced with an on-site spare

(

main turbine shaft seals were replaced to reduce air leakage j

into the main condenser drywell cooler problems were resolved drywell wall thickness was measured at selected locations using UT to assure no thinning selected electrical splices were inspected to assue EQ compliance Power ascension to 100% is continuing.

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ABWR The Tokyo Electric Power Company has announced its intention to construct two nuclear power plants of the ABWR design.

It has begun negotiations with the fisherman's union and the local governments at the Kashiwazaki-Kariwa DECEMBER 19, 1986 EflCLOSURE B

site north of Tokyo on 9 inland sea, where the ABk'R plants will be units #6 and 7.

TEPCO will file a fonnal application for permission to construct the plant in early 1988, and expects to begin construction in 1989. Comercial operation is scheduled for 1996 for unit 6 and 1998 for unit 7.

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.. 3 DECEftBER 19, 1986 ENCLOSURE B

9 NRC TMI-2 CLEANUP PROJECT DIRECT 0' RATE WEEKLY STATUS REPORT FOR DECEMBER 8 - 21, 1986 NOTE: Due to the Christmas holiday, the next Weekly Status Report will be issued on January 5,1986, covering the period December 22, 1986 through January 4, 1987.

1.

DEFUELING The licensee is continuing efforts to identify tooling and techniques which will facilitate defueling.

Since completing the core drilling operation (November 14,1986) the licensee has been unable to resume removal of the damaged core. The drilling r.

operation has not been successful in reducing the

.. I previously-identified "hard crust" region to easily-removed rubble.

Relatively large pieces of the hard crust remain and existing tooling has not yet proved effective in moving or reducing it.

Operation of the Defueling Water Cleanup System (DWCS) and the Temporary Reactor Vessel Filtration System has improved reactor coolant system (RCS) clarity.

Work continues on the modifications needed for full system testing of the coagulant addition to the DWCS. The use of coagulants in parallel with DWCS filtration may provide a more effective means of maintaining the clarity of water in the reactor vessel. Testing of the system is planned to being the week of December 22.

2.

UNUSUAL EVENT On December 16, 1986, a worker was injured in the reactor building containment when a temporary lead shield fell on him. The shielding, consisting of lead-filled curtains hung from a rack, is used to shield a contaminated stairway in the building. The worker was removed from the reactor building after being given first aid by the emergency response crew. The worker was transported to Hershey Medical Center by a company owned ambulance at 10:00 AM. Although the worker was initially believed to have been slightly contaminated by the accident, it was later determined that no contamination resulted from this event. The worker was examined and found to have no serious injuries, and he reported back to work the same day.

3.

ENVIRONMENTAL MONITORING US Environmental Protection Agency (EPA) sample analysis results show that TMI site liquid effluents are in accordance with regulatory limits, NRC requirements, and the City of Lancaster Agreement.

DECEMBER 19, 1986 ENCLOSURE B

TMI water effluents are sampled from the station (Units 1 and 2)

EPA. Gamma spectrum analyses of the seven discharge and analyzed by(November 29 - December 6, 1986) indicated daily composited samples no TMI-2 related radioactivity.

EPA's ganum spectrum analysis of the NRC's TMI outdoor air sample for December 11 - 18, 1986 showed no reactor related radioactivity.

The Lancaster water works intake composited seven daily samples (November 30 - Decerber 6,1986). The gamma spectrum analyzed by

' EPA showed no reactor related radioactivity.

4.

AUXILIARY AND FUEL HANDLING BUILDING ACTIVITIES Reclamation of DWCS filters continues.

Testing of the Fuel Handling Building ventilation system mod.ificJtions are complete.

5.

NRC EVALUATIONS IN PROGRESS t

T

2 Technical Specification Change Request numbers 49, 51, 52, and 54.

Recovery Operations Plan Change numbers 31 and 33.

Solid Waste Facility Technical Evaluation Report.

Heavy Load Safety Evaluation Report, Revision 3.

Disposal of Processed Water Report.

Safety Evaluation Report for Use of Plasma Arc Cutting Torch.

Ex-Vessel Defueling Safety Analysis.

Temporary Reactor Vessel Filtration System Safety Evaluation Report, I

Revision 3.

Safety Evaluation for the Addition of Coagulant to the RCS.

6.

MEETING The next meeting Advisory Panel for the Decontamination of Three Mile Island Unit 2 is tentatively scheduled for January 21, 1987 in Lancaster, PA. The exact date, time, location and agenda will be confirmed at a later date.

Persons desiring to speak before the Advisory Panel are requested to contact Mr. Thomas Smithgall at 717-291-1042, or write him at 2122 Marietta Avenue, Lancaster, PA 17603.

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DECEMBER 19, 1986 ENCLOSURE B i

- ~.._ -,,. _.~.- - -.____..._ _ -..., - -- _,,,

OFFICE OF NUCLEAR MATERIAL SAFETY AND SAFEGUARDS Items of Interest Week Ending December 19, 1986 Mixed Waste On December 11, 1986, Sher Bahadur participated as a mixed waste panel member in a 2-day seminar, " Integrating the Waste Management System," sponsored by the Illinois Department of Nuclear Safety in Chicago.

Mr. Bahadur presented an overview of the mixed waste problem, outlined principal issues, summarized recent history, and presented the current NRC approach.

The other panel members represented the U.S. EPA, Brookhaven National Laboratory, US Ecology, 7

and Duke Power Company.

Meeting With DOE on High Level Defense Waste On December 9-10, 1986 NRC and DOE held a public technical exchange in Washington, DC on the activities at the Defense Waste Processing Facility (DWPF) at Savannah River, South Carolina and the West Valley Demonstration Project at West Valley, New York as they relate to the Waste Acceptance Process for radioactive waste to be disposed of in a geologic repository.

DOE reviewed the overall status of the waste glass projects, description of the process, product description, qu.ality control programs and schedules.

Agreements were reached between NRC and DOE on the scope of plans for sampling the radioactive production glass and basic elements of the process control programs to assure the quality of the waste glass. Agreement was also reached relative to future meetings to resolve outstanding major open items such as the Waste Compliance Plan and quality assurance for DWPF.

Meeting With Atomic Energy Forum The Division of Waste Management (DWM) met with the Atomic Industrial Forum, Subcommittee on High-Level Waste (HLW) on December 16.

NRC staff presented briefings on current NRC HLW activities and on the draft staff Generic Technical Position on Items and Activities Subject to 10 CFR Part 60, Quality Assurance Requirements.

Briefings were also given by DOE on the status of their HLW activities.

This meeting is part of an ongoing effort by DWM to set up an exchange on HLW issues and topics with members of the technical community, industry, states, and Indian tribes.

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1 DECEMBER 19, 1986 ENCLOSURE C

2 Isotope Enrichment On December 17, staff members of NMSS, OGC and SEC met with representatives of All Chemical Isotope Enrichment (A1ChemIE) for further discussions on the firm's plans to obtain and use DOE centrifuge machines for enrichment of stable isotopes.

If negotiations with DOE are successfully concluded by mid-March 1987, AlChemIE expects to submit a license application under 10 CFR Part 50 by May 1987.

A license is required because the definition of a production facility in the Atomic Energy Act and 10 CFR Part 50 includes any equipment and facility capable of and designed for the separation of uranium isotopes, even though AlchemIE would limit its use of the centrifuges for enrichment of only certain stable isotopes for medical and industrial purposes. The proposal by AlchemIE to DOE includes the leasing of the facility at Oak Ridge used for centrifuge testing and demonstration or a facility at Piketon, Ohio constructed by DOE for production-scale centrifuge enrichment. 'The minimal procedural aspects of Part 50 licensing were discussed and the scope of information necessary for preparation of an

,t environmental assessment was reviewed.

A1ChemIE requested further clarification on security requirements, particularly personnel clearance processing, and the role of NRC and DOE on these matters.

Additional discussions are to be held between NRC and DOE staff regarding implementation' of NRC and DOE responsibilities in this area.

Sequoyah Fuels Update Sequoyah Fuels (SFC) has had difficulties maintaining UFg production during the week of December 12 because of residual moisture in the system.

However, they now feel that all moisture has been removed and anticipate continued operation of the fluorination system.

SFC checked a fill station on Friday, December 12, 1986, by draining 80 pounds of UF into a cylinder.

This opera-6 tion was successful and fluorination continued over the weekend.

SFC began filling the first cylinder (14-ton cylinder) on Monday December 15th. When completed, the cylinder contained 27,310 pounds of UF.

All other operations 6

are progressing without incident.

I DECEMBER 19, 1986 ENCLOSURE C

Office of Inspection and Enforcement Items of Interest Week Ending December 19, 1986 1.

Items of Interest Surry Synopsis IE Information Notice No.86-106, Feedwater Line Break, was issued this week to all nuclear reactor facilities to alert them to the potentially generic problem with feedwater pipe thinning and circumstances surrounding the event. The licensee and NRC continues followup inspections at the facility.

Preliminary results from ultrasonic testing (UT) outside containment indicates that pipe thinning has been detected to various degrees else-where in the secondary system, and thinning has also been detected in the discharge line. The UT program is continuing. The licensee has postu-r.

lated that the pipe thinning phenomenon may be attributable, in part, conditions (puritywaterscavengingofmagneticbuildupunderharsh to the high

_. I hightemperature-turbidenvironment).

Two additional fatalities were reported this week bringing the total to four. Two workers remain in the hospital; one in serious condition.

2.

Civil Penalties Paid None.

3.

The following Significant Enforcement Actions were taken during the past week:

Civil Penalties was issued to Texas Utilities An Order Imposing (Comanche Peak) in the amount of $50,000.

a.

Electric Company This action was based on two issues aivolving the applicant's cable tray reinspection program and electrical penetration assemblies.

(EN86-27A) b.

An Order Imposing Civil Penalties was issued to Philadelphia Electric Company (Peach Botton 3) in the amount of $200,000.

This action was based on errors by personnel regarding their rod withdrawal program.

l (EN86-37A) c.

An Order Imposing Civil Monetary Penalties was issued to Star Jet Services (Oklahoma City, OK) in the amount of $500. This action was based on multiple violations which include failure to perform surveys and failure to properly store licensed materials.

(EN 86-66A) d.

A Notice of Violation and Proposed Imposition of Civil Penalty was issued to Illinois Power Company (Clinton 1) in the amount of

$50,000. This action was based on an incident of discrimination in i

violation of 10 CFP 50.50.7.

(EN86-93)

I OECEMBER 19, 1986 ENCLOSURE D f

,y.

. e.

A Notice of Violation and Proposed Imposition of Civil Penalty was issued to Omaha Public Power District (Ft. Calhoun) in the amount of

$15,000. This action was based on a Severity Level IV violation involving an inadequate vital area barrier; the civil penalty was proposed because this violation is similar to a previous violation for which the licensee failed to take effective corrective actions.

(EN86-94)

-4.

The following IE Information Notices and Bulletins were issued during the past week:

a.

IE Information Notice No. 86-14, Supplement 1, Overspeed Trips of AFW, HPCI, and RCIC Turbine was issued to all nuclear power reactor facilities holding an operating license or a construction permit.

~

b.

IE Information Notice No.86-102, Repeated Multiple Failures of Steam r.

Generator Hydraulic Snubbers Due to Control Valve Sensitivity was i

I issued to all nuclear power reactor facilities holding an operating u.

license or a construction permit.

c.

IE Information Notice No.86-103, Respirator Coupling Nut Assembly Failures was issued to all nuclear power reactor facilities holding an operating license or a construction permit and fuel fabrication facilities.

d.

IE Information Notice No.86-104, Unqualified Butt Splice Connectors Identified in Qualified Penetrations was issued to all pressurized and boiling water reactor facilities holding an operating license or a construction permit.

2 e.

IE Information Notice No.86-105, Potential for Loss of Reactor Trip I

Capability at Interrediate Power Levels, was issued to all holders of an operating license or a construction permit for pressurized water reactors or boiling water reactors.

f.

IE Information Notice No.86-10e Feedwater Line Break was issued to all nuclear power reactor facilities holding an operating license or j

a construction permit.

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The following IE Preliminary Notifications were issued during the past week:

a.

PNO-TMI-86-05, GPU Nuclear Corporation (TMI-2), Worker Injured in Reactor Building.

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b.

PNO-I-86-97, Pennsylvania Power and Light (Susquehanna 2), Unplanned Shutdown to Repair Instrument Gas System Leak.

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c.

PNO-I-86-98, E. I. Dupont (Billerica, MA) - Hand Exposure in Excess of Regulatory Limits.

DECEMBER 19, 1986 ENCLOSURE D

t d.

PNO-I-86-99, Del-Med, Inc. (South,Plainfield, NJ) - Spent Molybdenum-99/ Technetium-99m Generators Stolen from Carrier.

e.

PN0-II-86-91B, Virginia Electric Power Company (Surryl&2), Update on December 9 Secondary System Pipe Failure and Fatalities.

f.

PNO-II-86-91C, Virginia Electric and Power Company-(Surry 182),

Secondary System Pire Failure (Update).

g.

PNO-II-86-91D, Virginia Electric and Power Company (Surry 182),

Secondary System Pipe Failure - Update.

h.

PNO-II-86-92, Duke Power Company (Oconee-3) - Shutdown Due to Increased Reactor Coolant Pump Violation.

E 1.

PNO-III-86-144A, Toledo Edison Company (Davis-Besse), State Petitions to Halt Davis-Besse Startup (Update).

j.

PNO-III-86-145, St. Luke's Memorial Hospital (Racine, WI), Diagnostic Misadministration of Iodine-131.

k.

PNO-III-86-146,ConsumersPowerCompany(Palisades), Threatening Call.

1.

PNO-III-86-147, Washington University (St. Louis, MO), Unauthorized Repair of Teletherapy Units.

m.

PNO-III-86-148, Detroit Edison Company (Fermi 2), Weapons, Marijuana Confiscated, i

n.

PNO-III-86-149, Commonwealth Edison Company (LaSalle 2), Feedwater Pump Seal Leak.

l O.

PNO-III-86-150, Toledo Edison Company (Davis-Besse) - MSIV Repair.

p.

PNO-III-86-151, Comnonwealth Edison Company (Byron-2) - Pipe Crack.

q.

PNO-V-86-92, Southern California Edison Company (SONGS 3), Potential Hand Exposure of 512 REM.

i l

l I

l DECEMBER 19, 1986 ENCLOSURE D l

f 0FFICE OF NUCLEAR REGULATORY RESEARCH Items of Interest Week Ending December 19, 1986 2D/3D The final details of INEL instrument refurbishments during the Upper Plenum Test Facility (UPTF) outage period in January-February 1987 were worked out on December 11 and 12, 1986 at the facility site in W. Germany. Two representa-tives from INEL and MPR Associates participated in the working meeting with the German personnel.

Because of the additional degradations in the UPTF turbine flowmeters, RES has E

decided to order twu turbine flowmeters to replace the defective ones. These two turbines are part of the 36 instrument modules which are used to measure

- e the mass flow rates across the upper plenum-core interface. Two additional defective turbines in the upper plenum will not be replaced because of a lower.

measurement priority. RES is planning to replace defective instruments only if the data loss seriously impairs our ability to obtain useful technical results from the test program.

ROSA-IV The ROSA-IV system in Japan performs large-scale thermal hydraulic tests under a cooperative program with the NRC. The test results are used to help the NRC in resolving licensing and safety issue and in verifying scaling parameters in NRC safety analysis codes.

The experiments conducted in the ROSA-IV Large Scale Test Facility in October and November of 1986 included TR-LF-01 (i.e., a station blackout with feedwater terminated and no HPI) and ST-SG-03 (i.e., a steady-state steam generator heat transfer test with steam generator secondary inventory completely depleted), A test to simulate the pressure vessel lower plenum break will be conducted on December 17, 1986. The results of this test will help the NRC in resolving the instrument line rupture issue.

DECEMBER 19, 1986 ENCLOSURE E

2 Davis-Besse Uncertainty Study A loss of Feedwater transient occurred at the Davis-Besse Nuclear Power Station on June 9, 1985. The plant is a pressurized water reactor (PWR) of the raised-loop Babcock-Wilcox design and operated by Toledo Edison Co. This transient resulted in a temporary but total loss of main and auxiliary feedwater. Auxiliary feedwater was eventually restored and the plant was brought to a safe and stable condition.

The NRR staff performed analyses of the Davis-Besse incident including different variations of the recovery method of feed and bleed cooling to remove decay heat. The staff used the Nuclear Plant Analyzer (NPA) with the RELAP5 code. The calculations indicated that feed and bleed could successfully cool the core if initiated early enouoh. Upon completion of calculations the NRR staff requested RES to determine the uncertainties in these calculations.

L

- I Idaho National Engineering Laboratory (INEL) performed the uncertainty study and completed a draft report (EGG-RTH-7458) and submitted it to NRC for comments.

Comparisons between the NRR calculations and Davis-Besse transient data showed that the maximum deviations between the calculated and measured reactor coolant pressures and temperatures were about 50 psi and 25*F respectively. Corresponding errors in the time to reach a given coolant temperature ranged from 1 to 6 minutes. The study performed by INEL showed that the largest contributor to deviations (uncertainties) was an error in the core decay power following the reactor trip. Other contributors included errors in modeling of pressurizer sprey flow and inaccuracies in representing the plant geometry.

INEL produced a quality-assured plant model and used it to predict the Davis-Besse transient. These calculations were in better agreement with the measured transient data both qualitatively and quantitatively. The maximum deviation between calculated and measured reactor coolant pressures was 50 psi, which was the same as the NRR calculations, but deviations in temperatures were less than 6*F.

The RELAP5 code was previously assessed against OTIS test data covering feed and bleed recovery procedure. Maximum deviations for pressure and temperatures were about 100 psi and 9*F respectively. The phenomena in the full-scale feed and bleed transient are expected to be similar to those observed in the appropriate portions of the OTIS experiments and Davis Besse transient.

Hence, uncertainties for a feed and bleed procedure in a B&W plant are expected to be of a similar order of magnitude. The analysis indicates that if feed and bleed is initiated within 20 minutes and full makeup water is available, feed and bleed can be successfully used to cool the core.

i a

DECEMBER 19, 1986 ENCLOSURE E

3 Meeting of NRC Staff with Utility Workers Union of America Members of the NRC staff met with about 70 representatives of the Utility Workers Union of America (UWUA) on December 9,1986, in Washington, DC (UWUA 1986 Nuclear Safety Conference). At the invitation of the union, staff members made presentations and led subsequent discussions on the following topics:

current regulatory initiatives in safeguards (Priscilla A. Dwyer, NMSS);

industrial implementation of fitness for duty program (Loren L. Bush, Jr., IE);

the Chernobyl accident (Frank J. Congel, NRR); and the proposed major revision of NRC radiation protection standards (R.E. Alexander, RES). The union representatives participated actively in the discussions and made a number of points for further consideration by the staff.

Symposium on " Flow and Transport Through Unsaturated Fractured Rock" t.

An important aspect of NRC's waste management program for implementing the Nuclear Waste Policy Act of 1982 (Public Law 97-425) is its confirmatory research program to resolve important characterization and analysis issues for high-level waste sites. The Office of Nuclear Regulatory Research has developed, supported, and monitored technical research on unsaturated flow and transport in fractured media in support of NMSS's program in HLW.

In order to stay actively abreast of the evolving technology in waste management, the staff participates in national and international symposiums on relevant topics.

Tom Nicholson, RES, was co-chairman of a special symposium on " Flow and Transport Through Unsaturated Fractured Rock" at the American Geophysical Union's Fall Meeting held in San Francisco, CA, December 11-12, 1986. The majority of the 26 papers presented dealt with DOE's funded work on Yucca Mountain site characterization studies. Mr. Nicholson presented the keynote paper on " Overview of flow and transport processes and characterization methods for unsaturated fractured media." Other invited papers were "Modeling of isothernal and non-isothermal flow in unsaturated fractured media" (LBL),

"Radionuclide transport in an unsaturated fractured medium" (SPECTRA),

" Application of hydrologic techniques in characterization of unsaturated fractured rocks" (USGS), and "Three-dimensional computer model of flow and transport in variably-saturated fractured rock" (U. of Arizona). A panel discussion on natural analogues, rock mechanics, unsaturated zone characterization methods, and modeling strategies completed the symposium.

DECEMBER 19, 1986 ENCLOSURE E

4 Publications to be Issued in the Near Future

Title:

Qualification and Training of Personnel for Nuclear Power Plants (Reg. Guide 1.8, Rev. 2)

==

Description:==

Reg. Guide 1.8 provides guidance on training and qualifications of nuclear power plant personnel.

Contact:

Clare Goodman, NRR 492-9483

Title:

Medical Evaluation of Licensed Personnel for Nuclear Power Plants (Reg.. Guide 1.134, Rev. 2)

L

==

Description:==

Reg. Guide 1.134 provides guidance on medical qualification of applicants for operator or senior operator licenses and and on notifying the NRC of disability.

Contact:

S. Shankman, NRR 492-9806

Title:

Nuclear Power Plant Simulation Facilities for Use in Operator License Examinations (Reg. Guide 1.149 Rev. 1)

==

Description:==

Reg. Guide 1.149 provides guidance on certification and approval of a simulation facility.

Contact:

J. Wachtel, NRR 492-8508

Title:

Electric Penetration Assemblies in Containment Structures for Nuclear Power Plants (Reg. Guide 1.63, Rev. 3)

==

Description:==

This regulatory guide endorses IEEE Standard 317-1983, "IEEE Standard for Electric Penetration Assemblies in Containment Structures for Nuclear Power Generating Stations", for meeting Commission's regulations with respect to the design, construction, testing, cualification, and installation of electric penetration assemblies.

Contact:

S. Aggarwal, RES 443-37840 DECEMBER 19, 1986 ENCLOSURE E

5 l

RES RULEMAKING ACTIVITIES Licenses and Radiation Safety Requirements for Well Logging Operations (Part 39)

The rule would establish specific radiation safety requirements applicable to licensees who perform operations such as well logging, mineral logging, radioactive markers, and subsurface use of radioactive materials in tracer studies. The proposed rule is necessary to provide the specific guidance necessary to ensure that these operations are performed safely.

The final rulemaking package (SECY-86-366) was signed by the EDO and forwarded to the Commission on December 9, 1986.

Improved Personnel Dosimeter Processing (Part 20)

E

-i Present NRC regulations require NRC licensees to provide personnel monitoring equipment (dosimeters) to certain workers, but provides no standards for processing those dosimeters. This rule will require all NRC licensees to have-their personnel dosimeters that require processing processed by a dosimetry service that is accredited by the National Voluntary Laboratory Accreditation Program (NVLAP) operated by the National Bureau of Standards.

The final rulemaking package (SECY-86-360) was forwarded by the EDO to the Commission for consideration on December 3, 1986.

Residual Radioactive Contamination Limits for Decommissioning (Part 20)

This rulemaking would provide limits of residual contamination for land and structures for NRC-licensed facilities to be decommissioned for unrestricted use. The rulemaking has parallelled and is being coordinated with an EPA effort to develop Federal guidance in this area through an Interagency Working Group, in which NRC staff is participating.

It has become apparent that Federal guidance on this topic will take a long time to complete (years).

Therefore, a recommendation to the EDO to terminate this rulemaking, pending formulation of the Federal guidance, was sent to the EDO on December 12, 1986.

DECEMBER 19, 1986 EflCLOSURE E

ITEMS OF INTEREST OFFICE OF INTERNATIONAL PROGRAMS WEEK ENDING DECEMBER 19, 1986 ABWR Decision Made in Japan Tokyo Electric Power Co. has decided to propose construction and operation of two power plant units utilizing the Advanced Boiling Water Reactor (ABWR) design. The two units will be located at the Kashiwazaki site (Units 6 and 7) in Niigata prefecture on the Sea of Japan. The General Electric Co. is a main participant and contributor in the ABWR design.

Formal negotiations with the local government will start shortly. The present schedule calls for start of construction of Unit 6 in 1989 with start-up in 1996.

b

~

International Meeting Notices The following international meeting notices supplement those announced previously:

IAEA Advisory Group Meeting on Quality Assurance for Installation and Connissioning of Instrumentation, Control and Electrical Equipment of Nuclear Power Plants, February 23-27, 1987, Vienna, Austria IAEA Specialists Meeting on Reliability of Active Components of Nuclear Power Plants, April 22-24, 1987, London, United Kingdom IAEA Specialists Meeting within the Framework of the International Working Group on Fast Reactors (IWGFR) on Fission and Corrosion Products Behaviour in Primary Circuits of LMFBRs, May 5-8, 1987, Ka rlsruhe, Federal Republic of Germany IAEA Advisory Group Meeting on Promising Locations for Small and Medium Power Reactors, May 11-15, 1987, Vienna, Austria IAEA International Symposium on Safety Aspects of the Ageing and Maintenance of Nuclear Power Plants, June 29-July 3, 1987, Vienna, Austria NEA Specialists Meeting on Improving Technical Specifications for Nuclear Power Plants, September 7-11, 1987, Madrid, Spain IAEA International Conference on Nuclear Power Performance and Safety, September 28-October 2, 1987, Vienna, Austria DECEMBER 19, 1986 ENCLOSURE G

2 Foreign Visitors On Tuesday Boris Semenov, Deputy Chairman of the State Committee for the Utilization of Atomic Energy in the USSR, met with Chairman Zech, Commissioners Bernthal and Carr, EDO V. Stello, NRP Director H. Denton, and IP Director J. Shea to discuss nuclear safety cooperation and other topics of mutual interest. Mr. Yuri Nazarkin from the Ministry of Foreign Affairs accompanied Mr. Semenov to the meetings and on his tour of the Incident Response Center. Mr. Lawrence Goodrich, Science Officer at the American Embassy in Moscow, also attended the meeting with Commissioner Bernthal.

On Thursday Mr. Irving Wang of the Taiwan Power Company met with staff from International Programs and the Safety Research Applications Branch, RES, to discuss NUREG-1160 and the current status of revisions to 10 CFR Part 20.

DECEMBER 19, 1986 ENCLOSURE G

OFFICE FOR ANALYSIS AND EVALUATION OF OPERATIONAL DATA ITEMS OF INTEREST Week Encina December 19, 1986 1.

A preliminary AE0D Case Study report on " Air Systems Problems at U.S.

Light Water Reactors" was issued for peer review on December 12, 1986.

The study analyzes and evaluates the operational experience related to, and the safety implications associated with, failures and degradations of air systems at U.S. LWRs.

The report presents aspects of air system degradations and plant responses to air system losses which are not addressed in previous studies.

It also highlights more than two dozen events in which, contrary to licensing assumptions, a safety-related system failed due to an air system degradation or failure. Operating events involving the E

loss or degradation of air systems were judged to be safety significant because they may lead, under different circumstances, to potentially serious events and conditions which have not been analyzed in the FSAR.

The report presents five recommendations which, if implemented, should e

reduce reactor accident risks by reducing the likelihood for common mode failure of safety systems and by enhancing plant recovery from anticipated and unanticipated transients.

2.

AE0D Engineering Evaluation Report, AE00/E612. " Emergency Diesel Generator Component Failures Due to Vibration," was issued on December 17, 1986.

The report provides a review of events involving cracking of small bore pipino that resulted in inoperability of emergency diesel generators (EDGs). The cracked lines were found in EDG lube oil, fuel oil and cooling water systems. The piping cracks, which were caused by cyclic fatigue that resulted from engine-induced vibration, were not detected by the inservice inspection or the preoperational testing program for the piping. The failures were only discovered after the cracks propagated completely through the tube wall and fluid was observed leaking from the pipes. There were a total of eight such events which have occurred at eight plants with the EDGs supplied by four different manufacturers.

Our review indicates that fatigue failures induced by steady-state operation, such as plant equipment or engine-induced vibration, are not normally analyzed in the original piping design. A more complete design review is typically done only after related problems are identified during plant operation. Often the problem is not detected until a leak l

occurs. Such leaks could result in sudden disabling of the EDGs when needed and could adversely affect a safe plant shutdown in the event of a loss of offsite power.

Based on the results of this review, AE00 suggested that IE issue an information notice to the potential safety concern of fatigue cracks in fuel oil, lube oil and cooling lines associated with EDGs.

DECEMBER 19, 1986 ENCLOSURE J

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3.

Technical Review Report, AE0D/T609 entitled, " Foreign Material and Debris i:

in Safety-Related Fluid Systems," was issued on December 16, 1986. The t

report was prompted by(a recent event at Pilgrim in which the standby liquid control system SLCS) was declared inoperable after debris was found in both the main and test SLCS tanks. The study found that formal written procedures are commonly used at nuclear power plants to minimize the introduction of foreign material and debris into safety-related fluid systems during system maintenance and modification activities md that these procedures appear to be generally effective. The study also found that at limited number of operating events have been attributed to foreign material and debris contamination during maintenance or modification and that there is relatively minor safety significance associated with these events. The study concluded there is limited risk significance which can be associated with the effect of foreign material and debris on safety-related systems.

J.'

Technical Review Report, AE0D/T610 entitled, " ADS /RCIC System Interaction N(

Events at River Bend I" was issued on December 19, 1986. This study was E

inidated in response to an LER in which the actuation of certain ADS

~

- i relief valves caused the isolation valves of the RCIC to activate and close rendering the RCIC unavailable. The study found that the events at River Bend 1 involving the ADS /RCIC system interaction appear to have Ifmf ted safety significance. Each event resulted in the RCIC system b'etng unavailable for' less than an hour until the system was returned to the standby condition.

The resultant unavailability of the RCIC system' was estimated to be nearly insignif,1 cant compared to the system's expected yearly total unavailabili3y. The study also found that the ADS /RCIC system interaction events at River Bend 1 were plant-specific events and'are not a generic' concern.

Finally, it appears that the licensee's corrective actions are adequate to prevent recurrence of an ADS /RCIC system, interaction. Therefore, it is suggested that no further AE00 action concerning this subject be taken at this time.

5.

Technical Review Peport, AE0D/T611 entitled " Denied Access Due to Negative Room Pressure" was issued on December 19, 1986. The report was based.on an incident in which personnel entry was denied to.several areas within the reactor enclosure due to a negative rcom pressure differential. Th is '

negative pressure differential was caused by the inadvertent trippfng of the ventilation supply fan while the exhaust fan cdntinued to operate.' 3 The regulatory concern that was timely access necessary for operation action might not be available into areas containing safety-related equip-ment in a plant emergency with a similar failure. The licensee manually tripped the area exhaust fan to reduce the negative room pressure.

Whoever, it was noted that automatic tripping of the exhaust fan upon failure of the supply fan would have avoided this event. A search for delayed access events due to a negative room pressure differential did not find any similar events. Therefore, this event appeared to be an isolated case without significant generic safety concern, t

s

MCEMBER 19, 1986 EflCLOSURE J

9

,,,, p.

NMSS MEETING NOTICES FOR WEEK ENDING:

Division of Fuel Cycle and Material Safety 12/29/86 g;

h!

DOCKET ATTENDEES /

ll 'DATE/ TIME NUMBER LOCATION PURPOSE APPLICANT NRC CONTACT U$

[,',12)!!-22/86 40-8027 Gore, OK To participate in oversight for S. Pennington (FC) - Crow /

g restart of Sequoyah Fuels Corp.

Pennington,k.c os 12/18/86 70-143 Nashville, To meet with State of Tennessee W. T. Crow (FC)

Crow TN to discuss a problem of contamina-8 tion at the Erwin City sewage treatment plant.

j' 12/29/86-1/5/87 40-8027 Gore, OK To participate in oversight for restart of Sequoyah Fuels Corp.

M. Lauer (FC)

Crow /Lauer Division of Waste Management 12/21-23/86 Denver, 00 Technical Meeting with Field Michael Young Michael Young Office on Hydrology Division of Safeguards None E

P S?

E rn T

i